18
Complaints
0
Crashes
0
Fires
0
Deaths

This Problem Across All Years

All Engine And Engine Cooling Complaints

Showing 18 of 18
May 8, 2005 97,000 mi

NO WARNING OTHER THAN A SLIGHT ANIT-FREEZE SMELL. UPON CHECKING OUT THE ODOR, UPPER RADIATOR NECK BETWEEN HOSE CLAMP AND RADIATOR JUST BROKE OFF SPEWING SCALDING HOT FLUID EVERYWHERE. LUCKILY HOOD WAS NOT COMPLETELY OPEN AT THE TIME. RADIATOR NEEDED TO BE REPLACED, NOT REPAIRABLE. OLD PART TOSSED.

May 8, 2005 97,000 mi

NO WARNING OTHER THAN A SLIGHT ANIT-FREEZE SMELL. UPON CHECKING OUT THE ODOR, UPPER RADIATOR NECK BETWEEN HOSE CLAMP AND RADIATOR JUST BROKE OFF SPEWING SCALDING HOT FLUID EVERYWHERE. LUCKILY HOOD WAS NOT COMPLETELY OPEN AT THE TIME. RADIATOR NEEDED TO BE REPLACED, NOT REPAIRABLE. OLD PART TOSSED.

Apr 5, 2005 80,000 mi

LOW COOLANT MESSAGE CAME ON WHILE DRIVING. WITHIN A FEW MILES, RADIATOR CAP OVERPRESURED AND STEAM BURST OUT WHILE ON THE HIGHWAY. PULLED OVER AND WAS TOWED TO THE DEALER. REPLACED COOLANT HOSES. 4 MONTHS LATER, LOW COOLANT MESSAGE CAME ON AGAIN WHILE TRAVELING; STOPPED AT A SERVICE STATION TO CHECK LEVEL; LEVEL WAS VERY LOW, AND A SLOW LEAK WAS VISIBLE. REPLACED COOLANT RESERVOIR ASSEMBLY. 6 MOS LATER, CHECK ENGINE LIGHT CAME ON. DEALER REPLACED SENSOR. ONE WEEK LATER, THE LOW COOLANT MESSAGE CAME ON AGAIN (3RD TIME). COOLANT WAS LOW; TOOK TO DEALER FOR REPAIR. ALL WORK WAS AT OWNER'S EXPENSE (NON-WARRANTY).*AK

Apr 5, 2005 80,000 mi

LOW COOLANT MESSAGE CAME ON WHILE DRIVING. WITHIN A FEW MILES, RADIATOR CAP OVERPRESURED AND STEAM BURST OUT WHILE ON THE HIGHWAY. PULLED OVER AND WAS TOWED TO THE DEALER. REPLACED COOLANT HOSES. 4 MONTHS LATER, LOW COOLANT MESSAGE CAME ON AGAIN WHILE TRAVELING; STOPPED AT A SERVICE STATION TO CHECK LEVEL; LEVEL WAS VERY LOW, AND A SLOW LEAK WAS VISIBLE. REPLACED COOLANT RESERVOIR ASSEMBLY. 6 MOS LATER, CHECK ENGINE LIGHT CAME ON. DEALER REPLACED SENSOR. ONE WEEK LATER, THE LOW COOLANT MESSAGE CAME ON AGAIN (3RD TIME). COOLANT WAS LOW; TOOK TO DEALER FOR REPAIR. ALL WORK WAS AT OWNER'S EXPENSE (NON-WARRANTY).*AK

Apr 5, 2005 80,000 mi

LOW COOLANT MESSAGE CAME ON WHILE DRIVING. WITHIN A FEW MILES, RADIATOR CAP OVERPRESURED AND STEAM BURST OUT WHILE ON THE HIGHWAY. PULLED OVER AND WAS TOWED TO THE DEALER. REPLACED COOLANT HOSES. 4 MONTHS LATER, LOW COOLANT MESSAGE CAME ON AGAIN WHILE TRAVELING; STOPPED AT A SERVICE STATION TO CHECK LEVEL; LEVEL WAS VERY LOW, AND A SLOW LEAK WAS VISIBLE. REPLACED COOLANT RESERVOIR ASSEMBLY. 6 MOS LATER, CHECK ENGINE LIGHT CAME ON. DEALER REPLACED SENSOR. ONE WEEK LATER, THE LOW COOLANT MESSAGE CAME ON AGAIN (3RD TIME). COOLANT WAS LOW; TOOK TO DEALER FOR REPAIR. ALL WORK WAS AT OWNER'S EXPENSE (NON-WARRANTY).*AK

Apr 5, 2005 80,000 mi

LOW COOLANT MESSAGE CAME ON WHILE DRIVING. WITHIN A FEW MILES, RADIATOR CAP OVERPRESURED AND STEAM BURST OUT WHILE ON THE HIGHWAY. PULLED OVER AND WAS TOWED TO THE DEALER. REPLACED COOLANT HOSES. 4 MONTHS LATER, LOW COOLANT MESSAGE CAME ON AGAIN WHILE TRAVELING; STOPPED AT A SERVICE STATION TO CHECK LEVEL; LEVEL WAS VERY LOW, AND A SLOW LEAK WAS VISIBLE. REPLACED COOLANT RESERVOIR ASSEMBLY. 6 MOS LATER, CHECK ENGINE LIGHT CAME ON. DEALER REPLACED SENSOR. ONE WEEK LATER, THE LOW COOLANT MESSAGE CAME ON AGAIN (3RD TIME). COOLANT WAS LOW; TOOK TO DEALER FOR REPAIR. ALL WORK WAS AT OWNER'S EXPENSE (NON-WARRANTY).*AK

Oct 22, 2003 65,656 mi

FAULTY RADIATORS THAT HAVE A DESIGN FLAW THAT ALLOWS FOR THE RADIATOR NECK TO BREAK OFF WITHOUT NOTICE AND SPRAY HOT COOLANT EVERYWHERE. THIS PROBLEM IS WELL KNOWN JUST VISIT ROADFLY.ORG E38 MESSAGE BOARD AND SEARCH FOR "RADIATOR NECK." THIS TYPICALLY OCCURS BETWEEN 50,000-70,000 MILES. *LA

Oct 22, 2003 65,656 mi

FAULTY RADIATORS THAT HAVE A DESIGN FLAW THAT ALLOWS FOR THE RADIATOR NECK TO BREAK OFF WITHOUT NOTICE AND SPRAY HOT COOLANT EVERYWHERE. THIS PROBLEM IS WELL KNOWN JUST VISIT ROADFLY.ORG E38 MESSAGE BOARD AND SEARCH FOR "RADIATOR NECK." THIS TYPICALLY OCCURS BETWEEN 50,000-70,000 MILES. *LA

May 20, 2002

WHILE DRIVING ON A HIGWAY AND TAKING A TURN OVER A CURVED PORTION OF THE HIGHWAY I FOUND THE POWER IN THE STEERING WAS NOT FUNCTIONING AND THE STEERING WHEEL BECAME EXTREMELY HARD. WHE I TRIED TO BRAKE AND PULL TO THE SIDE THE BRAKE WAS ALSO QUITE HARD. THE CAR HAD THEN TO BE TOWED TO A BMW DEALERSHI, AND THE PROBLEM WAS DETECTED AND FIXED. I WAS INFORMED THAT THE WATER PUMP HAD FAILED WHICH RESULTED IN THE BELTS TO BREAK, CAUSING A LOSS OF POWER IN THE STEERING AND THE BRAKES. THIS WAS QUITE A DISTURBING EXPERIENCE WHIEL DRIVING THIS CAR ON A HIGWAY AND COULD HAVE CAUSED A MAJOR ACCIDENT. THE BMW 740 IL IS QUITE A HEAVY CAR AND WITHOUT POWER IN THE STEERING AND THE BRAKES IT IS VERY DIFFICULT TO CONTROL THE CAR AT HIGHWAY SPEEDS. THE POWER SYSTEM FAILING DUE TO WATER PUMP FAILURE APPEARS TO BE OF SERIOUS CONCERN IN A VEHICLE THAT IS ADVERTISED AS ONE OF THE MARVELS OF ENGINEERING. THE CAR IS STILL UNDER WARRANTY. *AK

May 20, 2002

WHILE DRIVING ON A HIGWAY AND TAKING A TURN OVER A CURVED PORTION OF THE HIGHWAY I FOUND THE POWER IN THE STEERING WAS NOT FUNCTIONING AND THE STEERING WHEEL BECAME EXTREMELY HARD. WHE I TRIED TO BRAKE AND PULL TO THE SIDE THE BRAKE WAS ALSO QUITE HARD. THE CAR HAD THEN TO BE TOWED TO A BMW DEALERSHI, AND THE PROBLEM WAS DETECTED AND FIXED. I WAS INFORMED THAT THE WATER PUMP HAD FAILED WHICH RESULTED IN THE BELTS TO BREAK, CAUSING A LOSS OF POWER IN THE STEERING AND THE BRAKES. THIS WAS QUITE A DISTURBING EXPERIENCE WHIEL DRIVING THIS CAR ON A HIGWAY AND COULD HAVE CAUSED A MAJOR ACCIDENT. THE BMW 740 IL IS QUITE A HEAVY CAR AND WITHOUT POWER IN THE STEERING AND THE BRAKES IT IS VERY DIFFICULT TO CONTROL THE CAR AT HIGHWAY SPEEDS. THE POWER SYSTEM FAILING DUE TO WATER PUMP FAILURE APPEARS TO BE OF SERIOUS CONCERN IN A VEHICLE THAT IS ADVERTISED AS ONE OF THE MARVELS OF ENGINEERING. THE CAR IS STILL UNDER WARRANTY. *AK

Apr 28, 2002

RADIATOR BLEW AT 70MPH ON THE FREEWAY. THIS IS A KNOWN PROBLEM WITH THIS MODEL AND BMW NOTH AMERICA REFUSES TO ADMIT THERE IS A PROBLEM. LUCKILY NO INJURIES WERE CAUSED, BUT EASILY COULD HAVE AS THE ENTIRE ENGINE BAY WAS SPRAYED WITH HOT COOLANT. ANTIFREEZE ALSO SPRAYED DOWN SIDE OF VEHICLE. *AK

Apr 28, 2002

RADIATOR BLEW AT 70MPH ON THE FREEWAY. THIS IS A KNOWN PROBLEM WITH THIS MODEL AND BMW NOTH AMERICA REFUSES TO ADMIT THERE IS A PROBLEM. LUCKILY NO INJURIES WERE CAUSED, BUT EASILY COULD HAVE AS THE ENTIRE ENGINE BAY WAS SPRAYED WITH HOT COOLANT. ANTIFREEZE ALSO SPRAYED DOWN SIDE OF VEHICLE. *AK

Nov 29, 2000

LIGHTS DIMMED AND VEHICLE ALMOST STALLED AT IDLE, DEALER REPLACED CATALYTIC CONVERTER. *SLC

Nov 29, 2000

THERMOSTAT WAS REPLACED. *SLC

Nov 29, 2000

LIGHTS DIMMED AND VEHICLE ALMOST STALLED AT IDLE, DEALER REPLACED CATALYTIC CONVERTER. *SLC

Nov 29, 2000

THERMOSTAT WAS REPLACED. *SLC

Oct 21, 1999

VEHICLE STALLED FOR NO REASON WHILE DRIVING APPROXIMATELY 70 MPH. HAPPENED ONCE BEFORE. TOOK TO DEALER, HAD ENTIRE COMPUTER SYSTEM REPLACED. *AK

Oct 21, 1999

VEHICLE STALLED FOR NO REASON WHILE DRIVING APPROXIMATELY 70 MPH. HAPPENED ONCE BEFORE. TOOK TO DEALER, HAD ENTIRE COMPUTER SYSTEM REPLACED. *AK