10
Complaints
0
Crashes
0
Fires
0
Deaths

This Problem Across All Years

All Electrical System Complaints

Showing 10 of 10
Dec 9, 2016 166,000 mi

TL* THE CONTACT OWNS A 2002 BMW 540I. THE CONTACT STATED THAT IT TOOK TEN ATTEMPTS TO START THE VEHICLE. THE FAILURE OCCURRED AT LEAST THIRTY TIMES. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 166,000.

Dec 9, 2016 166,000 mi

TL* THE CONTACT OWNS A 2002 BMW 540I. THE CONTACT STATED THAT IT TOOK TEN ATTEMPTS TO START THE VEHICLE. THE FAILURE OCCURRED AT LEAST THIRTY TIMES. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 166,000.

Dec 16, 2013 151,345 mi

AFTER STARTING UP MY CAR, THERE WAS A SLIGHT WHINE UNDER THE HOOD. I GAVE THE CAR A LITTLE BIT OF THROTTLE TO SEE IF THE WHINE WENT AWAY AND HEARD A LOUD BANG. THE CAR WAS STILL RUNNING BUT MY BATTERY LIGHT WAS ON. I NEEDED TO GET HOME, AND I THOUGHT THAT MY CAR MAY NOT START AGAIN IF I TURNED IT OFF SO I DROVE HOME. IMMEDIATELY I NOTICED THAT I DIDN'T HAVE ANY POWER STEERING. AS I DROVE MY ENGINE TEMPERATURE GOT HIGHER AND I BARELY MADE IT HOME WITHOUT OVERHEATING. A FEW DAYS LATER I LOOKED IN THE ENGINE COMPARTMENT AND SAW THAT THE POWER STEERING PUMP HAD BROKEN FREE OF THE ENGINE - THE BRACKET HAD SHEARED OFF. THAT IN TURN CAUSED THE BELT TO FALL OFF WHICH WAS TURNING THE WATER PUMP AND ALTERNATOR. I GOT ON THE COMPUTER AND LOOKED UP THE PROBLEM AND FOUND A LOT OF PEOPLE EXPERIENCING THE SAME PROBLEM, SOME DRIVING DURING THE INCIDENT. THIS IS A REAL DEFECTIVE DESIGN AND CAUSES ME TO BE CONCERNED ABOUT THE SAFETY. I HOPE NOTHING TRAGIC HAS TO HAPPEN TO SOMEONE FOR THIS TO BE CONSIDERED A RECALL. *TR

Dec 16, 2013 151,345 mi

AFTER STARTING UP MY CAR, THERE WAS A SLIGHT WHINE UNDER THE HOOD. I GAVE THE CAR A LITTLE BIT OF THROTTLE TO SEE IF THE WHINE WENT AWAY AND HEARD A LOUD BANG. THE CAR WAS STILL RUNNING BUT MY BATTERY LIGHT WAS ON. I NEEDED TO GET HOME, AND I THOUGHT THAT MY CAR MAY NOT START AGAIN IF I TURNED IT OFF SO I DROVE HOME. IMMEDIATELY I NOTICED THAT I DIDN'T HAVE ANY POWER STEERING. AS I DROVE MY ENGINE TEMPERATURE GOT HIGHER AND I BARELY MADE IT HOME WITHOUT OVERHEATING. A FEW DAYS LATER I LOOKED IN THE ENGINE COMPARTMENT AND SAW THAT THE POWER STEERING PUMP HAD BROKEN FREE OF THE ENGINE - THE BRACKET HAD SHEARED OFF. THAT IN TURN CAUSED THE BELT TO FALL OFF WHICH WAS TURNING THE WATER PUMP AND ALTERNATOR. I GOT ON THE COMPUTER AND LOOKED UP THE PROBLEM AND FOUND A LOT OF PEOPLE EXPERIENCING THE SAME PROBLEM, SOME DRIVING DURING THE INCIDENT. THIS IS A REAL DEFECTIVE DESIGN AND CAUSES ME TO BE CONCERNED ABOUT THE SAFETY. I HOPE NOTHING TRAGIC HAS TO HAPPEN TO SOMEONE FOR THIS TO BE CONSIDERED A RECALL. *TR

Oct 2, 2012 76,854 mi

I WAS DRIVING IN STOP AND GO TRAFFIC WHEN I NOTICED THE STEERING FELT A LITTLE STIFFER THAN USUAL. AFTER ABOUT 5 MILES AND BETTER FLOWING TRAFFIC I PULLED INTO A RESTAURANT FOR DINNER WHEN MY UPPER RADIATOR HOSE EXPLODED. I PULLED INTO A STALL AND OPENED THE HOOD TO INSPECT WHAT HAPPENED. THE HOSE WAS VERY APPARENT AND AFTER FURTHER INVESTIGATION I NOTICED THE POWER STEERING PUMPS PULLEY AT A VERY SHARP ANGLE COMPARED TO LINEAR WITH THE SERPENTINE BELT. I CAN ONLY ASSUME THAT FROM THE BRACKET ON THE PUMP BREAKING, IT CAUSED A CHAIN REACTION OF EVENTS. FIRST THE BRACKET BROCKET PUTTING THE PUMP AT A STEEP ANGLE N FORCING THE BELT TO GO OFF TRACK WHICH THEN CAUSED ALL THE OTHER ACCESSORIES TO BE DISABLED INCLUDING THE WATER PUMP WHICH OVERHEATED THE CAR. *TR

Oct 2, 2012 76,854 mi

I WAS DRIVING IN STOP AND GO TRAFFIC WHEN I NOTICED THE STEERING FELT A LITTLE STIFFER THAN USUAL. AFTER ABOUT 5 MILES AND BETTER FLOWING TRAFFIC I PULLED INTO A RESTAURANT FOR DINNER WHEN MY UPPER RADIATOR HOSE EXPLODED. I PULLED INTO A STALL AND OPENED THE HOOD TO INSPECT WHAT HAPPENED. THE HOSE WAS VERY APPARENT AND AFTER FURTHER INVESTIGATION I NOTICED THE POWER STEERING PUMPS PULLEY AT A VERY SHARP ANGLE COMPARED TO LINEAR WITH THE SERPENTINE BELT. I CAN ONLY ASSUME THAT FROM THE BRACKET ON THE PUMP BREAKING, IT CAUSED A CHAIN REACTION OF EVENTS. FIRST THE BRACKET BROCKET PUTTING THE PUMP AT A STEEP ANGLE N FORCING THE BELT TO GO OFF TRACK WHICH THEN CAUSED ALL THE OTHER ACCESSORIES TO BE DISABLED INCLUDING THE WATER PUMP WHICH OVERHEATED THE CAR. *TR

Mar 27, 2012 105,000 mi

MULTIPLE INSTANCES OF NO START. EVERY TIME THE CAR WAS TOWED TO A BMW SPECIALIST WHO OVER AND OVER AGAIN DIAGNOSED COMPLETELY DRAINED BATTERY, BUT CHARGING SYSTEM WAS OK. I HAVE JUST FOUND OUT THAT BMW HAS BEEN RECALLING 2003-2010 MODELS WITH THE EXACT SAME DEFECT. *TR

Mar 27, 2012 105,000 mi

MULTIPLE INSTANCES OF NO START. EVERY TIME THE CAR WAS TOWED TO A BMW SPECIALIST WHO OVER AND OVER AGAIN DIAGNOSED COMPLETELY DRAINED BATTERY, BUT CHARGING SYSTEM WAS OK. I HAVE JUST FOUND OUT THAT BMW HAS BEEN RECALLING 2003-2010 MODELS WITH THE EXACT SAME DEFECT. *TR

Mar 11, 2010 41,000 mi

APPARENT COMPUTER MALFUNCTION CAUSED WINDOWS TO FOG UP, CLOCK TO FAIL, DIRECTIONAL SIGNALS TO FAIL AND THE ENGINE TO REFUSE TO RESTART. ALSO, THE DASH DISPLAY AND BRAKE LIGHTS REMAINED ON EVEN WITH THE IGNITION KEY REMOVED. DISCONNECTING THE BATTERY, WAITING ABOUT ONE HOUR, RECONNECTING THE BATTERY RESTORED NORMAL OPERATION. *TR

Mar 11, 2010 41,000 mi

APPARENT COMPUTER MALFUNCTION CAUSED WINDOWS TO FOG UP, CLOCK TO FAIL, DIRECTIONAL SIGNALS TO FAIL AND THE ENGINE TO REFUSE TO RESTART. ALSO, THE DASH DISPLAY AND BRAKE LIGHTS REMAINED ON EVEN WITH THE IGNITION KEY REMOVED. DISCONNECTING THE BATTERY, WAITING ABOUT ONE HOUR, RECONNECTING THE BATTERY RESTORED NORMAL OPERATION. *TR