14
Complaints
4
Crashes
6
Fires
0
Deaths
!

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Electrical System Complaints

Showing 14 of 14
May 11, 2018 180,500 mi

TAKATA THERE ARE SEVERAL THINGS THAT I HAVE SEEN AS A RECALL ON A DODGE STRATUS AND TRIED TO REPORT IT AND WHOMEVER I BE TALKING TO IS IN DENIAL ABOUT THAT MY CAR IS SHOWING ME THE SIGNS THAT IT'S NEEDS TO BE FIXED BECAUSE IT'S A MALFUNCTION MY BALL JOINT IS BAD BECAUSE OF THE FRONT RIGHT STEERING KNUCKLE HAS MESSED IT UP AND MY GAS GAUGE IS MESSED UP WITH THE ALARM AND TEMP CONTROL IS ALSO MESSED UP

May 11, 2018 180,500 mi

TAKATA THERE ARE SEVERAL THINGS THAT I HAVE SEEN AS A RECALL ON A DODGE STRATUS AND TRIED TO REPORT IT AND WHOMEVER I BE TALKING TO IS IN DENIAL ABOUT THAT MY CAR IS SHOWING ME THE SIGNS THAT IT'S NEEDS TO BE FIXED BECAUSE IT'S A MALFUNCTION MY BALL JOINT IS BAD BECAUSE OF THE FRONT RIGHT STEERING KNUCKLE HAS MESSED IT UP AND MY GAS GAUGE IS MESSED UP WITH THE ALARM AND TEMP CONTROL IS ALSO MESSED UP

Feb 25, 2017 Crash 121,517 mi

THE VEHICLE WAS PURCHASED IN 2013 " AS IS" (USED) F ROM A CAR LOT. THERE WERE AT LEAST 2 OR 3 ALIGNMENTS COMPLETED DUE TO REPAIRS ON RELATED PARTS. AFTER EACH ALIGNMENT, THE STEERING WHEEL WOULD TURN TO AN ANGLED POSITION AFTER A FEW DAYS OR A WEEK. WHEN TURNING THE STEERING WHEEL TO THE RIGHT OR TURNING IT TO THE RIGHT WHILE BACKING UP IN REVERSE, A LOUD POP CAN BE HEARD COMING FROM THE VEHICLE. THE NOISE HAS ALWAYS SEEMED TO COME FROM THE LEFT SIDE OF THE CAR. EVERYTHING SUGGESTED AS REPAIRS HAS BEEN DONE. BOTH BALL JOINTS WERE REPLACED. ALL FRONT AND BACK STRUTS WERE REPLACED. ALSO THERE HAS BEEN A PROBLEM WITH THE SUSPENSION CAUSING NOISE AND BOUNCING WHILE DRIVING. ALL OF THIS HAS HAPPENED ON CITY STREETS, DRIVING ABOUT 35 MPH OR MUCH LESS. A MECHANIC SUGGESTED IN 2013 THAT THE CAR MIGHT HAVE AN ELECTRICAL PROBLEM BUT ALMOST EVERYTHING HAS WORKED WELL FOR THE PAST 4 YEARS WITH NO PROBLEMS EXCEPT FOR THE WINDSHIELD WIPER SPEED WHICH DOES NOT WORK ON THE REGULAR BACK AND FORTH AND SUPER FAST SPEED. THE WIPER SWITCH WAS REPLACED WHICH DIDN'T HELP. A DODGE DEALERSHIP CHECKED IT LAST WEEK AND SAID THAT THE WIPER MOTOR WORKS. ONLY ONE OF MANY AUTO REPAIR PLACES TRIED TO CHARGE ME FOR AN ELEC ISSUE. ALSO IN 2013, THE FIRST CAR REPAIR SHOP I TOOK IT TO DID NOT DETECT ANY RECALLS AND THEY LISTED A DIFFERENT VIN # WHICH IS:[XXX], ON MY PAPERWORK. A DEALERSHIP TOLD ME IT WAS NOT VALID WHEN I CONTACTED IT FOR PARTS. A DIFFERENT VIN # IS ON THE CAR TITLE WHICH IS IN MY NAME. COULD THIS CAR BE PART OF A CHOP SHOP SCAM? I'VE HAD A PROBLEM TRYING TO FIND PARTS THAT MATCH THE COLOR AND YEAR ESPECIALLY FOR AN INSIDE DOOR PANEL. ALSO I FILED POLICE REPORTS BECAUSE SOMEONE HAS ENTERED THE CAR REPEATEDLY AND ILLEGALLY WITHOUT FORCED ENTRY AND MAY HAVE A KEY. THE SELLER OF THE CAR WAS DISHONEST WHEN THE CAR WAS PURCHASED. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TR

Feb 25, 2017 Crash 121,517 mi

THE VEHICLE WAS PURCHASED IN 2013 " AS IS" (USED) F ROM A CAR LOT. THERE WERE AT LEAST 2 OR 3 ALIGNMENTS COMPLETED DUE TO REPAIRS ON RELATED PARTS. AFTER EACH ALIGNMENT, THE STEERING WHEEL WOULD TURN TO AN ANGLED POSITION AFTER A FEW DAYS OR A WEEK. WHEN TURNING THE STEERING WHEEL TO THE RIGHT OR TURNING IT TO THE RIGHT WHILE BACKING UP IN REVERSE, A LOUD POP CAN BE HEARD COMING FROM THE VEHICLE. THE NOISE HAS ALWAYS SEEMED TO COME FROM THE LEFT SIDE OF THE CAR. EVERYTHING SUGGESTED AS REPAIRS HAS BEEN DONE. BOTH BALL JOINTS WERE REPLACED. ALL FRONT AND BACK STRUTS WERE REPLACED. ALSO THERE HAS BEEN A PROBLEM WITH THE SUSPENSION CAUSING NOISE AND BOUNCING WHILE DRIVING. ALL OF THIS HAS HAPPENED ON CITY STREETS, DRIVING ABOUT 35 MPH OR MUCH LESS. A MECHANIC SUGGESTED IN 2013 THAT THE CAR MIGHT HAVE AN ELECTRICAL PROBLEM BUT ALMOST EVERYTHING HAS WORKED WELL FOR THE PAST 4 YEARS WITH NO PROBLEMS EXCEPT FOR THE WINDSHIELD WIPER SPEED WHICH DOES NOT WORK ON THE REGULAR BACK AND FORTH AND SUPER FAST SPEED. THE WIPER SWITCH WAS REPLACED WHICH DIDN'T HELP. A DODGE DEALERSHIP CHECKED IT LAST WEEK AND SAID THAT THE WIPER MOTOR WORKS. ONLY ONE OF MANY AUTO REPAIR PLACES TRIED TO CHARGE ME FOR AN ELEC ISSUE. ALSO IN 2013, THE FIRST CAR REPAIR SHOP I TOOK IT TO DID NOT DETECT ANY RECALLS AND THEY LISTED A DIFFERENT VIN # WHICH IS:[XXX], ON MY PAPERWORK. A DEALERSHIP TOLD ME IT WAS NOT VALID WHEN I CONTACTED IT FOR PARTS. A DIFFERENT VIN # IS ON THE CAR TITLE WHICH IS IN MY NAME. COULD THIS CAR BE PART OF A CHOP SHOP SCAM? I'VE HAD A PROBLEM TRYING TO FIND PARTS THAT MATCH THE COLOR AND YEAR ESPECIALLY FOR AN INSIDE DOOR PANEL. ALSO I FILED POLICE REPORTS BECAUSE SOMEONE HAS ENTERED THE CAR REPEATEDLY AND ILLEGALLY WITHOUT FORCED ENTRY AND MAY HAVE A KEY. THE SELLER OF THE CAR WAS DISHONEST WHEN THE CAR WAS PURCHASED. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TR

Jul 26, 2013 Crash

A TRUCK MADE AN ILLEGAL LANE CHANGE AND HE HIT ME ON THE FRONT DRIVERS SIDE AND DAMAGED MY LIGHT, HOOD, WINDSHIELD, THE COMPUTER, AND OTHER THINGS UNDER THE HOOD. THE IMPACT WAS VERY STRONG AND NONE OF THE AIR BAGS DEPLOYED. *TR

Jul 26, 2013 Crash

A TRUCK MADE AN ILLEGAL LANE CHANGE AND HE HIT ME ON THE FRONT DRIVERS SIDE AND DAMAGED MY LIGHT, HOOD, WINDSHIELD, THE COMPUTER, AND OTHER THINGS UNDER THE HOOD. THE IMPACT WAS VERY STRONG AND NONE OF THE AIR BAGS DEPLOYED. *TR

May 27, 2008 Fire 52,500 mi

TL*THE CONTACT OWNS A 2005 DODGE STRATUS. THE CONTACT STATED THAT THERE WERE NO AIR BAGS AND NO HORN IN HER VEHICLE. IN ADDITION, THE CRUISE CONTROL AND FUEL GAUGE WERE NOT WORKING. SHE ALSO NOTICED THE IGNITION (WHERE THE KEY IS INSERTED) WAS SMOKING. THE DEALER PERFORMED A DIAGNOSTIC AND THE CONTACT WAS INFORMED THAT THE BATTERY WAS THE CAUSE OF THE FAILURE. SHE WAS LATER INFORMED THAT THERE WAS A FAULTY DIAGNOSTIC TEST; THEREFORE, THE BATTERY WAS NOT THE CAUSE OF THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 52,500.

May 27, 2008 Fire 52,500 mi

TL*THE CONTACT OWNS A 2005 DODGE STRATUS. THE CONTACT STATED THAT THERE WERE NO AIR BAGS AND NO HORN IN HER VEHICLE. IN ADDITION, THE CRUISE CONTROL AND FUEL GAUGE WERE NOT WORKING. SHE ALSO NOTICED THE IGNITION (WHERE THE KEY IS INSERTED) WAS SMOKING. THE DEALER PERFORMED A DIAGNOSTIC AND THE CONTACT WAS INFORMED THAT THE BATTERY WAS THE CAUSE OF THE FAILURE. SHE WAS LATER INFORMED THAT THERE WAS A FAULTY DIAGNOSTIC TEST; THEREFORE, THE BATTERY WAS NOT THE CAUSE OF THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 52,500.

May 27, 2008 Fire 52,500 mi

TL*THE CONTACT OWNS A 2005 DODGE STRATUS. THE CONTACT STATED THAT THERE WERE NO AIR BAGS AND NO HORN IN HER VEHICLE. IN ADDITION, THE CRUISE CONTROL AND FUEL GAUGE WERE NOT WORKING. SHE ALSO NOTICED THE IGNITION (WHERE THE KEY IS INSERTED) WAS SMOKING. THE DEALER PERFORMED A DIAGNOSTIC AND THE CONTACT WAS INFORMED THAT THE BATTERY WAS THE CAUSE OF THE FAILURE. SHE WAS LATER INFORMED THAT THERE WAS A FAULTY DIAGNOSTIC TEST; THEREFORE, THE BATTERY WAS NOT THE CAUSE OF THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 52,500.

May 27, 2008 Fire 52,500 mi

TL*THE CONTACT OWNS A 2005 DODGE STRATUS. THE CONTACT STATED THAT THERE WERE NO AIR BAGS AND NO HORN IN HER VEHICLE. IN ADDITION, THE CRUISE CONTROL AND FUEL GAUGE WERE NOT WORKING. SHE ALSO NOTICED THE IGNITION (WHERE THE KEY IS INSERTED) WAS SMOKING. THE DEALER PERFORMED A DIAGNOSTIC AND THE CONTACT WAS INFORMED THAT THE BATTERY WAS THE CAUSE OF THE FAILURE. SHE WAS LATER INFORMED THAT THERE WAS A FAULTY DIAGNOSTIC TEST; THEREFORE, THE BATTERY WAS NOT THE CAUSE OF THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 52,500.

May 27, 2008 Fire 52,500 mi

TL*THE CONTACT OWNS A 2005 DODGE STRATUS. THE CONTACT STATED THAT THERE WERE NO AIR BAGS AND NO HORN IN HER VEHICLE. IN ADDITION, THE CRUISE CONTROL AND FUEL GAUGE WERE NOT WORKING. SHE ALSO NOTICED THE IGNITION (WHERE THE KEY IS INSERTED) WAS SMOKING. THE DEALER PERFORMED A DIAGNOSTIC AND THE CONTACT WAS INFORMED THAT THE BATTERY WAS THE CAUSE OF THE FAILURE. SHE WAS LATER INFORMED THAT THERE WAS A FAULTY DIAGNOSTIC TEST; THEREFORE, THE BATTERY WAS NOT THE CAUSE OF THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 52,500.

May 27, 2008 Fire 52,500 mi

TL*THE CONTACT OWNS A 2005 DODGE STRATUS. THE CONTACT STATED THAT THERE WERE NO AIR BAGS AND NO HORN IN HER VEHICLE. IN ADDITION, THE CRUISE CONTROL AND FUEL GAUGE WERE NOT WORKING. SHE ALSO NOTICED THE IGNITION (WHERE THE KEY IS INSERTED) WAS SMOKING. THE DEALER PERFORMED A DIAGNOSTIC AND THE CONTACT WAS INFORMED THAT THE BATTERY WAS THE CAUSE OF THE FAILURE. SHE WAS LATER INFORMED THAT THERE WAS A FAULTY DIAGNOSTIC TEST; THEREFORE, THE BATTERY WAS NOT THE CAUSE OF THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 52,500.

Aug 10, 2006 19,002 mi

IN LATE JULY, I WAS PARKED IN MY 2005 DODGE STRATUS RT 2 DOOR COUPE WITH THE CAR STILL RUNNING. I ADJUSTED MY STEERING WHEEL WHICH IN TURN CAUSED THE CAR TO TURN OFF. EVERY TIME I RAISED MY STEERING WHEEL, MY CAR WOULD TURN OFF. IT DIDN'T MATTER IF THE CAR WAS MOVING OR NOT, THE CAR WOULD TURN OFF (THE KEY WOULD STAY ON). BIG SAFETY ISSUE IF I WOULDN'T OF NOTICED UNTIL I BEGAN DRIVING. I COULD HAVE LOST MY POWER BRAKES AND STEERING. I TOOK THE CAR TO A DODGE DEALERSHIP ON 8-7-06. THE DEALERSHIP SAID THAT THE CONNECTOR FOR THE IGNITION SWITCH WAS BROKE AND THEY COULD TEMPORARILY FIX IT. A NEW CONNECTOR IS BEING ORDERED. THE DEALERSHIP SAID THAT THE CONNECTOR COULDN'T HAVE BROKEN WITHOUT SOMEONE BEING IN THE STEERING COLUMN PREVIOUSLY. I BOUGHT THIS CAR BRAND NEW AND TO MY KNOWLEDGE, THE STEERING COLUMN HAS NEVER BEEN TAKEN APART. THEREFORE, I MUST ASSUME THAT THE CONNECTOR IS EITHER FAULTY OR WAS BROKEN DURING THE INITIAL INSTALLATION. *JB

Aug 10, 2006 19,002 mi

IN LATE JULY, I WAS PARKED IN MY 2005 DODGE STRATUS RT 2 DOOR COUPE WITH THE CAR STILL RUNNING. I ADJUSTED MY STEERING WHEEL WHICH IN TURN CAUSED THE CAR TO TURN OFF. EVERY TIME I RAISED MY STEERING WHEEL, MY CAR WOULD TURN OFF. IT DIDN'T MATTER IF THE CAR WAS MOVING OR NOT, THE CAR WOULD TURN OFF (THE KEY WOULD STAY ON). BIG SAFETY ISSUE IF I WOULDN'T OF NOTICED UNTIL I BEGAN DRIVING. I COULD HAVE LOST MY POWER BRAKES AND STEERING. I TOOK THE CAR TO A DODGE DEALERSHIP ON 8-7-06. THE DEALERSHIP SAID THAT THE CONNECTOR FOR THE IGNITION SWITCH WAS BROKE AND THEY COULD TEMPORARILY FIX IT. A NEW CONNECTOR IS BEING ORDERED. THE DEALERSHIP SAID THAT THE CONNECTOR COULDN'T HAVE BROKEN WITHOUT SOMEONE BEING IN THE STEERING COLUMN PREVIOUSLY. I BOUGHT THIS CAR BRAND NEW AND TO MY KNOWLEDGE, THE STEERING COLUMN HAS NEVER BEEN TAKEN APART. THEREFORE, I MUST ASSUME THAT THE CONNECTOR IS EITHER FAULTY OR WAS BROKEN DURING THE INITIAL INSTALLATION. *JB