2009 BUICK ENCLAVE Power Train Problems

33 complaints about Power Train

33
Complaints
0
Crashes
0
Fires
0
Deaths

This Problem Across All Years

All Power Train Complaints (33)

Mar 10, 2023

The contact owns a 2009 Buick Enclave. The contact stated that the rear driver’s side and center seat belt failed to latch securely. The vehicle was taken to an independent mechanic where it was diagnosed but no failure could be determined. could not be determined. The contact then stated that on another occasion, while driving at an undisclosed speed, the gear shifter failed to operate in drive(D). The contact stated that the shifter was stuck in drive (Low). As a result, while the accelerator pedal was depressed, the vehicle failed to exceed 30 MPH. Additionally, the contact stated that on multiple occasions, the instrument panel digital display failed to illuminate, and the contact was unable to state whether there were any warning lights illuminated. The vehicle was taken to an independent mechanic where the instrument panel light bulb was replaced; however, the failure recurred. The vehicle was not repaired. Neither the dealer nor the manufacturer was notified of the failure. The failure mileage was approximately 150,000.

Mileage: 150,000

May 16, 2021

MY WIFE TOOK A TRIP TO SPRINGFIELD ILL. FROM PARIS MO. ON 5/5/21 SHE DROVE APPOX 50 MILES TOWARD SPRINGFIELD ON I72 E.HER TACHOMETER STARTED SHOOTING UP ABOUT 5-6 THOUSAND RPM AT 70MPH .HOT TRANSMISSION LIGHT CAME ON.I TOLD HER TO STOP AN LET IT COOL.THE LIGHT WENT OFF AND SHE PUT IT IN GEAR ONLY TO FIND SHE ONLY HAD LOW GEAR.WE TOOK IT TO S & K BUICK IN SPRINGFIELD ILL. WHERE THEY DIAGNOSED IT . THE WAVE PLATE IN THE TRANSMISSION HAD EXPLODED.WHEN WE EXPLAINED THIS VEHICLE ONLY HAS 52,000 MILES THEY OR GM WOULD DO NOTHING FOR US.WE FIND THAT RIDICULOUS.THEY ONLY USED THAT TRANSMISSION FOR 2 YEARS AND ABRUPTLY STOPPED USING IT.WE HAVE READ OF MANY OF THESE WITH THE SAME ISSUE ON THE INTERNET SITES. KNOW THEY WANT US TO PAY NEARLY $5000.00 TO REPLACE TRANSMISSION.ONCE AGAIN THIS VEHICLE ONLY HAS 52,000 ORIGINAL MILES IS GARAGE KEPT AND IS PAMPERED .THIS IN OUR MIND SHOULD BE A RECALL AND THEY SHOULD HAVE SOME RESPONSIBITY IN THIS ISSUE AT GENERAL MOTORS.ANY HELP WOULD BE APPRECIATED.ALSO WEDNESDAY 5/19/2021 THE DEALER WILL HAVE HAD THIS VEHICLE 2 WEEKS.ANOTHER JOKE.

Mileage: 52,000

Sep 23, 2020

TL* THE CONTACT OWNS A 2009 BUICK ENCLAVE. THE CONTACT STATED THAT UPON PLACING THE GEAR SHIFTER INTO PARK, THE VEHICLE REVERTED TO NEUTRAL WITH THE CIRCUIT RELAY WARNING MESSAGE DISPLAYED ON THE INSTRUMENT PANEL. DUE TO THE FAILURE, THE CONTACT WAS UNABLE TO REMOVE THE KEY FROM THE IGNITION AND WAS UNABLE TO RESTART THE VEHICLE. SHE ALSO MENTIONED THAT THE VEHICLE BEGAN TO ROLL AWAY AS THE FAILURE OCCURRED. THE CONTACT APPLIED THE PARKING BRAKE TO STOP THE VEHICLE. UPON INVESTIGATION, THE CONTACT LINKED THE FAILURE TO NHTSA CAMPAIGN NUMBER: 09V073000 (POWER TRAIN) HOWEVER, THE VEHICLE WAS NOT INCLUDED IN THE RECALL. NEITHER THE DEALER NOR THE MANUFACTURER HAD BEEN NOTIFIED OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS UNKNOWN.

Oct 21, 2019

TL* THE CONTACT OWNS A 2009 BUICK ENCLAVE. WHILE DRIVING 50 MPH, THE VEHICLE STARTED TO JERK, THE GEARS SLIPPED, THE RPMS INCREASED, THE VEHICLE FAILED TO ACCELERATE, AND THE CHECK ENGINE WARNING INDICATOR ILLUMINATED. THE CONTACT COASTED THE VEHICLE TO THE SIDE OF THE ROAD AND POWERED OFF THE ENGINE. THE VEHICLE WAS RESTARTED, BUT THE FAILURE RECURRED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE TRANSMISSION FAILED AFTER HAVING THE VEHICLE FOR 9 MONTHS AND NEEDED TO BE REPLACED. THE VEHICLE WAS NOT TAKEN TO A DEALER AND WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 100,000.*DT*JB

Mileage: 100,000

Mar 29, 2019

WE PURCHASED A 2009 GMC BUICK ENCLAVE FROM GILLIE HYDE USED CARS IN GLASGOW, KY ON 3-15-19. IMMEDIATELY UPON DRIVING THE VEHICLE HOME, WE NOTED THAT THE VEHICLE SHOOK WHEN ACCELERATING. WE IMMEDIATELY TOOK TO OUR MECHANIC WHO NOTED THE TRANSMISSION ISSUE AND WE RESEARCHED THE VEHICLE AND FOUND THAT THERE WAS A RECALL ON THE VEHICLE WITH AN EXTENDED WARRANTY TO THE TRANSMISSION AS WELL AS THE TIMING AS WELL AS THE REAR TAILGATE FALLING AFTER AUTOMATICALLY OPENING. NONE OF THESE ITEMS WERE LISTED. HTTPS://WWW.CONSUMERREPORTS.ORG/CARS/BUICK/ENCLAVE/2009/RELIABILITY#RECALLS THE RECALLS WERE NOT NOTED ON THE CARFAX PROVIDED BY THE DEALERSHIP. WE FEEL AS THOUGH WE HAVE BEEN MISLEAD AND COMPLETELY LIED TO ABOUT THIS VEHICLE. THE VEHICLE SHAKES BAD. WE HAD TRANSMISSION FLUID CHANGED, OIL CHANGED AND STILL SHAKES. GM KNEW OF THE SHAKING RESULTING FROM THE TIMING CHAIN STRETCHING AND OUR DEALER DID NOT INFORM US OF THIS (EVEN WHEN THEY HAD ANOTHER ENCLAVE ON THE LOT WITH THIS ISSUE AND TOLD US NOT TO BUY IT). GM CONTINUED TO MANUFACTURE THIS ENGINE AND FINALLY ISSUED AN EXTENDED WARRANTY: IN NOVEMBER 2012, GM RELEASED A SPECIAL COVERAGE ADJUSTMENT (#11340C) FOR TIMING CHAIN WEAR IN 2.8L AND 3.6L V6 ENGINES (LP1/LY7/LLT).

Mileage: 150,458

Sep 23, 2018

WAS DRIVING ON RAMP TO ENTER HIGHWAY, WITH MY THREE 6 AND YOUNGER CHILDREN, AND ALSO 7 MONTHS PREGNANT! THE ENCLAVE JUST STALLED AND STILL CAN NOT START BUT ONE TIME IT DID, BUT IT SOUNDED LIKE IT WAS GOING TO BLOW UP MAKING WEIRD NOISES SO I SHUT IT OFF RIGHT AWAY. I HAVE BEEN RESEARCHING THIS AND I SEE IT IS VERY COMMON WITH 2009 & 2010 ENCLAVES. I DON'T UNDERSTAND WHY NOTHING HAS BEEN DONE? IF THIS HAPPENED SHORTLY LATER I WOULD HAVE BEEN ON THE HIGHWAY AND SEVERAL PEOPLE COULD BE INVOLVED GETTING HURT OR KILLED. I HAVE HAD IT LESS THAN A YEAR, WITH LESS THAN 104,000 MILES ON IT. ALSO HAS WHEEL BEARING ISSUES WHICH I REPLACED FRONT NOW THE REAR ONES NEED TO BE DONE. WHAT IS UP WITH THIS NEGLECT AND NO ONE TO ASSIST US CONSUMERS UNTIL SOMEONE GETS SERIOUSLY HURT OR KILLED! NOW THE VEHICLE IS SITTING AT A GARAGE WHERE TOWED WAITING FOR REPORT AND I HAVE NO VEHICLE SO LOST MY JOB I HAVE FOUR KIDS TO SUPPORT. FIGURED I BUY A NEWER DECENT VEHICLE TO BE DEPENDABLE & RELIABLE ONLY TO FIND OUT IT'S NEITHER ONLY UNSAFE FOR MY FAMILY.

Mileage: 103,926

Sep 21, 2018

DRIVING ON THE HIGHWAY THE RPMS STARTED RACING AND IT FELT LIKE THE TRANSMISSION WAS SLIPPING. WE STARTED LOSING POWER AND EVENTUALLY THE CAR WOULD NOT SHIFT OUT OF FIRST GEAR. CARMAX HAD A DEALERSHIP REPAIR THE TRANSMISSION. WE DON'T USE THIS VEHICLE OFTEN SO WHEN WE DRIVE IT SEVERAL MONTHS LATER IT SEEMED FINE INITIALLY THEN AFTER DRIVING IT A LITTLE MORE WE STARTED HAVING THE ENGINE LIGHT COME ON AND GETTING SEVERAL FAULT CODES AND VERY ROUGH SHIFTING AT LOWER SPEEDS 30-35 MPH. IN THE PROCESS OF TRYING TO GET THE ISSUE FIXED AGAIN.

Mileage: 92,000

Apr 11, 2018

WHEN DRIVING ON HIGHWAY BETWEEN 70 AND 75 MPH THE TRANSMISSION STARTS SLIPPING AND RPM JUMPS UP TO 4500. ALSO ENCOUNTER THE SAME PROBLEM ON LOCAL STREET DRIVING BETWEEN 30 AND 40 MPH, TRANSMISSION STARTS SLIPPING AND RPM RACES FROM ABOUT 1500 TO 2800. TOOK THE VEHICLE TO LOCAL BUICK DEALER. THEY STATED THERE IS RECALL ON THE TRANSMISSION FOR THAT YEAR BUT NOT THIS PARTICULAR VIN. THIS IS DANGEROUS AS THE LOSS IN POWER ALMOST RESULTED IN ME BEING REAR ENDED A COUPLE OF TIMES.

Mileage: 83,500

Dec 19, 2017

TL* THE CONTACT OWNS A 2009 BUICK ENCLAVE. AFTER THE VEHICLE WAS PLACED IN PARK, THE CONTACT EXITED THE VEHICLE AND HEARD AN ABNORMAL NOISE. THE VEHICLE ROLLED BACK TOWARDS THE WOODS. THE CONTACT CALLED SOUTHTOWNE CHEVROLET (695 BULLSBORO DR, NEWNAN, GA 30265) AND WAS INFORMED OF A RECALL. THE VEHICLE WAS TOWED TO SOUTHTOWNE CHEVROLET WHERE IT WAS DIAGNOSED THAT THE GEAR SHIFTER NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS UNKNOWN.

Sep 10, 2017

CAR SHUDDERS AND HAS PROBLEMS ACCELERATING WHEN GEARS SHIFTS. DIAGNOSIS=REPLACE BANK 1 CAMSHAFT ACTUATOR WORN TIMING CHAINS, REPLACE ALL SPARK PLUGS AND 3 IGNITION COILS AGAIN. (PERFORMED PFI SYSTEM DIA TEST. CODES FIRED P0017 AND P0300 STORED. CORRELATION AND MISFIRE COES).

Mileage: 135,000

Sep 8, 2017

HARD SHIFTING NOTED IN GEARS. CAR ACTS LIKE IT'S IN NEUTRAL WHEN IN REVERSE. BUICK DEALERSHIP SAYS THE WAVE PLATE IS DEFECT. OTHER 09 BUICK ENCLAVES ARE COVERED BY SPECIALTY POLICY. 14404 A. BUT NOT MY VIN VIN. SAME MAKE MODEL AND TRANSMISSION. I WAS TOLD BY GMC CUSTOMER SERVICE TO COMPLAIN HERE.

Mileage: 104,000

Aug 11, 2017

DRIVING ON A FREEWAY SPEED POSTED 80MPH, 2009 BUICK ENCLAVE RPM'S BEGAN TO SHOOT FROM 2000 RPM TO 5000RPM WHEN PUSHING ON ACCELERATOR. FORWARD MOVEMENT CONTINUED FOR SHORT DISTANCE AT 2000 RPM. TRAFFIC WAS MERGING TO ONE LEFT LANE FOR CONSTRUCTION ON A BRIDGE. PULLED OFF TO THE RIGHT AND STOPPED. BEFORE ENTERING ONE LANE OF TRAFFIC OVER BRIDGE. AFTER PUTTING CAR IN PARK, I TRIED TO MOVE FORWARD IN DRIVE AND THEN REVERSE. THE TRANSMISSION WAS COMPLETELY GONE. IF I HAD ENTERED THAT BRIDGE WITH TRAFFIC PUSHED INTO ONE LANE IT COULD HAVE BEEN A DISASTER. CARS WERE ENTERING THAT BRIDGE AT AT LEAST 70 MPH. I FEEL THIS IS A VERY DANGEROUS SITUATION AND SEE THAT GM HAS EXTENDED THE WARRANTY ON THESE VEHICLE TRANSMISSIONS TO 120,000 MILES. I HAVE OWNED THE CAR SINCE 30 ,000 MILES AND HAVE BEEN THE ONLY DRIVER. I AM 68 YEARS OLD AND HAVE NEVER TOWED ANYTHING WITH IT. I BABY A CAR. THIS PART FAILURE IS VERY DANGEROUS. IF I HAD NOT PULLED OFF, I WOULD HAVE PUT MYSELF AND MANY OTHER MOTORISTS IN DANGER.

Mileage: 138,000

Apr 12, 2017

TL* THE CONTACT OWNS A 2009 BUICK ENCLAVE. WHILE DRIVING 45 MPH, THE VEHICLE HESITATED, JERKED, AND FAILED TO ACCELERATE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE #1 CYLINDER MISFIRED AND THE PLUGS AND PCV VALVES WERE REPLACED. THE MECHANIC THEN TOOK THE VEHICLE FOR A TEST DRIVE AND DIAGNOSED THAT THE TRANSMISSION FAILED AND THE VEHICLE COULD NO LONGER BE SHIFTED INTO RESERVE, THIRD GEAR, OR SIXTH GEAR. IT WAS DIAGNOSED THAT THE TRANSMISSION WAVE PLATE FAILED AND NEEDED TO BE REPAIRED OR REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER STATED THAT THERE WERE NO OPEN RECALLS. THE APPROXIMATE FAILURE MILEAGE WAS 130,000.

Mileage: 130,000

Dec 2, 2016

WHEN IN REVERSE, THE VEHICLE WILL STILL ROLL FORWARD ON A DECLINE AND WHEN DRIVE, IT ROLLS BACKWARDS WHEN ON AN INCLINE. IT ACTS AS A STICK SHIFT. I WAS GOING UP AN INCLINE COMING OUT OF A PARKING LOT AND STOPPED. WHEN I TOOK MY FOOT OFF OF THE BRAKE TO GO, THE CAR ROLLED BACKWARDS AND ALMOST HIT THE CAR BEHIND ME. I PULLED INTO MY DRIVEWAY AND TOOK MY FOOT OFF OF THE BRAKE AND IT ROLLED TWO LENGTHS BEFORE I PUT ON THE BRAKE TO STOP IT FROM GOING IN THE STREET. WHILE REVERSING INTO MY INCLINED DRIVEWAY, IF I DON'T KEEP MY FOOT ON THE GAS TO CONTROL MOMENTUM OR IT WILL ROLL FORWARD.

Mileage: 99,000

Aug 25, 2016

HAVE ISSUES WITH VEHICLE IDLING AND THE CAR JUMPS AT THE POINT OF SWITCHING GEARS. WHEN DRIVING ON THE EXPRESSWAY THE CAR GOES ABOVE 50 HESITANTLY.

Mileage: 110,000

Apr 19, 2016

CAR LOST POWER STEERING AT LOW SPEED WHEN MAKING TURNS.

Mileage: 90,595

Jan 6, 2016

STABILITRAC LIGHT ON. FOUND THE MASTER CYLINDER LEAKING INTO BRAKE BOOSTER AND REPLACED. THE FRONT MOTOR MOUNT WAS ALSO BROKEN.

Mileage: 96,207

Jan 6, 2016

CHECK ENGINE LIGHT ON WITH REDUCED ENGINE POWER MESSAGE. ALSO DISPLAY AC OFF MESSAGE AND OVERHEAT MESSAGE. VEHICLE TOWED. PRESSURE TESTED SYSTEM FOUND WATER PUMP LEAKING. REMOVED AND REPLACED WATER PUMP. FRONT TIMING COVER LEAKING. REMOVED FRONT ENGINE COVER AND RESEALED. FOUND BOTH FRONT STRUTS LEAKING. REMOVED AND REPLACED FRONT STRUTS.

Mileage: 115,699

Jan 6, 2016

CAR SPUDDERING ON ACCELERATION AND INCLINES. CHECK ENGINE LIGHT ON. NEEDS ALL SPARK PLUGS AND COILS REPLACED AGAIN. CODES P0300, P0302, P0303 STORED. MISS FIRE ON 2 AND 3 CYCLINDERS. ALSO, NEEDS REPLACE LINE AND RECHARGE SYSTEM AS AC DISCHARGE LINE IS LEAKING.

Mileage: 116,210

Jul 16, 2015

DRIVING ON INTERSTATE 75 NORTH OF CINCINNATI OH IN BUMPER TO BUMPER TRAFFIC ON 7-13-15 IN LEFT LANE WHEN BUZZER SOUNDED ,TRACTION CONTROL LIGHT CAME ON AND ENGINE LOST POWER. TRYING TO GET TO SHOULDER WAS A BAD EXPERIENCE AS TRAFFIC WAS HAVING ONE HELL OF A TIME TRYING TO COPE WITH A CAR THAT SUDDENLY WASN'T MOVING. HOW A BAD ACCIDENT DIDN'T HAPPEN, I JUST SAY IT WAS GOOD LUCK! WE REALLY LIKE OUR BUICK ENCLAVE AND WOULD LIKE TO KEEP IT. I HAVE A CODE READER AND NO CODE WAS REVEALED. I PUSHED THE TRACTION CONTROL BUTTON SEVERAL TIMES AND REENTERED TRAFFIC AND THE CAR RAN FINE FOR THE NEXT TWO HOURS TO HOME......

Mileage: 72,000

Jun 30, 2015

I HAD TAKEN THE CAR TO BUICK DEALER FOR AN OIL CHANGE. I ASKED THEM TO CHECK IF THEY SAW A POSSIBLE OIL LEAK BECAUSE I SAW A FEW SPOTS IN THE GARAGE. THEY SAID THERE WAS A LEAK FROM A RUBBER BEARING AND THE COST TO FIX THAT WAS 2700. TOOL THE CAR SEARS TO HAVE THEM DOUBLE CHECK. SEARS SAID THERE WAS NOT LEAK. THERE WAS RESIDUAL OIL FROM OIL CHANGE. THIS WAS ON 06/20. CHECKED EVERY DAY AFTER THAT TO SEE IF THE OIL LEAKED AGAIN AND IT DID NOT. ON 06/28, WHILE COMING HOME WITH MY KIDS, HEAR SUDDEN NOISE, AND IN A FEW SECONDS SMOKE COMING OUT FROM LEFT FRONT SIDE OF THE CAR...LOT OF SMOKE. GOT THE KIDS AND DOG OUT SAFELY. TRIED TO TURN OFF THE CAR...I HAD THE KEY OUT BUT THE CAR WAS STILL ON. IT JUST WOULD NOT TURN OFF. TRIED TAKING IT OUR OF THE GARAGE AND THE STEERING WOULD NOT TURN. SOMEHOW GOT THE CAR ON THE CURB AND AFTER TRYING A FEW TIME, THE CAR DID TURN OFF. NOTICED ALL THE COOLANT HAD FLUSHED ON THE FLOOR. GOT IT TOWED TO THE DEALER. DEALER SAID POWER STEERING GEAR AND POWER STEERING PUMP BURNED AND NEEDS REPLACEMENT. ALSO SAID IT WAS BECAUSE OF A MINOR OIL LEAK THAT WAS UNDER THE ENGINE THAT CAUSED IT. COOLANT FLUSHING WAS COVERED AND GM WILL PAY FOR THE FIX BUT I WILL NEED TO PAY 2500 FOR THE STEERING GEAR AND PUMP REPLACEMENT. THIS COULD HAVE BEEN A DISASTER AND LIFE THREATENING IF IT HAD HAPPENED AT HIGH SPEED. GM LEAST CONCERNED ABOUT IT AND NOT SUPPORTIVE OR STANDING BEHIND THEIR CARS. I HAVE ONLY 36K MILES ON IT AND WOULD NOT HAVE EXPECTED SOMETHING LIKE THIS. I READ ON SOME FORUMS WHERE A LOT OF PEOPLE HAVE HAD SIMILAR ISSUES. FOR THE SAFETY OF OTHER BUICK ENCLAVE HOLDERS, I PLEASE REQUEST YOU TO HAVE BUICK ACT ON THIS AND SEND A RECALL.

Mileage: 36,650

Jun 23, 2015

TL* THE CONTACT OWNS A 2009 BUICK ENCLAVE. WHILE DRIVING 40 MPH, THE VEHICLE FAILED TO SHIFT INTO FOURTH OR FIFTH GEAR. THE VEHICLE WAS TAKEN TO THE DEALER, BUT WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 91,000. MA 10/19/2015 UPDATED 10/26/2017*CN

Mileage: 91,000

Apr 13, 2015

WHILE DRIVING,VEHICLE MISSES OCCASIONALLY,ENGINE LIGHT BLINKS AND TRANSMISSION HAS A HARD TIME SHIFTING,THEN WILL RUN FINE FOR A FEW MINUTES AND DO IT AGAIN,THIS HAPPENS DAILY AND EVERY FEW MINUTES. *TR

Mileage: 88,000

Mar 20, 2015

MY DEALERSHIP IDENTIFIED A SIGNIFICANT PROBLEM WITH THE POWER STEERING GEAR ON MY VEHICLE THAT CONSTITUTED A SIGNIFICANT SAFETY ISSUE. HAD IT NOT BEEN CAUGHT, MY POWER STEERING INEVITABLE WOULD HAVE FAILED WHILE DRIVING AND RESULTED IN A CRASH. I WAS ALSO ADVISED BY THE DEALER AND HAVE LEARNED THROUGH RESEARCH THAT THIS IS A VERY COMMON PROBLEM AFFECTING BUICK ENCLAVES AND OTHER SIMILAR GM SUVS AND CROSSOVERS. THE REPAIR WORK TO CORRECT THIS MANUFACTURER DEFECT IS OVER $1500 AND CONVENIENTLY NOT COVERED BY WARRANTY. THIS IS A SIGNIFICANT AND UNACCEPTABLE ISSUE AND SHOULD RESULT IN A RECALL OF ALL AFFECTED VEHICLES AND REIMBURSEMENT OF REPAIR COSTS TO AFFECTED OWNERS. *TR

Mileage: 69,952

Mar 10, 2015

NO SOUND, JUST QUIT WHEN I TRIED TO INCREASE SPEED. ONTO HIGHWAY I.HAD TO PULL OVER AND WENT SLOWLY INTO GARAGE. THE CAR HAS COMPLETE TRANSMISSION FAILURE, BAD BEARING ON TRANSFER CASE SHAFT, WHICH IS LEADING TO 7 THOUSAND DOLLARS IN REPAIRS. I TAKE GREAT CARE OF MY CARS AND AM VERY DISAPPOINTED IN THE PERFORMANCE OF THIS VEHICLE. I AM SURPRISED THERE ARE NO RECALLS. WHY WOULD A TRANSMISSION FAIL AT THIS MILEAGE? I AM LOOKING AT ANOTHER CAR MANUFACTURER FOR MY NEXT VEHICLE. I HAVE ALWAYS PURCHASED GM PRODUCTS. *TR

Mileage: 140,000

Dec 1, 2014

IN AUGUST OF 2014, AROUND 60K MILES, I NOTICED A MOAN WHEN I STEERED AS WELL AS A "KNOCK" THAT I HAD HEARD PREVIOUSLY AND TAKEN INTO THE DEALERSHIP UNDER WARRANTY (THEY SAID IT WAS A TIRE ROD; CLEARLY IT WAS NOT). I WAS AWARE THE MOAN MAY BE MY POWER STEERING PUMP, SO I BROUGHT IT IN FOR DIAGNOSTIC APPOINTMENT TO A LOCAL REPAIR SHOP. NOT ONLY DID I FIND MY POWER STEERING PUMP NEEDED REPLACEMENT, BUT THAT WAS THE CAUSE AND EFFECT OF A MUCH LARGE ISSUE- MY STEERING RACK WAS LOOSE, AND WAS DISENGAGING FROM THE MOUNT, WHICH IN TURN, CAUSED THE CORRUPTION OF MY POWER STEERING PUMP. I WAS TOLD IT WAS WORSENING VERY QUICKLY AND IF I LOST MY STEERING RACK FROM THE MOUNT, I COULD LOSE STEERING, WHICH COULD RESULT IN A CRASH. I WAS INFORMED THIS TYPE OF REPAIR IS HIGHLY UNUSUAL FOR A CAR THIS NEW, WITH NO ACCIDENT HISTORY, AND OTHERWISE IN EXCELLENT CONDITION, AND IS LIKELY AN "ENGINEERING ISSUE." I AM APPALLED AT NOT ONLY THE PRICE OF THESE REPAIRS WHICH I PAID OUT OF POCKET ($1,968.51), BUT AFTER SOME RESEARCH, HOW COMMON THIS PARTICULAR PROBLEM IS WITH 2008 & 2009 BUICK ENCLAVES, ESPECIALLY AROUND 60K MILES. THE MILEAGE ON MY VEHICLE NOW IS 65,342. *JS

Mileage: 45,000

Nov 11, 2014

PURCHASED A 2009 BUICK ENCLAVE IN SEPTEMBER 2014 WITH 49013, I DROVE IT TO GEORGIA OCTOBER AND NOTICED ON THE TRIP THAT THE VEHICLE WOULD ROLL BACK WHILE IN DRIVE ON AN INCLINE, BOTH FORWARD WHILE IN REVERSE AND BACKWARD WHILE IN DRIVE. AFTER RETURNING I SCHEDULED AN APPOINTMENT WITH MY DEALER ABOUT THE PROBLEM AND WAS INFORMED THAT THE ROLL BACK WAS NORMAL, I HAVE DRIVEN MANY VEHICLES WITH AUTOMATIC TRANSMISSIONS AND HAVE NEVER ENCOUNTERED THIS PROBLEM. I CHECKED ON LINE AND FOUND MANY COMPLAINTS ABOUT THIS FROM 2009 TO 2011, I BELIEVE THEY CORRECTED THE PROBLEM IN 2012. I FEEL THIS IS A MAJOR SAFETY PROBLEM AND SHOULD BE CORRECTED BEFORE SOMEONE GETS HURT OR KILLED. ARE THEY GOING TO LET THIS SAFETY HAZARD CONTINUE LIKE THEY LET THE IGNITION SWITCH PROBLEM WITH GENERAL MOTORS VEHICLES CONTINUE UNTIL PEOPLE WERE INJURED AND KILLED. I HAVE READ THAT IF THEY FIX THE PROBLEM IT WOULD INCREASE THE FUEL CONSUMPTION, I WOULD RATHER HAVE A SAFE AUTOMOBILE THAT GET A LITTLE LESS MILES PER GALLON THEN AN UNSAFE CAR THAT COULD END UP KILLING SOMEONE. THIS PROBLEM SHOULD BE CONVEYED TO PEOPLE WHO ARE LOOKING TO PURCHASE A BUICK ENCLAVE WITH THIS DEFECT SO THEY CAN DECIDE IF THEY WANT TO DRIVE A UNSAFE VEHICLE. I BELIEVE MOST OF THESE PROBLEMS BEGAN RIGHT AFTER THE BAILOUTS BY THE GOVERNMENT, COULD IT BE GENERAL MOTORS DECIDED TO CUT BACK ON SAFETY FEATURES ON ITS VEHICLES IN ORDER TO REGAIN THEIR PROFITABILITY IN THE CAR MARKET AND MAKE THEM LOOK GOOD. *TR

Mileage: 52,000

Nov 4, 2014

BATTERY WAS COMPLETELY DEAD. ELECTRICAL SYSTEM WAS SHORTED. INSTALLED NEW BATTERY. VEHICLE STARTED BUT WOULD NOT SHUT OFF EVEN WITH KEY REMOVED. CHECK ENGINE LIGHT STAYED ON AND WOULD NOT GO OFF EVEN WITH KEY REMOVED. FOUND WATER LEAKED INTO DASH. CHECKING INTERNET BROUGHT OTHER REPORTS OF OTHER POSSIBLE WATER LEAKS. *TR

Mileage: 68,140

Jul 29, 2014

IN THE PAST I HAD JERKING OR SLIPPING OF TRANSMISSION AT APPROXIMATELY 40 MILES AN HOUR, OR THE ENGINE WAS HAVING A COIL MISS FIRE. I HAD 3 NEW COILS INSTALLED BY DEALER UNDER WARRANTY WITH SIMILAR PROBLEMS BEFORE. TOOK TO DEALER AND THEY COULD NOT DETERMINE IF TRANSMISSION WAS SLIPPING OR ENGINE MISS FIRING, BUT NO CODE ON MISS FIRING ENGINE. SLIPPING OR HESITATING OF TRANSMISSION IS MORE LIKELY BUT CAN NOT DETERMINE SINCE DOES NOT ACT THE SAME CONSISTENTLY. STEERING NOISE STARTED IN THE WINTER APPROXIMATELY NOVEMBER 2013, BUT OFF AND ON SINCE; STEERING SEEMS A LITTLE STIFF BUT NOT FAILING YET LIKE SO MANY OTHER COMPLAINTS I HAVE READ ABOUT HERE. I WAS CHARGED $342.81 FOR DIRTY THROTTLE BODY AND OIL IN THE AIR DUST TUBE WHICH MIGHT CAUSE MISFIRE, THEY CLEANED AND REPLACED BANK 2 VALUE COVER AND CLEARED CODES, PERFORMED IDLE LEAN RESET. THIS DID NOT FIX PROBLEM ON 05/19/2014. I RETURNED ON 06/10/14 AND LEFT CAR TILL 06/11/14 THE DEALER LET ME USE A LOANER OVER NIGHT. THE DEALER SAID STUMBLE/MISFIRE AT TIMES WAS NOT ACTING UP ENOUGH TO DIAGNOSE. I HAD THE CARS AUTOMATIC TRANSMISSION FLUSH SERVICE ON 02/26/14 AND THERE WAS NO PROBLEM AT THAT TIME. IN THE COURSE OF OWNING THIS VEHICLE I HAD 3 COILS REPLACED WITH PROBLEMS STARTING 01/05/10 ONE COIL, SECOND COIL ON 08/11/10. THIRD COIL SHORTLY THEREAFTER, THIS IS AFTER COMPLAINING SINCE 12/02/2009 ABOUT ENGINE SHUDDER. THE MISFIRE/STUMBLE IS STILL HAPPENING ABOUT 40 MPH AND SOMETIMES AROUND 20MPH IF YOU ARE SLOW GOING BUT NOT ON A PULL OR ACCELERATING. WE LOVE THE CAR, BUT THE PROBLEMS ARE GETTING EXPENSIVE AND THE WORRY OF WHAT ELSE CAN GO WRONG IS STRESSFUL. I DID NOT MENTION THE WARRANTY REPAIRS OF WATER PUMP GOING OUT FRONT MOTOR MOUNT FAILURE, SHIFT LEVER, AIRBAGS, SEAT BELTS, LEFT OUT REMOTE MIRROR FAILURE, ENGINE AND TRANSMISSION CODE UPDATES. DEALER SEEM OK, SO GM CAN NOT FIX OR WILL NOT DUE TO COST. *JS

Mileage: 67,878

Jul 28, 2014

WHILE STOPPING FOR A TRAFFIC SIGNAL ON A SLIGHT INCLINE THE VEHICLE BEGAN TO ROLL BACKWARD. THE ENGINE WOULD NOT HOLD EVEN FOR THE AMOUNT OF TIME TO MOVE MY FOOT ONTO THE BRAKE. VEHICLE ROLLED BACKWARDS APPROXIMATELY 1-2 FEET IN PROCESS DUE TO WEIGHT OF AUTO AND INABILITY FOR DRIVE TRAIN TO RETAIN THE ORIGINAL POSITION. UPON INVESTIGATION I FOUND THIS PROBLEM EXISTS AND WILL NOT BE ADDRESSED BY THE MANUFACTURER. *JS

Mileage: 59,304

Dec 1, 2013

I TOOK MY CAR IN TO BE FIXED AGAIN. I NEEDED THE RUNNING LIGHTS AND A HESITATION IN THE CAR FIXED. SO THEY FIXED THE PROBLEMS, BUT WHEN THEY WENT TO TEST DRIVE IT THE POWER STEERING FAILED. NOW THE POWER STEERING NEEDS TO BE REPLACED. IT SEEMS THIS CAR IS NEEDS TO BE FIXED ALL THE TIME. I HAVE HAD A LOT OF CARS AND THIS IS THE MOST I HAVE EVER HAD PROBLEMS WITH A CAR. IT REALLY SCARES ME THAT THIS CAN BE FIXED BUT WILL MOST LIKELY FAIL AGAIN DUE TO THE PROBLEMS WITH GM'S STEERING. *TR

Mileage: 57,000

Aug 29, 2013

TL* THE CONTACT OWNS A 2009 BUICK ENCLAVE. WHILE STOPPED AND ON A SLIGHT INCLINE, THE CONTACT STATED THAT THE VEHICLE ROLLED AWAY IN REVERSE. THE FAILURE RECURRED SEVERAL TIMES. THE VEHICLE WAS NOT REPAIRED OR DIAGNOSED. THE MANUFACTURER WAS NOT NOTIFIED OF THE ISSUE. THE APPROXIMATE FAILURE MILEAGE WAS 85,000.

Mileage: 85,000

Mar 21, 2013

VEHICLE TRANSMISSION EITHER, SLIPS, DOESN'T SHIFT OR SHIFTS ERRATICALLY. THE ENGINE MISFIRES AT TIMES. STEERING ISSUES. NAVIGATION SYSTEM ISSUES, STRUT FAILURE, HEATED SEAT FAILURE. *TR ## VIN FAILED ##

Mileage: 55,000