1997 BUICK LESABRE Electrical System Problems

45 complaints about Electrical System

45
Complaints
0
Crashes
3
Fires
0
Deaths

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Electrical System Complaints (45)

Aug 21, 2018

THE HORN WILL SOUND WITHOUT PRESSING THE HORN BUTTON(S) WHEN THE CAR IS IN MOTION OR UNOCCUPIED. THIS OCCURS WHEN THE WEATHER IS COLD. I HAVE RESEARCHED THIS ONLINE AND IT IS APPARENTLY AN ISSUE FOR MANY OWNERS. PART OF THE AIR BAG CONTRACTS DURING THE WINTER MONTHS PRESSING ON PART OF THE HORN BUTTON. THE ONLY WAY TO SHUT IT OFF IS TO PULL THE HORN FUSE. I AM CONCERNED THIS MAY LEAD TO AN ELECTRICAL FIRE IF THE HORN SOUNDS FOR TOO LONG OR AN AIR BAG MALFUNCTION. ALSO, THE VEHICLE HAS TO BE DRIVEN WITHOUT THE ABILITY TO USE THE HORN.

Mileage: 65,000

Jun 27, 2015

I OWN A 1997 BUICK LE SABRE CUSTOM (3.8) THE CAR WILL SHUTDOWN WHEN I AM DRIVING IT.ALSO IT DRAINS THE BATTERY.THE DATE IS THE YEAR THAT I PURCHASED THE CAR.

Mileage: 12,344

Aug 20, 2014

HAS A 1997 BUICK LESABRE AND HAVING PROBLEMS WITH IGNITION AND I CAN BE DRIVING AND IT JUST LIKE IT DON,T GET NO JUICE FROM ENGINE THEN WHEN TRIED TO START UP IT DON,T CATCH IN IGNITION SWITCH. I HAVE SPEND OVER 2,000 IN THIS CAR BUT EVERY ONE I TAKE IT TO SAYS IT IN THE IGNITION IT SOUNDS LIKE IT WANTS TO START SOMETIMES IT TAKES UP TO 6 HOURS BEFORE IT STARTS. *TR

Apr 17, 2012

I HAVE NOT SEEN A FIRE YET BUT IT HAS BEEN SMOKING IN THE FRONT OF THE CAR SINCE 2010 WHEN I BROUGHT THE CAR USED FOR 2800.00 AT JIMS TOWING SERVICE IN ELIZABETH NEW JERSEY AND EVERY TIME THE CAR BROKE DOWN WHETHER IT WAS ELECTRICAL OR WHAT HE HAD GOTTEN MAD AT ME FOR NOT BRINGING IT TO HIM AND THEN THE CHECK ENGINE KEPT ON COMING ON AND COME TO FIND OUT LAST MONTH AND THE CAR COST ME 2000.00 DOLLARS TO FIX AND THE MONTH BEFORE THAT THE GARAGE I WENT TO NAVARRO'S HAD FIXED THE HORN BECAUSE THAT WAS GOING ON AND OFF AGAIN AND SOMETIMES THE LIGHTS FLICKER AND OTHER THINGS AND NOW THE SECURITY ALARM DOES NOT WORK AND YESTERDAY WHILE SHOPPING I ASKED MY DAUGHTER WHAT THAT SOUND WAS IT WAS MY HORN AGAIN SHORTING AND DISCONNECTED IT AGAIN IT HAS DONE THAT TOO MANY TIMES AND I CANNOT AFFORD A NEW CAR WITH 6 PEOPLE LIVING IN MY HOUSE AND IAM THE ONLY ONE WORKING RIGHT NOW AND DOES ANY MECHANIC KNOW WHAT THEY ARE DOING ANYMORE AND I NEED THE CAR TO GET BACK AND FORTH I DON'T KNOW WHAT TO DO ANYMORE AND WHEN I SAID THAT THE CAR COST ME 2000.00 TO FIX THERE WAS A CRACK IN THE BLOCK OF THE ENGINE AND FOR AWHILE NOW I HAVE MANUALLY DO THE LOCKS ON MY DOORS AND CANNOT REPLACE THE PASSENGER SIDE ELECTRIC SWITCH BECAUSE NO ONE HAS IT ANYMORE HELP DON'T NEED CAR TO CATCH ON FIRE AND IT HAS BEEN SMOKING ALOT LATELY WITH THE HORN CONNECTED IT IS NOT CONNECTED NOW. WHEN THE NEW INCIDENT HAPPENED IT WAS PARKED IN THE PARKING LOT AND SECURITY OFFICER CAME. *JS

Mileage: 98,000

Apr 5, 2010

TL*THE CONTACT OWNS A 1997 BUICK LESABRE. WHILE DRIVING AT SPEEDS OF 30 MPH, THE HORN BEGAN TO SOUND. THE HORN CONTINUED TO SOUND UNTIL THE VEHICLE WAS STOPPED AND THE HOOD WAS LIFTED. UPON CLOSING THE HOOD THE HORN BEGAN TO SOUND AGAIN AND WOULD NOT STOP UNTIL PRESSURE WAS APPLIED TO THE CENTER OF THE STEERING WHEEL. THE FAILURE CONTINUED INTERMITTENTLY. THE VEHICLE WAS TAKEN TO AN INDEPENDENT VEHICLE CARE CENTER AND THE HORN WAS DISABLED. THE FAILURE MILEAGE WAS 173,130 UPDATED 06/25/10 UPDATED 07/16/10*JB

Mileage: 173,130

Aug 16, 2009

THIS CAR HAS HORN PROBLEMS. THE HORN STARTS BLOWING FOR NO REASON AND THE MECHANIC SAID THAT THE SENSOR IS DEFECTIVE AND THAT TO REPLACE IT WOULD COST SEVERAL HUNDRED DOLLARS. *TR

Mileage: 30,000

Sep 20, 2005

DT: THE CONSUMER STATED THE HORN WILL NOT STOP BLOWING, AND THE AIR BAG ASSEMBLY IS MAKING A NOISE. THE SOUND IS COMING OUT OF THE STEERING WHEEL. WHEN DRIVING THE HORN JUST STARTS BLOWING OUT OF NOWHERE, IT JUST STARTS BLOWING, SPECIFICALLY STATES THE CONSUMER. WHEN PRESSING THE HORN PAD IT WILL STOP SOMETIMES. ONE HAS TO PRESS IN A CERTAIN SPOT. THE CAR IS A 1997 BUICK LESABRE. THE CONSUMER IS GOING TO CALL AND SEE WHAT GM CAN DO. THIS HAS BEEN HAPPENING FOR TWO WEEKS.*AK

Mileage: 77,000

Aug 12, 2005

DT: CONSUMER OWNS A 1997 BUICK LESABRE. CONSUMER WAS DRIVING WHEN VEHICLE SHUT OFF. SHE WAS ABLE TO COAST A LITTLE BUT NOT ENOUGH TO GET COMPLETELY OUT OF TRAFFIC. SHE WAS STUCK IN VEHICLE BECAUSE EVERYTHING ON VEHICLE SHUT DOWN DUE TO THE GROUND CABLE COMING LOOSE, NOT LOOSE FROM THE MOTOR BLOCK. VEHICLE HAS BEEN WORKED ON, SHE DID NO FEEL THAT CABLE COMING LOOSE WAS DUE TO A DEFECT. SHE WAS MORE CONCERNED THAT WHEN VEHICLE LOST POWER SHE WAS STUCK IN VEHICLE WITH NO WAY TO ESCAPE. THE DOOR LOCKED AND POWER WINDOWS DID NOT WORK. THE BIGGEST CONCERN WAS THAT THERE WAS NO MANUAL LOCK THAT COULD BE USED TO UNLOCK THE DOOR WHEN POWER FAILED. SHE WAS STUCK IN VEHICLE WITH VEHICLE IN THE ROAD AND IN DANGER OF ONCOMING TRAFFIC. SHE STAYED IN VEHICLE ONE HOUR ON A VERY HOT DAY UNTIL SHE WAS ABLE TO CONTACT A FRIEND ON CELL PHONE, AND HE CAME TO HELP HER. *AK

Nov 22, 2004

THE HORN REPEATEDLY WENT OFF AND EVENTUALLY IT BECAME INOPERABLE. THE CAUSE IS UNDETERMINED. *JB

Apr 1, 2004 Fire

WHILE ATTEMPTING TO START THE VEHICLE THERE WAS A LOUD POPPING NOISE WHEN TURNING THE IGNITION. SMOKE BEGAN TO COME FROM UNDER THE DASH. *AK

Mileage: 83,981

May 15, 2003

I HAVE REPLACED THE INSTRUMENT CLUSTER PANEL (DASHBOARD) IN MY CAR TWICE WITHIN THE LAST 2 1/2 YEARS. EACH TIME I HAD TO ORDER A REPLACEMENT AND LOST THE USE OF MY CAR FOR AN EXTENDED PERIOD OF TIME. *JB

Mileage: 106,000

Mar 4, 2003

BATTERY SULFATES FROM POST DAMAGED ELECTRICAL CABLES AND CAUSED THE VEHICLE TO STALL. SCC *NLM

Nov 15, 2002

WHEN SLOWING DOWN OR AFTER COMING TO A STOP THE VEHICLE STALLS, THE DEALER SCANED DATA AND CHECKED THE BATTERY, THE DEALER REPLACED THE BATTERY AND POSITIVE CABLE TO THE FIREWALL. *SCC

Jan 18, 2002

NO SUMMARY LISTED FOR ABOVE VEHICLE. *AK

Dec 1, 2001

ON11/22/2001 IN THE MORNING HOURS,I TRY TO START THE CAR WHEN I HEARD A BACKFIRE EXPLOSION AND THEN SMOKE CAME FROM UNDER THE HOOD. I DID OPEN THE HOOD TO DO A VISUAL INSPECTION OF THE CAR TO SEE WHAT COULD BE WRONG, I SEEN NOTHING WRONG WITH THE CAR I STARTED IT AND WENT TO WORK.THE SAME DAY I WAS DRIVING FROM WORK TO MY HOME, WHEN ALL OF THE SUDDEN THE CAR STARTED JERKING UP AND HESITATING, I SAW A THICK AND WHITE CLOUD OF SMOKE CAME FROM THE THE EXAUST . SMOKE CAME FROM UNDER THE HOOD AND I DID TURN OFF THE CAR TO INVESTIGATE WHAT COULD BE THE POSSIBLE CAUSE.WHEN I OPENED THE HOOD OF THE CAR, A STRONG GASOLINE ODOR CAME FROM THE ENGINE. I LET THE CAR TO COOL DOWN AND THEN I DROVE HOME. I HAD THE CAR TAKEN TO A BUICK DEALERSHIP AND THEY TOLD ME THAT THE PLENUMUPPER INTAKE MANIFOLD WAS WARP AND NEEDED TO BE REPLACED,FUEL REGULATOR WAS BAD AND BECAUSE OF THAT THE TRANSMISSION MODULATOR WAS FLODDED AND HAD TO BE REPLACED. I WOULD LIKE TO GIVE YOU SOME MORE DETAILS ABOUT THIS PROBLEM, BUT ALL THE DOCUMENTS ARE AT THE DEALER AT THIS MOMENT. I'M LOOKING FOWARD TO HEAR FROM YOU.THANKS FOR YOUR TIME AND HAPPY HOLIDAYS. *AK

Aug 16, 2001

I HAD TAKEN THIS VEHICLE BACK TO THE BUICK DEALERSHIP WHERE I PURCHASED IT AT 34K MILES AND TOLD THEM IT HAD A "MISS" AND THAT IT "HESITATED" DRIVING DOWN THE ROAD. THEY SAID IT WAS A SPARK PLUG AND REPLACED ONE. THE LAST TIME I TOOK IT TO ANOTHER BUICK DEALER IT NEEDED 4,200.00 TO MAKE IT ROAD WORTHY INCLUDING A NEW WATER PUMP, NEW TRANSMISSION, NEW BRAKES AND ROTORS. THE SERVICE CODE ON THE CAR SHOULD HAVE INDICATED FAILURE OF THESE PARTS WHEN I TOOK IT TO THE FIRST DEALER.

Jun 18, 2001

THE WIRE THAT HAD SHORETED OUT CAUSING THE VEHICLE'S COMPUTER,THE BATTERY NEEDLE AND THE RPMS TO MALFUNCTION. THE CONSUMER FEELS UNSAFE TO DRIVE THE VEHICLE. *YH

Jun 9, 2001

VEICLE WAS IN FOR TRANSMISSION REPAIR AT LOCAL DEALER/ SERVICEMAN WAS TEST DRIVING VEHICLE AFTER REPAIR WHEN VEHICLE CAUGHT FIRE UNDERNEATH BETWEEN TRANSMISSIOM AND GAS TANK, DEALER CLAIMS NOT RESPONSIBLE, VEHICLE BURNED COMPLETELY. HAS THERE BEEN ANY PROBLEMS COMPARABLE TO THIS SITUATION ?

Mar 30, 2001 Fire

ENGINE CAUGHT ON FIRE WHILE TRYING TO START VEHICLE , VEHICLE WAS A TOTAL LOSS, AND MANUFACTURER WAS UNABLE TO DETECT ORGIN OF FIRE.*AK AAA DETECTED A HOT SPOT IN THE MANIFOLD AND THE FUEL LINE RUNS ALONG THE MANIFOLD, ALSO VEHICLE HAD AN INTAKE MANIFOLD LEAK, FIRE POSSIBLY FUEL RELATED. *SLC

Jan 9, 2001

ALTERNATOR FAILED PREMATURELY. NLM

Nov 22, 2000

VEHICLE STALLED BETWEEN 25-65MPH. IT HAS HAPPENED 5-6 TIMES. DEALER HAD VEHICLE TWICE, EACH TIME FOR A WEEK. THEY COULDN'T FIX IT UNTIL IT FAILED AGAIN.*AK

Oct 25, 2000

WHILE DRIVING AT 25 MPH VEHICLE WILL STALL. THEN, CONSUMER COULD START CAR AGAIN. ABOUT 4 DAYS LATER, IT STALLED AGAIN, AND WOULD NOT START FOR ABOUT 5 MINUTES. TOOK TO DEALER , AND THEY COULD NOT DUPLICATE THE PROBLEM. IF ON THE HIGHWAY, THERE WOULD HAVE BEEN AN ACCIDENT.*AK

Oct 17, 2000

WHILE DRIVING AT HIGHWAY SPEED ENGINE WILL STALL OUT ON THIS VEHICLE, BUT VEHICLE WILL START RIGHT BACK UP. DEALER HAS BEEN CONTACTED.*AK

Apr 9, 2000

SINCE I BOUGHT THE VEHICLE, THE CAR HAS GOTTEN HORRENDOUS GAS MILEAGE, THE HORN INTERMITTENTLY DOES NOT WORK AND THE TRANSMISSION HAS SLIPPED. THE CAR WAS TAKEN BACK TO THE DEALER AND NOTHING WAS DONE. I WAS TOLD "WE WERE UNABLE TO FIND A PROBLEM." THE HORN ISSUE NEARLY RESULTED IN A CAR ACCIDENT LASTNIGHT AS THE HORN, AGAIN, DECIDED TO TAKE THE NIGHT OFF. THIS IS NOT RIGHT!!

Apr 4, 2000 Fire

CONSUMER PUT THE KEY IN THE IGNITION AND TURNED IT TO START UP, AND VEHICLE EXPLODED INTO FLAMES. MANUFACTURER WAS CONTACTED, AND SAID THEY HAD NO RESPONSIBLITY IN THE CASE. CONSUMER HAD BUMPER TO BUMPER WARRANTY WITH APROXIMATELY 22.200 MILES ON VEHICLE WARRANTY. *AK

Jan 3, 2000

THE INTEGRATION OF THE AIR BAG SYSTEM TO THE HORN FAILED CAUSING THE HORN TO SOUND VERY LOUDLY CONTINUOUSLY. YH

Jul 26, 1999

MULTI FUNCTION ALARM MODULE FOR LIGHTING AND LOCK FAILED. MJS

Feb 1, 1999

BATTERY FAILED. MJS

Feb 1, 1999

IGNITION WOULD NOT START. *YC

Feb 1, 1999

BATTERY POSITIVE POST WAS DEFORMED AND NARROW AT A POSITION WITHIN THE BATTERY HOUSING CAUSING IT TO SEPARATED AND RESULT IN AN OPEN CIRCUIT. NLM

Feb 1, 1999

BATTERY LEAKING. *YC

Feb 1, 1999

ON TWO OCCASIONS THE IGNITION FAILED TO START. *YC

Jun 11, 1998

FRONT END MISALIGNMENT, CAUSING VEHICLE TO PULL TO THE RIGHT AND PREMATURE WEAR OF TIRES. ALSO, BATTERY LEAKED ACID, AND TERMINAL WAS WORN OUT TO THE POINT OF BEING BROKEN.

May 5, 1998

WHILE DRIVING THE VEHICLE WILL STALL WITHOUT INDICATIONS. DEALER HAS BEEN CONTACTED. DEALER ALSO REPLACED BATTRY/ALTERNATOR/IGNITION AND COMPUTER. HOWEVER, VEHICLE CONTINUED TO STALL. *AK

May 5, 1998

WHILE DRIVING THE VEHICLE WILL STALL WITHOUT INDICATIONS. DEALER HAS BEEN CONTACTED. DEALER ALSO REPLACED BATTRY/ALTERNATOR/IGNITION AND COMPUTER. HOWEVER, VEHICLE CONTINUED TO STALL. *AK

May 5, 1998

WHILE DRIVING THE VEHICLE WILL STALL WITHOUT INDICATIONS. DEALER HAS BEEN CONTACTED. DEALER ALSO REPLACED BATTRY/ALTERNATOR/IGNITION AND COMPUTER. HOWEVER, VEHICLE CONTINUED TO STALL. *AK

May 5, 1998

WHILE DRIVING THE VEHICLE WILL STALL WITHOUT INDICATIONS. DEALER HAS BEEN CONTACTED. DEALER ALSO REPLACED BATTRY/ALTERNATOR/IGNITION AND COMPUTER. HOWEVER, VEHICLE CONTINUED TO STALL. *AK

Sep 10, 1997

ECM FAILED.

Sep 9, 1997

WHILE DRIVING VEHICLE AT NIGHT THE HEADLIGHTS GO DIM FOR NO REASON. OWNER HAS TAKEN VEHICLE TO DEALER, AND WAS TOLD ITS THE DESIGN OF VEHICLE. OWNER FURTHER NOTES THAT THIS PROBLEM HAS ALMOST CAUSED ACCIDENTS. *AK SES LIGHT ILLUMINATED. WHEN THERE IS NOT EVEN 300 POUNDS IN VEHICLE AND GOING OVER BUMPS, IT BOTTOMS OUT, DEALER REPLACED REAR SPRINGS AND WEAK COIL SPRINGS. CONSUMER HAD TO WIGGLE KEY TO GET IT OUT OF THE DOOR, DEALER FILED KEY AND LUBRICATED THE LOCK CYLINDER. *SLC

Jul 10, 1997

FAULTY COMPUTER CHIP CAUSED CAR TO STALL IN THE MIDDLE OF A BUSY INTERSECTION.

Mar 18, 1997

VEHICLE'S ELECTRICAL SYSTEM MALFUCTIONED WHEN COMING FROM A DESCENDING OR STOPPING POSITION. THE VEHICLE'S FRONT HEADLIGHTS DIMMED/FLICKERED, CAUSING EXTREME VISIBILITY DIFFICULTIES. *AK

Jan 8, 1997

OWNER STATES THAT HE WAS DRIVING DOWN THE HIGHWAY HIS TRUNK LID CAME OPEN, WAS TOLD BY DEALER THAT HIS COMPUTER MODULE WAS BAD. *AK

Nov 15, 1996

FROM TIME TO TIME WHEN SLOWING DOWN THE VEHICLE LOSES POWER/ STALLS. PLEASE DESCRIBE IN DETAIL. *AK

Aug 29, 1996

DEFECTIVE ECM CAUSES VEHICLE TO BACKFIRE.

Aug 14, 1996

COMPUTER FAILURE.