High Severity Issue
This component has been associated with crashes, fires, or deaths.
This Problem Across All Years
THE VEHICLE HAD BEEN PARKED FOR ABOUT 1 HOUR WHEN AN EXPLOSION INCURRED WHICH RESULTED IN THE TRUCK BURNING UP. THE MOTOR AREA, FRONT WHEELS AND COMPLETED CAB WERE DESTROYED. GAS TANK DID NOT BLOW UP. *TR
THE VEHICLE HAD BEEN PARKED FOR ABOUT 1 HOUR WHEN AN EXPLOSION INCURRED WHICH RESULTED IN THE TRUCK BURNING UP. THE MOTOR AREA, FRONT WHEELS AND COMPLETED CAB WERE DESTROYED. GAS TANK DID NOT BLOW UP. *TR
WHILE TRAVELING ON VACATION 600 MILES FROM HOME I EXPERIENCED A WELL KNOWN FAILURE TO FORD TRITON ENGINE OWNERS KNOWN AS A SPARK PLUG EJECTION FAILURE. I WAS TRAVELING @ 65 MPH AND UP TO THE FAILURE THE ENGINE WAS RUNNING NORMAL THERE WERE NO ABNORMAL SOUNDS. AT THE TIME OF THE FAILURE IT SOUNDED AS IF THE EXHAUST OR THE INTAKE WAS COMING APART. I PULLED OVER ON THE SIDE OF THE HIGHWAY AND REMOVED THE DOGHOUSE AT THE REAR OF THE ENGINE TO DISCOVER THE RIGHT BANK AND 2ND CYLINDER FROM THE REAR HAD EJECTED THE SPARK PLUG AND DESTROYED THE IGNITION COIL. I UNPLUGGED THE IGNITION COIL AND THE POWER CABLE FROM THE FUEL INJECTOR FROM THAT CYLINDER AND NURSED THE VAN TO A FRIENDS HOUSE 40 MILES AWAY WHICH TOOK OVER 3 HOURS. I CALLED SEVERAL FORD DEALERS TO EXPLAIN WHAT HAPPENED AND THEY FINISHED THE STORY FOR ME, THEY SAID THEY HAVE SEEN THIS PROBLEM SEVERAL HUNDRED TIMES AND THE FIX WOULD COST $1000.00 PER CYLINDER NEEDING REPAIRED. THIS IS A KNOWN FORD TRITON FLAW AND SHOULD BE ADDRESSED BY FORD WITH A RECALL. THIS COULD BE A SAFETY ISSUE BECAUSE WHEN THE SPARK PLUG LET GO THERE WAS A EXTREME LOSS OF POWER IF IN HEAVY TRAFFIC THIS COULD CAUSE A ACCIDENT, AND THE RAW FUEL COMING FROM THE CYLINDER ALONG WITH SPARK FROM A LIVE IGNITION COIL IS A FIRE HAZARD. *TR
WHILE TRAVELING ON VACATION 600 MILES FROM HOME I EXPERIENCED A WELL KNOWN FAILURE TO FORD TRITON ENGINE OWNERS KNOWN AS A SPARK PLUG EJECTION FAILURE. I WAS TRAVELING @ 65 MPH AND UP TO THE FAILURE THE ENGINE WAS RUNNING NORMAL THERE WERE NO ABNORMAL SOUNDS. AT THE TIME OF THE FAILURE IT SOUNDED AS IF THE EXHAUST OR THE INTAKE WAS COMING APART. I PULLED OVER ON THE SIDE OF THE HIGHWAY AND REMOVED THE DOGHOUSE AT THE REAR OF THE ENGINE TO DISCOVER THE RIGHT BANK AND 2ND CYLINDER FROM THE REAR HAD EJECTED THE SPARK PLUG AND DESTROYED THE IGNITION COIL. I UNPLUGGED THE IGNITION COIL AND THE POWER CABLE FROM THE FUEL INJECTOR FROM THAT CYLINDER AND NURSED THE VAN TO A FRIENDS HOUSE 40 MILES AWAY WHICH TOOK OVER 3 HOURS. I CALLED SEVERAL FORD DEALERS TO EXPLAIN WHAT HAPPENED AND THEY FINISHED THE STORY FOR ME, THEY SAID THEY HAVE SEEN THIS PROBLEM SEVERAL HUNDRED TIMES AND THE FIX WOULD COST $1000.00 PER CYLINDER NEEDING REPAIRED. THIS IS A KNOWN FORD TRITON FLAW AND SHOULD BE ADDRESSED BY FORD WITH A RECALL. THIS COULD BE A SAFETY ISSUE BECAUSE WHEN THE SPARK PLUG LET GO THERE WAS A EXTREME LOSS OF POWER IF IN HEAVY TRAFFIC THIS COULD CAUSE A ACCIDENT, AND THE RAW FUEL COMING FROM THE CYLINDER ALONG WITH SPARK FROM A LIVE IGNITION COIL IS A FIRE HAZARD. *TR
1997 FORD F150 CAUGHT ON FIRE WILL IT WAS PARKED AT MY SONS WORK. *AK
1997 FORD F150 CAUGHT ON FIRE WILL IT WAS PARKED AT MY SONS WORK. *AK
MY VAN HAS BEEN IN THE SHOP 3 TIMES AND THEY TELL ME I NEED TO CLEAN THE INJECTORS. WELL IT HAS BEEN STARTING SLUGGISH FROM DAY ONE. TODAY IT WILL NOT START. SAME SYMPTOMS AS EVERYBODY ELSE. WEAK BATTERY AND SMOKE STILL WILL NOT START. I'M AFRAID TO DRIVE IT AGAIN. I THINK IT'S GOING TO CATCH ON FIRE. *JB
MY VAN HAS BEEN IN THE SHOP 3 TIMES AND THEY TELL ME I NEED TO CLEAN THE INJECTORS. WELL IT HAS BEEN STARTING SLUGGISH FROM DAY ONE. TODAY IT WILL NOT START. SAME SYMPTOMS AS EVERYBODY ELSE. WEAK BATTERY AND SMOKE STILL WILL NOT START. I'M AFRAID TO DRIVE IT AGAIN. I THINK IT'S GOING TO CATCH ON FIRE. *JB
DT: CONTACT STATES BECAUSE OF HIS DISABILITY THE VEHICLE IS HARD TO PUT INTO GEAR, ALSO IT IS HARD TO START THE ENGINE. THE VEHICLE HAS NOT BEEN TO A SERVICE DEALER.*AK *JB
DT: CONTACT STATES BECAUSE OF HIS DISABILITY THE VEHICLE IS HARD TO PUT INTO GEAR, ALSO IT IS HARD TO START THE ENGINE. THE VEHICLE HAS NOT BEEN TO A SERVICE DEALER.*AK *JB
TAIL LIGHT WENT OUT. UPON TRYING TO REPLACE THE LIGHT FOUND OUT THAT HOUSING STRUCTURE FOR BULB HAD BEEN RECONSTRUCTED. CALLED DEALER. PROBLEM WAS NOT REMEDIED. PLEASE PROVIDE ANY FURTHER INFORMATION.*AK
TAIL LIGHT WENT OUT. UPON TRYING TO REPLACE THE LIGHT FOUND OUT THAT HOUSING STRUCTURE FOR BULB HAD BEEN RECONSTRUCTED. CALLED DEALER. PROBLEM WAS NOT REMEDIED. PLEASE PROVIDE ANY FURTHER INFORMATION.*AK
VEHICLE STALLS INTERMITTENTLY AND UNEXPECTEDLY WHILE DRIVING IN HOT WEATHER, SLOWING OR STOPPED FOR TRAFFIC , CONSUMER BELIEVES THE STALLING IS CAUSED BY A FAULTY IGNITION. NLM
VEHICLE STALLS INTERMITTENTLY AND UNEXPECTEDLY WHILE DRIVING IN HOT WEATHER, SLOWING OR STOPPED FOR TRAFFIC , CONSUMER BELIEVES THE STALLING IS CAUSED BY A FAULTY IGNITION. NLM
GROUND WIRE TO THE AIR BAG AND SERVICE ENGINE LIGHT WAS CUT.
GROUND WIRE TO THE AIR BAG AND SERVICE ENGINE LIGHT WAS CUT.