1993 BUICK LESABRE Structure Problems

11 complaints about Structure

11
Complaints
0
Crashes
0
Fires
0
Deaths

This Problem Across All Years

All Structure Complaints (11)

Jul 21, 2008

1993 BUICK LESABRE - THE MOTOR-TRANSMISSION MOUNT FAILED AT THE POINT OF ACCELERATING FROM AND INTERSECTION. THE REAR OF THE MOUNT DROPPED TO THE PAVEMENT RESULTING IN A COMPLETE LOSS OF STEERING AND BRAKING. DIAGNOSIS BY THE BUICK DEALER MAKING THE REPAIR IS THAT THIS FAILURE IS DUE TO RUST. THE CAR WAS ORIGINALLY SOLD IN ROCHESTER, MICHIGAN. I AM THE SECOND OWNER IN NORTHWEST OHIO. DUE TO BOTH STATES AND AREAS USING ROAD SALT, THE MOUNT FAILED. THE OHIO DEALER STATES THEY HAVE NEVER HAD THIS TYPE OF FAILURE BEFORE, BUT THE TOW-TRUCK DRIVER STATED HE PICKED UP A PONTIAC BONNEVILLE, SAME FRAME/CHASSIS, LAST YEAR. FORTUNATELY I HAD JUST LEFT AN INTERSECTION AND THE SPEED WAS ABOUT 15 M.P.H. WHEN THE MOUNT DROPPED. THE CAR STEERED ITSELF ACROSS THE ROAD AND I WAS ABLE TO STOP IT WITH THE EMERGENCY BRAKE BEFORE GOING DOWN INTO THE DITCH ON THE OPPOSITE SIDE OF THE ROAD. AT HIGHER SPEEDS THIS COULD EASILY BE FATAL FOR ANY OF THE OCCUPANTS. *TR

Mileage: 113,140

Dec 10, 2007

TL*THE CONTACT OWNS A 1993 BUICK LESABRE. WHILE MAKING A LEFT TURN AT 2 MPH, THE CONTACT HEARD A CLUNKING SOUND. THERE WAS A LOSS OF POWER STEERING AND THE VEHICLE VEERED TO THE OTHER SIDE OF THE ROAD. THE VEHICLE WAS TOWED AND THE DEALER STATED THAT 4 OUT OF 6 BOLTS HAD RUSTED AND DROPPED THE STEERING COLUMN. THE FAILURE MILEAGE WAS 168,000 AND CURRENT MILEAGE WAS 175,000. UPDATED 03-04-08 *BF THE CONSUMER STATED THE 4 WASHERS IN THE BACK OF THE FRAME WHICH HELD THE ENGINE AND TRANSMISSION BROKE THROUGH CAUSING THE ENGINE TO DROP. UPDATED *JB

Mileage: 168,000

Aug 8, 2001

WHILE TURNING A CORNER, THE REAR ENGINE CRADLE DROPPED TO THE PAVEMENT, CAUSING A LOSS OF FLUID AND STEERING. A COLLISION WITH A VEHICLE IN THE OPPOSITE LANE WAS NARROWLY MISSED. THIS SITUATION SROSE WITH VIRTUALLY NO WARNING OTHER THAN A SLIGHT DIFFICULTY IN STEERING SHORTLY BEFORE THE INCIDENT OCCURRED. THE FAILURE OF THIS COMPONENT WAS IMMEDIATE AND CATASTROPHIC, AND I FIND IT UNCONSCIONABLE THAT GENERAL MOTORS HAS NOT ADDRESSED THIS PROBLEM, ESPECIALLY IN LIGHT OF THE FACT THAT THE DEALER TOLD ME THAT A RECALL WAS MADE TO OTHER BUICK MODELS FOR THE SAME PROBLEM. WITH THE AGEING OUT OF OTHER SIMILAR VEHICLES MORE ACCIDENTS OF THIS KIND ARE BOUND TO HAPPEN. THE NHTSA SHOULD FULLY INVESTIGATE THIS SITUATION BEFORE THERE IS A LOSS OF LIFE. I HAVE THE FULL INFORMATION REGARDING THE REPAIRS REQUIRED TO THE VEHICLE IF YOU WISH IT.*AK

Aug 8, 2001

WHILE TURNING A CORNER, THE REAR ENGINE CRADLE DROPPED TO THE PAVEMENT, CAUSING A LOSS OF FLUID AND STEERING. A COLLISION WITH A VEHICLE IN THE OPPOSITE LANE WAS NARROWLY MISSED. THIS SITUATION SROSE WITH VIRTUALLY NO WARNING OTHER THAN A SLIGHT DIFFICULTY IN STEERING SHORTLY BEFORE THE INCIDENT OCCURRED. THE FAILURE OF THIS COMPONENT WAS IMMEDIATE AND CATASTROPHIC, AND I FIND IT UNCONSCIONABLE THAT GENERAL MOTORS HAS NOT ADDRESSED THIS PROBLEM, ESPECIALLY IN LIGHT OF THE FACT THAT THE DEALER TOLD ME THAT A RECALL WAS MADE TO OTHER BUICK MODELS FOR THE SAME PROBLEM. WITH THE AGEING OUT OF OTHER SIMILAR VEHICLES MORE ACCIDENTS OF THIS KIND ARE BOUND TO HAPPEN. THE NHTSA SHOULD FULLY INVESTIGATE THIS SITUATION BEFORE THERE IS A LOSS OF LIFE. I HAVE THE FULL INFORMATION REGARDING THE REPAIRS REQUIRED TO THE VEHICLE IF YOU WISH IT.*AK

Sep 28, 1999

WHEEL WELL WAS RUSTED INSIDE. YH

Jul 27, 1999

REAR DOOR LOCK ACTUATOR FAILED. MJS

Nov 30, 1998

POWER LOCK ACTUATOR FAILED.

Oct 4, 1998

PAINT ON BUMPER GUARD AND TOP OF CAR (ROOF) IS PEELING.

Jun 19, 1998

ELECTRIC DOOR LOCKS FAILED.

May 17, 1998

PAINT HAS PEELED OFF JUST ABOVE THE WINDSHIELD.

Mar 11, 1997

POWER DOOR LOCK ON PASSENGER'S SIDE FAILED.