10
Complaints
0
Crashes
2
Fires
0
Deaths
!

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Engine Complaints

Showing 10 of 10
May 14, 2021

ENGINE INTAKE GASKET FAILURE

May 14, 2021

ENGINE INTAKE GASKET FAILURE

Aug 27, 2019 59,000 mi

TL* THE CONTACT OWNS A 2005 BUICK LESABRE. WHILE DRIVING 60 MPH ON THE FREEWAY, THE CHECK ENGINE WARNING INDICATOR ILLUMINATED. THE CONTACT ATTEMPTED TO DEPRESS THE ACCELERATOR PEDAL, WHICH FAILED TO ENGAGE AND CAUSED THE VEHICLE TO DECELERATE. THE CONTACT MANAGED TO DRIVE THE VEHICLE TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE CO2 SENSORS NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED; HOWEVER, THE VEHICLE STALLED WITHOUT WARNING AFTER TWO YEARS. THE VEHICLE WAS TAKEN BACK TO THE INDEPENDENT MECHANIC WHERE MULTIPLE DIAGNOSTIC TESTS WERE PERFORMED, BUT NO FAILURE CODES APPEARED. THE INDEPENDENT MECHANIC STATED THAT THEY WOULD REPLACE THE MASS AIR FLOW SENSORS FOR THE CONTACT'S SAFETY. THE VEHICLE WAS NOT REPAIRED. BROWN & WOOD INC. (329 GREENVILLE BLVD SW, GREENVILLE, NC 27834, (252) 227-0948) WAS CONTACTED AND ADVISED THE CONTACT TO CALL THE MANUFACTURER FOR FURTHER REPAIR INFORMATION. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND INFORMED THE CONTACT THAT THE VIN WAS NOT INCLUDED IN A RECALL. THE FAILURE MILEAGE WAS APPROXIMATELY 59,000.

Aug 27, 2019 59,000 mi

TL* THE CONTACT OWNS A 2005 BUICK LESABRE. WHILE DRIVING 60 MPH ON THE FREEWAY, THE CHECK ENGINE WARNING INDICATOR ILLUMINATED. THE CONTACT ATTEMPTED TO DEPRESS THE ACCELERATOR PEDAL, WHICH FAILED TO ENGAGE AND CAUSED THE VEHICLE TO DECELERATE. THE CONTACT MANAGED TO DRIVE THE VEHICLE TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE CO2 SENSORS NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED; HOWEVER, THE VEHICLE STALLED WITHOUT WARNING AFTER TWO YEARS. THE VEHICLE WAS TAKEN BACK TO THE INDEPENDENT MECHANIC WHERE MULTIPLE DIAGNOSTIC TESTS WERE PERFORMED, BUT NO FAILURE CODES APPEARED. THE INDEPENDENT MECHANIC STATED THAT THEY WOULD REPLACE THE MASS AIR FLOW SENSORS FOR THE CONTACT'S SAFETY. THE VEHICLE WAS NOT REPAIRED. BROWN & WOOD INC. (329 GREENVILLE BLVD SW, GREENVILLE, NC 27834, (252) 227-0948) WAS CONTACTED AND ADVISED THE CONTACT TO CALL THE MANUFACTURER FOR FURTHER REPAIR INFORMATION. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND INFORMED THE CONTACT THAT THE VIN WAS NOT INCLUDED IN A RECALL. THE FAILURE MILEAGE WAS APPROXIMATELY 59,000.

Nov 6, 2015 Fire 108,000 mi

2014 CAR CAUGHT FIRE WHILE DRIVING ON CITY STREET AND HAD TO BE TOTALED BY THE INSURANCE COMPANY.

Nov 6, 2015 Fire 108,000 mi

2014 CAR CAUGHT FIRE WHILE DRIVING ON CITY STREET AND HAD TO BE TOTALED BY THE INSURANCE COMPANY.

Aug 21, 2014 47,800 mi

TL* THE CONTACT OWNS A 2005 BUICK LESABRE. WHILE DRIVING 3 MPH, THE VEHICLE SUDDENLY STALLED WITHOUT WARNING. THE VEHICLE WAS ABLE TO BE RESTARTED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE VIN WAS UNAVAILABLE. THE FAILURE MILEAGE WAS 47,800.

Aug 21, 2014 47,800 mi

TL* THE CONTACT OWNS A 2005 BUICK LESABRE. WHILE DRIVING 3 MPH, THE VEHICLE SUDDENLY STALLED WITHOUT WARNING. THE VEHICLE WAS ABLE TO BE RESTARTED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE VIN WAS UNAVAILABLE. THE FAILURE MILEAGE WAS 47,800.

Oct 22, 2013 48,000 mi

TL* THE CONTACT OWNS A 2005 BUICK LESABRE. THE CONTACT STATED THAT WHILE DRIVING VARIOUS SPEEDS, THE VEHICLE BEGAN TO EXHIBIT HESITATION AND A SEVERE VIBRATION. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE THE MOTOR MOUNT AND GASKET WERE REPLACED. THE MANUFACTURER WAS NOTIFIED OF THE PROBLEM. THE APPROXIMATE FAILURE MILEAGE WAS 48,000. ...UPDATED 12-24-13 *BF THE LOWER INTAKE GASKET WAS FAULTY AND LEAKING OIL AND COOLANT. THE TECHNICIAN ALSO FOUND THE PLASTIC UPPER INTAKE PLENUM WARPED AND LEAKING COOLANT INTO THE LOWER INTAKE MANIFOLD CAUSING THE ENGINE TO MISFIRE. UPDATED 12/31/13

Oct 22, 2013 48,000 mi

TL* THE CONTACT OWNS A 2005 BUICK LESABRE. THE CONTACT STATED THAT WHILE DRIVING VARIOUS SPEEDS, THE VEHICLE BEGAN TO EXHIBIT HESITATION AND A SEVERE VIBRATION. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE THE MOTOR MOUNT AND GASKET WERE REPLACED. THE MANUFACTURER WAS NOTIFIED OF THE PROBLEM. THE APPROXIMATE FAILURE MILEAGE WAS 48,000. ...UPDATED 12-24-13 *BF THE LOWER INTAKE GASKET WAS FAULTY AND LEAKING OIL AND COOLANT. THE TECHNICIAN ALSO FOUND THE PLASTIC UPPER INTAKE PLENUM WARPED AND LEAKING COOLANT INTO THE LOWER INTAKE MANIFOLD CAUSING THE ENGINE TO MISFIRE. UPDATED 12/31/13