14
Complaints
0
Crashes
6
Fires
0
Deaths
!

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Engine And Engine Cooling Complaints

Showing 14 of 14
Dec 10, 2021 Fire 215,000 mi

The contact owns a 2004 Chevrolet Monte Carlo. The contact stated that while operating the vehicle, there was a burning odor blowing through the air vents into the cabin of the vehicle. While depressing the accelerator pedal, the oil gauge increased to high. Additionally, the engine overheated. The vehicle was taken to the local dealer regarding NHTSA Campaign Number: 15V201000 (Engine and Engine Cooling) however, the part had to be ordered,ed and the vehicle was not yet repaired. The manufacturer was not yet contacted. The failure mileage was 215,000.

Dec 10, 2021 Fire 215,000 mi

The contact owns a 2004 Chevrolet Monte Carlo. The contact stated that while operating the vehicle, there was a burning odor blowing through the air vents into the cabin of the vehicle. While depressing the accelerator pedal, the oil gauge increased to high. Additionally, the engine overheated. The vehicle was taken to the local dealer regarding NHTSA Campaign Number: 15V201000 (Engine and Engine Cooling) however, the part had to be ordered,ed and the vehicle was not yet repaired. The manufacturer was not yet contacted. The failure mileage was 215,000.

Mar 16, 2017 135,652 mi

TL* THE CONTACT OWNS A 2004 CHEVROLET MONTE CARLO. THE CONTACT STATED THAT ENGINE OIL WAS DRIPPING FROM THE MANIFOLD. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE PART NEEDED TO BE REPLACED. THE VEHICLE HAD NOT BEEN REPAIRED. THE MANUFACTURER WAS NOTIFIED. THE VIN WAS UNKNOWN. THE FAILURE MILEAGE WAS 135,652.

Mar 16, 2017 135,652 mi

TL* THE CONTACT OWNS A 2004 CHEVROLET MONTE CARLO. THE CONTACT STATED THAT ENGINE OIL WAS DRIPPING FROM THE MANIFOLD. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE PART NEEDED TO BE REPLACED. THE VEHICLE HAD NOT BEEN REPAIRED. THE MANUFACTURER WAS NOTIFIED. THE VIN WAS UNKNOWN. THE FAILURE MILEAGE WAS 135,652.

Jul 16, 2015 107,000 mi

TL* THE CONTACT OWNS A 2004 CHEVROLET MONTE CARLO. WHEN THE CONTACT PLACED OIL INTO THE VEHICLE, OIL LEAKED ONTO THE MANIFOLD. THE CHANGE OIL AND LOW ENGINE OIL INDICATORS ILLUMINATED. THE FAILURE RECURRED FOUR OR FIVE TIMES. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE ENGINE OIL WAS DRIPPING ON THE MANIFOLD AND THE GASKET AND WIRING NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER STATED THAT THE VIN WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 15V201000 (ENGINE AND ENGINE COOLING). THE APPROXIMATE FAILURE MILEAGE WAS 107,000.

Jul 16, 2015 107,000 mi

TL* THE CONTACT OWNS A 2004 CHEVROLET MONTE CARLO. WHEN THE CONTACT PLACED OIL INTO THE VEHICLE, OIL LEAKED ONTO THE MANIFOLD. THE CHANGE OIL AND LOW ENGINE OIL INDICATORS ILLUMINATED. THE FAILURE RECURRED FOUR OR FIVE TIMES. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE ENGINE OIL WAS DRIPPING ON THE MANIFOLD AND THE GASKET AND WIRING NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER STATED THAT THE VIN WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 15V201000 (ENGINE AND ENGINE COOLING). THE APPROXIMATE FAILURE MILEAGE WAS 107,000.

Jun 3, 2009 Fire 82,000 mi

TL*THE CONTACT OWNS A 2004 CHEVROLET MONTE CARLO. WHILE DRIVING APPROXIMATELY 55 MPH, THE VEHICLE LOST POWER. THE CONTACT PULLED THE VEHICLE OVER TO THE SIDE OF THE ROAD. UPON FURTHER INSPECTION, HE NOTICED FLAMES NEAR THE ENGINE. HE WAS ABLE TO SAFELY EXTINGUISH THE FIRE. THE VEHICLE WAS TOWED TO A DEALER TO DETERMINE THE CAUSE OF THE FAILURE. THE REPAIR WOULD COST $7,000. THE VEHICLE WAS EXCLUDED FROM NHTSA CAMPAIGN ID NUMBER 09V116000 (ENGINE AND ENGINE COOLING), ALTHOUGH THE FAILURES WERE IDENTICAL. THE VIN WAS UNKNOWN. THE FAILURE AND CURRENT MILEAGES WERE 82,000.

Jun 3, 2009 Fire 82,000 mi

TL*THE CONTACT OWNS A 2004 CHEVROLET MONTE CARLO. WHILE DRIVING APPROXIMATELY 55 MPH, THE VEHICLE LOST POWER. THE CONTACT PULLED THE VEHICLE OVER TO THE SIDE OF THE ROAD. UPON FURTHER INSPECTION, HE NOTICED FLAMES NEAR THE ENGINE. HE WAS ABLE TO SAFELY EXTINGUISH THE FIRE. THE VEHICLE WAS TOWED TO A DEALER TO DETERMINE THE CAUSE OF THE FAILURE. THE REPAIR WOULD COST $7,000. THE VEHICLE WAS EXCLUDED FROM NHTSA CAMPAIGN ID NUMBER 09V116000 (ENGINE AND ENGINE COOLING), ALTHOUGH THE FAILURES WERE IDENTICAL. THE VIN WAS UNKNOWN. THE FAILURE AND CURRENT MILEAGES WERE 82,000.

Apr 5, 2006 32,161 mi

DT*: THE CONTACT STATED WHILE DRIVING 40 MPH,THE VEHICLE LOST POWER WITHOUT WARNING. NO DASH PANEL LIGHTS ILLUMINATED TO INDICATE A FAILURE. THE ENGINE WAS EASILY RESTARTED, BUT THE VEHICLE WAS TAKEN TO A DEALER FOR INSPECTION. A DIAGNOSTIC TEST WAS PERFORMED WHICH INDICATED THE FUEL RELAY CONNECTOR HOSE WAS LOOSE. ALTHOUGH THIS WAS REPAIRED, THE PROBLEM PERSISTED. THE VEHICLE IS CURRENTLY AT THE DEALERSHIP AWAITING FURTHER INSPECTION. UPDATED ON 05/16/2006. THE BRAKES PULSATED WHILE BRAKING. THE DEALER REPLACED THE ROTORS BECAUSE THE WERE PITTED AND WARPED. THEY ALSO REPLACED THE REAR BRAKES. *AK *NM

Apr 5, 2006 32,161 mi

DT*: THE CONTACT STATED WHILE DRIVING 40 MPH,THE VEHICLE LOST POWER WITHOUT WARNING. NO DASH PANEL LIGHTS ILLUMINATED TO INDICATE A FAILURE. THE ENGINE WAS EASILY RESTARTED, BUT THE VEHICLE WAS TAKEN TO A DEALER FOR INSPECTION. A DIAGNOSTIC TEST WAS PERFORMED WHICH INDICATED THE FUEL RELAY CONNECTOR HOSE WAS LOOSE. ALTHOUGH THIS WAS REPAIRED, THE PROBLEM PERSISTED. THE VEHICLE IS CURRENTLY AT THE DEALERSHIP AWAITING FURTHER INSPECTION. UPDATED ON 05/16/2006. THE BRAKES PULSATED WHILE BRAKING. THE DEALER REPLACED THE ROTORS BECAUSE THE WERE PITTED AND WARPED. THEY ALSO REPLACED THE REAR BRAKES. *AK *NM

Mar 1, 2006 22,965 mi

DT*: THE CONTACT STATED, INTERMITTENTLY, THE VEHICLE STALLED AT ANY SPEED. ONCE, THE BATTERY LIGHT ILLUMINATED THEN THE VEHICLE STALLED. THE OTHER TIMES, THE CHECK ENGINE LIGHT ILLUMINATED PRIOR TO THE VEHICLE STALLING. THE VEHICLE DID RESTART EACH TIME. THE DEALERSHIP CLEANED THE MAP SENSOR CONNECTOR; THIS DID NOT CORRECT THE PROBLEM.

Mar 1, 2006 22,965 mi

DT*: THE CONTACT STATED, INTERMITTENTLY, THE VEHICLE STALLED AT ANY SPEED. ONCE, THE BATTERY LIGHT ILLUMINATED THEN THE VEHICLE STALLED. THE OTHER TIMES, THE CHECK ENGINE LIGHT ILLUMINATED PRIOR TO THE VEHICLE STALLING. THE VEHICLE DID RESTART EACH TIME. THE DEALERSHIP CLEANED THE MAP SENSOR CONNECTOR; THIS DID NOT CORRECT THE PROBLEM.

Nov 22, 2004 Fire

AT 2700 MILES IT BLEW THE ENGINE. REPLACED ENGINE AND DROVE HOME, WHOLE FRONT STARTED ON FIRE. *BF THE CONSUMER WAS INFORMED THAT THE FIRE WAS FROM A GAS LEAK IN THE PIPE. THE CONSUMER FELT THAT THE FAULT WAS DUE TO GREEN CHEVY MECHANICS. PER INVOICE: THE ENGINE LIGHT HAD COME ON, FOUND CODES FOR ENGINE MISFIRE, CYLINDER #3, KNOCK SENSOR MELTED, PERFORMED COMPRESSION TEST, CYLINDER #3 SHOWED ZERO COMPRESSION, REMOVED #3 SPARK PLUGS, ELECTRODE WAS GONE, REMOVED THE ENGINE, DISASSEMBLED THE ENGINE DOWN TO THE PISTONS, HOLES WERE PRESENT IN THE PISTON, CYLINDER WALLS WERE SEVERELY GOUGED AND THE ENGINE ASSEMBLY NEEDED TO BE REPLACED. *SC

Nov 22, 2004 Fire

AT 2700 MILES IT BLEW THE ENGINE. REPLACED ENGINE AND DROVE HOME, WHOLE FRONT STARTED ON FIRE. *BF THE CONSUMER WAS INFORMED THAT THE FIRE WAS FROM A GAS LEAK IN THE PIPE. THE CONSUMER FELT THAT THE FAULT WAS DUE TO GREEN CHEVY MECHANICS. PER INVOICE: THE ENGINE LIGHT HAD COME ON, FOUND CODES FOR ENGINE MISFIRE, CYLINDER #3, KNOCK SENSOR MELTED, PERFORMED COMPRESSION TEST, CYLINDER #3 SHOWED ZERO COMPRESSION, REMOVED #3 SPARK PLUGS, ELECTRODE WAS GONE, REMOVED THE ENGINE, DISASSEMBLED THE ENGINE DOWN TO THE PISTONS, HOLES WERE PRESENT IN THE PISTON, CYLINDER WALLS WERE SEVERELY GOUGED AND THE ENGINE ASSEMBLY NEEDED TO BE REPLACED. *SC