1999 FORD E-250 Engine And Engine Cooling Problems

10 complaints about Engine And Engine Cooling

10
Complaints
0
Crashes
0
Fires
0
Deaths

This Problem Across All Years

All Engine And Engine Cooling Complaints (10)

Aug 4, 2011

SUBJECT: FORD V-8 TRUCK ENGINE SPARK PLUG BLOWOUT COMMENTS: I AM A CONSTRUCTION COMPANY BUSINESS OWNER THAT USES FORD VANS FOR OUR WORK. THIS PAST WEEK WE HAD A SPARK PLUG BLOW OUT OF THE HEAD OF ONE OF OUR VEHICLES THIS IS THE THIRD TIME IT HAS OCCURRED ON THIS PARTICULAR VEHICLE EACH TIME WE HAVE TO PLACE IT IN THE SHOP IT COSTS NEARLY $300.00 TO HAVE IT REPAIRED. NOT TO MENTION THE LOSS OF USE OF THE TRUCK FOR 2 -3 DAYS. WHILE RESEARCHING THE PROBLEM ONLINE I HAVE DISCOVERED THAT THIS HAS BEEN A FAIRLY COMMON OCCURRENCE ON MANY OF THESE ENGINES FOR SEVERAL YEARS. I WONDER IF THEIR IS SOME RECOURSE THRU FORD OTHER THAN A CLASS ACTION LAW SUITE TO RECOVER THE EXPENSE? PLEASE RESPOND YOURS TRULY[XXX] INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TR

Mileage: 110,000

Mar 19, 2010

I RETURNED TO MY TRUCK AFTER WORK TO GO HOME. WHEN I STARTED IT, THERE WAS A LOUD POPPING NOISE FROM UNDER THE HOOD. AFTER INVESTIGATION, I FOUND THE #3 SPARKPLUG ON THE PASSENGER SIDE GONE. IT WAS BLOWN OUT. *TR

Mileage: 82,000

Mar 31, 2008

1999 FORD ECONOLINE WITH MULTIPLE ISSUES. CONSUMER STATES THAT THIS VEHICLE HAS MULTIPLE ISSUES WITH BREAKING DOWN. HE ALSO STATES THAT THIS VEHICLE HAS HAD SEVERAL ENGINE PROBLEMS, TIRE PROBLEMS, WINDSHIELD WIPER MOTOR PROBLEMS. *KB THE CHECK ENGINE LIGHT ILLUMINATED, THE LEFT REAR DOOR HANDLE, BATTERY, ALTERNATOR, RADIO, BALL JOINTS WERE REPLACED. THE BRAKE ROTORS AND PADS WERE REPLACED. THE AXLE SHAFT SEALS, MASS AIR FLOW SENSOR, CATALYTIC CONVERTER WERE REPLACED. THE VALVE SPRING WAS BROKEN, THE FRONT TIE ROD ENDS AND DRAG LINKS WERE REPLACED, THE TIRES, WIPER BLADES AND GASKETS WERE REPLACED. THE VAN WAS SERVICED 9 TIMES FOR THE CHECK ENGINE WARNINGS. *JB

Mar 31, 2008

1999 FORD ECONOLINE WITH MULTIPLE ISSUES. CONSUMER STATES THAT THIS VEHICLE HAS MULTIPLE ISSUES WITH BREAKING DOWN. HE ALSO STATES THAT THIS VEHICLE HAS HAD SEVERAL ENGINE PROBLEMS, TIRE PROBLEMS, WINDSHIELD WIPER MOTOR PROBLEMS. *KB THE CHECK ENGINE LIGHT ILLUMINATED, THE LEFT REAR DOOR HANDLE, BATTERY, ALTERNATOR, RADIO, BALL JOINTS WERE REPLACED. THE BRAKE ROTORS AND PADS WERE REPLACED. THE AXLE SHAFT SEALS, MASS AIR FLOW SENSOR, CATALYTIC CONVERTER WERE REPLACED. THE VALVE SPRING WAS BROKEN, THE FRONT TIE ROD ENDS AND DRAG LINKS WERE REPLACED, THE TIRES, WIPER BLADES AND GASKETS WERE REPLACED. THE VAN WAS SERVICED 9 TIMES FOR THE CHECK ENGINE WARNINGS. *JB

Feb 2, 2008

MY NAME IS [XXX] . I AM A SMALL BUSINESS OWNER IN BARTLETT ILLINOIS. I OWN A FORD ECONOLINE 250 & A FORD EXPEDITION. BOTH VEHICLES HAVE BEEN "FORD SERVICED" SINCE NEW. I RECENTLY HAD A SPARK PLUG BLOW OUT OF THE ENGINE. I HAVE HAD MANY A CAR IN MY DAYS AND I HAVE NEVER HEARD OF THIS FAILURE. FORD INSISTED THIS WAS NOT AN ENGINE DEFECT, AND ALTHOUGH THEY WERE THE ONLY SERVICE PEOPLE THAT EVER WORKED ON THE VEHICLE, I WAS STILL RESPONSIBLE FOR THIS REPAIR. THE COST AROUND $750. MONEY IS IMPORTANT, BUT PRINCIPLE IS MORE IMPORTANT. AFTER SEARCHING THE WEB I FOUND THIS: HTTP://WWW.CONSUMERAFFAIRS.COM/AUTOMOTIVE/FORD_SPARK.HTML HUNDREDS OF COMPLAINTS WITH THE SAME FAILURE. IT IS MY HOPE THAT YOU CAN DO SOMETHING TO BRING THIS TO THE PUBLIC'S ATTENTION AND FORCE FORD INTO ADMITTING FAULT. THIS IS WHY PEOPLE DO NOT BUY AMERICAN ANY LONGER; TO BE HONEST I HAVE ALWAYS BEEN A FORD PERSON; NOT ANY MORE. I AM SELLING BOTH VEHICLES AND NEVER BUYING ANOTHER FORD AGAIN. THANKS IN ADVANCE FOR ANY HELP YOU CAN GIVE IN THIS MATTER. SINCERELY, [XXX] CES, INC. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TR

Mileage: 115,100

Jan 13, 2006

SPARK PLUG BLEW OUT OF RH HEAD OF FORD E-250 VAN. *JB

Mileage: 9,580

Jul 29, 2004

BEGINING IN THE YEAR 2000, THE 98 E150 WENT THROUGH THE FACTORY MOTOR AT 90,000 MILES. COOLANT MIXING WITH OIL WITHOUT EVER OVERHEATING. FORD WAS GOING TO FIX UNTIL I TOLD THEM THAT MY MY VEHICLE WAS REPAIRED AT A PRIVATELY OWNED SHOP VERSUS THE DEALERSHIP (MY BROTHER OWNS THE SHOP AND THE LOCAL DEALER SENDS HIM ALL OF THEIR DIFFICULT REPAIRS). IT TOOK ME APPROXIMATELY 16 MONTHS COME UP WITH THE MONEY TO HAVE THE MOTOR MACHINED AND REPAIRED PROPERLY. TOTAL COST $4000. I FINALLY FELT CONFIDENT THAT THE VEHICLE WOULD SERVE ME WELL, UNTIL TWO WEEKS AGO, THE TRANSMISSION LOCKED UP . OVERDRIVE MESSED UP AND CAUSED OTHER PROBLEMS AS WELL. NOW I HAVE NO WHEELS UNTIL I COME UP WITH $1700 MORE. I'M IN THE CONSTRUCTION INDUSTRY,AND IF USE INFERIOR TECHNIQUES OR PRODUCTS I AM HELD ACCOUNTABLE. SHOULDN'T FORD LIVE BY AT LEAT THE SAME STANDARDS AS A LOWLY CARPENTER.*AK

Mileage: 9,000

Apr 4, 2003

THE HEAD GASKET FAILED, WHICH CAUSED OIL TO LEAK. *JB

May 24, 2000

MASTER CYCLINDER WENT OUT, SIDE DOORS NEEDED TO BE ALIGNED, OIL, LEAK, HEAD GASKET,BRAKES NOT OPERATING PROPERLY, HARD STARTING, BACK FIRING, TRANS SHIFTING EARLY INTO OVERDRIVE,

May 24, 2000

MASTER CYCLINDER WENT OUT, SIDE DOORS NEEDED TO BE ALIGNED, OIL, LEAK, HEAD GASKET,BRAKES NOT OPERATING PROPERLY, HARD STARTING, BACK FIRING, TRANS SHIFTING EARLY INTO OVERDRIVE,