2007 DODGE MAGNUM Engine And Engine Cooling Problems

10 complaints about Engine And Engine Cooling

10
Complaints
0
Crashes
0
Fires
0
Deaths

This Problem Across All Years

All Engine And Engine Cooling Complaints (10)

Jun 22, 2016

TL* THE CONTACT OWNS A 2007 DODGE MAGNUM. WHILE THE VEHICLE WAS PARKED WITH THE ENGINE RUNNING, THE CONTACT HEARD A LOUD NOISE. THE CONTACT NOTICED UNDER THE VEHICLE THAT THE RADIATOR FAN WAS PUNCTURED AND SHATTERED. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC, BUT WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 171,000.

Mileage: 171,000

Aug 14, 2014

TL* THE CONTACT OWNS A 2007 DODGE MAGNUM. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 45 MPH, THE VEHICLE MADE A LOUD ABNORMAL NOISE. AFTER INSPECTING THE VEHICLE, THE CONTACT NOTICED THAT THE RADIATOR FAN HAD SEPARATED CAUSING DAMAGE TO THE RADIATOR. THE CONTACT REPLACED BOTH THE RADIATOR FAN AND RADIATOR. THE MANUFACTURER HAD BEEN NOTIFIED OF THE FAILURE. THE APPROXIMATELY FAILURE MILEAGE WAS 136,962. ..UPDATED 11/11/14*BF *BF UPDATED 12/02/14*JB

Mileage: 136,962

Aug 14, 2014

TL* THE CONTACT OWNS A 2007 DODGE MAGNUM. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 45 MPH, THE VEHICLE MADE A LOUD ABNORMAL NOISE. AFTER INSPECTING THE VEHICLE, THE CONTACT NOTICED THAT THE RADIATOR FAN HAD SEPARATED CAUSING DAMAGE TO THE RADIATOR. THE CONTACT REPLACED BOTH THE RADIATOR FAN AND RADIATOR. THE MANUFACTURER HAD BEEN NOTIFIED OF THE FAILURE. THE APPROXIMATELY FAILURE MILEAGE WAS 136,962. ..UPDATED 11/11/14*BF *BF UPDATED 12/02/14*JB

Mileage: 136,962

Jul 19, 2013

FIRST INSTANCE, WHILE SLOWING DOWN FOR A STOP LIGHT FELT A SHUDDER AND ENGINE SHUT OFF, ALL OTHER SYSTEMS APPEARED NORMAL. COASTED TO STOP, ENGINE RESTARTED WITHOUT TROUBLE. NEAR FULL TANK OF FUEL. SECOND INSTANCE, WHILE IN A PARKING LOT SHIFTING FROM PARK TO REVERSE ENGINE SHUT OFF, ALL OTHER SYSTEMS APPEARED NORMAL AND ENGINE RESTARTED WITHOUT TROUBLE. FILLED FUEL TANK THE PREVIOUS DAY, 3/4 TANK TODAY. HAS HAPPENED ON OTHER OCCASIONS WHILE DRIVING AT SLOW SPEEDS BUT I DO NOT REMEMBER THE QUANTITY OF FUEL, EACH TIME THAT CAR HAS RESTARTED WITHOUT INSTANCE AND EACH TIME EVERYTHING ELSE APPEARED NORMAL. THE ENGINE ALWAYS SEEMS TO RUN PROPERLY AND ALL OF THE CARS OTHER SYSTEMS SEEM TO OPERATE NORMALLY. *TR

Mileage: 102,000

Oct 19, 2012

CAR WOULD NOT SHIFT OUT OF PARK. PLASTIC RETAINER INSIDE THE SHIFTER ASSEMBLY WAS BROKEN. REMOVED SHIFTER ASSEMBLY AND DISASSEMBLED. REPLACED BROKEN PLASTIC PART WITH NEW METAL PART, REASSEMBLED AND REINSTALLED SHIFTER AND VERIFIED OPERATION. PARTS 11.79 MISC 13.86 LABOR 277.20 DODGE REFUSED ANY GOODWILL, SHOULD BE A RECALL DUE TO DEFECTIVE ORIGINAL PARTS BEING REPLACED WITH NEW AND IMPROVED PARTS. *TR THE CONSUMER STATED RECENTLY, THE CHECK ENGINE AND ETC LIGHTS ILLUMINATED. THE LOCAL DODGE DEALER CONSUMER THE CONSUMER THE VEHICLE A VERY LOW COMPRESSION IN CYLINDER #5 AND RECOMMENDED HAVING A VALVE JOB, AS WELL AS REPLACING THE WATER PUMP AND TIMING BELT, AT A COST OF $3,500. THE CONSUMER FOUND A LOCAL REPAIR SHOP THAT WAS WILLING TO DO THE WORK FOR $2,103. WHILE FIXING THE VEHICLE, IT WAS DISCOVERED THAT ONE OF THE VALVE GUIDES ON CYLINDER #5 HAD LET THE STEM RUN AT AN ANGLE CUTTING A COLLAR INTO THE ALUMINUM ROCKER ARM. UPDATED 03/19/13

Mileage: 87,795

Sep 8, 2011

TL* THE CONTACT OWNS A 2007 DODGE MAGNUM RT. THE CONTACT WAS DRIVING 50 MPH WHEN THE VEHICLE OVERHEATED. THE VEHICLE WAS TAKEN TO THE DEALER WHO DIAGNOSED THAT THE COOLING FAN WAS FRACTURED AND HAD PUNCTURED THE RADIATOR. AS A RESULT, THE RADIATOR, FAN AND FAN MOTOR NEEDED TO BE REPLACED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE WHO DID NOT OFFER ANY ASSISTANCE SINCE THE VEHICLE WAS NOT INCLUDED IN ANY RECALLS. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND CURRENT MILEAGE WAS 55,000.

Mileage: 55,000

Aug 22, 2011

TL* THE CONTACT OWNS A 2007 DODGE MAGNUM. THE CONTACT STATED THE VEHICLE WOULD ROAR AND THEN DECELERATE WHEN ATTEMPTING TO ACCELERATE FROM A STOP. THE DEALER PERFORMED A SOFTWARE UPDATE HOWEVER, THE FAILURE PERSISTED. THE VEHICLE WAS TAKEN TO THE DEALER A SECOND TIME AND THE CONTACT WAS INFORMED THAT SHE NEEDED TO REPLACE THE ACTUATOR IDLE SENSOR AND THE UPPER INTAKE MANIFOLD. THE VEHICLE WAS ALSO TAKEN TO A PRIVATE MECHANIC WHO INFORMED THE CONTACT THAT THE VEHICLE WAS UNSAFE TO DRIVE. NO REPAIRS WERE PERFORMED. THE MANUFACTURER WAS AWARE OF THE FAILURE. THE CURRENT MILEAGE WAS 75,900. THE APPROXIMATE FAILURE MILEAGE WAS 35,000. UPDATED 01/03/12*LJ UPDATED 01/11/12

Mileage: 35,000

Aug 19, 2010

MY 2007 MAGNUM HAS 48K MILES AND RECENTLY HAD THE ENGINE LIGHT COME ON SHOWING CODE 1004. RESEARCH ONLINE SHOWS THIS CODE TO BE VERY PREVALENT WITH THIS MODEL OF DODGE, YET THEY CLAIM IT IS NOT AN ISSUE, AND ARE ASKING $1300+ FOR REPLACEMENT/PARTS FOR THE INTAKE AND SHORT-RUNNER ACTUATORS. AS WELL, MY SUNROOF TRACK FAILED AND THE SUNROOF WILL NOT MOVE. BOTH THE GUIDE ATTACHED TO THE GLASS AND THE SUNROOF ASSEMBLY BOTH HAVE BROKEN PLASTIC PARTS. *TR

Mileage: 47,598

Mar 11, 2009

2007 DODGE MAGNUM WHEN COMING TO A STOP OR IDLING ENGINE REVS UP AND GOES FORWARD A LITTLE. *TR

Mileage: 14,500

Feb 23, 2009

HEAT HAS BEEN OUT IN CAR 3 TIMES IN JUST OVER 1 YEAR BOUGHT CAR NEW IN NOV 2007 BY DEC 2008 HEAT WAS OUT FOR 3RD TIME, HAD TO PAY DEDUCTIBLE FOR REPAIR BECAUSE OF MILES PUT ON CAR. PART IS A COOLER UNIT THAT HAS BEEN REPLACED, TO THIS DAY WHEN TURN ON HEAT I SMELL ANTIFREEZE AND IT TAKES ABOUT 30 MINUTES FOR WARM AIR. *TR

Mileage: 43,000