38
Complaints
4
Crashes
0
Fires
0
Deaths
!

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Engine And Engine Cooling Complaints

Showing 20 of 38
Aug 29, 2011 140,000 mi

TL* THE CONTACT OWNS A 1996 BUICK LESABRE. THE CONTACT STATED THAT WHILE DRIVING 20 MPH, HE HEARD A LOUD CLUNKING NOISE, THE ENGINE DROPPED, AND THE STEERING WHEEL SEIZED. THE VEHICLE WAS TOWED TO A LOCAL REPAIR SHOP, WHERE THEY DIAGNOSED THAT THE ENGINE CRADLE AND BUSHING WERE CORRODED AND NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND CURRENT MILEAGES WERE 140,000.

Aug 29, 2011 140,000 mi

TL* THE CONTACT OWNS A 1996 BUICK LESABRE. THE CONTACT STATED THAT WHILE DRIVING 20 MPH, HE HEARD A LOUD CLUNKING NOISE, THE ENGINE DROPPED, AND THE STEERING WHEEL SEIZED. THE VEHICLE WAS TOWED TO A LOCAL REPAIR SHOP, WHERE THEY DIAGNOSED THAT THE ENGINE CRADLE AND BUSHING WERE CORRODED AND NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND CURRENT MILEAGES WERE 140,000.

Mar 17, 2010 90,000 mi

TL* THE CONTACT OWNS A 1996 BUICK LESABRE. UPON STARTING THE VEHICLE, THE CONTACT COULD HEAR THE VEHICLE BACK FIRE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE REPAIRS WERE MADE TO STOP AN EVAPORATOR LEAK. THE REPAIR DID NOT STOP THE VEHICLE FROM BACK FIRING. THE MANUFACTURER STATED THAT BECAUSE THE VEHICLE WAS OLDER THAN 10 YEARS OF AGE, THEY COULD NOT PROVIDE ANY ASSISTANCE. THE APPROXIMATE FAILURE MILEAGE WAS 90,000 AND THE CURRENT MILEAGE WAS 98,000.

Mar 17, 2010 90,000 mi

TL* THE CONTACT OWNS A 1996 BUICK LESABRE. UPON STARTING THE VEHICLE, THE CONTACT COULD HEAR THE VEHICLE BACK FIRE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE REPAIRS WERE MADE TO STOP AN EVAPORATOR LEAK. THE REPAIR DID NOT STOP THE VEHICLE FROM BACK FIRING. THE MANUFACTURER STATED THAT BECAUSE THE VEHICLE WAS OLDER THAN 10 YEARS OF AGE, THEY COULD NOT PROVIDE ANY ASSISTANCE. THE APPROXIMATE FAILURE MILEAGE WAS 90,000 AND THE CURRENT MILEAGE WAS 98,000.

Dec 19, 2008 227,000 mi

1996 BUICK LESABRE CUSTOM SUDDENLY STARTED SMOKING,OVERHEATED AND SHUT OFF ON INTERSTATE AT 60 MPH. OWNER HAD CAR TOWED AND CHECKED BY MECHANIC. CRACKED MANIFOLD LEAKING COOLANT WAS THE CAUSE, ENGINE BLOWN IS DIAGNOSIS. *TR

Dec 19, 2008 227,000 mi

1996 BUICK LESABRE CUSTOM SUDDENLY STARTED SMOKING,OVERHEATED AND SHUT OFF ON INTERSTATE AT 60 MPH. OWNER HAD CAR TOWED AND CHECKED BY MECHANIC. CRACKED MANIFOLD LEAKING COOLANT WAS THE CAUSE, ENGINE BLOWN IS DIAGNOSIS. *TR

Jan 3, 2007 119,000 mi

TL* - THE CONTACT HAS A 1996 BUICK LESABRE WHICH HAS A HOLE IN THE UPPER INTAKE MANIFOLD. THE GENERAL MOTORS DEALER STATED THAT THERE WAS NO RECALL ON THE VEHICLE. HE THEN CALLED THE BUICK DEALER WHO CONCERURED. THE CONTACT FOUND RECALL 96V116000 ON THE NHTSA WEBSITE. *AK

Jan 3, 2007 119,000 mi

TL* - THE CONTACT HAS A 1996 BUICK LESABRE WHICH HAS A HOLE IN THE UPPER INTAKE MANIFOLD. THE GENERAL MOTORS DEALER STATED THAT THERE WAS NO RECALL ON THE VEHICLE. HE THEN CALLED THE BUICK DEALER WHO CONCERURED. THE CONTACT FOUND RECALL 96V116000 ON THE NHTSA WEBSITE. *AK

Jan 6, 2005

A LOUD CLANKING NOISE WAS COMING FROM THE FRONT WHILE DRIVING, VEHICLE STALLED. CONSUMER WAS UNABLE TO RESTART VEHICLE, AND HAD IT TOWED TO THE DEALER. MECHANIC DETERMINED THAT THE WARPED INTAKE MANIFOLD NEEDED TO BE REPLACED. *AK

Jan 6, 2005

A LOUD CLANKING NOISE WAS COMING FROM THE FRONT WHILE DRIVING, VEHICLE STALLED. CONSUMER WAS UNABLE TO RESTART VEHICLE, AND HAD IT TOWED TO THE DEALER. MECHANIC DETERMINED THAT THE WARPED INTAKE MANIFOLD NEEDED TO BE REPLACED. *AK

Feb 12, 2004

THE UPPER MANIFOLD HAD DETERIORATED OR CRACKED ALLOWING COOLANT FLUID TO ENTER THE COMBUSTION CHAMBER. VEHICLE'S ENGINE SEIZED. *PH *MR

Feb 12, 2004

THE UPPER MANIFOLD HAD DETERIORATED OR CRACKED ALLOWING COOLANT FLUID TO ENTER THE COMBUSTION CHAMBER. VEHICLE'S ENGINE SEIZED. *PH *MR

Jan 22, 2004

ENGINE STOPPED UNEXPECTEDLY AND SUDDENLY AT 25 MPH. VEHICLE HAD TO BE TOWED TO THE DEALER. THE DEALER STATED THE PROBLEM WAS A CRACKED MANIFOLD. *AK

Jan 22, 2004

ENGINE STOPPED UNEXPECTEDLY AND SUDDENLY AT 25 MPH. VEHICLE HAD TO BE TOWED TO THE DEALER. THE DEALER STATED THE PROBLEM WAS A CRACKED MANIFOLD. *AK

Nov 18, 2003 105,000 mi

CONSUMER TOOK VEHICLE TO DEALER FOR INSPECTION, AND MECHANIC NOTICED THAT THE PLASTIC INTAKE MANIFOLD CRACKED, CAUSING FLUID TO LEAK ONTO THE ENGINE.*AK

Nov 18, 2003 105,000 mi

CONSUMER TOOK VEHICLE TO DEALER FOR INSPECTION, AND MECHANIC NOTICED THAT THE PLASTIC INTAKE MANIFOLD CRACKED, CAUSING FLUID TO LEAK ONTO THE ENGINE.*AK

Sep 8, 2003 71,197 mi

NAR 9-8-03. MINOR KNOCK NOISE IN ENGINE. ENGINE WAS REPLACED IN THE AMOUNT OF $4200.00 ON 71000 MILE VEHICLE. *CB

Sep 8, 2003 71,197 mi

NAR 9-8-03. MINOR KNOCK NOISE IN ENGINE. ENGINE WAS REPLACED IN THE AMOUNT OF $4200.00 ON 71000 MILE VEHICLE. *CB

Aug 11, 2003

CONSUMER STATES VEHICLE GOT OVERHEATED AND COOLANT WENT INSIDE THE ENGINE DUE TO PLASTIC INTAKE MANIFOLD. DEALER CHANGED TWICE THE INTAKE MANIFOLD. *AK

Aug 11, 2003

CONSUMER STATES VEHICLE GOT OVERHEATED AND COOLANT WENT INSIDE THE ENGINE DUE TO PLASTIC INTAKE MANIFOLD. DEALER CHANGED TWICE THE INTAKE MANIFOLD. *AK

Jan 13, 2003

WHILE TRAVELING ON THE HIGHWAY AND WITHOUT PRIOR WARNING, THERE WAS ANTIFREEZE LEAKING FROM UNDERNEATH THE MANIFOLD, THE DEALER HAD BEEN NOTIFIED, PLEASE PROVIDE ADDITIONAL INFORMATION.*JB

Jan 13, 2003

WHILE TRAVELING ON THE HIGHWAY AND WITHOUT PRIOR WARNING, THERE WAS ANTIFREEZE LEAKING FROM UNDERNEATH THE MANIFOLD, THE DEALER HAD BEEN NOTIFIED, PLEASE PROVIDE ADDITIONAL INFORMATION.*JB

Dec 22, 2002 88,985 mi

ENGINE SUSTAINED DAMAGE DUE TO OIL SLUDGING (GELLING). OIL PRESSURE WAS INFLATED,KNOCKING SOUND WAS NOTICED. PENZOIL 10W30 WAS BEING USED AT REGULAR INTERVALS. DIMSII IVOQ ENTRY POSTED AFTER 12/12/02 CUT-OVER TO ARTEMIS----770781. *AK *NLM

Dec 22, 2002 88,985 mi

ENGINE SUSTAINED DAMAGE DUE TO OIL SLUDGING (GELLING). OIL PRESSURE WAS INFLATED,KNOCKING SOUND WAS NOTICED. PENZOIL 10W30 WAS BEING USED AT REGULAR INTERVALS. DIMSII IVOQ ENTRY POSTED AFTER 12/12/02 CUT-OVER TO ARTEMIS----770781. *AK *NLM

Dec 18, 2002 48,035 mi

THE UPPER MANIFOLD CRACKED AND LEAKED ANTIFREEZE.TS *JB

Dec 18, 2002 48,035 mi

THE UPPER MANIFOLD CRACKED AND LEAKED ANTIFREEZE.TS *JB

Dec 5, 2002 48,305 mi

CONSUMER NOTICED ANITFREEZE ON THE DRIVEWAY UNDER THEIR VEHICLE. THE CONSUMER TOOK VEHICLE TO THE DEALERSHIP TO HAVE IT SERVICED. THE DEALERSHIP INDICATED THAT THERE WAS A CRACK IN THE UPPER MANIFOLD, WHICH WAS THE CAUSE OF THE LEAK. THERE'S A SERVICE BULLETIN FOR THIS PART, THE EGR VALVE WAS REPLACED BECAUSE OF EXCESSIVE HEAT. THE CONSUMER REQUESTED REIMBURSEMENT FOR REPAIRS. *TS *JG *NLM

Dec 5, 2002 48,305 mi

CONSUMER NOTICED ANITFREEZE ON THE DRIVEWAY UNDER THEIR VEHICLE. THE CONSUMER TOOK VEHICLE TO THE DEALERSHIP TO HAVE IT SERVICED. THE DEALERSHIP INDICATED THAT THERE WAS A CRACK IN THE UPPER MANIFOLD, WHICH WAS THE CAUSE OF THE LEAK. THERE'S A SERVICE BULLETIN FOR THIS PART, THE EGR VALVE WAS REPLACED BECAUSE OF EXCESSIVE HEAT. THE CONSUMER REQUESTED REIMBURSEMENT FOR REPAIRS. *TS *JG *NLM

Nov 9, 2000 Crash

A DETERIORATING PLENUM WAS CAUSING COOLANT TO GET INTO ENGINE CYLINDERS. DEALER NOTIFIED, AND REPAIRS MADE AT CONSUMER'S COST. *AK THE HEAT FROM THE EGR VALVE BURNS A HOLE INSIDE THE WALL OF PLANAM ALLOWING THE ENGINE TO SUCK COOLANT INTO CYLINDERS AND CAUSING THE ENGINE TO LOSE POWER STEERING AND BRAKES RESULTING IN ACCIDENT. *YH

Nov 9, 2000 Crash

A DETERIORATING PLENUM WAS CAUSING COOLANT TO GET INTO ENGINE CYLINDERS. DEALER NOTIFIED, AND REPAIRS MADE AT CONSUMER'S COST. *AK THE HEAT FROM THE EGR VALVE BURNS A HOLE INSIDE THE WALL OF PLANAM ALLOWING THE ENGINE TO SUCK COOLANT INTO CYLINDERS AND CAUSING THE ENGINE TO LOSE POWER STEERING AND BRAKES RESULTING IN ACCIDENT. *YH

Nov 9, 2000 Crash

A DETERIORATING PLENUM WAS CAUSING COOLANT TO GET INTO ENGINE CYLINDERS. DEALER NOTIFIED, AND REPAIRS MADE AT CONSUMER'S COST. *AK THE HEAT FROM THE EGR VALVE BURNS A HOLE INSIDE THE WALL OF PLANAM ALLOWING THE ENGINE TO SUCK COOLANT INTO CYLINDERS AND CAUSING THE ENGINE TO LOSE POWER STEERING AND BRAKES RESULTING IN ACCIDENT. *YH

Nov 9, 2000 Crash

A DETERIORATING PLENUM WAS CAUSING COOLANT TO GET INTO ENGINE CYLINDERS. DEALER NOTIFIED, AND REPAIRS MADE AT CONSUMER'S COST. *AK THE HEAT FROM THE EGR VALVE BURNS A HOLE INSIDE THE WALL OF PLANAM ALLOWING THE ENGINE TO SUCK COOLANT INTO CYLINDERS AND CAUSING THE ENGINE TO LOSE POWER STEERING AND BRAKES RESULTING IN ACCIDENT. *YH

Oct 27, 1997

ONE CYLINDER LEFT BANK FAILED. MJS

Oct 27, 1997

ONE CYLINDER LEFT BANK FAILED. MJS

Sep 18, 1997

SEALS WITHIN THE EXHAUST SYSTEM FAILED.

Sep 18, 1997

SEALS WITHIN THE EXHAUST SYSTEM FAILED.

Feb 26, 1997

ABS/TRACTION CONTROL LOCKED UP AND MADE LOUD GRINDING NOISE SEVERAL TIMES. CAR ALSO ACCELERATED SUDDENLY AND DID NOT SLOW DOWN WITH APPLICATION OF BRAKE.

Feb 26, 1997

ABS/TRACTION CONTROL LOCKED UP AND MADE LOUD GRINDING NOISE SEVERAL TIMES. CAR ALSO ACCELERATED SUDDENLY AND DID NOT SLOW DOWN WITH APPLICATION OF BRAKE.