18
Complaints
0
Crashes
0
Fires
0
Deaths

This Problem Across All Years

All Electrical System Complaints

Showing 18 of 18
Sep 20, 2012 192,800 mi

TL* THE CONTACT OWNS A 1995 BUICK ROADMASTER. THE CONTACT STATED THAT THE HORN WOULD SOUND INDEPENDENTLY. THE FAILURE WAS SPORADIC BUT PROGRESSED INTO A CONTINUAL FAILURE. THE MALFUNCTION RECURRED WHETHER THE VEHICLE WAS IN OPERATION OR STATIONARY THE FUSE FOR THE HORN WAS DISENGAGED. THE VEHICLE HAD NOT BEEN DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE PROBLEM. THE APPROXIMATE FAILURE MILEAGE WAS 192,800.

Sep 20, 2012 192,800 mi

TL* THE CONTACT OWNS A 1995 BUICK ROADMASTER. THE CONTACT STATED THAT THE HORN WOULD SOUND INDEPENDENTLY. THE FAILURE WAS SPORADIC BUT PROGRESSED INTO A CONTINUAL FAILURE. THE MALFUNCTION RECURRED WHETHER THE VEHICLE WAS IN OPERATION OR STATIONARY THE FUSE FOR THE HORN WAS DISENGAGED. THE VEHICLE HAD NOT BEEN DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE PROBLEM. THE APPROXIMATE FAILURE MILEAGE WAS 192,800.

Sep 14, 2004 83,225 mi

WHEN THE CONSUMER ATTEMPTED TO USE THE HORN IT DID NOT WORK. *AK THE HORN WIRING WAS REPAIRED. *JB

Sep 14, 2004 83,225 mi

WHEN THE CONSUMER ATTEMPTED TO USE THE HORN IT DID NOT WORK. *AK THE HORN WIRING WAS REPAIRED. *JB

Dec 10, 2003 40,000 mi

ONCE THE FUEL GAUGE REGISTERED HALF FULL IT WOULD STOP OPERATING. THE DEALER FOUND THAT THE ELECTRICAL WIRING TO THE FUEL PUMP HAD MELTED AND THE FUEL PUMP HAD TO BE REPLACED. *AK *CB THE REAR TAIL LIGHT ASSEMBLY WAS CRACKED.*JB

Dec 10, 2003 40,000 mi

ONCE THE FUEL GAUGE REGISTERED HALF FULL IT WOULD STOP OPERATING. THE DEALER FOUND THAT THE ELECTRICAL WIRING TO THE FUEL PUMP HAD MELTED AND THE FUEL PUMP HAD TO BE REPLACED. *AK *CB THE REAR TAIL LIGHT ASSEMBLY WAS CRACKED.*JB

Oct 27, 2003

PROBLEMS STARTING VEHICLE, AND ONCE STARTED VEHICLE STALLS.*MR CONSUMER HAD BATTERY REPLACED AT 1 1/2 YEARS. STARTER WAS REPLACED.*TS

Oct 27, 2003

PROBLEMS STARTING VEHICLE, AND ONCE STARTED VEHICLE STALLS.*MR CONSUMER HAD BATTERY REPLACED AT 1 1/2 YEARS. STARTER WAS REPLACED.*TS

Oct 27, 2003

PROBLEMS STARTING VEHICLE, AND ONCE STARTED VEHICLE STALLS.*MR CONSUMER HAD BATTERY REPLACED AT 1 1/2 YEARS. STARTER WAS REPLACED.*TS

Oct 27, 2003

PROBLEMS STARTING VEHICLE, AND ONCE STARTED VEHICLE STALLS.*MR CONSUMER HAD BATTERY REPLACED AT 1 1/2 YEARS. STARTER WAS REPLACED.*TS

Jun 26, 2003

THE HORN BUTTON WORE OUT, WHICH CAUSED THE HORN TO BLARE INTERMITTENTLY WHILE DRIVING. THE CONSUMER STATED THE HORN HAD COMPLETELY FAILED. *JB *TS *JB

Jun 26, 2003

THE HORN BUTTON WORE OUT, WHICH CAUSED THE HORN TO BLARE INTERMITTENTLY WHILE DRIVING. THE CONSUMER STATED THE HORN HAD COMPLETELY FAILED. *JB *TS *JB

Jul 1, 1996

STARTER FAILED.

Jul 1, 1996

STARTER FAILED.

Mar 5, 1996

KEY STICKS IN IGNITION. *SD

Mar 5, 1996

KEY STICKS IN IGNITION. *SD

Dec 18, 1995

LOOSE WIRE, CAUSING HEADLIGHT SWITCH FAILURE. *AK

Dec 18, 1995

LOOSE WIRE, CAUSING HEADLIGHT SWITCH FAILURE. *AK