18
Complaints
2
Crashes
0
Fires
0
Deaths
!

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Engine And Engine Cooling Complaints

Showing 18 of 18
Jun 9, 2004 82,480 mi

STARTING WITH DIC MESSAGE OF "LOW COOLANT", I HAVE EXPERIENCED AN ENGINE OVERHEATING PROBLEM. AFTER THE CADILLAC DEALER IN DURANGO COLORADO WAS UNABLE TO FIND A PROBLEM ( REPLACED HOSES, WATER PUMP), MY MECHANIC (IN ALBUQUERQUE)FOUND A CRACKED HEAD THAT WAS LEAKING COOLANT INTERNALY. FIXED THE HEAD, BUT NOW THE HEAD BOLT HOLES STRIPPED. USED OVERSIZED HELICOILS , BUT BLOCK MATERIAL STILL TO SOFT AND CANNOT TORQUE DOWN THE HEAD BOLTS WITHOUT PULLING HELICOILS. ALUMINUM METAL GOT TO SOFT AND HAVE TO REPLACE THE ENGINE. THIS ENGIN ONLY HAS 82K+ MILES AND SHOULD NOT BE DOING THIS. ALUMINIUM FOR BLOCK/HEAD MATERIA IS STUPIDITY. WEIGHT SAVINGS CANNOT BE THAT MUCH TO HAVE SHORTER LIFE OF AN ENGINE.L *AK

Jun 9, 2004 82,480 mi

STARTING WITH DIC MESSAGE OF "LOW COOLANT", I HAVE EXPERIENCED AN ENGINE OVERHEATING PROBLEM. AFTER THE CADILLAC DEALER IN DURANGO COLORADO WAS UNABLE TO FIND A PROBLEM ( REPLACED HOSES, WATER PUMP), MY MECHANIC (IN ALBUQUERQUE)FOUND A CRACKED HEAD THAT WAS LEAKING COOLANT INTERNALY. FIXED THE HEAD, BUT NOW THE HEAD BOLT HOLES STRIPPED. USED OVERSIZED HELICOILS , BUT BLOCK MATERIAL STILL TO SOFT AND CANNOT TORQUE DOWN THE HEAD BOLTS WITHOUT PULLING HELICOILS. ALUMINUM METAL GOT TO SOFT AND HAVE TO REPLACE THE ENGINE. THIS ENGIN ONLY HAS 82K+ MILES AND SHOULD NOT BE DOING THIS. ALUMINIUM FOR BLOCK/HEAD MATERIA IS STUPIDITY. WEIGHT SAVINGS CANNOT BE THAT MUCH TO HAVE SHORTER LIFE OF AN ENGINE.L *AK

Apr 1, 2003 40,000 mi

WHEN THE VEHICLE CAME TO A STOP, THE ENGINE STALLED, WHICH RESULTED IN LOSS OF POWER STEERING, THE DEALER WAS UNABLE TO DUPLICATE THE PROBLEM. *JB

Apr 1, 2003 40,000 mi

WHEN THE VEHICLE CAME TO A STOP, THE ENGINE STALLED, WHICH RESULTED IN LOSS OF POWER STEERING, THE DEALER WAS UNABLE TO DUPLICATE THE PROBLEM. *JB

May 21, 2001

WHEN MAKING A TURN THERE IS A SCRUBBING NOISE HEARD IN STEERING WHEEL. DEALER HAS INSPECTED VEHICLE SEVERAL TIMES.*AK CONSUMER ALSO STATES AIR CONDITION WILL NOT BLOW OUT DASH VENTS, COMES OUT AT THE BOTTOM AND IN BACK, ALSO CONSUMER STATES THERE IS ENGINE NOISE. *JB

May 21, 2001

WHEN MAKING A TURN THERE IS A SCRUBBING NOISE HEARD IN STEERING WHEEL. DEALER HAS INSPECTED VEHICLE SEVERAL TIMES.*AK CONSUMER ALSO STATES AIR CONDITION WILL NOT BLOW OUT DASH VENTS, COMES OUT AT THE BOTTOM AND IN BACK, ALSO CONSUMER STATES THERE IS ENGINE NOISE. *JB

Feb 10, 2000

VEHICLE WILL STALL ON DEACCELERATION INTERMITTENTLY AND WITHOUT WARNING MOSTLY DURING WINTER MONTHS,CAUSE IS UNKNOWN.PLEASE PROVIDE FURTHER INFORMATION. *AK

Feb 10, 2000

VEHICLE WILL STALL ON DEACCELERATION INTERMITTENTLY AND WITHOUT WARNING MOSTLY DURING WINTER MONTHS,CAUSE IS UNKNOWN.PLEASE PROVIDE FURTHER INFORMATION. *AK

Feb 7, 2000 Crash

VEHICLE HAS EXPERIENCED CONTINUED ENGINE FAILURE (SHUT DOWN)ON ONE OCCASION WHILE DRIVING 40 MPH ACCIDENT OCCURRED DUE TO ENGINE SHUT DOWN (BRAKE,STEERING LOSS),VIOLENT DEPLOYMENT OF AIR BAG RESULTED IN INJURIES. YH

Feb 7, 2000 Crash

VEHICLE HAS EXPERIENCED CONTINUED ENGINE FAILURE (SHUT DOWN)ON ONE OCCASION WHILE DRIVING 40 MPH ACCIDENT OCCURRED DUE TO ENGINE SHUT DOWN (BRAKE,STEERING LOSS),VIOLENT DEPLOYMENT OF AIR BAG RESULTED IN INJURIES. YH

Feb 1, 1999

EXHAUST SYSTEM FAILED ON TWO OCCASIONS. *YC

Feb 1, 1999

EXHAUST SYSTEM FAILED ON TWO OCCASIONS. *YC

Sep 10, 1998

ENGINE BACKFIRES AND USES EXCESSIVE OIL.

Sep 10, 1998

ENGINE BACKFIRES AND USES EXCESSIVE OIL.

May 22, 1998

ENGINE GASKET BLEW OUT DUE TO POOR WORKMANSHIP. IN ADDITION, REPLACED WATER PUMP. *AK

May 22, 1998

ENGINE GASKET BLEW OUT DUE TO POOR WORKMANSHIP. IN ADDITION, REPLACED WATER PUMP. *AK

May 22, 1998

ENGINE GASKET BLEW OUT DUE TO POOR WORKMANSHIP. IN ADDITION, REPLACED WATER PUMP. *AK

May 22, 1998

ENGINE GASKET BLEW OUT DUE TO POOR WORKMANSHIP. IN ADDITION, REPLACED WATER PUMP. *AK