1999 BUICK LESABRE Electrical System Problems

31 complaints about Electrical System

31
Complaints
2
Crashes
6
Fires
0
Deaths

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Electrical System Complaints (31)

May 11, 2015

1999 BUICK LESABRE. CONSUMER WRITES IN REGARDS TO DEFECTIVE IGNITION SWITCH- ANTI THEFT WIRING ISSUES. *SMD THE CONSUMER STATED THE IGNITION SWITCH HAD TO BE REPLACED. AN EXAMINATION REVEALED THAT ONE OF THE ANTI-THEFT WIRES WAS BROKEN AND THE SECOND WIRE HAD THE PROTECTIVE INSULATION COATING CRACKED THROUGH TO THE COPPER WIRE. IT APPEARED THAT ROTATION OF THE CYLINDER HAD CHAFED OVER TIME AND COMPROMISED THE INTEGRITY OF BOTH WIRES AND THE CAUSE THE SECURITY DASH LIGHT TO ILLUMINATE AND THE VEHICLE NOT TO START. *JB

Nov 10, 2014

TL* THE CONTACT OWNS A 1999 BUICK LESABRE. THE CONTACT STATED THAT WHILE DRIVING AT APPROXIMATELY 40 MPH MAKING A RIGHT TURN, THE VEHICLE STALLED WITHOUT WARNING. THE VEHICLE RESTARTED AND WAS TAKEN TO AN INDEPENDENT MECHANIC. THE TECHNICIAN DIAGNOSED THAT THE IGNITION SWITCH NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 98,927.

Mileage: 98,927

Nov 10, 2014

TL* THE CONTACT OWNS A 1999 BUICK LESABRE. THE CONTACT STATED THAT WHILE DRIVING AT APPROXIMATELY 40 MPH MAKING A RIGHT TURN, THE VEHICLE STALLED WITHOUT WARNING. THE VEHICLE RESTARTED AND WAS TAKEN TO AN INDEPENDENT MECHANIC. THE TECHNICIAN DIAGNOSED THAT THE IGNITION SWITCH NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 98,927.

Mileage: 98,927

Sep 20, 2014

TRAVELING ABOUT 65 - 70 MPH I NOTICED MY SPEEDOMETER WENT 'WACKY', MEANING IT WENT DOWN TO 0 - 20 MPH AND BACK UP AGAIN TO THE SPEED I WAS TRAVELING. NOTHING ELSE HAPPENED. THE NEXT TIME, MAYBE A WEEK TO A COUPLE WEEKS LATER IT DID I IT AGAIN, ONLY I HEARD THE DOORS UNLOCK AND IT HAD DIED. SINCE THEN IT HAS BEEN HAPPENING MORE FREQUENTLY. I HAVE ALWAYS BEEN ABLE TO START IT RIGHT BACK UP. I CAN BE OUT ON THE HIGHWAY OR IN TOWN. I USUALLY PUT IT INTO NEUTRAL, START IT AND KEEP GOING. IT HAS HAPPENED AS MANY TIMES AS 3 TIMES A DAY, OR IT WON'T DIE FOR 3-4 DAYS. I DID HAVE ONE ESPECIALLY DANGEROUS SITUATION WITH A SEMI-TRAILER TRUCK BEHIND ME ON THE HIGHWAY WHEN THE VEHICLE JUST DIED. *TR

Mileage: 190,000

Sep 15, 2014

BATTERY WENT DOWN WHEN CLOCK LEFT ON BECAUSE IGNITION WAS LOOSE OR FAULTY. SO NOW I MAKE SURE CLOCK IS OFF WHEN I SHUT IT DOWN. CAR STARTED UP FINE - DROVE IT 6 MILES - CAME BACK OUT TO START IT AFTER AN HOUR AND NOTHING-NO SOUND NOTHING-ABOUT 20 MINUTES LATER I TRIED IT AGAIN AND IT STARTED RIGHT UP. THERE HAS BEEN A GRINDING SOUND N CASSETTE PLAYER WITH NO CASSETTE IN IT AT ONE TIME. DASH LIGHTS LIT UP WHILE DRIVING SO AUTOMATICALLY THOUGHT THERE IS SHORT IN DASH BOARD. SECOND TIME I PUT KEY IN AND NOTHING HAPPENED-NO SOUND-NOTHING, WHEN IT FINALLY DECIDED TO START THIS TIME I TOOK TO AUTO ZONE. FIRST THEY SAID BATTERY, BUT BATTERY IS PRETTY NEW, THEN ANOTHER MAN SAID ALTERNATOR. GOT ALTERNATOR FROM SHOP THAT REBUILDS ALTERNATORS AND THEY DON'T THINK IT IS ALTERNATOR. REAR DEFROSTER DOESN'T WORK AND FOR SOME REASON I THINK SHORT OR PROBLEM COULD BE HERE, BUT NOT SURE. I'VE DRIVEN IT MANY TIMES WITH DASH LIGHTS ON, KNOWING THAT NOTHING IS WRONG WITH CAR. OIL IS GOOD, COOLING GOOD, TRANSMISSION GOOD. IT HAS TO BE AN ELECTRICAL PROBLEM. ALTERNATOR BELT IS NOT LOOSE. TODATE, THE PROBLEM HAS NOT BEEN FIXED. I EVEN THOUGHT IT WAS KEY, SO GOT SECOND KEY AND TRIED IT - NOT THE KEY. *TR

Mileage: 187,000

Aug 15, 2014

TL* THE CONTACT OWNS A 1999 BUICK LESABRE. THE CONTACT STATED THAT WHILE HAVING MAINTENANCE PERFORMED FOR AN OIL LEAK, THE TECHNICIAN NOTICED THAT THE IGNITION SWITCH CABLE WAS FRACTURED CAUSING THE SECURITY SYSTEM AND ELECTRICAL SYSTEM TO MALFUNCTION. THE TECHNICIAN STATED THAT THE IGNITION SWITCH NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. HOWEVER, THE CONTACT MENTIONED THAT AFTER THE REPAIRS THE VEHICLE FAILED TO START UNTIL AFTER SEVERAL ATTEMPTS AND IN SEVERAL OCCASIONS IT STALLED WHILE DRIVING. THE VEHICLE WAS TAKEN BACK TO DEALER. THE TECHNICIAN STATED THAT THE ELECTRONIC PART IN THE IGNITION WAS NOT COMMUNICATING WITH THE KEY. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 140,000.

Mileage: 140,000

Aug 15, 2014

TL* THE CONTACT OWNS A 1999 BUICK LESABRE. THE CONTACT STATED THAT WHILE HAVING MAINTENANCE PERFORMED FOR AN OIL LEAK, THE TECHNICIAN NOTICED THAT THE IGNITION SWITCH CABLE WAS FRACTURED CAUSING THE SECURITY SYSTEM AND ELECTRICAL SYSTEM TO MALFUNCTION. THE TECHNICIAN STATED THAT THE IGNITION SWITCH NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. HOWEVER, THE CONTACT MENTIONED THAT AFTER THE REPAIRS THE VEHICLE FAILED TO START UNTIL AFTER SEVERAL ATTEMPTS AND IN SEVERAL OCCASIONS IT STALLED WHILE DRIVING. THE VEHICLE WAS TAKEN BACK TO DEALER. THE TECHNICIAN STATED THAT THE ELECTRONIC PART IN THE IGNITION WAS NOT COMMUNICATING WITH THE KEY. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 140,000.

Mileage: 140,000

Aug 3, 2014

IN APPROX 2010 MY BUICK LESABRE HAD ISSUES STARTING AND WOULD OCCASIONALLY STOP OPERATING DURING TRAVEL. ALL IGNITION FUNCTIONS WOULD CEASE TO WORK. TOWED TO BUICK DEALERSHIP TO RESOLVE AND REPLACED IGNITION SWITCH. THIS YEAR A SIMILAR ACTION HAPPENED WHERE THE CAR WOULD NOT START. AGAIN AT THE DEALERSHIP THE IGNITION SWITCH WAS REPLACED. IS THIS IGNITION SWITCH ISSUE INCLUDED IN THE GM RECALL? *TR

Mileage: 164,000

Jul 13, 2014

WIRE IN STEERING COLUMN OPENS. CAR WON'T START. *TR

Mileage: 80,000

Jun 13, 2014 Crash

RE: ACCIDENT MAY, 27, 2014, NCIC 9245, OFFICER ID 17604 THE ABOVE ACCIDENT WAS CAUSED BY A MECHANICAL FAILURE OF THE BUICK LE SABRE, 1999, LICENSE # [XXX]. NOT DRIVER ERROR. LEAVING HIGHWAY 193 TURNING ONTO HWY 49, (GOING TOWARD AUBURN) BEING A 2 LANE NARROW WINDING ROAD, THE ENGINE OF THE ABOVE VEHICLE DIED, LOCKED UP THE STEERING, AND HAD NO BRAKES. I WAS UNABLE TO STOP OR CONTROL THE CAR. THIS WAS THE FIRST TIME THERE WAS A LOSS OF BRAKES. IN TRYING TO CONTROL THE CAR IT CAUSED ME TO VEER OFF THE ROAD TO THE RIGHT HAND SIDE. UPON LEAVING THE ROAD AND CRASHING THE AIR BAGS DID NOT DEPLOY. THE VEHICLE HAS HAD THIS PROBLEM BEFORE VERIFIED BY WITNESSES WITH THE EXCEPTION OF THE LOSS OF BRAKES. PASSENGER IN CAR ON TRIP FROM FRESNO TO AUBURN, IN MARCH OF 2013, (MECHANICAL FAILURE OF CAR ENGINE, DIED, NO STEERING), THIS HAPPENED TWICE, ON SAME DAY. CSAA WAS CALLED TO TOW CAR. CONTACT: [XXX] CAR BEING DRIVEN BY [XXX]., (MECHANICAL FAILURE OF CAR, ENGINE DIED, NO STEERAGE), ON HWY 49 AND LONESTAR ROAD. CALLED CSAA. [XXX] THE ENGINE TURNING OFF WHILE DRIVING HAD HAPPENED ON OTHER OCCASIONS AND THERE WAS DIFFICULTY IN THE CAR STARTING DURING COLD WEATHER. THE BUICK LESABRE HAS HAD REGULAR SERVICE AND MAINTENANCE. RECORDS OF SERVICE AND REPAIRS CAN BE PROVIDED UPON REQUEST. THE IGNITION KEYS FOR THE BUICK HAD EXTRA KEYS ATTACHED TO IT. THERE WERE 4 ADDITIONAL KEYS, PLUS KEY LIGHT. LOOK FORWARD TO YOUR REPLY. SINCERELY, [XXX] INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6) *JS

Mileage: 240,000

Jul 22, 2011 Fire

THE EVENT LEADING TO THE INCIDENT INVOLVED TURNING ON THE REAR DEFROSTER. AFTER TURNING ON THE REAR DEFROSTER I SMELT SMOKE AND BURNT ELECTRONICS. THE REAR WINDOW WOULD NOT DEFROST. I TURNED THE CAR OFF AND PULLED OFF THE PANEL NEAR THE WIRE RUNNING TO THE REAR WINDSHIELD AND DISCOVERED THE "POWER RADIO AMPLIFIER" HAD MELTED AND CAUGHT FIRE, RESULTING IN BURNS TO THE PANEL AND COMPLETE LOSS OF RADIO AND REAR DEFROSTER. THIS OF COURSE MADE IT IMPOSSIBLE TO DEFROST THE REAR WINDSHIELD. A REPLACEMENT PART WAS BOUGHT AND INSTALLED BY MYSELF (THE WIRING HARNESSES AND CABLES NEEDED TO BE REPAIRED DUE TO SEVERE BURNING AS WELL). I STILL OWN THE OLD BURNT PART. *TT

Mileage: 140,000

Jan 5, 2011

IN DEC 2010 I TURNED ON MY REAR WINDOW DEFROSTER ON MY 1999 BUICK LESABRE. IT DID NOT WORK. AFTER CHECKING REPAIR OPTIONS IN THE AUTO MANUALS AND ON LINE, I STILL COULD NOT GET IT WORKING. WHEN MY SON CAME IN FOR THE HOLIDAYS, WE DECIDED TO CHECK THE WIRES AT THE REAR WINDOW. WE DISCOVERED A SQUARE UNIT ATTACHED TO THE BODY UNDER THE ROOF PANEL. THIS UNIT HAD AN ENTRY PLUG WHICH WAS BURNED AND AN OUTLET PLUG LEADING TO THE GRIDS ON THE REAR WINDOW. IT ALSO HAD THE RADIO ANTENNA LEADING INTO IT. THE UNIT AND THE ENTRY PLUG WERE BURNED. MY WIFE AND I BOTH SMELLED SOMETHING LIKE A ELECTRICAL AT ONE TIME BUT DID NOT KNOW WHERE IT CAME FROM. WHAT I AM ASKING IS THAT: COULD THIS UNIT CAUSE A FIRE OR BE SUBJECT TO A RECALL? I KNOW IT IS IN OTHER GM CARS AS WELL AS OUR BUICK. THE PART IN QUESTION IS GM 25623688. I HAVE SINCE REPLACED MY UNIT AND REPAIRED THE WIRING. THANK YOU FOR YOUR CONSIDERATION! *TR

Mileage: 91,620

Apr 25, 2005

CONSUMER'S VEHICLE WAS TOWED TO A DEALER FOR A NEW STARTER ASSEMBLY. WHILE THE MECHANIC WAS INSPECTING THE VEHICLE THE INTAKE MANIFOLD EXPLODED. THE MECHANIC SUSTAINED MINOR INJURIES AND WAS TRANSPORTED TO A HOSPITAL. THE CAUSE HAS NOT BEEN DETERMINED AT THIS TIME. *AK WHEN THE NEW STARTED WAS BEING TESTED THE MANIFOLD BLEW UP. *JB *NM

Mileage: 47,000

Sep 13, 2004

DEALERSHIP INFORMED THE CONSUMER THAT BATTERY CABLES WERE NOT GETTING ENOUGH CHARGE TO START THE VEHICLE. DEALERSHIP REPAIRED THE PROBLEM. *AK THE VEHICLE QUIT RUNNING AFTER SHIMMYING ALL OVER THE ROAD. *SC

Mileage: 48,000

Aug 4, 2004 Fire

CONSUMER WAS PULLING INTO A PARKING LOT WHEN SHE HEARD A LOUD BOOM. THEN FLAMES CAME FROM BENEATH THE VEHICLE, SAID A WITNESS. CONSUMER GOT OUT AND VEHICLE CAUGHT ON FIRE. *AK IN JUNE THE CONSUMER RECEIVED A RECALL NOTICE WHICH EXPLAINED THE FAILURE THAT SHE EXPERIENCED SEVERAL MONTHS EARLIER. *NM

Mileage: 44,161

Apr 16, 2004

CONSUMER WAS COMING TO A STOP WHEN SUDDENLY THERE WAS A LOUD BOOM, AND SPARKS BEGAN TO COME FROM BENEATH THE VEHICLE. *AK

Mar 31, 2004 Fire

UPON STARTING THE VEHICLE THERE WAS A LOUD BANG, THEN THE VEHICLE CAUGHT ON FIRE. THE FIRE DEPARTMENT WAS CALLED. *AK

Mileage: 20,000

Mar 19, 2004

AIR BAG DESIGN FLAW - A LIFE THREATENING DESIGN FLAW. I AM THE ORIGINAL OWNER OF A 1999 BUICK LESABRE CUSTOM (PURCHASED AT THE END OF THE MODEL YEAR). THE CAR OFTEN SPENDS TIME IN THE BRIGHT FLORIDA SUN. ALTHOUGH I USE A REFLECTIVE WINDSHIELD SUN SCREEN, THE CAR STILL GETS HOT INSIDE (AS DO MOST FLORIDA CARS). RECENTLY, THE HORN BEGAN TO HONK CONTINUOUSLY. I TOOK IT INTO THE ORANGE BUICK AND GMC DEALER IN ORLANDO FL. THE PROBLEM IS THAT THE AIR BAG HAS SWOLEN UP AND COMPRESSED THE HORN RELAY. THE AIR BAG IS BROKEN AND NEEDS TO BE REPLACED. THIS IS APPARENTLY A FLAWED AIR BAG DESIGN, WHICH MUST ALSO ENDANGE PEOPLE WITH THIS STEERING WHEEL/AIR BAG DESIGN, LIVING THROUGHOUT THE HOT SOUTHERN UNITED STATES. THE COST TO REPLACE THE POORLY DESIGNED AIR BAG (WITH ANOTHER ONE HAVING THE SAME POOR DESIGN) IS OVER $700 (DIFFICULT FOR ME TO DO SINCE I RECENTLY LOST MY JOB, WHICH HAS MOVED OFF SHORE TO INDIA). IT SEEMS THAT THE BUICK MANUFACTURER SHOULD BE REQUIRED TO CORRECT THEIR LIFE-THREATENING FLAWED AIR BAG DESIGN. I HOPE TO HEAR BACK FROM THE D.O.T. ABOUT THIS LIFE-THREATENING SAFETY ISSUE.*AK

Mileage: 47,500

Mar 4, 2004

FAILURE OF CAR TO START WHEN IGNITION KEY TURNED. STILL HAD LIGHTS & DASHBOARD. THIS OCCURED 9:00 AT NIGHT AND COULD HAVE LEFT ME STRANDED. AS IT WAS, I HAD BEEN WITH A GROUP OF FOLKS AND SOMEONE WAITED TO FOLLOW ME. NEXT DAY MECHANIC TOWED CAR TO SHOP, UNABLE TO FIX BECAUSE HE NOT SET UP FOR DIAGNOSTICS. REFERRED ME THE GM DEALER. DEALER DETERMINED THEFT DETERRANT MODULE SHOT. ONCE FIXED, TWO DAYS LATER, SECURITY LIGHT SHOWING ON DASH. NOW WE NEED A NEW KEY LOCK IGNITION CYLANDER SWITCH AND KEY. MY COMPLAINT IS THIS COULD HAVE BEEN A SITUATION WHERE I COULD HAVE BEEN LOCKED INSIDE MY CAR WITHOUT A WAY TO GET OUT! THIS, IN MY MIND, IS A SERIOUS SAFETY ISSUE. THESE PARTS NEED TO BE RECALLED! I TAKE GOOD CARE OF MY CAR AND IT IS NOT OLD. THEREFORE I SEE NO GOOD REASON FOR THESE PARTS TO FAIL. MY BILL WILL BE APPROXIMATELY $700.00 PER THE GARAGE ESTIMATE. I PURCHASED AN EXTENDED WARANTY, BUT THESE PARTS NOT COVERED, NATURALLY. I GUESS THEY WEREN'T EXPECTED TO FAIL. (MILEAGE I SUBMITTED IS AN ESTIMATE AND I DO NOT KNOW WHAT OEM MEANS, SO I LET IT DEFAULT TO NO.)

Mileage: 63,700

Mar 4, 2004

FAILURE OF CAR TO START WHEN IGNITION KEY TURNED. STILL HAD LIGHTS & DASHBOARD. THIS OCCURED 9:00 AT NIGHT AND COULD HAVE LEFT ME STRANDED. AS IT WAS, I HAD BEEN WITH A GROUP OF FOLKS AND SOMEONE WAITED TO FOLLOW ME. NEXT DAY MECHANIC TOWED CAR TO SHOP, UNABLE TO FIX BECAUSE HE NOT SET UP FOR DIAGNOSTICS. REFERRED ME THE GM DEALER. DEALER DETERMINED THEFT DETERRANT MODULE SHOT. ONCE FIXED, TWO DAYS LATER, SECURITY LIGHT SHOWING ON DASH. NOW WE NEED A NEW KEY LOCK IGNITION CYLANDER SWITCH AND KEY. MY COMPLAINT IS THIS COULD HAVE BEEN A SITUATION WHERE I COULD HAVE BEEN LOCKED INSIDE MY CAR WITHOUT A WAY TO GET OUT! THIS, IN MY MIND, IS A SERIOUS SAFETY ISSUE. THESE PARTS NEED TO BE RECALLED! I TAKE GOOD CARE OF MY CAR AND IT IS NOT OLD. THEREFORE I SEE NO GOOD REASON FOR THESE PARTS TO FAIL. MY BILL WILL BE APPROXIMATELY $700.00 PER THE GARAGE ESTIMATE. I PURCHASED AN EXTENDED WARANTY, BUT THESE PARTS NOT COVERED, NATURALLY. I GUESS THEY WEREN'T EXPECTED TO FAIL. (MILEAGE I SUBMITTED IS AN ESTIMATE AND I DO NOT KNOW WHAT OEM MEANS, SO I LET IT DEFAULT TO NO.)

Mileage: 63,700

Jan 26, 2004 Fire

THE OWNER WENT OUT TO THE VEHICLE TO LEAVE AND THE VEHICLE WOULD NOT START. HE THEN CONTACTED THE AUTO CLUB AND THEY CAME OUT AND ATTACHED JUMPER CABLES. WHEN THE OWNER TURNED THE IGNITION AS INSTRUCTED BY THE MECHANIC HE IMMEDIATELY HEARD A "BANG" FOLLOWED BY A FIRE. PLEASE PROVIDE ANY ADDITIONAL INFORMATION. *NM

Mileage: 33,225

Nov 4, 2003

CONSUMER BOUGHT NEW BUICK, LASABRA IN 1999, WITHIN 4 YEARS OF OWNERSHIP, BATTERY DIED AND WAS REPLACED TWICE. AVERAGE BATTERY LIFE WAS 5 YEARS OR 60 MONTHS.*AK

Feb 12, 2003 Fire

THE VEHICLE CAUGHT ON FIRE UNDER THE HOOD.*JB *TS

Mileage: 52,000

Aug 2, 2002

HORN BLE WOUT INTERMITTENTLY. TOOK VEHICLE TO DEALER, AND THEY STATED THAT DRIVER'S SIDE AIRBAG NEEDED REPLACEMENT. PLEASE PROVIDE ANY FURTHER INFORMATION.*AK

Nov 5, 2001 Fire

WHEN I STARTED THE ENGINE IN THE MORNING, THERE WAS A LOUD BANG, FOLLOWED BY SMOKE COMING FROM UNDER THE HOOD. I OPENED THE HOOD, AND THERE WAS A FIRE COMING FROM THE ENGINE.*AK

Jul 10, 2001

WHEN DRIVING SUSPENSION IS ROUGH. WHEN APPLING PRESSURE VEHICLE SHAKES. DEALERSHIP IS AWARE OF PROBLEM.*AK DEALER REFUSES TO REPLACE THE SHOCKS. AIR CONDITIONER LEAK, DEALER REPLACED COMPRESSOR SHAFT SEAL. PRESSURE OCNTROL SOLENOID REPLACED, CONSUMER STATED WHEN SHIFTING INTO REVERSE OR DRIVE, THERE IS A SHUDDER FELT AT TIMES, DEALER REPLACED THE TURBINE SHAFT SEAL BECAUSE IT WAS WORN AND AGAIN THE VEHICLE JUMPS WHEN PUTTING INTO GEAR AS IF GEAR IS NOT ENGAGING, DEALER CAN NOT REMEDY THIS PROBLEM. ENGINE LIGHT HAS ILLUMINATED. FRONT ROTORS WARPED CAUSING VIBRATION. TURN SIGNALS INOPERABLE, DEALER FOUND WIRE OUT OF TERMINAL. *SLC

Jun 8, 2001

AFTER COMING TO A COMPLETE STOP OR WHEN MAKING A VERY SLOW TURN, VEHICLE WILL STALL.DEALER HAS INSPECTED VEHICLE NUMEROUS TIMES OVER LAST YEAR, AND REPLACED COMPUTER. HOWEVER IT DID NOT REMEDY DEFECT. *AK OCCURS INTERMITTENTLY. WHEN THE DRIVER WAS IN LINE OF HEAVY TRAFFIC WAITING TO MAKE A LEFT TURN AT A VERY BUSY INTERSECTION AND THE ENGINE QUIT IN THE MIDST OF THE TURN. *YH

Jan 8, 2001 Crash

WHILE TRAVELING 35MPH VEHICLE STALLS FOR NO REASON UNDER VARIABLE CONDITIONS. THIS INCIDENT HAD OCCURRED SEVERAL TIMES, AND HAS RESULTED IN ACCIDENTS. *AK

Oct 18, 2000

WHILE DRIVING 20- 35 MPH ON FOUR OCCAISIONS ENGINE COMPLETELY SHUT DOWN WITHOUT WARNING. DEALER REPLACED CRANKSHAFT POSITIONING SENSOR AND FAULTY IGNITION MODULE WHICH DID CORRECT THE PROBLEM. ALSO, CONSUMER STATED THERE WA SNO NO CORRECTION FOR THE PROBLEM . PLEASE GIVE ANY FURTHER DETAILS. *AK

Jan 7, 2000

POSSIBLE COMPUTER PROBLEMS CAUSED OIL PRESSURE GAUGE LIGHT TO ILLUMINATE, LOSS OF POWER AND CAUSED THE VEHICLE TO STALL. *NLM

Aug 12, 1999

HORN SOUNDS WHEN VEHICLE STEERING WHEEL IS BEING TURNED TO THE RIGHT. VEHICLE BEGINS TO VIBRATE AT 65 MPH. WHEN VEHICLE HAS BEEN DRIVEN AT LEAST 5 MILES, THE TRANSMISSION SEEMS TO LOCK UP OR REMAIN IN HIGH GEAR AND GIVES THE DRIVER THE IMPRESSION THAT THE VEHICLE IS STALLING. SEVERAL TIMES THE VEHICLE, FAILED TO LOCATE THE CORRECT GEAR, RESULTING IN A NEAR MISS COLLISION WITH ANOTHER VEHICLE THAT WAS APPROACHING THE INTERSECTION.