2014 FORD ESCAPE Engine Problems

691 complaints about Engine

691
Complaints
2
Crashes
70
Fires
0
Deaths

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Engine Complaints (691)

Jan 9, 2026

Using up coolant/possible coolant intrusion issue, I have owned my 2014 Ford Escape for almost 2 years, and have to top up coolant every 2 to 3 months of daily driving, as low as 10 km a day. The engine itself has not had issues YET, but is using coolant when A. It should not. and B. At an alarming rate. There are also no leaks on my driveway, and dealerships cannot find the issue.

Jan 8, 2026

It had a recall for leak coolant, they installed a new expansion tank and new hoses, however for some reason it is still leaking, the inside of the car smells like burnt, when I’m stopped, Ford said the leak might be repaired when they changed the hoses it wasn’t the case it’s still leaking, they were supposed to install a sensor to let me know when the coolant level is low, however last time the compartment was almost empty and the car didn’t show any warning, looks like it’s not working as it should be, it could catch fire it could be even worst.

Jan 5, 2026

Coolant Intrusion on Cylinder 3, potential to overheat engine posing fire safety risks. Problem has been confirmed at Ford Dealership. Vehicle has been inspected by manufacturer. Check engine light came on Dec. 31st 2025, car was not driven until Jan. 2nd 2026, when it was given to dealership mechanic for inspection/diagnosis. Ford is aware of the dangers of coolant intrusion and the flawed engine design.

Dec 18, 2025

I have had problems with coolant leaks, coolant sensor, valve gaskets and coolant intrusion in my engine. The coolant reservoir was replaced at 36,580 miles on 07/13/17. The coolant sensor recall was completed at 37,315 miles on 07/31/17. The coolant overflow line was was replaced at 66,910 miles on 01/14/22. The coolant light came on and coolant was added at 69,882 miles on 02/16/23. There was a coolant leak and the valve cover gaskets replaced at 76,910 MILES ON 01/23/25. The engine started surging and the coolant light came one. The ignition coil was replaced and the sensor light was adjusted at 78,709 miles on 09/05/25. The sensor light came back on the next day. I went into the dealership 3 different times to tell them there had to be a leak. Since they assured me that it was just the sensor and I had no leak, they did not give me another appointment to check it out. On 12/04/25 a message came on that said it was overheating and to park the car immediately. It then went into limp mode. I was given an appointment on 12/10/25 and I had the car towed in. At 80,158 miles the dealership informed me that there was coolant intrusion in the engine and the cylinders and the car would need a new engine.

Dec 11, 2025

Coolant light indicates coolant should be added often. Coolant has been added to frequently. Last time coolant light came on another Error Code: P1299 and the engine stopped running properly. Vehicle was inspected by a repair shop who stated the coolant was leaking into the motor. If this keeps occurring engine may overheat, fail and possibly catch fire. Ford said there is no recall on this issue. Bring it in for diagnostics and stated it would take three months to just look at the issue. This is no exaggeration. We have read an astonishing amount of other people have and are having similar issues with the Ford Escape

Dec 11, 2025

My 1.6l ecoboost was leaking coolant and smoking on the side of the reservoir and burning coolant smells went thought the heater and ac vents when on especially at a stop light and it even leaks oil a little bit but I have got the “coolant leak” fixed but I have an internal leak somewhere clearly and all the symptoms add up to sound like the ford recalls 17S09 and also similar to 12S39 but that’s for 2013 escapes but there’s clearly an unsafe issue hear that cause cause fire underneath my hood I called ford and they said to try to make a claim because there should be no reason I’m not covered under warranty when it’s the same cars same engines and same issues

Dec 10, 2025

Intrusive coolant leak

Dec 8, 2025

My 2014 Ford escape started leaking coolant into the engine, producing a terrible odor throughout the cab and causing overheating. The mechanic pressure tested the coolant system and identified coolant leaking into the cylinders. This is a common occurrence in this make and model.

Dec 7, 2025

The Ford EcoBoost engine in my Ford Escape 2014 has consistent coolant leaking issues as reported by several other vehicle owners. I spent the last 4 years of owning it constantly returning to the dealership over this issue when my car was under warranty because the coolant tank kept leaking. They never fixed the leaking issue and when my warranty expired, they refused to help fix it any longer. I cannot afford a new car or the work I need to keep getting on it yet need it to get to work, and the constant need for my refilling of the coolant in the tank that progressively gets worse and can cause engine failure warrants a recall on behalf of the company and compensation.

Nov 22, 2025 Fire

Engine caught fire at the coolant reservoir

Nov 4, 2025

This vehicle has had a bad electrical problem where it makes a real bad clicking noise and sometimes it doesn't turn off the radio also the radio doesn't turn on at times. The major problem is it has not passed emissions for almost a year it gives out bad sensor readings and clearing the code so I can pass emissions don't help it comes back on. I have tried to let Ford know that this car is having recall issues . I have had a purge valve put on it but it's still it's not capable of passing the emissions because the sensors at all Ford dealerships said they can reset the sensors but they want me to pay I don't think that is fair to me because these are recall issues that I'm having! even though it's older .I think it's only fair to have it analyzed at a Ford dealership free of charge.. I'm paying car notes and I cannot even drive the vehicle safely now it's leaking antifreeze if you check the past recalls on 2014 Ford escapes there were fuel injector problems and that's probably why it cannot pass emissions so I need this recall handled properly thank you.

Nov 3, 2025

My coolant system has leaked for the last 5 or 6 years. It has been worked on by Ford and by independent mechanics. The last time, Ford said it was fixed and I shouldn’t have any problems. It still leaks and it is unknown where it is going.

Nov 1, 2025

The back up camera goes out at times.it says report too ford.tranmission issues and turbo issues.

Oct 23, 2025

Coolant leak at the 3 way heater hose going to the heater core. I'm seeing a lot of complaints about leaks at the quick connect and nothing being done about it. Ford made a replacement part thats upgraded. I believe they should be replacing the defected parts with the new one. They knew this was an issue for some time now and refuse to take care of the problem.

Oct 21, 2025

Head gasket blew and coolant leaked into engine. This applies to the Ford Escape 2013 - 2019. Ford's 1.5L, 1.6L, or 2.0L Ecoboost engines manufactured, marketed, and distributed by Ford Motor Company. They know about the problem but refuse to fix the problem. There is currently a class action lawsuit. But we all know that does noting.

Oct 18, 2025 Crash

see attached documents: Subject: Ongoing Unresolved Recall Issues and Safety Concerns with My Ford Vehicle I am writing to formally express my deep concern and frustration regarding my Ford vehicle, which currently has 15 open recalls that have gone unresolved for nearly two years. During this time, I have contacted every Ford dealership within a 50-mile radius of my home in repeated attempts to have these recalls addressed. Each dealership has provided a different excuse for not completing the necessary repairs. Some initially allowed me to schedule service appointments, only to cancel them once they realized the work involved recall issues. In several cases, I was never notified that my appointment had been canceled—I only discovered this when no one showed up. Other dealerships claimed they did not have the required parts and assured me they would contact me once the parts became available. To date, none have followed up. One dealership required that I speak with a supervisor before scheduling any recall work, but despite multiple messages, my calls were never returned. On one dealership’s website, I attempted to schedule the recall repairs online. The system showed numerous open appointment dates until I selected “recall service,” at which point all availability disappeared, and I was unable to proceed. Each dealership I contacted referred me elsewhere, passing responsibility without resolution. Ford has been fully aware of the potential safety risks—including the risk of serious injury or death—associated with these recalls, yet I was repeatedly told it was “safe to continue driving.” This was clearly not the case. Recently, while driving, my vehicle suddenly lost all power and stopped moving. I managed to pull over to the side of the road and called for a tow truck. As the tow truck driver prepared to load my car, it unexpectedly lurched forward on its own and crashed into the tow truck. Fortunately, no one was injured, but the incident caused significant front-end damage to my vehicle. It could have easil

Oct 9, 2025

Issues with coolant leakage in multiple places. One is with the HVAC heater core valve and hose and the other is with the turbocharger cooling input put up and oil lines. Has been leaking for a while diagnosed on 10/03/2025 Similar to other issues reported by ford escape 1.6L drivers on complaints and documented issues.

Oct 1, 2025

I have experienced multiple coolant leaks. The first one was repaired with a new engine coolant bypass housing, and I am now experiencing the issue again. The heater core hoses are degraded and swollen causing the leak. The coolant bypass (which was replaced a year ago) is made of plastic and cracked. The valve cover is leaking and is a fire hazard. This has impacted my means of transportation. The error messages of “overheating” occur abruptly and at times when I have not been able to safely pull over or stop. The problem has been confirmed by an independent service center. No, not inspected by manufacturer, police, or insurance representatives. The first time this occurred I only received 2 error messages. And this time I only received one.

Sep 23, 2025

Purchsed a 2014 Ford Escape Titanuim 1.6L Eco Boost in April of 2024. Since then, my vehicle has been to three different mechanics, one was a Ford dealership, because the sensor keeps coming on and coolant keeps leaking out. The first incident occured barely a week after the purchase and I've actually been stranded 2 out of the 3 times. In my research I've learned that Ford is aware of this issue, however, there's no recall on my vehicle.

Sep 22, 2025

I purchased the car in April 2023, a few days later the sensor light came on and coolant leaked out and I was stranded. I took it to my local Ford dealership and they "repaired it". About a month ago the same thing happened and I was stranded. Got it towed to a mechanic, was told it's been repaired, a couple of weeks later the sensor came back on, but I was able to make it to the mechanic before I was stranded. He put a mark on the reservoir and told me to add more coolant if it got before that line. I shouldn't have to keep doing this.

Sep 18, 2025

Vehicle hesitates when shifting mainly from secon to third gear and hesitates to accelerate. The rpms go up but not going any faster and then jerks. If I was to try and pull out onto a highway there is no way the car will accelerate fast enough. Took it to the dealer to see if they could check a previous recall item to see if it was maybe defective and they would not look at it unless I paid 220 dollars for a diagnostics even though the recall was for the transmission shifting cable bushing. This has been happening since I bought the car about a year ago which wa previously owned by an elderly person that got it from the dealer with 35000 miles on it and it now only has 50000 miles on it and the dealer could not tell me what else was fixed on the car. I have read about the same issues with tje same transmission that I have amd the dealer does nothing to help. It is the 6f35 transmission. There are no warning lights on and no codes popping up. The transmission fluid has been changed and was not dirty along with the filter. I am afraid that when I go to accelerate my car will not go fast enough and hesitate and possibly cause an accident. I have read many of the same complaints about this vehicles transmission had I known about them before I got the vehicle I would not have bought it as the dealership is not helpful at all. This happens everytime I drive the vehicle especially going from a complete stop to going.

Aug 21, 2025

The contact owns a 2014 Ford Escape. The contact stated that while operating the vehicle, the instrument cluster screen malfunctioned and turned black or flickered off and on. Additionally, the headlights, turn signals, and brake lights intermittently failed to operate as needed. The transmission and check engine warning lights were illuminated. The cause of the failures was not yet determined. The local dealer was contacted regarding the failures, but no assistance was provided. The manufacturer was not contacted. The failure mileage was 130,000.

Mileage: 130,000

Aug 21, 2025

I received a notification on the my dash and the car was diagnosed the codes came back Code: P018B and it states Fuel Pressure/ misfire. I've noticed the car misfiring prior to the dash light coming on and now it does it while I'm on the freeway or streets as if it's going to just stop which os very dangerous. This has to be a recall may 2014 ford vehicles are having this issue along with the coolant leak. This needs to be recalled

Aug 19, 2025

Coolant leak just like as listed in other 2014 Ford Escape recalls. It leaked into the engine block causing misfire of spark plugs and thus the Ford dealership tells me I am required $14,000 engine rebuild which I can't afford. It is dangerous for me to drive as the engine may misfire or overheat at any time. The Ford company says I have no recalls and yet this issue was a recalled issue on this year of Ford Escapes.

Aug 14, 2025

The contact owns a 2014 Ford Escape. The contact stated that the local dealer sent a mobile mechanic to the residence to repair a bushing on the vehicle. The contact stated that the ABS warning light was illuminated. The vehicle was repaired, but the mechanic had forgotten to replace a tubing on the vehicle. The vehicle failed to start, and the contact's husband noticed that the tubing was disconnected. The contact's husband was able to attach the tubing, and the vehicle restarted. While her husband was driving the vehicle and making a turn, the vehicle stopped. The vehicle was restarted after several attempts. The contact stated that the transmission was slipping. Roadside Assistance was contacted and left the parking brake activated during towing. The vehicle was towed to the local dealer and several DTC were retrieved. The vehicle was not diagnosed or repaired. The contact called the customer service at the manufacturer, but no assistance was provided. The vehicle was taken to an independent mechanic who discovered an failure with the muffler. The failure mileage was approximately 115,000.

Mileage: 115,000

Aug 12, 2025

On [XXX] - vehicle was started and when turning out of the driveway I notice a puddle which was coolant. The vehicle started to overheat. I turned back and went home then called a tow truck to retrieve the vehicle which they were able to do on Monday. The vehicle was towed and investigated by Fosters Towing in Fraser, MI. They found no evidence of a leak but there was a code (which they did not write down). They cleared the code and tried to replicate the issue but, after running it for an hour and searching for leaks, nothing was found. The vehicle has not been taken to a dealership. The mechanic at Fosters is certified to deal with this vehicle. At the time of the incident I had my kids in the car - ages [XXX] and [XXX] - and their safety was more important than the trip to the grocery store. Fosters performed an oil change (filter and oil) and test drove the vehicle several times to replicate the issue but could not. This is the first time this issue has occurred. I have 128,000 miles on the vehicle. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6)

Aug 9, 2025

Coolant leak into engine gasket/block. Moderate acceleration or freeway driving depletes coolant then overheats. No signs of coolant underneath vehicle upon stopping. Vehicle is now lurching/jerking with any acceleration at any speed.

Aug 6, 2025

The 1.6L EcoBoost engine is leaking coolant into the #3 cylinder. The vehicle lost power while in motion on a busy road. The check engine light came on with a warning that the engine was overheating, and traffic behind me had to slow down, causing a potential rear-end accident. The engine was scanned, and the fault code P1299 was discovered.

Aug 1, 2025 Fire

I was driving up a hill on the highway with my father in the car with me when my car began to rattle slightly. I looked down and saw that my engine heat dial was somewhat higher than its standard setting, which was weird because I had just put engine coolant in a day or two prior. A second later, my dash said, "Severe engine failure. Pull over." At the same time, the smell of smoke wafted into the car, and soon after, smoke began billowing into the vehicle as well. We pulled to the side of the highway and got out to check what was happening with the engine. At this point, tons of smoke was coming out of the hood. I tried to lift the hood to inspect the engine, but I couldn't because the metal was too hot. I peered through the slit of the hood and saw flames. At this point, we began grabbing all of our belongings from the car and moving out of the way. A few minutes later, the fire became much larger and ended up jumping onto the side of the hill next to the highway. It then continued up the hill and spread to 8 acres before the fire department was able to halt it. I am not sure exactly what part of the engine failed, but I suspect it was the coolant. I had always had issues with the coolant leaking or running out fast, but figured nothing of it, as there was no recall and whenever the car was serviced nothing was said. I don't know where the car is but I do know the front half was completely destroyed by the fire. My dad's and my safety were at risk due to the car we were driving bursting into flames while we were inside. Additionally, one of the doors were broken and we lucked out not sitting in the seat with the broken door. I dont know if the problem has been confirmed. I dont think it has been inspected yet. There was an engine coolant warning minutes before the fire started. But it was just one time and I had put in engine coolant days before. It was not enough warning.

Jul 29, 2025

The contact owns a 2014 Ford Escape. The contact stated that while driving at 50 MPH, the messages "Temperature High" and "Pull Over Safely" were displayed. In addition, the vehicle failed to accelerate as intended while depressing the accelerator pedal. The vehicle was able to pull to the side of the road. The vehicle was taken to an independent mechanic who diagnosed that the coolant was leaking. The vehicle was repaired. The contact stated that, on a separate occasion, the coolant reservoir was constantly low. The vehicle was taken to a different independent mechanic who diagnosed coolant intrusion into cylinders 2 or 3, causing engine failure. The contact was informed that the engine needed to be replaced. The vehicle was not repaired. The manufacturer was not notified of the failure. The failure mileage was approximately 140,000.

Jul 22, 2025

Left my home and drown about 1 mile and car Oil light came on then battery light came on then car started rolling I had no control of the speed and car stopped in middle of street got it towed to mechanic . Mechanic advises known issue with fords and should be under a recall. coolant leaking from turbo lines

Jul 15, 2025

Vehicle overheated caused the cylinder head that crack. I am concerned it may catch fire as others before the recall. When I key in the VIN it shows no recall. However the NHTSA recall no 17V-209 or 17S09 shows all Escapes produced 2/12/13-9/2/14 have this issue and should have gotten a part to prevent this. With a production date of 5/14, shouldn't this vehicle be included?

Jul 10, 2025

Engine overheated, lost power, and smoke came from the exhaust. Mechanics opinion is the engine block is cracked and what had caused the heating is a blown head gasket.

Jul 8, 2025

1. The transmission has continuously slipped and stuck in gears when significantly outside of standard RPM:Speed standards for the vehicle. 2. The vehicle has recently started leaking oil via a lower pressure valve. 3. The engine thermostat and/or sensor need to be replaced with faulty internal temperatures being registered. 4. The rear collision warning and camera system started malfunctioning after an update that happened middle of 2024. The camera won't work at all approximately 50% of the time. 5. The brake issues haven't been fully diagnosed, but I'm aware of the model year/series of vehicle having several faulty components that could have a hand in the weakened braking. 6. I recently had AAA come diagnose the vehicle (reference the photos provided). My objective is to have my vehicle included in the widespread recalls that were released for my car model, year, and overall series. For some reason my VIN in registering as a vehicle that qualifies for the recalls but seems to have the exact same issues. I'm more than happy to take part in an investigation and or third-party inspection to expedite the process as well. I've also included the reports I've found when searching for the 2014 Ford Escape recall/repair list (via your website and others).

Jun 24, 2025

While doing oil change, I realized car has rear seal oil leak. Transmission experiences slippage in cold weather. Car has a very good maintenance record.

May 7, 2025

Engine light came on and over heates

May 5, 2025

The car has been in the shop on and off for two years because of coolant leaking but the coolant pressure test show no leaks. As of March 2025 the car was checked again and showed no pressure leaks. Over the course of time, The radiator was replaced and several other things have been attempted. We are at the point where we don’t want to put more money into the vehicle because we are afraid it is the classic coolant intrusion situation with this car. I have read many reports of this problem. I am only reporting on the most recent incident below. I do not have an invoice for the March, 2025 visit for coolant pressure test.

Apr 18, 2025

The contact owns a 2014 Ford Escape. The contact stated while driving at an undisclosed speed, the engine overheated and the vehicle stalled with the check engine warning light illuminated. The vehicle was able to be restarted. The vehicle was taken to an independent mechanic but was not diagnosed or repaired. The dealer was not contacted. The vehicle was not diagnosed or repaired. The manufacturer was made aware of the failure. The approximate failure mileage was 150,000.

Mileage: 150,000

Mar 21, 2025

A few months ago, Engine coolant light came on and had more coolant added. Then the week after my card stopped in the middle of the road because the engine was over heating, I had to get it towed. Took it to mechanic and there was a hole and coolant leaking. My engine coolant light just came on again, requiring further inspection.

Mar 15, 2025

Initially diagnosed as a coolant leak due to requirement to constantly add coolant. There was no evidence of a leak. Shortly thereafter the car began experiencing hard starts and illumination of the check engine light (CEL). Code showed number 3 cylinder misfire. Subsequent starts had white smoke in conjunction with rough idle and CEL. Took to my mechanic and he said this is a known issue with this Engine and quoted me 9K for repairs. I did some searching online and found that this issue is VERY well known and Ford is currently in litigation over it.

Feb 14, 2025

Coollant leak

Feb 12, 2025

The contact owns a 2014 Ford Escape. The contact stated that upon starting the vehicle, there was an abnormal amount of smoke coming out of the exhaust pipes. The contact stated that the check engine warning light remained illuminated. The vehicle was taken to a local independent mechanic to be diagnosed and the contact was informed that there was coolant leaking into the engine and that the engine needed to be replaced. The vehicle was not repaired. The contact related to NHTSA Campaign Number: 17V209000 (ENGINE AND ENGINE COOLING); to the cause of the failure. The manufacturer was notified of the failure. The approximate failure mileage was 121,656.

Mileage: 121,656

Feb 10, 2025

while driving on a busy road, the vehicle went into LIMP mode and would not move forward, the coolant was below the sensor and the vehicle said it would over heat, the block leaks coolant into the engine cylinder and there is no fix for this but to replace entire engine as per dealer. I was almost hit from the rear from traffic. the car had to be pushed into our driveway via a police car bump guard. the dealer could not find where the coolant was going too.

Feb 6, 2025

The contact owns a 2014 Ford Escape. The contact stated while driving approximately 30 MPH, the vehicle hesitated to accelerate while depressing the accelerator pedal. The check engine warning light illuminated. The vehicle was taken to a local dealer to be diagnosed. The contact was informed that the cylinder head was cracked, the spark plugs were seized, and there was coolant intrusion into the engine. The contact was informed that the engine needed to be replaced. The vehicle was not repaired. The manufacturer was not made aware of the failure. The failure mileage was approximately 63,000.

Mileage: 63,000

Feb 4, 2025

Engine has antifreeze leak. (white smoke and bad smell noticed in [XXX] On August 9th, Ford Motor stated that I need a new engine due to antifreeze leak. $9,999.00 is what they quoted me for a new engine. The car has sat for months since August. I do not have $9,999.00 for a new engine. Per other recall information on the same type of vehicle and engine. The engine could catch on fire. Yes, diagnosed and confirmed by Ford Motor Auto Ranch, Ontario Oregon on 8/9/2024. No, the vehicle has not been inspected by police or insurance. No, there has not been any warning lamps or messages. Any and all help is very welcome. I do not have the money for a new engine and have to rend a car for my medical appointments. I now get a ride to my job daily. Please help me, thank you, [XXX] INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6)

Jan 28, 2025

The engine failed on due to coolant intrusion causing misfires on cylinder 3.

Jan 13, 2025

I saw that there is a current recall dealing with the cooling system on the Escape. My car has been over heating saying engine fault for the past two months. There now appears to be coolant in the engine.

Jan 6, 2025

The contact owns a 2014 Ford Escape. The contact stated while driving at various speeds, the check engine warning light illuminated. The failure persisted with the message that the engine was overheating before the vehicle went into LIMP Mode. The vehicle was towed to an independent mechanic on two separate occasions where the spark plugs and other engine repairs were performed; however, the failure persisted. The vehicle was taken back to the independent mechanic where the vehicle was diagnosed with engine failure, and the contact was provided an estimate for the repair. The dealer and the manufacturer were notified of the failure but offered no assistance. The contact was referred to the NHTSA Hotline to report the failure. The vehicle was not repaired. The failure mileage was approximately 98,000.

Mileage: 98,000

Jan 5, 2025

Rapidly losing coolant without being able to find any leaks with the assumption it’s going into my engine. This also explains why my engine has been acting a bit funny.

Jan 2, 2025

Coolant In Cylinders, White Exhaust Smoke

Dec 4, 2024

The contact owns a 2014 Ford Escape. The contact stated while the vehicle was parked and running, there was a cloud of gray smoke coming from the vehicle and the engine was overheating. The vehicle was taken to two independent mechanics and was diagnosed a cracked cylinder. The vehicle was not repaired; however, the thermostat and water pump were replaced. The manufacturer was notified of the failure but offered no assistance. The failure mileage was 150,000.

Mileage: 150,000

Dec 2, 2024

The smokes very excessively at startup. If the vehicle sits it will do it again,

Dec 1, 2024

Constant Coolant Leaks affecting the engine The vehicle is available for inspection Vehicle breaks down very easily now so safety is a concern This problem has been repaired several times. Yes the vehicle has been inspected Yes there were warnings. The vehicle now has a constant engine light that will not go away

Nov 11, 2024

Slow coolant leak that can’t be located

Nov 5, 2024

My engine is leaking coolant and requiring me to have to constantly add it! Now coolant is leaking while I am driving it causing my car to overheat.

Nov 5, 2024

There is a engine coolant leak into the cylinder 2 due to a faulty casing from the manufacturer (Ford). It is a known issue across several models (Escape, Edge) and model years. A mechanic has confirmed the engine block needs to be replaced as the issue will continue to get worse and eventually the engine will die due to the faulty casing which allows coolant to seep into the cylinder. Ford is at fault for this and countless claims have been filed online and there should be a recall to cover the repairs.

Oct 31, 2024

The Ecoboost engine in this year/model has a known defect with coolant intrusion into the #3 cylinder. At 83,000 miles the car reported cylinder 3 misfires and the mechanic said coolant was leaking from the head gasket....a known issue with these engines. He warned of catastrophic failure and the potential of an engine fire. He said Ford knows of this issue and recalled several models. My car has the engine issue that Ford knows about and needs to correct before an accident happens. In addition, the coolant does not seem to circulate correctly and when it does, it burns in the cylinder. The has overheated 3 times in the past month.

Oct 24, 2024 Fire

The contact owns a 2014 Ford Escape. The contact stated while the vehicle was parked on the driveway during nighttime, the contact's wife noticed a light underneath the front end of the vehicle. The contact discovered that the vehicle had caught on fire. The contact extinguished the fire using a water hose avoiding opening the hood to not expose the fire to oxygen. The contact's wife then also assisted in extinguishing the fire by using a fire extinguisher as the husband opened the hood and then used the water hose as well. The contact stated that the vehicle had been driven and then parked before the fire was experienced. The origin of the fire was unknown however the contact discovered that the valve cover was charred and melted. No fire report or police report was filed. No injuries were sustained. The vehicle was towed to the dealer; however, the vehicle had not been diagnosed. The vehicle was not repaired. The manufacturer was made aware of the failure and a case was filed. The contact was informed of an unknown recall however, the VIN was not associated with the recall. The contact was advised to contact the NHTSA Hotline to report the failure. The failure mileage was 151,000.

Mileage: 151,000

Oct 24, 2024

Coolant leak occurred out of no where. Roughly 90,000 miles on my car, it's been well taken care of. With no warning, the engine overheated in a drive through. Checked the coolant, it was low and bubbling. Check engine light went on. Difficult to find where the leak is coming from, not sure if it is the water pump, hoses, coolant reservoir or radiator. I refilled the coolant and lost it all in a matter of 2 days. Looked it up and this is very common in Ford Escapes, they need to offer assistance on the matter.

Oct 8, 2024

The contact owns a 2014 Ford Escape. The contact stated that while the vehicle was parked, the coolant warning light illuminated. The vehicle was towed to the local dealer where the vehicle was diagnosed. The contact was informed that the cylinder head was cracked, and the engine needed to be replaced. The vehicle was not repaired. The manufacturer was not notified of the failure. The approximate failure mileage was 163,000.

Mileage: 163,000

Oct 1, 2024

Coolant fluid is leaking into engine cylinder #3. Yes, the vehicle would be available for inspection upon request. The coolant leak can cause the car can overheat, leading to a loss of power, poor performance, and potential engine damage An engine coolant system pressurized diagnostic test was performed by Stuckey Ford in Bellefonte, PA. I will have the report from this test when I pick up the car from the shop. Previous owner stated that one of the spark plugs needed to be changed, but did not disclose engine coolant leak. After purchasing, an indicator light came on stating that the coolant level was low. We have been adding coolant as needed.

Sep 23, 2024

Hello, I'm writing to see if the Ecoboost lawsuits also include 2014 Ford Escapes? Mine cut off on me while on the highway Saturday (XXX). The Engine failed while driving, no light or warning. This is even after me dishing out a little over $8k in 2021 when I purchased it used from Bommarito Ford in St. Louis. I had transmission/engine issues from the start. When the car stopped on me a few folks that work on cars pulled over to see if they could assist. They all said the same thing... that the engine was done... oil was everywhere. They kept asking if it overheated but my gage always stayed between C and H. No lights or warnings ever. It was horrifying to be going about 60 mph to hear something break and lose power without warning. I'm grateful no accident was caused while I merged over to the exit ramp shoulder. I had the car towed back to my apartment while I try to figure out how to get the engine repaired. I'm currently re-starting after a very messy divorce so I do not have extra funds laying around to have a new engine installed. Currently in Chapter 13 due to issues with the divorce. Now I'm catching the bus and I'm still dealing with his stalking/harassment. I've been told my additional warranty ended in June of 2023. I contacted Ford and they told me I would need to have their dealer look at the car which will be towing plus the $250 fee. But that my car type is not included in the class action. The dealer said the same, but I do have an ecoboost engine and have been having issues with the engine/transmission since I purchased it in 2021. Do you know how I could add my name to the Class Action? Thanks, [XXX] INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6)

Sep 23, 2024

My 2014 Ford Escape had run into coolant fluid issues such as leaking fluid and a cylinder misfire. Took it to a Ford dealership where they stated the only option for a fix was a replacement of the long block assembly. My car has just about 72,000 miles on it and it already needs an engine replacement due to coolant intrusion and the Ford dealership cited codes P0303, P0316, and P1299. These are codes that are referenced to Ford's recall of engines on Ford Escapes in the years 2017-2019, and it states it applies to Ford Escapes built from late 2015 to 2019. The 2014 Ford Escape experienced an unfixable engine failure that requires the customer to pay for replacement when Ford should be the one paying for damages. It is clear that their coolant intrusion failure affected more years of production that NHTSA has previously found. There is no reason a care with regular service should have its engine fail at 72,000 miles, and the driver shouldn't be shouldering the cost when this specific issue and PCM codes is commonplace among Ford Escape engines outside of the recalled production years of 2015-2019, or even limiting the recall to 2017-2019. Whoever decided to limit which production years applied to the engine coolant recall made a mistake and it needs to be revisited because Ford customers are being forced to pay for Ford's poor design failures.

Sep 11, 2024

The transmission on my 2014 Ford Escape went totally bad at 91,000 miles. I had to replace the transmission at a cost of $6,780. I have read that this has happened to many 2014 Ford Escapes with low mileage. There should be a recall on this vehicle.

Aug 22, 2024

The contact owns a 2014 Ford Escape. The contact stated while driving at an undisclosed speed, the engine misfired, with the check engine warning light illuminated. Additionally, the contact stated that the engine overheated. The contact stated that the vehicle was parked and allowed for the engine to cool down. The vehicle was later started and taken to the dealer. The vehicle was diagnosed with coolant intrusion into the engine. The contact was informed that the engine needed to be replaced. The vehicle was not repaired. The manufacturer was made aware of the failure but provided no assistance. The failure mileage was approximately 71,669.

Mileage: 71,669

Aug 21, 2024

104,340 miles and diagnosed with coolant consumption and coolant intrusion into cylinder #2 causing engine misfire. known defect of the 1.6L EcoBoost engine. Needs engine replacement.

Aug 10, 2024

While driving at highway speeds, the engine began to miss resulting in a sudden loss of power that forced me to pull over. I had the vehicle towed to a garage where they found the code for a misfire in cylinder 4. When they looked in cylinder 4, they found coolant intrusion and a crack in the cylinder. I discovered this is a common experience with this engine in Escapes and other vehicles. The vehicle only had around 89,000 miles at the time of the incident.

Aug 9, 2024

Engine failure due to coolant intrusion

Aug 2, 2024

We had our vehicle engine light come on, vehicle would shake and misfire, we had the spark plugs replaced. No sooner the vehicle light came on again, vehicle still shake and misfire and had it looked at with Ford service Ford service replaced the power packs. No sooner once again, the engine light came on, this time the vehicle over heated. The vehicle would shake and misfire. Took it in again to Ford service, they concluded that it was the throttle body they replaced and fixed. No sooner once again, the vehicle still shooked, but this time the vehicle started to lose power and would not go while driving on the highway, it over heated, misfired. Returned once again to Ford service whom finally revealed the truth and said these vehicles are notorious for a new engine. We were told that the design of the engine revealed that coolant was leaking into the block/heads. It was unsure if the blocked cracked and that we needed a new engine. If we just replace the head gaskets that later down the road we would need to replace the engine. We were left with replacing the vehicle with Ford service in replacing the engine at the mileage of 96,812

Aug 1, 2024

Car overheated due to intrusion of coolant into head gasket. Repair shop identified issue and warned it's a safety risk for fire when overheating. Only symptom before overheating was white smoke from exhaust on startup. Shop said maintenance looked fine, wasn't low on oil and coolant had just been checked less than 6 months earlier at a regular oil change. Mentioned that they have seen a ton of these from the 2.0L EcoBoost engines and it's a known risk in the industry.

Jul 30, 2024

The car had a coolant leak which caused the car to overheat. The car is now leaking oil which has lead to oil leaking into the fuel.

Jul 25, 2024

The contact owns a 2014 Ford Escape. The contact stated while driving 30-35 MPH, the vehicle stalled. The contact was unable to pull over to the side of the roadway. The contact was able to restart the vehicle and continued driving. The check engine warning light was illuminated. The vehicle was taken to the dealer, where it was diagnosed that the canister purge valve had failed and needed to be replaced. The dealer related the failure to an unknown recall and referred the contact to the NHTSA Hotline for assistance. The vehicle was not repaired. The manufacturer was not notified of the failure. The failure mileage was unknown.

Jul 23, 2024

The contact’s mother owns a 2014 Ford Escape. While the contact's mother was driving at an undisclosed speed, the check engine warning light illuminated. The vehicle was taken to the dealer where it was diagnosed with coolant leak and engine failure. The contact was informed that the engine needed to be replaced. The vehicle was repaired. The manufacturer was made aware of the failure but provided no assistance. The failure mileage was approximately 117,000.

Mileage: 117,000

Jul 17, 2024

The car was smoking whitish gray smoke. I had something repaired. About 3 week later the smoke returned. Took to dealership told it needed an engine. Given a price of $14,000. With that info my car has been parked. I never received info that ford had a class action about engines until a month ago. Please advise.

Jul 12, 2024

The low coolant level came on the car. We were told that they sensor needed to be replaced. We paid $1500 to replace that. The low coolant level light has back on 5 times, then the check engine light comes on and the car shuts off. It has left me, and my daughter stranded on the side of the road and in the middle of the highway. We were told they are not sure what else to do, here is a bottle of coolant from the dealership and keep bringing it back in. Next issues are it won't go over 20 MPG, my daughter was crossing a major highway, she lost power and the car started to shake. We are now told that it is the transmission. There was a recall replaced on it back in 2023. Not happy at all with ford and very unsafe.

Jul 11, 2024

The prior reported issue of coolant intrusion of the Ford Ecoboost into the engine. They only recalled a select number and it seems from both own experience and reviews online that this is happening to a wide variety of years and people even though they "fixed" the issue. Had I not been diligent regarding my car this could have ended poorly and in this economy it's ridiculous to not have a reliable and SAFE vehicle

Mileage: 112,916

Jul 10, 2024

My car has a bad failure of the head gasket. Coolant leaking into cylinder 3 and 2 and using up my coolant. This has been ongoing despite me having had the recalls done to it for the coolant system. This is a pervasive, prevalent and common issue with these Ecoboost engines. I have spoken with many people who have this same issue. It happens subtly and then gets much worse. Causing overheating and undue wear on the cylinder walls. For the first year of the problem beginning, there were no check engine lights associated with it. But it recently has started throwing cylinder 3 misfire codes as a result of this problem. This has been checked by a mechanic and the dealer refuses to repair or replace the head gasket or engine due to no recall for the head gasket being made, however there is at least one or two service bulletins put out by Ford about it. This is putting me and my family at risk of being stranded on the road somewhere, ancient failure at highway speeds and unreliable equipment to keep us safe.

Jul 1, 2024

The problem first arose as the car started going through engine coolant very quickly. Usually the warning would come up saying the engine coolant was low. I would refill, but the car would need more within a day or two. So, I scheduled an appointment to get it checked. In the meantime, I would refill every time the warning came on. Soon after, as we were waiting for the appointment, and as my wife, infant son, and I were driving (with no warning of low coolant), the engine overheated and the car started shaking and would not respond (with a warning that said to pull over safely). Thankfully, we were on side streets in a neighborhood. But with no warning of low coolant beforehand, this is absolutely a safety issue.

Jun 29, 2024

Engine overheats.

Jun 28, 2024

Coolant leak into engine. Engine replacement needed

Jun 14, 2024

Check engine light in 2023 for P1299, Cylinder head overtemperature protection code. Coolant was heavily leaking, and engine overheated while in use on the interstate highway. I had a red error message telling me to immediately pull over and shut the vehicle off, which I did. I called for roadside service and had my coolant topped in a safe location. Car was towed to the dealership where a leak was found as well as a crack in the degass bottle engine mount, which sprayed coolant directly onto the engine. The degass bottle and mount were replaced, and the issue was fixed. Now, in 2024, I pulled a P2681 engine light error for an issue with the coolant bypass valve. I drove the car into the same dealership, where they're currently assessing it for issues. Mentioned that the coolant bypass solenoid is out of spec for a resistance issue and needs to be replaced, otherwise the engine will overheat due to improper temperature regulation. Both issues above have been confirmed by Ford mechanics, and neither issues have pulled recalls, though this seems to be reminiscent of a 17S09 recall with coolant sensor issues, engine cylinder head overheating, and subsequent leaks.

Jun 12, 2024 Fire

Unknown. Something at the backside of the motor caught on fire. The car overheated and would not drive. Pulled over, cooled off, added coolant, drove home. Car won't go over 40, shakes, and makes noises. Took it to automotive place. They took the manifold(?) and stopped! Called and told us there had been a fire in the motor, we need to call our insurance company and take it to a Ford dealership. Warranty and insurance company are both fighting with us. Neither one wants to pay!!! This is total BS!!!! No recalls?! Google this cars problems and their #1 problem is they catch on fire!!! WHY IS THERE NO RECALLS?!?!? Does someone have to die to get a recall?

Mileage: 171,732

Jun 11, 2024 Fire

The contact owns a 2014 Ford Escape. The contact stated that while driving at an undisclosed speed, the engine overheated. In addition, the contact stated that at times the vehicle stalled. The vehicle was towed to an independent mechanic where it was diagnosed with a failed coolant valve. The contact was informed that the coolant valve needed to be replaced. The vehicle was repaired. The contact stated that while the independent mechanic was driving at an undisclosed speed and test-driving the vehicle, the independent was flagged down by a nearby Police Officer. The independent was advised to pull the vehicle off to the shoulder of the road. The independent mechanic was advised that flames were exiting the rear undercarriage and the front undercarriage of the vehicle. The independent mechanic drove the vehicle to the shoulder of the road and exited the vehicle. The Police officer extinguished the fire. The local Fire Department arrived on the scene. A Police report was filed. No injuries were sustained. The vehicle was towed to the dealer. The vehicle was not diagnosed or repaired by an independent mechanic or the dealer. The manufacturer was made aware of the failure but provided no assistance. The contact was advised to contact the NHTSA Hotline to report the failure. The failure mileage 63,000

Mileage: 63,000

Jun 7, 2024

Has to replace the Fan Assembly Coolant sensor three years in a row beginning in 2022, 2023, and 2024. 2023 January, also has the Right Side CV Axcle replaced because a/c coolant was leaking. This leaking went in to the transmission and the transmission also had to be rebuild. Then in 2024 of May the transmission fault service light came on again after being rebuild in January 2023. Took it back to AAMCO and was provided the following codes as errors: P0087- Fuel/Rail system pressure; P0217 engine coolant over temperature; P0219 Engine over speed condition, P0732 gear 2 incorrect ratio, P0733 gear 3, 4, 4 all incorrect ratio. They stated my transmission needed to be rebuilt again and was out of warranty.

Jun 5, 2024

the instrument panel cluster gets inoperative including a blank multiple functional display (MFD), and non-functional warning chimes, messages and warning lights. The engine cylinder head overheats crack and leak oil. Other 2014 Ford escapes have had recalls for the same issues but they are saying mine isn't affected. Obviously it is.

May 15, 2024

While driving this vehicle in traffic, the engine began to fail causing the car to abruptly stall. During this incident, the engine light and low coolant indicator illuminated. Vehicles behind my car nearly slammed into the rear of my vehicle due to this engine failure. Upon inspection, two independent certified service centers confirmed engine coolant had been ingested into the cylinder block causing this engine to fail. Upon full investigation, numerous Ford Ecoboost engines have a manufactures defect on top of the cylinder head that causes this problem. This particular engine only has 52,000 original miles.

Apr 29, 2024

Head gasket and coolant leak. Burning smell entering cabin. Issue comparable to recall 17S09

Apr 24, 2024

I have maintained my vehicle as I always have with previous autos in the past. In 11/22 I had to replace the transmission, which left me 6k+ in debt. My auto is now seemingly going into limp mode for no reason whatsoever and just shutting off while driving. This almost caused an accident, there was NO forewarning of any mechanical issues prior to it doing this. The check engine light came on, rpm’s declined, tried to move to side of the road by pressing gas pedal with no acceleration. Shut car off, called a tow truck mechanic could not diagnose any problem. Since this first incident it has happened almost everytime I’ve driven it. This last time left me and my dog on side of road, unable to move to safe place due to no acceleration with gas pedal. My car is now leaking oil once parked, there’s oil all over hood and internal parts of car, auto is now spuddering with intermittent bursts of power. I’ve never had as many issues with a vehicle as I have with my ‘14 Ford escape ecoboost titanium suv. Upon researching common problems with this year and make this is a MAJOR COMMON ISSUE. For an auto to be “known” for these mechanical issues, these should be ALL covered by the manufacturer!! Transmission is a known issue, the deacceleration and oil leak issue once this issue starts are all known issues. Every mechanic I’ve either brought it to or discussed my issues tell me the same thing, “ oh yeah, that year is known for these issues” so what does one do, when they can’t afford a new vehicle , they owe more on the car due to the repairs? I’ve also needed to replace minimum of 5 headlight bulbs and tail light bulbs within the last 6 months. That’s not normal. Please advise

Apr 17, 2024

My vehicle has a severe oil leak, including leaks at the T valve, vacuum pumps, and transmission fluid. My local garage said this should be covered under the Ford Escape Oil Leak recall, but Ford said it is not. The Ford dealership in Bridgeport, CT, said they were unaware of any oil leak issues with the 2014 Escape, which was not part of the recall. They asked for $3000.00 to cover repairs and said they could not guarantee that the issue would be corrected entirely. My local garage said the vehicle should not be driven as the issue can cause the car to catch fire. I have seen many recalls on the Ford Escape for the problem below. Ford Escape Recall: Certain vehicles with 1.5L engines may have vulnerable engine oil separator housing that can crack and allow oil to leak. A fire can occur if fuel leaks onto an ignition source at high temperatures. Ford states that at least four drivers experienced car fires within five minutes of shutting down the engines in their vehicles. It is disappointing that Ford does not own up to this oil leak issue in their vehicles. I have had nothing but problems with my 2014 Ford Escape. The repair costs are incredibly high. I am making car payments on a vehicle that I can no longer drive due to the dangers of a possible car fire. In addition, Ford knows this is an issue but has not issued a recall for my Ford 2014 vehicle. This is very disheartening as it shows they do not value the safety and lives of their customers. I would appreciate it if this can be looked into further,

Apr 16, 2024

The contact owns a 2014 Ford Escape. The contact stated while driving 35-45 MPH, the vehicle stalled. The vehicle was restarted after several attempts. There were no warning lights illuminated. The vehicle was taken to an unknown local dealer where it was diagnosed that the PCM, electrical system, fuel system and power train had failed. The vehicle was not repaired. The contact stated that the failure was related to NHTSA Campaign Numbers: 22V413000 (Power Train), 14V495000 (Electrical System), and 14V525000 (Fuel System, Gasoline). The manufacturer was not contacted. The failure mileage was approximately 100,000.

Mileage: 100,000

Apr 16, 2024

The contact owns a 2014 Ford Escape. The contact stated that the vehicle was intermittently consuming twice the amount of fuel while driving at various speeds. There was no warning light illuminated. The contact documented that a certain routine trip with the vehicle showed that a 25-mile trip was consuming 55 miles worth of gasoline. The dealer was notified of the failure but could not duplicate or diagnose the failure. The manufacturer was also notified of the failure and referred the contact to the NHTSA Hotline. The vehicle was not repaired. The failure mileage was approximately 81,000.

Mileage: 81,000

Apr 14, 2024

The vehicle engine block has a weak spot in which it has allowed coolant to leak into the number 3 cylinder and thus ruining the engine as my local ford dealer (Greiner Ford. Casper, Wyoming) confirmed. Apparently it's a known issue with ford and they won't do anything to fix it. A check engine light came on and the car started having a bunch of hesitation which led me to the dealership. The issue runs the risk of fire which could cause bodily injury to me and also causes me to be without a vehicle even though I'm currently making payments on it.

Apr 12, 2024

veh running hot and low on coolant; took nearly a gallon to set coolant level when checked. after cycling coolant & getting heat into engine found coolant entering the combustion chamber cracked head or gasket. engine misfire upon start up; white exhaust smoke. check egine light also on.

Apr 11, 2024

The contact owns a 2014 Ford Escape. The contact stated while the vehicle was parked, there was engine oil leaking onto the ground. The vehicle was taken to an independent mechanic, where it was determined that the failure was related to the pistons. The vehicle was then taken to the dealer but was not diagnosed or repaired. The contact related the failure to an unknown recall. The manufacturer was notified of the failure and referred the contact to the NHTSA Hotline for assistance. The failure mileage was approximately 184,080.

Mileage: 184,080

Apr 2, 2024

There's coolant intrusion in my engine due to - as best I can figure - a manufacturing defect that Ford acknowledges in their 2.0L EcoBoost engines (per TSB 22-2229), but NOT in their 1.5L and 1.6L EcoBoost engines (mine is a 1.6L and was produced in parallel with the 2.0L, though they later replaced it with a 1.5L). This is an acknowledged defect, plain and simple, and a safety issue because the engine can catastrophically fail during use due to it! The only fix is literally replacing the engine. Ford won't do anything because it's past the drivetrain warranty.

Mar 28, 2024

My coolant has been leaking starting early this month and I took it to my repair shop. My car has 94,347 miles on it. They told me it could be related to Safety Recall Notice 17S09/NHTSA Recall 17V-209. They put in Stop Leak to help. It did for a while but continues to leak. In searching the internet about this problem, I found that many other people are having this problem and are not getting satisfaction from Ford. In the end, they have to have the engine replaced. I'm worried that this problem will advance to more problems like other people are having. On March 11, 2024, I took the car to my repair shop.

Mar 28, 2024

My daughter's 2014 Ford escape low coolant light came on today and the thermostat jumped straight to over heating and the check engine light came on. The coolant has been going down very quickly during normal use and she has to continually fill the coolant more and more recently. Today was the first time the light came on and it overheated.

Mar 26, 2024

The contact owns a 2014 Ford Escape. The contact stated that while starting the vehicle, the engine overheated immediately. The check engine and engine temperature warning lights were illuminated, and the "Low Coolant" message was displayed. The vehicle was towed to an independent mechanic, who advised the contact to tow the vehicle to the dealer. The vehicle was then towed to the dealer, where it was diagnosed with coolant intrusion into the engine, and the engine needed to be replaced. The vehicle was not repaired. The manufacturer was made aware of the failure and a case was opened. The manufacturer advised the contact to file a complaint with the NHTSA Hotline. The failure mileage was approximately 107,000.

Mileage: 107,000

Mar 14, 2024 Fire

The contact owned a 2014 Ford Escape. The vehicle was taken to an independent mechanic for a service appointment which included a system scan and replacement of the coolant valves. The contact stated that after the repair was completed and the mechanic was test-driving the vehicle, the engine caught on fire. A nearby Police Officer alerted the mechanic to pull the vehicle over to the shoulder of the road because the vehicle was on fire. The mechanic drove the vehicle to the shoulder of the road and exited the vehicle. The Police Officer extinguished the fire by using a fire extinguisher that was in the trunk of the officer's vehicle. No injuries were sustained. The vehicle was towed back to the independent mechanic. The contact was informed that the cause of the fire was the engine and the engine coolant. The vehicle was destroyed due to the fire. The manufacturer was made aware of the failure and a case was filed. The failure mileage was approximately 65,000.

Mileage: 65,000

Mar 14, 2024

Per mechanic, cylinder head crack causing to oil leak

Mar 5, 2024

Coolant system leaking continuously causing overheating; frequent issue in 2014 ford escapes

Feb 27, 2024

Vehicle has been to Ford dealer several times for loosing coolant. The error message for low coolant is always on, even after verifying the level. The dealer states not to worry about the error message and that they cannot locate the leak. Recently the vehicle warnings for overheating went off and found that the coolant reservoir was low. The dealer maintains they are unable to find a leak or root cause of the problem.

Feb 22, 2024

I have had coolant issues with this car for 7+ years. No matter what work I have done to it, it still looses coolant. I'm currently topping off the reservoir every 3-4 days. Pressure test does not find a leak but it must be going somewhere!! Within the past 3 months I have had: - heater hose replaced ($500+ at dealership) - valve cover gasket and turbocharger wastegate control solenoid replaced ($800+) - coolant tube and vac system replaced ($1000+ at dealership) I have had other extremely expensive repairs done over the years, including recalls, and the car still looses coolant somehow.

Feb 18, 2024

Coolant circulation as part of recall 17S09. Not sure if my car was affected but it’s not right. We have change coolant bottle and coolant seems to be going somewhere and can’t figure out if my car was with this recall. Also already had to rebuild transmission. It was destroyed. $5000. Will never buy a ford again

Feb 14, 2024

The contact owns a 2014 Ford Escape. The contact stated while the vehicle was idling, the vehicle stalled. The contact stated that several attempts were needed to restart the vehicle while depressing the accelerator pedal. The check engine warning light was illuminated. The contact became aware of NHTSA Campaign Numbers: 14V495000 (Electrical System) and 15V005000 (Fuel System, Gasoline) however, the VIN was not included in the recalls. The failure persisted and occurred more frequently. The vehicle was taken to an independent mechanic where it was diagnosed that the fuel injector line had failed as well as there was a wiring failure causing the battery and engine to engage or disengage unintentionally by the driver. The alternator and battery had been replaced; however, a third repair had not been completed. The manufacturer was made aware of the failure where it was confirmed that the failure was related but was not included in the recall with the NHTSA Campaign Number: 14V495000 (Electrical System). The manufacturer referred the contact to the NHTSA Hotline to file a complaint. The failure mileage was 65,000.

Mileage: 65,000

Feb 9, 2024

Coolant intrusion around 130,000 miles. I swapped the motor from a 2013 Escape that had 107,000 miles on it and the coolant intrusion is happening with that one after driving 15,000 more miles.

Feb 9, 2024

My car has 15 recalls. I was only notified of 2. According to one of the letters I received It states that repairs were done but not completed and that is a lie. I have never had any recall work done, mainly because the first letter said they didn't have parts. I was only made aware of the latest 2 and no work has ever been done that I am aware of nor have I ever been notified until recently. So why are they saying work was done when I know it wasn't? One of the recalls says my car should not be driven for safety reasons. How can they be trusted? I know the repairs were not done even though the letter says it has been done. How can they claim it was fixed, when I know for a fact it wasn't. What can I do to prove they are lying? Shouldn't there be records? I would love to see these records. My name is [XXX] [XXX] . or [XXX] . My car is a 2014 ford escape. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6)

Feb 4, 2024

My 14 Escape will not turn off. This is a standard start not push button. Been running for an hour without key in ignition. Recall for this issue is not for 2014 models it seems. Does have factory dealer installed remote start that was put in years ago.

Jan 31, 2024

After remote starting the vehicle, the vehicle timed out. Upon entering and starting the vehicle, a check engine light and overheating notification were received. The vehicle was undrivable and this occurred during single-digit temperatures. The vehicle was left overnight (single-digit cold weather) and upon return the following day, the vehicle was started and still had a check engine light and engine overheating notification. The vehicle was towed to the dealership for diagnosis. The dealership determined that coolant was leaking into cylinders 1 and 2. The dealer indicated that the necessary repair would be an entire engine replacement and was quoted $10,000 dollars. The repair estimate was declined and the vehicles check engine light was cleared and ran fine.

Jan 30, 2024

The contact owns a 2014 Ford Escape. The contact stated that while driving at an undisclosed speed, the vehicle overheated. The contact stated that a year ago, the vehicle was serviced under an engine recall repair due to coolant leak. The contact stated on several occasions, the vehicle had been taken back to the dealer due to the failure after the recall repair had been completed. The vehicle was towed to the dealer and remained at the dealer since the beginning of January 2024. The vehicle was not diagnosed or repaired by an independent mechanic or dealer. The manufacturer was made aware of the failure. The failure mileage was approximately 90,000.

Mileage: 90,000

Jan 29, 2024

The contact owns a 2014 Ford Escape. The contact stated that while she and a guest were driving at 35 MPH, the vehicle lost motive power, with unknown warning lights flickering. The contact stated that she observed white smoke coming from the rear of the vehicle. The vehicle was steered to the side of the road where the vehicle was shut off. On another occasion, that engine started to overheat. The vehicle was steered to the side of the road where coolant was added; however, the failure persisted. The vehicle was turned off and was not able to operate. The vehicle was towed to the residence. The vehicle was then towed to a dealer where it was diagnosed that the cylinder head was cracked, and coolant and oil were leaking into the engine. The manufacturer was not notified of the failure. The failure mileage was approximately 132,000.

Mileage: 132,000

Jan 27, 2024

While driving down the interstate, this car started smoking and i was unable to use the brakes. Its like the braking system locked up. I couldn't push the brakes because it was down to the floor hard with NO intentions on stopping. Emergency brakes were needed to stop this vehicle. The gear shift does not seem to in the correct position. Seems to be some type of powertrain issue. The coolant was leaking and there was no vacuum on the motor. The drivers door latch is defective, when opening the door it doesn't retreat, the latch stays in the open position. The backup camera is defective, doesn't show you are backing up. Dashboard shows brake lamp default an brake lights not out.

Jan 24, 2024

The contact owns a 2014 Ford Escape. The contact stated that the service engine warning light was illuminated on the instrument panel. The vehicle was initially taken to an independent mechanic where a coolant leak was discovered between cylinders #2 and #3. The vehicle was then taken to the dealer and the failure was confirmed. The contact was informed that the engine needed to be replaced. The manufacturer was notified of the failure but offered no assistance. The engine was replaced out of pocket. Recently, another coolant leak was discovered during an engine inspection. The vehicle was repaired; however, there was a strong fuel odor coming from the vehicle. The vehicle was taken back to the dealer and the contact was informed that the fuel odor was not detected. The vehicle was not repaired. The failure mileage was 124,173.

Mileage: 124,173

Jan 18, 2024

The contact owns a 2014 Ford Escape. The contact stated that while driving at an undisclosed speed, the engine misfired. The contact stated that occasionally, the vehicle failed to start. Additionally, the contact stated that coolant had been leaking out of the reservoir and the contact noticed a burning odor coming from under the hood. The vehicle was taken to the dealer where it was diagnosed that coolant leaked into the engine and caused engine failure. The contact was informed that the engine needed to be replaced. The vehicle was not repaired. The manufacturer was made aware of the failure. The failure mileage was approximately 70,000.

Mileage: 70,000

Jan 16, 2024

I've had to send this car into the shop multiple times since I bought it 2 years ago. It has cost me thousands. Every time it gets 'fixed' the same issue pops up a month or two later. Disaster of a vehicle.

Jan 15, 2024

A repeated low coolant light continues to show up after refilling the system and having it flushed. The system message center presented a message that said "Stop Safely Now" due to low coolant. The engine temperature gauge was reading completely cold.

Jan 10, 2024

The contact owns a 2014 Ford Escape. The contact stated while driving 45 MPH, the "High Engine Temperature - Stop Safely" message was displayed on the instrument panel with the temperature gauge indicating that the engine was hot. The contact pulled over and allowed the engine to cool down. Upon inspection, the contact discovered that the coolant reservoir was empty. The contact replenished the coolant and drove the vehicle home. The dealer was notified of the failure and the contact was informed that there were no recalls on the vehicle. The manufacturer was not notified of the failure. The vehicle was not repaired. The failure mileage was approximately 78,000.

Mileage: 78,000

Jan 10, 2024

The contact owns a 2014 Ford Escape. The contact stated while driving at an undisclosed speed, the "High engine temperature, stop safely" message was displayed before the vehicle lost motive power. The check engine warning light was illuminated. The vehicle was coasted to the side of the road. Upon inspection, the contact discovered that the coolant reservoir was empty. The contact had to add water or coolant to the coolant reservoir for the vehicle to restart. The vehicle was taken to an independent mechanic; however, the cause of the failure could not be determined. The vehicle was not repaired. The contact stated that the vehicle previously had two unknown repairs for coolant intrusion; however, the failure recurred. The manufacturer was made aware of the failure and a case was opened. The contact was advised to file a complaint with the NHTSA Hotline. The failure mileage was approximately 112,000.

Mileage: 112,000

Jan 10, 2024

After no signs of overheating or leaks the coolant level of the car has dropped significantly after topping off several times. The heat stopped working and the coolant reservoir never stayed filled. We took it to the dealership for diagnosis. The service representative told us the coolant was leaking directly into the engine and the only solution is to replace the cracked engine block.

Jan 8, 2024

Engine slowly loses antifreeze which is leaking into cylinders. This causes overheating and cracked block. This is a problem with all Ford 1.6 litre motors. Ford knows this!

Dec 22, 2023

UNKNOWN My engine is cracked and leaking fluid. This has been verified by an independent mechanic inspection. Passenger safety is threatened by stalling in traffic or engine fire. The check engine light signaled the issue. Strikingly similar issues for similar vehicles of the same make (2014 Ford Escape ) from the same factory (Louisville) built at the same time (2014) have already been documented in recall 17V09 (Ford recall 17s09). I am fearful my car will catch fire as well. I would have reported this issue sooner but I received misleading information from Ford which told me that NHTSA bore responsibility for including my vehicle in this recall. Since the incident I have been working with my mechanic, the dealer, and Ford, and finally called NHTSA on 12/22/2023 (call 1459052).

Dec 22, 2023

COOLANT INTRUSION FIRE CONFIRMED BY A DEALER ONLY A DEALER SYMPTOMS, VERY LOW COOLANT. APPEARED SEPT 2022 AND SEPT 2023

Dec 15, 2023

Vehicle is leaking coolant. This seem to be common on this model even after the coolant recall service was performed.

Dec 14, 2023

Engine overheated, loss of coolant, check engine light illuminated. Towed to Ford dealership. replaced valve cover gasket and spark plugs. Dealership said this would fix overheating issue. 3 weeks later engine overheated again, loss of coolant, check engine light illuminated. Towed for a different Ford dealership. No stored code for check engine light illuminated. Mechanics cannot reproduce overheating. Mechanics said they have found nothing wrong, no loss of coolant. There is a recall for 2014 Ford escape 1.6L ecoboost, Ford is saying my vin number does not fall in this recall of Engine and Engine cooling. Recall # 17V2009000. Both dealerships say nothing is wrong with the car, they cannot find an issue yet it has happened 2 times now.

Dec 11, 2023

I was not notified by Ford of two recalls issued on my vehicle.

Dec 9, 2023

I purchased this vehicle used in 2017. I’ve had no issues until this year with coolant level problems. Every time the car went in limp mode, coolant had to be added several times. I went online to see if my car had any recent non-repaired recalls-there were none. However, I did find that there was a recall-#17S09-which is a coolant issue. Went to Preston Ford in MD who told me I need a $10,000 new motor because coolant is leaking in cylinder 4. If the coolant problem was repaired prior to me purchasing the car, why am I now having a coolant problem. I don’t think I should be responsible for any repairs to correct this problem. Please let me know what my next steps should be in situation. Thank you!

Dec 2, 2023

My car was put into safety mode and dropped down to 3 miles per hour

Nov 7, 2023

My car began to overheat and enter limp mode, when diagnosed the codes that appeared correlated directly with a safety recall issued in 2017. I brought my car to ford 2x to have them service the recall. I was given my car back, with the check engine light on and still overheating.i went to another dealership, who diagnosed my car again and I paid 712$ for a “water outlet connector “ and this did not resolve the issue. Ford decided to keep the car for 2 months, unable to diagnose the issue, they kept dropping it off to me and it would overheat… they towed it 2x back to the dealership for overheating after they drove 100+ miles on it. Instead of fixing the issue, they kept telling me it was not overheating and dropped it off to me with the check engine light on, the same codes, and overheating… stopping abruptly at high speeds. I brought it back to ford after it cut power at 50 mph with my daughter in it… Now I am being told, I have a cracked cylinder head and the recalled part has nothing to do with the cracked cylinder head … which was not cracked prior too all the repairs done. I was not informed that it was cracked, until November 6 2023. My car has been serviced since July 21st 2023. A cracked cylinder head, is a direct result of a faulty recalled part… which ford replaced a coolant level sensor and stand pipe to prevent this issue. It is not resolved. The estimated the repair at 5800$ and failed to give me any invoices. Refusing to work on my vehicle.

Oct 30, 2023

The contact owns a 2015 Ford Escape. The contact stated while driving 45 MPH, the engine was overheating. Additionally, the contact stated that the vehicle was consuming an excessive amount of engine oil. The message to “Pull Over Safely” was displayed. The vehicle had not been diagnosed or repaired by an independent mechanic or dealer. The manufacturer was made aware of the failure. The failure mileage was approximately 114,000.

Mileage: 114,000

Oct 26, 2023

The contact owns a 2014 Ford Escape. The contact stated that while the brake pedal was depressed, the coolant temperature warning light illuminated. The vehicle was steered to the side of the road and turned off. The hood was lifted, and a sizzling sound was coming from the engine compartment. The vehicle was taken to two independent mechanics where it was diagnosed that the engine needed be replaced, due to coolant leaking into cylinder #4. The vehicle was not repaired. The manufacturer was not notified of the failure. The failure mileage was approximately 150,000.

Mileage: 150,000

Oct 23, 2023

*coolant level stand pipe and sensor. *the car just start doing the overheating while I was on the highway and the car just slow the running while I was there. *yes I bring the car to and authorize ford dealer. *no *yes a warning light saying that the coolant level was low but the coolant was full. Is being and issue since I buy the car. I bring it to the dealer where I buy it twice and they say they fix it. But because the car broke down because the transmission went down I didn’t notice that the problem never being fix. Until I take the car out of the transmission shop. And still have the same issue now is not running. *so the car is just shaking and slow down because it says the engine is overheating

Oct 20, 2023

Engine Coolant leak. Been getting repeated warnings about engine coolant being low, despite repeatedly replenishing the coolant. And yes, when I check to see if the coolant is actually low, it is, indeed. But it shouldn't be, given the recent replenishment.

Oct 15, 2023

I have been needing to add coolant to my car almost bi-weekly and just recently it lost power while getting on the freeway. The airbags have been problematic since I purchased the vehicle even after having the wire harness replaced twice at a Ford dealership. The light will not go off.

Oct 12, 2023

The contact owns a 2014 Ford Escape. The contact stated while driving at approximately 40 MPH in traffic, the vehicle stalled. The contact stated that the check engine warning illuminated. The contact stated that it took several attempts to restart the engine. The contact stated that the failure was intermittent at first but had become a recurring failure. The contact had taken the vehicle to an independent mechanic where it was diagnosed and found that there was a manufacturer bulletin associated with the repair (SSM47826). The vehicle had not been repaired. The manufacturer had been informed of the failure. The failure mileage was 83,809.

Mileage: 83,809

Oct 10, 2023

The contact owns a 2014 Ford Escape. The contact stated while the vehicle was idle, there was white smoke coming out of the exhaust pipe. There was no warning light illuminated. The vehicle was taken to the Toyota dealer where it was purchased. The Toyota dealer diagnosed that engine oil was leaking from the valve cover gasket. The dealer replaced the valve cover gasket, the coolant hoses, and the coolant reservoir; however, the failure recurred. The vehicle was taken back to the Toyota dealer, where the engine was replaced; however, the failure persisted, and the engine was replaced a second time. The contact stated that upon taking the vehicle to the Toyota dealer for an oil change, the dealer informed the contact that the Eco booster was leaking. There was no further information provided. The vehicle was not repaired. The local Ford dealer was not notified of the failure. The manufacturer was notified of the failure and a case was opened. The manufacturer referred the contact to the NHTSA hotline for assistance. The failure mileage was approximately 113,154.

Mileage: 113,154

Oct 3, 2023

The vehicle started to blow burning oil from the exhaust on a cold start. The vehicle started to occasionally lose acceleration. Also there was a clicking noise from the engine. After about a week, the low coolant trouble light came on. I took the vehicle to my mechanic and he stated that there were serious engine problems. He said the troubles were definitely engine problems. He said it was probably due to bad cylinders and cylinder heads.

Sep 23, 2023

Coolant leak into engine, resulting in recommended engine replacement

Sep 19, 2023

Vehicle coolant level sensor failed. This is causing the engine to overheat and broke the head gasket.

Sep 12, 2023

This vehicle was purchased by an “Authorized Dealer “ on August 31st 2023. I was unaware of the many issues that this vehicle had. Within the first few hours of driving off the lot in this car, I put the car in reverse and for one the back up camera stalled, secondly, a message appeared stating the camera is unavailable and for me to contact the dealer. Well I did, I contacted Five Star Ford and was told $165 just for a diagnostic. Additionally, I was driving on the highway Sept. 9th and the car just began to lose power. I literally was pedal to the metal trying to get home in hopes that this vehicle didn’t give out on me. Shortly after that, the check engine light came on and as I accelerated, this rough noise seemed as though it was getting louder and louder. Last but not least, this car drinks gas likes it’s going out of style. The overall mileage is bogus. According to the odometer after having this car for 11 days, I had supposedly put 1,000 miles on this vehicle!!!! That’s absurd to me!! I haven’t been out of the town or anything. I’ve watched the odometer jump from 120812 to 120837 after only traveling about 2 and half miles. Like what’s going on with this these faulty transmissions in these cars, FORD! What are you doing about it??? People work hard to purchase a car for them and their family. Why make our lives more difficult with these faulty vehicles??!!

Sep 11, 2023

My vehicle has had ongoing coolant issues. Come to find out the coolant has been leaking into the cylinder. I started my car it stalled and stared smoking like it was on fire.

Sep 10, 2023

While driving the vehicle, the car will stall without any warning. The oil light will display, as well as the check engine light, but only after the car shuts down and is not operational. This has occurred at least 4-5 times in the past year or so, the most recent 2 weeks ago. The stalls occur while the vehicle is in motion, and there is no prior warning given. The car has been hooked up to a code reader, which displayed the code P0087, which is a Fuel Rail/System Pressure Too Low. If we let the car set for a few hours, it will start up and be operational, but then will stall out again with no warning. We took the car to a Ford Dealership in Trinidad, CO, and the technician said he assumed it was a low fuel pressure sensor, which he replaced, but stated that he only suspected that was the problem since he could not get a code to come up at that time. After the sensor was replaced, the car has continued to stall out while being driven. I called Ford to ask if my car was part of a fuel system recall, they stated my vin was not listed, although my vehicle was manufactured within the time frame of two, 2014 Ford Escape fuel system issue recalls. The safety of myself and my family are put at risk every time the car stalls out because we have been traveling on the interstate and have almost been hit by other vehicles due to not being able to accelerate or have time to pull off to the shoulder immediately, We have also been crossing through intersections with heavy traffic when the car will stall out without warning, which has led to near collisions. My vehicle is available upon request for inspection.

Mileage: 102,293

Sep 9, 2023

Our ford escape has been leaking coolant excessively and is experiencing intermittent over-heating of the cylinder head. Ford has a recall for this matter however our local ford dealership refuses to service our vehicle, there are also two other recalls that they are refusing to acknowledge.

Aug 23, 2023

The contact owns a 2014 Ford Escape. The contact stated while his wife driving 35 MPH, the check engine warning light illuminated. The contact took the vehicle to the local dealer, where it was diagnosed with failure in cylinder #2 and #3. The contact was informed that the engine needed to be replaced. The vehicle was not repaired. The manufacturer had been informed of the failure. The failure mileage was approximately 92,000.

Mileage: 92,000

Aug 21, 2023

I bought this vehicle exactly 1 year ago back in June from The BMW dealership in Arlington, Texas Under the assumption that there was nothing wrong with it Mechanically. The dealership Lied to me because not even a week later. I had to take it to a Firestone to see what was wrong with it. And they said that there was coolant loss, They did do a pressure track and said at the time it was not the gasket period I have taken it to other mechanics since then trying to fix what they said the issue was but there has been a loss of coolant in that vehicle and we don't know where it's going period period I don't know what to do because there was a recall on it. From what I searched on the internet long ago? But it is no longer available. And that's unfortunate for me. Because I believe that the recall that they had back in 2017 I believe that's the issue that is currently wrong with the vehicle the recall code was 17s09. I don't know what else to do because I'm at a loss. I spent eight thousand dollars on a vehicle that I cannot even enjoy Because it has been in the shop more times than I have driven it

Aug 19, 2023

On August 19 2023 I brought my 2014 Ford Escape SE to an auto repair shop, because the engine temperature went up. The repair shop first told me that the coolant resevoir and the hose was leaking. After that was fixed. The repair shop could not start the car it overheated. The repair shop said that the head gasket blew and the engine was done. I paid almost 11000 dollars for this car with 87000 miles on it. The only car I have. I do not know what to do with this situation. I found out that the 2014 Escape models is a problem with coolant leaking into the engine. Now im out of a car and do not know what to do.

Aug 9, 2023

I own a 2014 Ford Escape Eco boost 2.0 liter. Vehicle started losing coolant but no visible leak. Took car to be diagnosed at a ford dealership where they told me vehicle was fine and passed a pressure test. Less than 600 miles later the vehicle is overheating, smoking from engine and tail pipe, even for an extended time after vehicle is off. I have video of vehicle smoking while engine off. Now I am told it is a head gasket issue and repair is over $7k. This is a known issue that Ford refuses to acknowledge and issue a recall. There's been nurmerus of people whom have experienced exact issue and are joining a class action lawsuit. If NHTSA doesn't do their part to put this ford 1.6-2.0 liter on a recall, then the wrong doing continues and should be held accountable as well. There have been cases where same make/model has been reported catching on fire. Someone is going to get physically injured if not already. Requesting an investigation to conducted and faulty engines replaced.I am unable to load pictures and videos from computer I am submitting this complaint with. If permitted I will email pictures video, dealership pressure test , and other documenation from my personal computer.

Aug 8, 2023

Car started having smoke out of tail pipe, been having to fill anti freeze once a month in to, vehicle , and has started misfiring not sure . Apparently antifreeze is leaking in to engine . May 2023 is when we have started having issues with anti freeze The consumer wanted to add that the vehicle also stalled out in traffic during a separate incident.

Aug 4, 2023

The car is no longer drivable. I have an earlier reference number 11526542. When I called at that time I was unaware of the actual problem. In 2019 I had taken the car to Future Ford for a coolant problem. They stated in paper work there was no leak in the coolant but more coolant needed to be added. I return to have oil changed and ask them to add coolant. They refused. I went to Green Valley Tire and brake and they refused. Thought that was weird. Went to Auto Zone Folsom and bought coolant and added myself. Future Ford still stating no problem. I had purchased a 7 year waranty on the car and a plan were they did all the service. The car was only serviced by Ford Dealer. I have just recently learned that there is an issue with the Ford 2014 Escape Eco Boost System. I am not a mechanic but from what I understand coolant goes into the engine. Maybe a head casket blows out. It then causes car to overheat. Coolant intursion present. Future Ford recomends replace engine block per Future Ford. Was told just tempory fix likely will happy again. Design flaw. Dangerous not sure when it will occur and then car undrivable. Overheats could cause fire. Should be under lemon law. Car only has 55,000 miles on it. Attached estimate of $16,000 to fix by Future Ford. Also said their was a recall on coolant in 2019 but Ford Corporate said it did not show on my Vin #. Your system does not show it .

Aug 2, 2023

Motor coolant went into engine cylinders and over heats and now my vehicle won't run.

Jul 28, 2023

I had bought my 2014 escape less then four years ago. Back in June 2023 I had my dashboard light up with engine overheating pull over safely while I was driving. I pulled my car over as best as I could and saw my coolant was low. I was able to drive the five miles or so home after refilling the coolant. The coolant was again empty when I got home. The dealership checked and said no leaks or anything but I still have to refill my coolant every two days. From researching there are many issues with ford escape and coolant leaking. I am too scared to even drive it especially with my family in it knowing this leak may cause a fire or something

Jul 26, 2023

The car began making noise an did not want to shift. After getting the vehicle into drive, the car stopped moving while driving in heavy traffic.

Jul 25, 2023

The car accelerates very choppy. I’ve also been getting a warning saying “ENGINE FAULT, SERVICE NOW.” I’m not sure what is wrong with it, it still drives as of right now and there is no recall for me to get it fixed.

Jul 21, 2023

Engine coolant is coming out of coolant reservoir! Car is smoking and their are no lights on dash untill it is low. If idle with auto starting it will over heat and car can't be started.

Jul 21, 2023

The contact owns a 2014 Ford Escape. The contact stated that while driving, the vehicle failed to exceed 4-5 MPH before the vehicle stalled. The vehicle was able to reverse but failed to move further. The vehicle was towed to a certified mechanic who diagnosed that the transmission failed and needed to be replaced. The vehicle was repaired. The contact stated that several days later there was a clunking sound coming from the front of the vehicle. The vehicle was returned to the mechanic who stated that the sway bar had loosened. The vehicle was repaired. The contact stated that the check engine warning then became illuminated. The vehicle was returned to the mechanic who diagnosed the vehicle with cam shaft failure. The spark plugs were replaced; however, the vehicle continued to sputter while starting and was leaking coolant and oil onto the cam shaft causing the head gasket to be blown. The vehicle was not repaired. The manufacturer was made aware of the failure and referred the contact to the NHTSA Hotline. The approximate failure mileage was 95,500.

Mileage: 95,500

Jul 17, 2023

The contact owns a 2014 Ford Escape. The contact stated that the check engine warning light was illuminated. The contact took the vehicle to an independent mechanic to be diagnosed. The contact was informed of a misfire in cylinder #2. The dealer reset the warning light however, the warning light returned. The vehicle was taken back to the dealer where the ignition coil was replaced; however, the failure recurred. The dealer replaced the engine with a used engine. Recently, the contact stated that the check engine warning light illuminated. The vehicle was taken to an independent mechanic and the contact was informed that there was a misfire in the engine. The manufacturer was notified and provided the contact with a case number. The vehicle was not repaired. The failure mileage was unknown.

Mileage: 167,525

Jul 1, 2023

Engine Coolant leak that causes over heating in car.

Jun 29, 2023

When driving vehicle on highway it slows down then have to push on gas pedal to exelarate like it sputters then shuts off. Dashboard says Engine Failure park vehicle immediately very frustrating!! I’m about to file a lawsuit if this doesn’t get taken care of!

Jun 28, 2023

The Escape in question has a reoccurring issue with the canister purge valve causing gas tank burping and rough engine idle. Mechanic replaced said item a couple of years ago and the problem has reoccured. There is a recall for a Ford Focus with the same year as This Ford Escape 2014. Should not this vehicle be repaired in the same manner by the dealer as the Ford Focus Recall? My mechanic also noted there is a TSB for this Ford Escape 2014 acknowledging Ford has updated the parts for repair to solve the know canister purge valve issue. Replacing the parts for a second time seems unfair and costing twice as much to resolve the same issue with an updated part. Frustrated 🥴 Update: Since composing the above information the cars condition has become more in need of repair. The 2014 Ford Escape is idling rougher, the gas tank flapper is burping while the car is running and the car is randomly stalling. These conditions correlate with a current safety recall for the Ford Focus of the same year 2014.

Jun 21, 2023

The contact owns a 2014 Ford Escape. The contact stated while driving at an undisclosed speed, the vehicle hesitated and started sputtering. The check engine warning light started flashing then remained illuminated. The vehicle was taken to an independent mechanic where it was diagnosed that coolant had leaked into the engine and the engine needed to be replaced. The vehicle was currently at the independent mechanic. An undisclosed dealer and the manufacturer were notified of the failure, but no further assistance was provided. The failure mileage was approximately 55,000.

Mileage: 55,000

Jun 12, 2023

The contact owns a 2014 Ford Escape. The contact stated while driving at an undisclosed speed, the vehicle was running rough. The contact stated that the engine had misfired. The engine warning light was illuminated. The contact stated that the coolant level was low. The vehicle was taken to an independent mechanic who topped off the coolant. The contact also received notification of NHTSA Campaign Number: 22V413000 (Power Train) however, the part to do the recall repair was not yet available. The local dealer was contacted. The contact stated that the manufacturer had exceeded a reasonable amount of time for the recall repair. The manufacturer was made aware of the issue. The approximate mileage at the time of the failure was 45,000. Parts distribution disconnect.

Mileage: 45,000

Jun 10, 2023

2014 Ford Escape titanium that has been having issues with coolant leaks and overheating. The first instance was in Dec 2022. The vehicle stalled while it was being driven at about 25-30 mph. The vehicle said that the coolant levels were low and the cars Engine heat level shot up. Checked the coolant level and it was full as I recently changed the oil and topped everything off. I towed it to Cortese Ford dealership in Henrietta and a appointment was set for about 4 days later. They said the issue was that the car was leaking coolant somewhere but they can’t find where, so our options were A.) use a pump process where they would pump air into the coolant system and see where the leak is or B.) reroute the entire coolant system and see if that resolves the issue. So I went with option B because it was the cheaper option and it costed about $996 dallors. About 3 months later the same issue occurred, car stalled, engines heat gage shot up but this time the coolant level was low even after a top off. I added coolant and the car came back but I still called Cortese to see if there was a bigger issue. Appoint was set for 5 days later and we took it there. They came back and said the issue was that one of the main heater hose was cracked and was leaking coolant, and that costed another $1000 to fix. Finally last Thursday, the car wouldn’t start up, the dashboard was saying the cars Engine was overheating and couldn’t be started. So I waited an hour later and tried to start it again, and it said the same thing. I drove it down to a local auto shop even with the warning to get it checked out. The mechanic checked the cars codes and we had 7 codes pop up. They were P0116, P050A, P050B, P050E, and P1299 and to my understand they all have to do with Temperature and overheating

Mileage: 184,634

Jun 7, 2023

On May 27, 2023, I took my Ford Escape SE to dealership for service (mileage: 99742). I had Works Synthetic Oil Change, Mutli-point inspection, rotation of tires, coolant system cleaning, brake systems fluid exchange, spark plugs replaced, air filter replaced. Diagnostic for A/C. Total cost: $1005.90. Results from service: (1) Emergency flasher or hazard light button does not work. $199.95 Diagnostic fee to repair flasher/hazard light button. Due to cost of Diagnostic fee, repair to Emergency flasher or hazard light button was not conducted. (2) AC not working. Diagnostic Fee $199.95. AC leakage. Repair parts, YN*19* Refrigera10009G and BV6Z*19850*B Evaporato22105B cost $486.96 and labor fee 2150.00 + tax $171.40. Total Cost: $2808.36. Due to total cost, repair to AC was not conducted. (3) When replacing the spark plugs, oil was found in the valleys of the spark plugs. Unsure if the valve cover or something else that pertains to it is damaged or some other type of issues. Due to cost of diagnostic test ($199.00), service was not conduct.

May 5, 2023

While driving down the road a warning pops up on the dash that says "High Engine Temperatures. Please Stop Safely" Had to have the car towed because it got stuck in Limp Mode and would not drive. Had the codes read and it comes up with code P1299 which says Cylinder Head Overtemperature Protection Active. Car stays in Limp Mode and is undriveable until code is cleared with a code reader. Happens several times over and over again within a 30 minute drive.

May 5, 2023

While driving 30 minutes home from work, High Engine Temperature Warning popped up and stuck car in Limp Mode 20+ times. Had to use a Code Reader to clear the code P1299 that says Cylinder Head Overtemperature Protection Active in order to get car to drive home. Meanwhile it was leaking coolant, car went thru 1.5 gallons of coolant during that time frame.

Apr 28, 2023

The contact owns a 2014 Ford Escape. The contact stated that while driving at an undisclosed speed, the vehicle overheated, with the engine overheated message displayed. The contact pulled over, and the vehicle was towed to an independent mechanic, who determined that the engine needed to be replaced. The vehicle was not repaired. The manufacturer was made aware of the failure and a case was opened. The manufacturer confirmed that there was no recall associated with the VIN and advised the contact to file a complaint with the NHTSA Hotline. The failure mileage was approximately 65,000.

Mileage: 65,000

Apr 19, 2023

The low coolant warning light came on a few times, top off coolant and took car to dealer for service and diagnosis. The service performed test and did not find leaks or damage. After a few times with not findings the engine light came on while driving and the vehicle had misfire. Contacted the dealer and the vehicle was diagnosed with coolant into the engine cylinders witch caused the misfire. According to service the engine has to be replaced and the car is not drivable. Based on research, this is a problem many costumers had to deal with.

Apr 18, 2023

2014 FORD ESCAPE. CONSUMER WRITES IN REGARD TO NHTSA SAFETY RECALL 17V-209. THE CONSUMER STATED WHILE DRIVING AN 1.5 HOURS TO THE BEACH BACK AND FORTH THE VEHICLE STOPPED ACCELERATING AND THE VEHICLE TO A FORD DEALERSHIP. THE MECHANIC STATED THE ENTIRE ENGINE HAD TO BE REPLACED DUE TO A CRACKED ENGINE AND OVERHEATING.

Apr 15, 2023

It seems like my transmission kicked out on me in the middle of a busy intersection. Now my car is stuck at work while I figure out where to take it and how to pay for transmission repairs.

Apr 12, 2023

I see there was a previous recall on the ford smaller eco boost engines. I am having the same issues with coolant leaks and head gasket. Not only me but hundreds of other owners have having the same exact issue of coolant leaking and head gasket going bad.

Apr 12, 2023

Car is burning and leaking coolant dude to faulty head gasket and engine over heating. Engine also stalls out when slowing down and shuts off. I see multiple people are having the same issues. This has been a on going thing I took it to the shop to have coolant leak fixed and it still has reoccurred.

Apr 5, 2023

The contact owns a 2014 Ford Escape. The contact stated that the vehicle failed to start as needed. While driving at various speeds, the vehicle stalled with unknown warning lights illuminated. The vehicle was taken to the local dealer and an independent mechanic, and the contact was informed that anti-freeze was intruding into the engine. The vehicle was repaired but the failure recurred. The vehicle was taken to the local dealer who provided an unknown diagnosis. The vehicle was not repaired due to parts being backordered. The manufacturer was not contacted. The failure mileage was approximately 86,000.

Mileage: 85,000

Apr 5, 2023

The contact owns a 2014 Ford Escape. The contact stated while driving 55 MPH, the check engine warning light illuminated, and the vehicle started to overheat. The contact was able to pull over on the side of the road and noticed that the coolant level was low. The contact added more coolant and the vehicle started operating normally. The vehicle was not diagnosed. The manufacturer was not contacted. The failure mileage was 140,000.

Mileage: 140,000

Apr 4, 2023

The contact owns a 2014 Ford Escape. The contact stated that while driving at an undisclosed speed, the check engine warning light illuminated. The vehicle was not diagnosed or repaired. Neither the dealer nor the manufacturer was notified of the failure. The failure mileage was approximately 160,000.

Mileage: 160,000

Mar 31, 2023

Car was taken to shop and advised there where engine issues. Took it to an authorized dealer and was advised it was a heating hose issue. Took it back in and after 2 weeks we were told it needed an engine. The car is constantly leaking coolant which has spilled onto the engine and could cause a fire while driving. Ford will not help with any repairs. Vehicle has been in the shop for 5 months

Mileage: 113,099

Mar 13, 2023

The contact’s mother owns a 2014 Ford Escape. The contact stated that while driving at approximately 5 MPH, the vehicle stalled. The vehicle was towed to a dealer where there was no cause for the failure determined. On another occasion, the contact stated that while driving 40 MPH, the vehicle stalled. The contact stated that the vehicle was pulled over to the side of the road. The contact stated that the failure had been reoccurring. The contact stated that the vehicle was towed to an independent mechanic where it was diagnosed with a cracked engine block. The vehicle was not repaired. The contact stated that the coolant temperature and engine warning lights were illuminated. The manufacturer was notified of the failure. The approximate failure mileage was 40,000.

Mileage: 40,000

Mar 1, 2023

The contact owns a 2014 Ford Escape. The contact stated that while driving at an undisclosed speed, the check engine warning light illuminated, and steam was coming from the engine compartment. The contact stated that a fluid leak was seen underneath the vehicle while parked. The coolant reservoir was refilled. The vehicle was taken to a local dealer to be serviced under NHTSA Campaign Number: 17V209000 (Engine and Engine Cooling). The contact made the mechanic aware of the failure, and the vehicle was diagnosed, and it was determined that the engine needed to be replaced because of coolant intrusion. The vehicle remained at the dealer awaiting the repair. The manufacturer was made aware of the failure and advised the contact to file a complaint with the NHTSA Hotline. The failure mileage was 81,830.

Mileage: 81,830

Feb 22, 2023

UNKNOWN SSM 48397 SSM 48397 - 2013-2015 Fusion/MKZ/Escape/MKC - 1.6L GTDI, 1.5L GTDI, Or 2.0L GTDI With DTC P00C6, P0087, P008A, P008B, P018C, Or P018D - FLP Sensor Available Some 2013-2015 Fusion/MKZ/Escape/MKC with a 1.6L GTDI, 1.5L GTDI, or 2.0L GTDI may exhibit a lack of power, loss of power, or stall when placed in gear with DTCs P00C6, P0087, P008A, P008B, P018C, or P018D. If normal diagnosis leads to a biased or failed Fuel Low Pressure (FLP) sensor, the sensor is available without the need to order the entire fuel line assembly. The FLP sensor, located on the fuel supply line to the high pressure pump, provides the low side fuel pressure input to the PCM so the Fuel Driver Module can be controlled accordingly. The FLP PID can be viewed in the Datalogger and then compared to a manual pressure gauge per pinpoint test HC in the PCED to validate the sensor is working properly. The Fusion/MKZ catalog has been updated to show the sensor availability.

Feb 14, 2023

This is ongoing issue that Ford is aware of, has been addresses by previous recall related to thermostat sensor. However this does not fix the issue that the car over heats loses all coolant automatically shuts down when driving. This car has been been serviced beginning in 2019 to now with the same problem. Yes all receipts, mileage diagnosis etc have been maintained. I have had hoses replaced 3 times am now on the 4th time (Just 6 weeks later). Car overheated on I294 tristate had to be towed 30 miles December 2022. Currently have my 2nd open case with FORD as they know the ECO boost is a major cause and are facing several class action lawsuits they disregard the fact that someone will be killed by their irresponsible disregard of the known problem. Well into the thousands to address a bandaid and not fix the root cause of the engine/hose/coolant overheating problems

Feb 14, 2023

The contact owns a 2014 Ford Escape. The contact stated that the engine was misfiring. The check engine warning light was illuminated. The vehicle was taken to an independent mechanic who replaced the spark plugs. The vehicle was repaired but the failure persisted. The contact called an independent mechanic and was informed that the fuel injector was faulty. The contact added fuel injector cleaner, but the failure persisted. The vehicle was taken to the local dealer where it was determined that antifreeze was leaking into the cylinder, and the engine needed to be replaced. The vehicle was not repaired. The manufacturer was notified about the failure and referred the contact to the NHTSA Hotline for assistance. The approximate failure mileage was 78,000.

Mileage: 78,000

Feb 13, 2023 Fire

I was driving on I95 southbound with my 3.5 month old daughter when my cars engine failed, my brakes and acceleration failed, and my car started being engulfed in smoke. I had to veer off of I95 as far as I could with my breaks or gas working. Within 2 minutes my car was in complete flames. I was able to get my daughter and I out in time but everything in the car was demolished. Ford has refused to reimburse for any value of the car as well as any value of the items that were in the car. The value of the items in the car totaled more than $5,000. My husband and I were forced to sell our other car in order to afford to buy a new car. Both of our cars were paid off.

Feb 7, 2023

Fumes from Car inside cabin Why is this not a recall This is not the only model doing this This needs to be addressed

Jan 30, 2023

The motor blew out on e-way at 70 miles hour in middle lane and was stuck there almost getting hit for over hour this is second 1.6 ecobosst motor thats been put in from ford first blew out at 32000 miles this one has 61000 miles both times regular oil changes on time and never ran low very dangerous for this to happen twice already

Jan 20, 2023

The contact owns a 2014 Ford Escape. The contact stated that upon turning off the vehicle, she noticed that the check engine warning light was illuminated. The vehicle was taken to the dealer where it was diagnosed that coolant had leaked into cylinder #3, and the long block needed to be replaced. The vehicle was not repaired. The manufacturer was notified of the failure and the contact was advised to call the NHTSA Hotline for assistance. The failure mileage was approximately 54,000.

Mileage: 54,000

Jan 13, 2023

The vehicle stop while driving I took it to the dealership they can’t figure out the problem this vehicle is very dangerous

Jan 11, 2023

Once the car is heated up and warm enough to drive it doesn’t want to go, it doesn’t shift correctly and it kicks back hard when shifting. Cylinder 3 keeps misfiring I had to replace it 3 times in the past 2 years, power to the windows aren’t as strong and the heat doesn’t come out as warm.

Jan 6, 2023

My 2014 Ford Escape titanium model has been diagnosed by Stamford Ford in Stamford CT as basically being totaled due to coolant which leaked into the engine. The cost they quoted to replace the engine is $10-11k. But no one would put that kind of money into an 8 year old Ford. The car has only ever been serviced at Stamford Ford Lincoln where it was purchased. Every oil change. Every service Every maintenance was done at this dealership. I had just paid them $1500 for new tires and new spark plugs. Interestingly they told me to replace the spark plugs on the recommended maintenance schedule but there was absolutely nothing wrong in the spark plug system. A mont later the front passenger side bulb went out so I took it right in and they said changing the bulb didn’t solve it so they had to replace the entire modular piece for about $600. I paid that. The next morning there was fluid leaking from my car. I drove right back and was told the soonest they could get me in to evaluate that was Jan 9. I had no choice but to take that appointment. In retrospect it was prob an engine coolant leak The coolant container/system is right behind that large modular headlight part which they said took a lot of labor and time to get in and out. Best explanation is that they damaged it or loosened some connection in the coolant system which caused a leak and then totaled my engine. However Stamford Ford owner Dominick Franchella is not taking any responsibility and instead says Ford 2014 Escapes are notoriously prone to coolant leaks and engine destruction for many years now. Ford takes no responsibility for their design/failure and has never issued any solutions. A recall of some cars (not mine) simply installed a coolant level reader so owners would know that their coolant level was dangerous. No fix.Ford was able to persist in selling these flawed cars which are extremely dangerous. And the incredible expense. So I just spent $2000+ and I now have NO CAR. Ford needs to reimburs

Jan 2, 2023

Coolant Leaked into engine cylinders causing engine to seize on road. My daughter driving the car. Now being told we need a new Engine. I contacted Ford Customer Service was advised there is a recall for this issue but it is VIN specific and I needed to contact NHTSA to get the VIN added...(VIN# [XXX]). Please advise...this is both a safety and poor customer support issue [XXX]([XXX] or [XXX] INFORMATION Redacted PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6).

Dec 12, 2022

The contact owns a 2014 Ford Escape. The contact stated while driving 45 MPH, the service engine soon warning light was illuminated. The contact took the vehicle to an independent mechanic, where it was diagnosed with needing the engine to be replaced due to piston #3 being fractured. The vehicle was not diagnosed or repaired. A dealer was not contacted. The manufacturer had been informed of the failure. The failure mileage was approximately 42,987. The consumer stated the vehicle was taken to Mike Castrucci Ford-Lincoln, but no repairs were made to the vehicle.

Mileage: 42,987

Dec 12, 2022

2014 FORD ESCAPE. CONSUMER WRITES IN REGARD TO ILLUMINATED ENGINE LIGHT.

Dec 3, 2022

while running car suddenly looses power and several engine lights come on, car does not accelerate becoming dangerous on the highway. Needed to pull over and turn the car off, wait a few minutes and turn it back on and then it works fine until the next episode. This is happening all the time and Ford Dealership can not find the problem. Ford Dealership mechanic drove the car and it happened to him while driving, replaced parts for about $1800 and the car is still doing the same thing! I have read blogs from many years ago and there are many Ford models with the same problem. I don't understand why there is no recall for this

Nov 23, 2022

First, my car had not a drop of antifreeze after driving two hours. Secondly, a week later, I was driving home routinely and began to drive forward when my car’s RPM’s went up very high and the car would not move as I was on a busy highway. Strangely, the vehicle had just had the transmission recall repair for the transmission bushing shifting cable a few weeks earlier. So although we he car was in drive it was not shifting. I turned the car off and on. Then the car did the same thing again and a message stating “transmission service” appeared on the dash board. I had to jump out of the car and run to the side of the road for safety as I broke down on a busy highway near my home. It was very scary.

Nov 23, 2022

coolant leaked into the cylinder causing a misfire and resulted in me having to replace the entire engine

Nov 21, 2022

Coolant intrusion into the engine. Coolant was low even after filling chamber causing overheating which is a safety risk. New engine need confirmed by local auto shop. No warning signal other than low coolant. AUL extended car warranty checked the vehicle and would not cover staring the engine had “ sludge” in it.

Nov 16, 2022

Intrusion of the antifreeze into the cylinders causing misfires .

Nov 12, 2022

Car has idling issues and coolant is repeatedly leaking onto the engine, which is causing smoking and could cause a fire. Car stalls often. It was diagnosed by a non certified Ford repair shop in one day and they suggested I take it to a Ford repair shop, because there are issues with the 2014 1.6 engine in the Ford Escapes. I took it to the shop and I was told a hose was leaking and it was not the engine. Car continued to smoke and stall. I took it back and after a week I was told it needed an engine because the coolant is leaking and it is not safe to drive. Ford said because the car has 113,000 miles on it it will cost $7-$8,000 to repair. The car is paid off and is not safe to drive. I was told by the dealer that they only fix 1.5 engines, but everything I am reading says the issue is with the 1.6 engines. I contacted Ford Customer Service and they told me to contact you because there is nothing they will do. The engine light has been coming on and we have been taking it in for repair for about 2 years. It should not have taken this long to diagnose

Oct 26, 2022

The contact owns a 2014 Ford Escape. The contact stated that while driving at 25 MPH, the vehicle lost motive power. The vehicle was towed to the dealer where it was diagnosed that the long block, air filter, battery, and engine needed to be replaced. The vehicle was not repaired. The manufacturer was made aware of the failure. The contact related the failure to NHTSA Campaign Number: 17V209000 (Engine and Engine Cooling) however, the VIN was not included in the recall. The failure mileage was approximately 85,000.

Mileage: 85,000

Oct 20, 2022

Vehicle was taken to local Ford dealer for recalls and coolant issue as noted on service right up as follows; Customer states coolant issue, no visible leak and holding pressure, customer adds about 1 gallon of coolant per month. Per technician; Customer in need of engine. We have researched and we have called two major engine rebuild companies and there are no 2.4 Liter engines to be found. We called a local Ford dealer and spoke to parts department and they stated that they do not have any new 2.4 Liter engines available nor is there any projected build times. I have checked into using a 2.5 Liter and the engines are not interchangeable and basically I have a good car with no engine and cannot be traded or sold.

Oct 12, 2022

The contact owns a 2014 Ford Escape. The contact stated that the vehicle previously had the transmission replaced due to a shift solenoid failure. The contact stated that while driving at an undisclosed speed, the vehicle overheated and a burning odor was detected with smoke coming from the engine compartment. The vehicle was not diagnosed nor repaired by an independent mechanic or dealer. The manufacturer was made aware of the failure and informed the contact that there was no recall associated with the VIN. The failure mileage was approximately 114,000.

Mileage: 114,000

Oct 6, 2022

The contact owns a 2014 Ford Escape. The contact stated while shifting into drive, the vehicle failed to shift into the intended gear. The check engine warning light was illuminated. The contact received notification of NHTSA Campaign Number: 22V413000 (Power Train) however, the part to do the recall repair was not yet available. The local dealer was contacted. The contact stated that the manufacturer had exceeded a reasonable amount of time for the recall repair. The manufacturer was not made aware of the issue. The approximate failure mileage was 54,000. VIN tool confirms parts not available.

Mileage: 54,000

Sep 25, 2022

My 2014 Ford Escape failed to moved forward when I put on gas. I took to ford dealership They refused to do repair. I showed them safety recall notice 22s43/nhtsa recall 22v413. They said is not related. They asked for $4800 transmission and $500 for batteries.

Sep 19, 2022

Car detected low coolant and coolant was added two days in row. On second day the coolant was gone and car warned of high engine temperature, it stopped accelerating and warned to pull over safely while going 75mph on a freeway. Once checked, coolant was completely out and refilled again. Took to a Ford Dealership where had to pay for diagnostic because the Recall for the coolant issue was "Fixed" in 2019. Cause was determined that all the coolant flowed into Cylinder 3 leaving car with only 3 cylinders. Car won't go over 40 mph, and Ford wants thousands to fix an issue that they recalled for. They masked the problem until the car is literally unusable.

Sep 15, 2022

The ECO boost engine has a design flaw that makes the coolant not correctly cycle through the machine. Instead, it sits in the hot engine and vaporizes, eroding the engine over time and it can catch fire. There is a current class action lawsuit against FORD, which does not recognize this as a fault. I've had overheating problems where I can't drive my car.

Sep 13, 2022

The contact owns a 2014 Ford Escape. The contact stated that the check engine warning light illuminated while refueling the vehicle. The contact stated that while driving, the check engine warning light was flashing off and on. The contact stated that the fuel cap was missing. The local dealer was not contacted. The vehicle was not diagnosed or repaired. The manufacturer was not contacted. The failure mileage was approximately 80,000.

Mileage: 80,000

Sep 7, 2022

2014 Titanium Escape EcoBoost AWD. NO WARNING LIGHTS RE LOW COOLANT. I have it serviced every three - four months change oil and check fluids. Last service 05/19/2022. 208,000 miles. Car stalled/idle rough in middle of four lane freeway during rush hour. This happened last year in heat wave also. Tonight Landmark Ford in Tigard OR called, said car is totaled, needs to be scrapped or replace engine $18,000 +. Also said torque is twisted and transmission is needed. Asked if this is a known problem. Ashley at Landmark Ford said yes, this particular engine is known to leak coolant into cylinders causing engine failure. I bought the car at Landmark and they assured me they repaired ALL recalls since vehicle was new. However the coolant recall says warning light is installed and THERE WAS NO WARNING LIGHT WITH LOW COOLANT. Can't afford to pay off loan and buy a another car at 63 years old. Currently searching for repair history to see if this recall repaired. Where is the recall notice on this when there is page after page of exactly the same complaint on nhsta site? Last time I had a known issue Ford dealer refused to repair said my only recourse was to report to nhsta. That doesn't seem to be working for anyone else. There are so many complaints re this here just this year WHY ISNT' THIS RECALLED AND FIXED BY FORD!!!!!

Sep 3, 2022

per the coolant recall issued in 2017/2018, I had my car repaired at Ted Britt Ford where I bought my card. I have now had a coolant issue and my car now has been towed to a car repair shop that is stating I will need to buy a new engine due to a crack at cylinder 3 (Which I see repeated over and over for the exact cause on the message boards due to poor recall and that it needs to be recalled again) at a cost of approx $9,000 even though Ford has had these recalls but did not fix the problem as many upon many complaints on the message boards and many phone calls, emails to Ford with no resolutions. I am reaching out to NHTSA in hopes that not only my issue will be resolved whether through a recall. I look forward to a positive, speedy remedy as my car is now sitting in a repair shop parking lot. I have reached out to Ted Britt via email asking for help but once they found out it was due to this recall issue they have stopped responding. The Manager's name is [XXX]. **Update he did respond to me on 9-3-2022 with the 2018 Recall record (which I have uploaded here) and said I need to call Ford directly at 800.392.3673. I will call on Tuesday due to them being closed for the Labor day holiday. INFORMATION Redacted PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6).

Aug 12, 2022

Coolant light came on low Coolant I added more than came on again and again low on Coolant had it checked out 2 times can't get parts for it because only Ford can only have parts took it to them 3 times and now they say option 1 tear down to find it or option 2 replace the whole motor because it would run into labor times been leaking since I had it last year only had about 89,000 miles on it and still waiting to get it fix engine warning light been coming on plus the low Coolant light

Aug 12, 2022

The contact owns a 2014 Ford Escape. The contact stated that while driving at an undisclosed speed, the vehicle hesitated to accelerate and then lost motive power. The vehicle was able to restart. The vehicle was taken to the dealer where it was diagnosed with a coolant leak in cylinder # 3. The dealer informed the contact that the long block and engine needed to be replaced. The vehicle was not repaired. The manufacturer was made aware of the failure. The failure mileage was approximately 100,000.

Mileage: 100,000

Aug 11, 2022

Cooling sensor triggered. Car has been inspected, there is not indication that car overheated. Have been advised it is related to Safety Recall 13S12-S2. Ford is stating this VIN does not fall into the set # of recalls processed for this recall.

Aug 8, 2022

The contact owns a 2014 Ford Escape. The contact stated that the vehicle received a routine oil change; however, after arriving to her residence she became aware that the check engine warning light had remained illuminated on the instrument panel. The contact turned off and restarted the vehicle and noticed smoke coming from underneath the hood. The contact inspected the vehicle and noticed there was no oil in the engine. The dealer was contacted and stated that the VIN was not under recall for the failure. The vehicle was not repaired. The manufacturer was not contacted. The failure mileage was 144,036.

Mileage: 144,036

Aug 3, 2022

One day after a scheduled oil change my Escape idled very rough upon start up. The check engine light came on. I returned to the Dealer and they found the code was for the cylinder 1 misfire. the code was cleared and reported to me then it did the same thing for the next several days but no check engine light would come on. Today, upon start it idled rough and "Low Coolant require service" message popped up on my dash. Having pressure tested tomorrow to see if coolant is leaking into the cylinder.

Aug 2, 2022

The car failed while driving, it was inspected by and independent mechanic and also the Ford dealership, van bortel Ford in Rochester NY - it's a 2014 Ford escape titanium with 60,000 miles on it. They said the coolant leaked into the engine and the engine now needs to be replaced. We routinely maintained the car. There was no indication or lights that went off warning us of the issue - the car just suddenly stopped working one day and said it was overheating but there was no smoke coming from the engine. We could have gotten hurt while driving since it stopped automatically.

Jul 27, 2022

For the past five years, I've been experiencing low coolant issues which I realize isn't a safety problem in and of itself. It's been an ongoing issue and I've spent hundreds of dollars to have the same problem continuing to recur. The mechanics claim there's no leak yet every 2-3 months I have to put antifreeze in my car. Several times without notice (low coolant light not working), a high temp light comes on telling me to pull over to safety. The engine goes to low power. Usually after about 10-15 minutes, the car is fine. I've explained this to the dealership and never have they been able to find a problem, but I think the two are connected. The most recent safety-related issue was without notice, the high temp warning came on in very busy traffic and the car powered-down, presenting a significant safety hazard. THE CONSUMER REFERENCED RECALL 22S43/22V413, STATING THE VEHICLE EXPERIENCED THE SAME FAILURE. THE CONSUMER REQUESTED TO BE REIMBURSED FOR THE REPAIR.

Jul 20, 2022

The contact owns a 2014 Ford Escape. The contact stated while driving at approximately 55 MPH, the vehicle was shaking abnormally. The vehicle then started losing motive power with the check engine warning light was illuminated. The contact pulled over and stopped the vehicle and noticed that smoke was coming from the exhaust pipe. The vehicle was towed to a dealer and diagnosed that the engine needed to be replaced. The vehicle had not been repaired. The manufacturer had been informed of the failure. The failure mileage was approximately 108,000. The contact has stated that the vehicle is still being held at the dealers and has yet to be fixed.

Mileage: 108,000

Jul 9, 2022

I have owned this Ford for 3 years now. It uses coolent excessively and I have replaced many parts. The Catalyic Converter went out, all motor mounts, font and rear suspension, engine burp valve, faulty throttle body, fried drivers side bulb socket, wiper arms stripped, weather stipping corroding on windshield near hood, front window cracked and damaged, coolent temperature control sensor and firmwware update not automated and dealer charges $250 to update car software for engine improved performance. Sluggish, bogging and unresponsive car until software update and throttle body repair. All around a lemon for as many parts I've put on in a short amount of time. I've spent over $3300 on parts alone. The dealer in Upland services the cars oil but fails to fill the fluids, spills oil on my spark plugs and ruins the fasteners to the skid plate by over torqueing them. It has been the worst car experience of my life and I've never had to replace so many parts in so short of time. I drove a 1974 Nova around for 20 years and still haven't replaced as many parts. This is ridiculous and predatary of Ford to put out cars with these many short term problems on them. Literally evering is going bad after 100k miles. I read post after post of people needing new engines and transmissions because of Fords incompetience. I just got a recall for the Transmission which means the car is unsafe to drive and Ford does not have the ability to fix it until the end of the year. Without a rental or replacement car I am risking my life driving this vehicle and the integety of the tranmissions. So if the tranmissison breaks before the recall is able to fixed then what happens then. Is it now a complicated legal matter where attorny's mitigate the age of the vehicle vs their incompetience. Ordering parts with Ford is a nightmare. They sometimes send the wrong parts and leave it up to the dealers to do the return or not. So it takes weeks between calling back and forth with Ford.com parts.

Jul 9, 2022

While driving on the highway at 65mph the engine began to fail. The Engine light came on and began flashing. I lost power in the engine, the car began to jerk and lost acceleration. Luckily I was able to make it to the side of the road and call for assistance. I had the vehicle towed to a repair shop, the mechanic ran a diagnostic test. It was determined that there is internal engine failure. The car is at 113,000 miles and hadn't had any issues or warnings prior to this happening. The mechanics can not find what has caused the engine failure. I was told that the engine needs to be replaced at an estimated cost of 7000 dollars! This vehicle has been maintained and taken care of, it's very dangerous having an engine spontaneously fail while driving on the highway. The engine should not be failing at 113,000 miles.

Jul 9, 2022

The mechanical brake booster is connected to the overhead cam on Fords Ecoboost engine. This part is a vacuum pump that is powered by the overhead cam shaft. Over time the vacuum pump begins to have issues and becomes increasingly harder for the cam to turn. As the vacuum pump slows, it causes the brakes to be less efficient and increases stopping distance. As the pump degrades, it eventually will fail and freeze up. When this happens, the internal connection to the overhead cam shaft shears off. This cause a complete loss of breaking power leaving only the emergency brake to stop the vehicle. It also drops the internal connectors from the vacuum pump into the motor which damages the motor to the point where the motor must be replaced at a very high cost (it exceeds $10,000). Fords warranty does not cover this design failure. Owners of these vehicles are forced to replace the motor at their own cost or to scrap the vehicle. I believe that ford was aware of the possibility of the mechanical vacuum pump failure when they tested the design on F150s. Ford made a design change on the F150s to an electric vacuum pump. This may have been due to the F150s use as work vehicle and as a towing vehicle which exasperated the issue. Please investigate this issue, I believe you will find many other people who have this same issue with the eco boost engine design.

Jun 30, 2022

Coolant is being leaked into the engine, have to "top" off coolant every couple of weeks, no visible leaks underneath, engine light has come on, and there has been rough idling and driving experienced. Engine light will go off (on its own) and car will run ok, but happening more frequently and feel the inevitable is an engine replacement (was told that this is what will need to happen)

Jun 19, 2022

I'll be driving along and sometimes going 30 miles an hour sometimes going up to 65 70 miles an hour on the interstate And while I'm accelerating the car will start shaking like the the whole thing wil. In the only way that it stops is if I let off the accelerator and go slower speed accelerate you know what it means there's that magic speed but like if I have my cruise control on then it has to be at a certain speed because otherwise it will just start shaking and shaking and shaking

Jun 15, 2022

What component or system failed or malfunctioned, and is it available for inspection upon request?-Coolant/temperature sensor causing the vehicle to overheat, cylinder head to crack, and coolant leak into the engine. Safety jeopardized?-Yes, the car was then burning the coolant and it was entering the air and inhaled. Possible connection to a confirmed cancer case in the main driver. Has the problem been reproduced or confirmed by a dealer or independent service center?-Yes, it was reported to two separate Ford dealerships a total of 5 times. Each time the dealership told me they could not diagnose the problem. I took the car to an independent service center and it was confirmed the head was visibly cracked in 3 locations and the car was burning coolant and emitting it through the exhaust. Has the vehicle or component been inspected by the manufacturer, police, insurance representatives or others?-The vehicle has been to Ford dealerships and inspected for service, recalls, and multiple times for this specific issue. Were there any warning lamps?-No warning lamps, no other symptoms prior to the failure. I purchased the vehicle from Fred Beans Ford, West Chester in Feb. 2016. In Oct. 2016 the vehicle overheated without any warning lamps or messages and it was towed to Fred Beans Ford. The service department stated there were no issues with the vehicle but replaced the temperature sensor that was recalled. The problem continued with the coolant level decreasing and no leaks could be found. The vehicle was taken to Fred Beans for a coolant leak 3 additional times and each time I was told they could not diagnose it and they just refilled the coolant. After this I checked the coolant daily and refilled it if needed to the appropriate level. October 2021 I took it to New Holland Ford where they could not diagnose it. May 2021 an independent center and machine shop where 3 cracks were found in the head causing coolant to leak into the engine and come out the exhaust.

Jun 15, 2022

Car is losing coolant. Had pressure tested and am told there is no leak but the issue is a blown head gasket. No warning signs were present regarding this issue, posing a huge safety risk. Coolant is leaking into engine due to faulty gasket. I am told that this issue is extremely prevalent with other Ford EcoBoost engine models as well.

Jun 15, 2022

IN THE FIRST FEW MINUTES OF OPERATION THE TRANSMISSION/ENGINE SPEEDS UP AND IF NOT EXPECTING IT A SURGE FORWARD COULD CAUSE AN ACCIDENT. SIMILIAR PROBLEMS ALMOST EVERY TIME THE CAR IS STARTED.

Jun 8, 2022 Fire

NHTSA Campaign Number: 17V209000 This current recall, is not attached to the VIN for my Ford Escape and the car is in the shop for the exact issue. Ford said the NHSTA would have to attach the known recall to the VIN Ford Repair order 787886

Jun 7, 2022 Fire

The contact owns a 2014 Ford Escape. The contact stated while idled and attempting to park in her driveway, there were flames coming from under the hood. The hood was opened and flames were visible from the engine. No warning lights illuminated. The contact mentioned that the vehicle overheated, there was a cracked cylinder and an oil leak prior to the fire. The origin of the fire was unknown. The contact extinguished the fire with a fire extinguisher. The fire department was not notified. A dealer was not contacted. The vehicle was not diagnosed or repaired. The manufacturer was informed of the failure and was referred to the NHTSA Hotline. The failure mileage was 100,000.

Mileage: 100,000

May 4, 2022

My vehicle suddenly displays a “Transmission Fault: Service Now” which rendered the vehicle unable to drive. The transmission has issues and it is a common issue among 2014 Ford Escapes. There should be a recall issued since it is a common problem. https://www.copilotsearch.com/posts/ford-escape-transmission-problems/ https://www.reddit.com/r/personalfinance/comments/cu2gki/i_need_advice_about_what_to_do_with_this_car_14/ Driving on a hill and all of the sudden car wouldn't go forward as the gear stopped shifting. Then the transmission gives out. It suddenly displayed "Transmission Fault: Service Now". Consumer was driving on a hill and all of the sudden the car wouldn't go forward as the gear stopped shifting. Then the transmission gives out. It suddenly displayed "Transmission Fault: Service Now".

Apr 28, 2022

The contact owns a 2014 Ford Escape. The contact stated that the transmission was previously replaced. The contact stated that while driving at an undisclosed speed, the check engine warning light illuminated. Additionally, the driver's side rear door had fractured from daily use, and the contact had to continuously refill the coolant reservoir due to the loss of coolant in the vehicle. The vehicle was not diagnosed nor repaired by an independent mechanic or dealer. The manufacturer was not made aware of the failure. The failure mileage was 82,024.

Mileage: 82,024

Apr 28, 2022

The contact owns a 2014 Ford Escape. The contact stated while reversing out of the driveway, the vehicle stalled. The contact stated that the engine was overheating and coolant started leaking from the vehicle. The warning light for the engine overheating was illuminated. The vehicle was not taken to a dealer or independent mechanic to be diagnosed or repaired. The manufacturer was notified of the failure. The failure mileage was 92,000.

Mileage: 92,000

Apr 26, 2022

Engine shutoff in the middle of a busy road after having vehicle for 3 days.

Apr 25, 2022

The contact owns a 2014 Ford Escape. The contact stated while driving 60 MPH, the RPM fluctuated before the vehicle lost motive power and stalled. There was no warning light illuminated. The contact was able to pull to the side of the roadway and had the vehicle towed to the dealer. The vehicle was not diagnosed or repaired. The manufacturer was notified of the failure. The approximate failure mileage was 93,000

Mileage: 93,000

Apr 20, 2022 Fire

Owner was driving vehicle approximately 40-45 mph when a yellow light appeared on the dash and message 'powering down' came on. Owner pulled over opened the hood to find smoke and then flames which caused damage to their vehicle. Claim 31V4FM458

Apr 18, 2022

I own a 2014 Ford Escape with 60,000 miles on it. Upon turning on the vehicle, the check engine light came on. Several days later, also also upon turning on the vehicle, the dash showed a "low coolant" warning. Ford's mechanics inspected the vehicle and found that coolant was leaking into the Escape's engine. Their determination is that it needs a new engine. Ford had previously installed a coolant level sensor in the vehicle as part of a 2018 recall. The recall states that, "[i]f the vehicle is started and driven with an insufficient level of coolant within the engine cooling system, the engine cylinder head may overheat, crack and leak oil. If the cylinder head cracks and leaks oil, the oil may contact a hot engine or exhaust component, increasing the risk of a fire." The sensor is unhelpful; it notifies you once the coolant is low - after coolant has leaked into your engine and you're already in the unsafe situation described in the recall. There was not any other indication (coolant under the vehicle, for example) of an issue before the check engine light came on. Ford performed an oil change on the vehicle 3,400 miles ago and noted no issues with the cooling system or the engine.

Apr 3, 2022

Head gasket was damaged but little to no signs that it was malfunctioning. Only warning code was spark plugs. Replaced spark plugs but light kept turning on. If the mechanic had not looked deeper at the issue my safety would have been compromised due to lack of notifications when car was being diagnosed

Mar 15, 2022

The contact owns a 2014 Ford Escape. The contact stated while starting the vehicle, the low coolant warning light illuminated. The vehicle would also stall with a burning odor was present coming from the antifreeze. The contact added coolant and the warning light was no longer displayed. The failure was persistent. The vehicle was towed to a dealer where it was diagnosed that the heater hose failed. The hose was replaced; however, the failure continued. The vehicle was returned to the dealer due to the coolant not circulating in the engine. The vehicle was not repaired. The contact linked the failure to NHTSA Campaign Number: 12V431000 (Engine and Engine Cooling) and 17V209000 (Engine and Engine Cooling) however, the VIN was not included in the recall. The approximate failure mileage was 115,189. Claim number is [XXX]. INFORMATION Redacted PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6).”

Mileage: 115,189

Mar 10, 2022

The contact owns a 2014 Ford Escape. The contact stated while driving at an undisclosed speed, the check engine warning light illuminated. The vehicle was taken to an independent mechanic where it was diagnosed that the spark plug in cylinder number four was welded into the head of the engine, causing an engine failure. The independent mechanic informed the contact that the engine needed to be replaced. The vehicle was not repaired. The manufacturer was made aware of the failure and advised the contact to file a complaint with NHTSA. The failure mileage was approximately 88,000.

Mileage: 88,000

Mar 9, 2022 Fire

Owner scheduled appointment with Lakeview Ford due to no heat in vehicle, stalling when fuel was full, an active indicator for airbags. They completed the repairs for total around $1500. Shop went to test drive and vehicle caught fire.

Feb 4, 2022

The car loses coolant but know leaks. The dash says coolant low so I add coolant to the reservoir and then it is fine till around a month and does it again so I do the same thing. Started doing it when got cold and use heater all the time. My daughter has a 2014 escape to and it is also doing it.

Jan 27, 2022

I have a coolant intrusion issue. This issue is causing a major problem to the engine and long block cylinders. This problem has occurred randomly causing the car to buffer, shut off on its own, and have white smoke come out of the exhaust and run terribly. I have taken this vehicle to multiple Ford Service centers in the last two years for its usual maintenance repairs and nobody has pointed out there has been an issue. My car is now in the shop with an $8,000 repair cost. Ford has decided to NOT fix the recall issue on my vehicle. This problem is a known issue for the 2014 Ford Escapes. I purchased this vehicle at Carmax and have paperwork saying there are 2 recalls associated with this vin. Manufacturer Number: 17S09 NHTSA Recall Number: 17V209 Recall Status: Recall incomplete The cycling head crack may cause an oil leak that may result in a fire in the engine compartment. This is an extremely dangerous issue for myself & others.

Jan 26, 2022

lost power, didn't seem to get into dive on freeway could't get power on to freeway when at a stop take time to get power up to a good speed Car at AAMCO for inspection needed to re build leaking bad brushing No did not get any warning warning light came on as i went to AAMCO of low coolant only

Jan 18, 2022

The contact owns a 2014 Ford Escape. The contact stated that while driving at an undisclosed speed, the vehicle overheated and shut off. The vehicle was towed to the local dealer where it was diagnosed that there was an air bubble in the coolant. The fluid was drained and refilled. The vehicle was repaired however, the failure recurred. The vehicle was taken to the same local dealer where it was diagnosed that the cooling fan was inoperable. The vehicle was towed to the same dealer to be diagnosed. The contact was informed that there was oil mixing with the coolant. The contact stated the failure was related to NHTSA Campaign Number: 17V209000 (Engine and Engine Cooling). The vehicle was not repaired. The manufacturer was notified of the failure and referred the contact to NHTSA for assistance. The approximate failure mileage was 51,479.

Mileage: 51,479

Dec 24, 2021

Coolant level sensor failed after repair for recall number 17S09. Mechanic reports that senior failed in same way as documented in the recall. However Ford refuses to conduct the repair a second time.

Dec 16, 2021

Lights come on for engine and gas pump while in motion throws vehicle to right at 55 mph when gas light comes one says empty all the time does at stops too slams into next gear shaking car badly with a bang it does often enough at 1/2 tank only or below but does not read more than 1/8 tank from full when filling up at pump all the time

Dec 13, 2021

In brief, It is my contention that safety recall# 17S09 service was not performed in its entirely on my vehicle and likely several others by the dealerships. The dealerships only replaced the engine coolant sensors & the motor mounts per their understanding of the recall instructions but did not replace the coolant system hoses as instructed in the Dec 13th correspondence to the dealers. After having several problems with coolant leakages in my vehicle which caused the check engine light to come on it was discovered that I had multiple hoses leaking. I spoke with a service manager at the dealership that performed my recall service in April/2018 about the hoses not being replaced which was my current problem? I was informed this was not what the dealerships were instructed to do by Ford Motors in their recall notices to them. Two different dealerships I visited were oblivious to this recall mandate. In the meantime I have incurred nearly $1500 in repair expenses because the recall that was investigated and mandated by NHTSA in 2017 was not performed in its entirety although Ford Motors assured this would be addressed in the recall. Investigation needed/warranted.

Nov 13, 2021

2014 Ford Escape presents with major engine cooling system issues for several years despite regular repair and maintenance to these systems. Heat blows cold unless driving 55 mph or more and coolant needs to be replaced every two weeks during the fall and winter. Engine coolant leaks onto engine block despite regular repair for several years. Serious safety hazard possible due to this.

Nov 13, 2021

It is an ongoing issue with the 2014 escape. They had a recall out for the coolant system. A healthy engine does not use coolant. I kept having it checked it had no visible leaks but was losing coolant No visible leaks. I got an engine light I took the car to Ford dealer here in Scarborough Toronto he told me the car coolant has been leaking into engine blocks. The dealer is claiming it has nothing to do with the recall. Ford won't fix it and is saying it's not part of the recall. They are saying I have to replace my whole engine. It is a 2014 Ford escape with 110000Km on it.

Nov 8, 2021

The car continues to have a leak of coolant even after the dealership claims it has been repaired. There is no visible sign of a coolant leak. The engine continues to run hot on a daily basis. The car does not even give a signal warning until it has already reached high temperatures and then states to shut the engine down immediately. The service center refuses to inspect my car as they state the recall has already been repaired. It appears to be an on going problem with 2014 1.6L Escape engines.

Oct 29, 2021

Coolant is leaking into the engine, Ford is aware of this issue and has owners install an engine coolant sensor to avoid a potential fire risk. This was done with this vehicle however it obviously does not fix the underlying problem.

Sep 30, 2021

The contact owns a 2014 Ford Escape. The contact stated that while driving at slow speeds, the vehicle overheated. There was an abnormal odor and detection of heat inside the vehicle. A message to pull over and check the engine was displayed. The vehicle was taken to the local dealer where it was diagnosed that there was anti-freeze in the engine and the engine needed to be replaced. The repair parts were not available. The vehicle was not repaired. The manufacturer was notified however, no further assistance was provided. The contact mentioned being extremely concerned about driving the vehicle and a possible fire. The failure mileage was 51,187.

Mileage: 51,187

Sep 10, 2021

The contact owns a 2014 Ford Escape. The contact stated while driving 50 MPH, the low on coolant level warning light illuminated. While driving, another message was displayed on the instrument panel stating that the engine was overheating, do not drive. The contact pulled over into a parking lot and attempted to restart the vehicle however, the vehicle failed to restart. The vehicle was towed to his residence. The next day the contact had the vehicle towed to the local dealer. The local dealer inspected the vehicle but was unable to restart the vehicle. The battery and starter were replaced, and the vehicle was diagnosed. The contact was informed that the engine needed to be replaced. The contact took the vehicle to an independent mechanic and the engine was replaced; however, the engine overheating message was still displayed on the instrument panel. The vehicle was not repaired. The manufacturer was not made aware of the failure. The failure mileage was approximately 98,000.

Mileage: 98,000

Aug 13, 2021

When putting my vehicle into reverse it wouldn't go into gear it was stuck in a neutral position unless it was in park. If I would step in the gas it would just rev up the engine.

Jul 31, 2021

Driving on the highway I lost braking power the brake vacuum pump ceased up and broke the bolt in the cam shaft that had to be drilled out and replaced then that caused more damage to the cam and bottom end of the motor for the motor to throw the following codes: p0365 p0369 p0012 p0299 b1215 p0234 U3008 U3003 U0300 p1594 U0140 U0154 U2300 U0422 B1B36 With all these codes I did the following and am now without a vehicle thanks to FORD. This vehicle only has 58000 Miles is single owner and was well maintained till this incident now I am told the motor has to be rebuilt as the cam and bottom end are the issues with this vehicle and this has happened to a lot of people and could have cause a crash or deadly accident as no brakes and now no vehicle. The three sensors were replaced and brake vacuum pump and bolt that drives the pump from the cam along with new spark plugs and valve cover gaskets plus oil change and filter plus new battery and tires along with front rotors calipers brake pads and rear rotors and brake pads. I blame Ford for this as this is a well known issue with 2014 to 2019 models of Ford Escape Titanium 2.0l Eco Boost Engine with turbo. Garages all over the US and Canada have been just replacing the engines due to poor engineering on Fords part and I believe Ford should be held responsible to the engines replacement as it is not even 60000 Miles and I try to take good car of my vehicle only to have none now to drive. Ford Should be held Responsible.

Jul 26, 2021

I have a cracked cylinder head on cylinder number 3 that is leaking coolant into my engine. My vehicle was bought directly from Ford in 2014 and has 68,900 miles on it. I have done all of the routine maintenance over the years and there is absolutely no reason my vehicle should be having this issue. I have already had my car in the shop multiple times for the same issue. Engine light kept coming on and I could barely get it too accelerate before I was told it will cost almost $9000 to fix. I attempted to call Ford and they claim there is nothing they can do for me.

Jun 3, 2021

The contact owns a 2014 Ford Escape. The contact stated while driving 35 mph, the vehicle stalled. The contact stated that there was no warning light illuminated. The vehicle was towed to a local dealer to be diagnosed. The contact was informed that the engine, the transmission, the manifold, and the computer needed to be replaced. The vehicle was not repaired. The contact was relating the failure to an unknown recall. The manufacturer had been informed of the failure and referred the contact to the NHTSA for assistance. The failure mileage was approximately 107,000.

Mileage: 107,000

May 21, 2021

The contact owns a 2014 Ford Escape. The contact stated that the check engine warning light illuminated while driving at an undisclosed speed. The vehicle hesitated to start with an abnormal odor. The vehicle stalled while parked in the driveway on three separate occasions. The vehicle was not taken to be diagnosed nor repaired. The manufacturer was notified of the failure. The dealer was contacted and the contact was informed to bring the vehicle in to be diagnosed. The contact felt that the vehicle was unsafe to be driven. The failure mileage was approximately 67,500.

Mileage: 67,500

May 13, 2021

MY DASH LIGHTS NEVER INDICATED ANY LOW OIL. ENDED UP RUNNING OUT OF OIL AND I STARTED KEEPING TRACK. I WAS PUTTING IN A QT A DAY. NO VISIBLE SIGNS ON MOTOR OR GROUND OF OIL LEAK. BUT SMOKE IN TAIL PIPE. THEN TODAY THE MOTOR BLOW COMPLETELY EVEN W OIL IN IT. I SEARCHED UP MY MAKE AND MODEL. THEIR ARE TONS OF RECALLS FOR THE OIL LEAK AD I SAID, AND FOR THE INSTRUMENT PANEL NOT WORKING. BUT MY DEALERSHIP SAID I HAVE NO RECALLS WHAT'S SO EVER AND NON HAVE BEEN DONE ON THIS CAR. SOME OF THOSE RECALLS I READ SAID IT COULD CATCH FIRE!!

Mileage: 164,000

May 12, 2021

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED SHE HAD NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING) COMPLETED AT AUTONATION FORD SANFORD (4911 WAYSIDE DR, SANFORD, FL 32771, (407) 680-0781) BACK IN 2019. THE CONTACT STATED SHE WAS UNABLE TO START THE VEHICLE IN APRIL 2021. THE CONTACT STATED THAT THE CHECK ENGINE WARNING LIGHT WAS ILLUMINATED. THE VEHICLE WAS NOT DRIVABLE. THE VEHICLE WAS TOWED BACK TO AUTONATION FORD SANFORD (4911 WAYSIDE DR, SANFORD, FL 32771, (407) 680-0781) WHERE IT WAS DIAGNOSED WITH A COOLANT LEAK WHICH NEEDED TO BE REPAIRED. THE VEHICLE WAS REPAIRED HOWEVER, THE FAILURE PERSISTED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC TO BE DIAGNOSED. THE CONTACT WAS INFORMED THAT THERE WAS COOLANT IN CYLINDER NUMBER 3. THE VEHICLE WAS NOT YET REPAIRED. THE DEALER WAS MADE AWARE OF THE FAILURE. THE MANUFACTURER WAS INFORMED OF THE FAILURE. THE MANUFACTURER INFORMED THE CONTACT THAT THE ENGINE NEEDED TO BE REPLACED. THE FAILURE MILEAGE WAS APPROXIMATELY 136,925.

Mileage: 136,925

Apr 30, 2021

I REPLACED THE SPARK PLUGS ON 4/25/2021 FOR MY 2014 FORD ESCAPE SE DUE TO AN P0303 ERROR INDICATING A MISFIRE FOR # 3 CYLINDER. ALL THE SPARK PLUGS WERE EASILY CHANGED EXCEPT CYLINDER #3, THIS SPARK PLUG SEIZED. AS A RESULT, I HAD MY FORD ESCAPE TOWED TO HASTINGS FORD (GREENVILLE, NC) ON 4/29/2021. GARY FROM THE SERVICE DEPARTMENT CALLED TO TELL ME (@5:00 4/29/2021) THAT THE MECHANIC WAS UNABLE TO REMOVE THE SEIZED SPARK PLUG AND THAT REPLACING THE CYLINDER HEAD WOULD NOT BE SUFFICIENT. THE ENGINE (1.6 L ECOBOOST) IS KNOWN TO LEAK COOLANT AND THAT IT WOULD BE A WASTE OF TIME AND MONEY TO JUST REPLACE THE CYLINDER HEAD. THE SERVICE DEPARTMENT RECOMMENDED THAT I REPLACE THE "LONG BLOCK" FOR A TOTAL COST OF $7800 (INCLUDING LABOR). MY VEHICLE ONLY HAS 104,954 MILE. THE DEALERSHIP KNOWINGLY ACKNOWLEDGES A DEFECT WITH THE MOTOR BUT WILL NOT ACCEPT RESPONSIBILITY TOWARDS FIXING THE ENGINE. I CALL FORD'S CUSTOMER SERVICE ON 4/29/2021 @ 6:06 TO ASK FOR ASSISTANCE IN REPAIRING MY VEHICLE (CASE # - CAS-31599643) AND RECEIVED A CALL FROM A SUPERVISOR ON 4/30/2021 @ 1:37. JOEL INDICATED THAT FORD ASSUMES NO RESPONSIBILITY TOWARDS THE REPAIR OF MY VEHICLE SINCE IT'S BEYOND THE POWERTRAIN WARRANTY. I HAVE FOUND 2 CLASS ACTION LAW SUITS AGAINST FORD FOR THE 1.6 L ECOBOOST DUE TO THE COOLANT LEAK DAMAGE TO THE ENGINE AND BELIEVE THAT FORD SHOULD BE RESPONSIBLE FOR THE REPAIRS.

Mileage: 104,954

Apr 20, 2021

DUE TO COOLANT LEAK/BURNING/LEAKING INTO ENGINE I AM HAVING TO ADD COOLANT TO MY VEHICLE EVERY OTHER MONTH WHEN THE VEHICLE ALERTS ME THAT COOLANT LEVEL IS LOW. I TOOK CAR IN BACK IN 2018 WHEN THE RECALL FOR THIS ISSUE WAS CREATED. THE RECALL DID NOTHING TO FIX THE ACTUAL ISSUE OF WHERE THE COOLANT WAS GOING AND ONLY INSERTED A SENSOR IN THE SYSTEM TO NOTIFY THE DRIVER OF THE ISSUE SOONER TO HOPEFULLY PREVENT ENGINE FROM CATCHING FIRE DUE TO RUNNING TOO HOT. MY VEHICLE HAS LESS THAN 55K MILES AND ENGINE IS NOT PERFORMING AS IT DID BEFORE AND I AM CONCERNED THAT COOLANT HAS DAMAGED MY ENGINE. FORD CUSTOMER SERVICE HAS SAID THAT SINCE MY VEHICLE IS 2014 MODEL YEAR THAT IT IS OUT OF ANY WARRANTY. THIS IS REALLY NOT ACCEPTABLE AS I MENTIONED THEY IDENTIFIED AN ISSUE WITH THE COOLANT BUT DIDN'T FIX IT AND ONLY PUT AN EARLY ALERT IN. PLEASE LOOK INTO AND ADVISE HOW I CAN GET THIS CORRECTED OR REPLACED. WHEN THIS HAPPENED IN 2018 THE VEHICLE SAID IT WAS RUNNING HOT AND REDUCED POWER AND I COULD ONLY DRIVE IT FOR A FEW MINS AT A TIME TO GET IT TO A DEALER TO CHECK IT OUT. THIS WAS IN JULY 2018 AND I HAVE BEEN ADDING COOLANT EVERY COUPLE OF FEW MONTHS SINCE JULY OF 2018.

Mileage: 40,000

Apr 16, 2021

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED WHILE DRIVING 20 MPH, THE VEHICLE MADE A LOUD GRINDING SOUND. THE CONTACT PULLED OVER AND SHUT-OFF THE VEHICLE. THE CONTACT STATED THAT THE FAILURE RECURRED A SECOND TIME AFTER THE VEHICLE WAS RESTARTED. THE VEHICLE WOULD NOT RESTART. NO WARNING LIGHTS WERE ILLUMINATED. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED WITH METAL SHAVINGS INSIDE THE TRANSMISSION FLUID. THE VEHICLE WAS NOT REPAIRED. A LOCAL DEALER WAS NOT CONTACTED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 102,000.

Mileage: 102,000

Apr 14, 2021

I HAVE A 2014 FORD ESCAPE SE WITH 67000 MILES AND WHEN I WAS PARKED BURGER KING PARKING LOT WITH ENGINE RUNNING A MESSAGE CAME ON THAT SAID IT WAS OVERHEATING SO I PARKED IT AND LOOKED UNDER HOOD SAW IT HAD AN ANTIFREEZE RESERVOIR THAT WAS LOW SO I PROCEEDED TO GET AN APPOINTMENT FOR CLONINGER FORD MORGANTON NC FOR THE WORKS OIL CHANGE AND COOLANT RESERVOIR AND THEY CHECKED IT PUT ANTIFREEZE IN IT AND SAID ANY PROBLEMS CALL THEM. I LEFT AND IT SEEMED OK, UNTIL I HAD IT RUNNUNG IN THE DRIVEWAY AND IT WAS OVERHEATING IT SAID AGAIN SO THEN I CALLED TOLD THEM WHAT HAPPENED AND GOT APPOINTMENT TO COME IN AGAIN AND I WENT AND SHOWED THEM THAT THE RESERVOIR WAS EMPTY AGAIN SO MAYBE I HAD A LEAK SINCE THEY JUST FILLED IT UP A WEEK AGO AT MY APPOINTMENT SAME DEALER SERVICE DEPT. AFTER THEY LOOKED AT IT THEY SAID THE ENGINE NEEDED TO BE REPLACED DUE TO THE ENGINE COOLANT SYSTEM CAUSING A CRACK IN THE ENGINE AND IT WOULD BE $8000. PLUS LABOR TO REPAIR AND THERE WAS NO RECALL FOR IT AND IT WAS OUT OF WARRANTY AND THEY WERE SEEING IT MORE AND MORE ON THIS CAR AND I WOULD BE BETTER TO TRADE IT IN. IT NOW SITS IN MY DRIVEWAY UNTIL SOMETHING CAN GET DONE. I TRULY BELIEVE CONSUMERS SHOULD BE COVERED FOR THIS WITH ALL THE COMPLAINTS HERE AND WITH ATTORNEYS ON THE INTERNET WHO ARE EXPLORING SAME PROBLEM.

Mileage: 67,000

Apr 5, 2021

THERE IS A COOLANT SYSTEM LEAK SIMILAR TO THAT IN FORD RECALL #17S09 (NHTSA CAMPAIGN #17V209), BUT THE DEALER SAYS MY CAR IS NOT COVERED BY THAT RECALL.

Mileage: 125,000

Mar 29, 2021 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED WHILE DRIVING 75 MPH, THE VEHICLE STALLED. THE CONTACT THEN SAW SMOKE EMERGING FROM THE ENGINE COMPARTMENT. THERE WERE NO CRASH OR INJURIES DUE TO THE FIRE. THE CONTACT WAS ABLE TO EXTINGUISH THE FIRE IN THE ENGINE COMPARTMENT. THE FIRE DEPARTMENT WAS CONTACTED AND WAS ABLE TO EXTINGUISH THE FIRE UNDERNEATH THE VEHICLE. A FIRE DEPARTMENT REPORT WAS FILED. THE VEHICLE WAS TOWED TO GORDY'S AUTOMOTIVE REPAIR (2639 S FIELDSPAN RD, DUSON, LA 70529). THE CONTACT HAS NOT NOTIFIED THE LOCAL DEALER. THE VEHICLE HAS BEEN NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER HAS NOT BEEN INFORMED OF FAILURE. THE FAILURE MILEAGE WAS 116,883.

Mileage: 116,883

Mar 18, 2021

THE CAR STARTED TO DELAY AND WOULDN'T ACCELERATE WHILE I WAS ON A THREE LANE INTERSTATE GOING 70MPH THEN SHORTLY AFTER THAT IT WOULD MAKE A LOUD BOOM SOUND THAT WOULD SHAKE THE VEHICLE EVERYTIME IT WAS SHIFTED INTO ANY OF THE GEARS. IT WON'T ACCELERATE AT ALL NOW. IT WILL MOVE FORWARD AND BSCKWARD AUTOMATICALLY WHEN PUT INTO GEAR BUT WILL ONLY REV WHEN THE GAS PEDAL IS PRESSED

Mileage: 160,000

Mar 13, 2021

DURING A ROUTINE OIL CHANGE, THE TECHNICIAN FOUND A COOLANT LEAK. AFTER AN IN DEPTH DIAGNOSIS, THE TECHNICIAN PREFORMED A COOLANT PRESSURE TEST. HE FOUND COOLANT INTRUSION IN TWO CYLINDERS. THE FORD SERVICE CENTER WROTE: RECOMMENDED IMMEDIATE ATTENTION TO REBUILT/REPLACE THE ENGINE. THEY PREFORMED COOLANT PRESSURE TEST LEAKING DOWN 10 PSI WITHIN 1 AND1/2 HOUR NO EXTERNAL LEAK. THEY REMOVED ALL 4 SPARK PLUGS, USED A BORESCOPE AND FOUND EVIDENCE OF COOLANT ON TOP OF #2 AND #3 PISTON. THUS THE NEED TO REPLACE THE LONG BLOCK ASSEMBLY. THE SERVICE CENTER RECOMMENDED THE NEED TO REPLACE THE ENGINE AT THE SUGGESTED COST OF $8,000. I HAVE CHANGED THE OIL REGULARLY SINCE OWNING THIS VEHICLE. I DO NOT HAVE THE FUNDS TO DO THIS MAJOR TYPE OF REPAIR. WHY HASN'T FORD RECALLED THE VEHICLE TO CORRECT THIS PROBLEM SINCE THIS HAVE BEEN A PROBLEM SINCE 2010?

Mileage: 170,730

Mar 11, 2021

ON OR ABOUT AUGUST OF 2019 MY CAR BEGAN PULLING WHEN I WAS ON THE FREEWAY. THE CAR THEN JUST TURNED OFF AND I WAS LUCK TO VEER OFF TO THE RIGHT WITHOUT HITTING ANY OTHER CARS. THE CAR WAS TOWED TO THE DEALERSHIP (SERRA FORD IN ROCHESTER, MI) ONLY TO FIND OUT I NEEDED A NEW TRANSMISSION. THE CAR WAS ONLY 5 YEARS OLD AND EVEN THOUGH IT WAS OUT OF WARRANTY (MILEAGE) 112,000 MILES ON THE CAR AND FORD REFUSED TO ASSIST ME IN REPAIRING THE CAR. I HAVE PURCHASED FORD CARS SINCE 1998 AND KEPT THEM FOR OVER 8 YEARS. I HAVE NEVER HAD TO REPLACE A TRANSMISSION ON A CAR LET ALONE WHEN ITS ONLY 5 YEARS OLD. SERRA FORD (MATT) STATED THAT THE OVERDRIVE BAND FAILED FIRST WHICH CAUSED THE TRANSMISSION TO OVERHEAT. THE MATERIAL THEN DESENAGRATED AND METAL WAS SUCKED INTO THE TUBE FOR THE ACTUAL TRANSMISSION PUMP. HE RECOMMENDED ANOTHER TRANSMISSION BUT I WANTED TO KNOW WHY THEY ENGINE LIGHT NEVER CAME ON WHEN THE OVERDRIVE BAND FAILED? I ASKED THE SAME QUESTION TO THE REP AT FORD AND NO ONE COULD ANSWER ME. I FEEL LIKE I WOULD NOT HAVE HAD TO PURCHASE ANOTHER USED TRANSMISSION HAD THE SENSOR INDICATED THAT SOMETHING WAS GOING ON WITH THE ENGINE. I REALLY WANT FORD TO REFUND ME FOR THE MONEY I HAD TO SPEND ON MY TRANSMISSION.

Mileage: 112,000

Mar 8, 2021

FORD ESCAPE SE 2014 ALL COOLANT LEAKED, CAR COULD NOT RUN, WHITE SMOKE AND NOW ALSO HAS OIL LEAK. THERE IS RECALL 17V209000 DATED 03/27/2017 THAT DESCRIBES WHAT HAPPENED TO MY VEHICLE YET THE DEALER MENTIONED THAT MY CAR HAS NO RECALLS OUTSTANDING. I WAS JUST LEAVING MY HOME WHEN THIS HAPPENED AND HAD TO STOP THE CAR. ONLY THE YELLOW CHECK ENGINE LIGHT CAME ON AND THE RED "I" IN CLUSTER. RIGHT NOW MY CAR IS IN THE SHOP AND THEY ARE CHECKING TO SEE EXACTLY WHY THIS HAPPENED. AS SOON AS I KNOW AND GET THE ESTIMATE, I WILL BE POSTING IT IN THIS COMPLAINT. ALSO CALLED FORD AND THEY SAID THAT ANY QUESTIONS HAD TO BE THRU THE DEALER WHICH I HAD ALREADY DONE. CHECKED MY RECALLS ONLINE AND ALSO SAYS NO RECALLS.

Mileage: 1

Feb 11, 2021

CAR DASH BOARD ELECTRICAL WIRING HAS GONE BAD. ORIGINALLY THE INFORMATION ON SCREEN WAS FADING AND AFTER ABOUT A MONTH NO LONGER SHOWS ANY INFORMATION. FORD STATED THE ENTIRE PANEL WOULD NEED TO BE REPLACED, INVOLVING RE-READING ENGINE MILEAGE AND PROGRAMMING KEYS AGAIN FOR $700. DID NOT GET THAT FIXED AS IT'S NOT A NECESSITY. DRIVER WINDOW MOTOR FAILED WITHOUT WARNING WHILE DRIVING WITH THE WINDOWS UP. NOW THE ENGINE HAS BEEN READING A TURBO ISSUE BUT IT CANNOT BE DETERMINED IF IT'S THE ACTUAL TURBO BOOST OR THE WASTE GATE. THIS LEAD TO TRANSMISSION SKIPPING AND ULTIMATELY STALLING WHILE DRIVING ON HIGHWAY AND THEN CITY ROADS AND HAVING TO RESTART CAR SEVERAL TIMES TO MAKE IT HOME AND THEN TOWED THE CAR TO LOCAL MECHANIC SHOP WHO STATED TRANSMISSION NEEDS TO BE REPLACED FOR $4500. ALONG WITH A FUEL LINE ISSUE THAT HAD ALREADY BEEN REPAIRED 2 YEARS PRIOR AND AGAIN UNABLE TO CONFIRM WHY THE TURBO SENSOR CODE IS POPPING UP. CAR IS USED FOR TYPICAL DAILY DRIVING WITH CHILDREN AND SHOULD NOT HAVE THESE ISSUES. THERE ARE RECALLS FOR THIS MAKE/YEAR BUT NOT ON MY SPECIFIC VIN THOUGH THEY ARE SIMILAR ISSUES. THE COST TO REPAIR THE VEHICLE IS MORE THAN IT IS WORTH AND I'M VERY UNSATISFIED WITH THE LONGEVITY OF IT. I DID GET THE RECALL FOR MY DOORS DONE AFTER ONE DAY DRIVING AND A BACK DOOR OPENED ON ITS OWN, COME TO FIND OUT THEY STILL NEED TO REPLACE THE OTHER DOORS.

Mileage: 110,000

Feb 10, 2021

I WAS DRIVING THE CAR WHEN IT STARTED HAVING PROBLEMS. I TOOK IT TO MY MECHANIC AND HE CHECKED THE CAR OUT AND CALLED ME TO TELL ME THAT THE VACUUM PUMP FAILED BECAUSE IT WASN'T GETTING ANY OIL FROM THE ENGINE AND IT CAUSED THE ENGINE TO LOCK UP. THE OIL GAUGE SHOWED THAT IT WAS FULL. NOW MY ENGINE NEEDS REPLACED! I HAVE ALWAYS BEEN A FORD OWNER AND FOR THIS TO HAPPEN TO A 2014 FORD ESCAPE WELL I GUESS I WON'T BE BUYING A FORD PRODUCT AGAIN. I STRUGGLE TO MAKE ENDS MEET AS IT IS BUT THE COST OF REPLACING THE ENGINE IS TOO EXPENSIVE FOR ME.

Mileage: 117,000

Feb 8, 2021

COOLANT LEAKING IN #3 CYL, LOOKS TO BE A BAD CASTING IN THE BLOCK FROM FACTORY, OVERHEATS AND USES COOLANT

Mileage: 84,000

Feb 3, 2021

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED WHILE DRIVING 15 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE VEHICLE WAS RESTARTED AND JERKED HOWEVER, THE FAILURE RECURRED. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHERE THE CONTACT WAS INFORMED THAT THE TRANSMISSION NEEDED TO BE REPLACED. THE LOCAL DEALER WAS NOT CONTACTED. THE VEHICLE WAS NOT DIAGNOSED NOR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 119,000.

Mileage: 119,000

Feb 3, 2021

2014 FORD ESCAPE TITANIUM, 1.6 ECOBOOST ENGINE, SINCE AROUND 55000 MILES, NOTHING BUT ISSUES RELATED TO ENGINE AND COOLING SYSTEMS...CAR HAD RECALL THAT FORD DID NOT HAVE PARTS FOR, ENGINE FROZE UP COOLANT AND OIL ALL OVER THE INSIDE OF THE ENGINE AND NEEDED TO BE REPLACED, FORD REPLACED ENGINE DUE TO THE FACT THAT IT WAS DOCUMENTED THEY DID NOT HAVE THE PARTS FOR THE RECALL YET AND THE WORST CASE SCENARIO HAPPENED. THIS SHOULDN'T HAPPEN IN A CAR THAT HAS 55000 MILES ON IT. THEY INSTALLED THE COOLANT SENSOR AT THAT TIME AS WELL. THEN AT 75,000 MILES, THE TRANSMISSION WENT WITHOUT WARNING WHILE DRIVING WITH 2 CHILDREN IN THE CAR. I HAD IT REPLACED BY MY PRIVATE MECHANIC FOR $4500. LAST WEEK, USED THE FACTORY INSTALLED REMOTE START X1 IN 20 DEGREE NEW ENGLAND WEATHER, AND WHEN TRIED TO GO OUT TO CAR, THE HIGH TEMP CODE WAS ON AND THE ENGINE WOULDNT START. LET IT SIT FOR 5 HOURS IN THE 20 DEGREE WEATHER, CLEARLY ENGINE NOW COOL BUT STILL WOULDN'T START...HAD IT TOWED TO MY MECHANIC, NEXT AM HE LET ME KNOW THAT THE 2018 COOLANT SENSOR WAS BLOWN AND LEAKING COOLANT...REPLACED AND REPAIRED AT COST OF $250...WHY SHOULD A SENSOR GO AFTER ONLY 2 YEARS? SO MANY ISSUES WITH THIS ONE CAR ALL AROUND THE COOLANT AND THE ENGINE. I HAVE CONTACTED THE LAWSUIT FILED IN DECEMBER TO JOIN THIS AS WELL.

Mileage: 120,000

Feb 2, 2021

I WAS DRIVING WHEN THE HIGH ENGINE TEMPERATURE STOP SAFELY ALERT POPPED UP ON THE SCREEN ABOVE THE STEERING WHEEL. I WAS DRIVING IN A RESIDENTIAL AREA WHEN THIS HAPPENED.

Mileage: 74,588

Jan 29, 2021 Crash

A CAR TOOK THE RED LIGHT AS WE HAD THE GREEN LIGHT SHE RAN INTO THE CAR IN FRONT OF ME AND THEN FISH TALED AND HER REAR CAR SMASHED INTO MY FRONT... NONE OF MY AIRBAGS DEPLOYED AT ALL BUT THE OTHER 2 CAR DID AND MY FRONT END DAMAGES ARE SEVERELY DAMAGED. THE PERSON RESPONSIBLE FOR THIS ACCIDENT WAS ARRESTED AT THE SCENE AND THEY DID A SOBRIETY TEST ON HER

Mileage: 101,000

Jan 29, 2021 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE DRIVING, THE VEHICLE OVERHEATED AND WENT INTO LIMP MODE. AS A RESULT, THE EXHAUST PIPE STARTED TO SMOKE. THE CONTACT STATED THAT THE ENGINE WAS HOT AND MAKING CRACKING SOUND. THE FAILURE CAUSE A COOLANT LEAK. THE WARNING INDICATOR LIGHT ILLUMINATED ENGINE OVERHEATING. THE VEHICLE WAS TAKEN TO COOK COUNTY FORD INC (1000 S. HUTCHINSON AVE, ADEL, GA 31620) AND THE CONTACT WAS INFORMED THAT THE COOLANT SENSOR AND HOSES FAILURE HAD TO DO WITH A RECALL AND THE VEHICLE WOULD BE REPAIRED UNDER NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE VEHICLE WAS REPAIRED HOWEVER, THE REPAIR FAILED TO FIX THE ISSUE. THE CONTACT STATED THAT TWO WEEKS LATER THE FAILURE RECURRED. THE VEHICLE WAS TOWED BACK TO THE SAME DEALER AND WAS DIAGNOSED THAT THE ENGINE CYLINDER HEAD WAS FRACTURED AND THE ENGINE NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND OPENED A CASE. THE FAILURE MILEAGE WAS APPROXIMATELY 108,000.

Mileage: 108,000

Jan 22, 2021 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE DRIVING AT 60 MPH, THE VEHICLE BEGAN TO MAKE AN ABNORMAL BEEPING SOUND. AS THE CONTACT PULLED OVER, A FLAME QUICKLY ERUPTED FROM UNDERNEATH THE VEHICLE. DUE TO THE IMMEDIATE SHOCK OF THE SITUATION, THE CONTACT BECAME FRANTIC AND KICKED OUT HER DRIVER SIDE WINDOW IN ORDER TO EXIT THE VEHICLE. THE CONTACT THEN CALLED THE AUTHORITIES AND THE POLICE AND FIRE DEPARTMENT ARRIVED ON THE SCENE. A POLICE AND FIRE REPORT WERE FILED AT THE SCENE. NO INJURIES WERE REPORTED AS A RESULT OF THE FIRE. DUE TO THE FAILURE, THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHERE IT WAS LATER DEEMED DESTROYED. THE DEALER NOR THE MANUFACTURER HAVE YET TO BE NOTIFIED OF THE FAILURE. UPON INVESTIGATION, THE CONTACT LINKED HER FAILURE TO NHTSA CAMPAIGN NUMBER: 17V209000(ENGINE AND ENGINE COOLING) WHICH SHE WAS UNAWARE OF PRIOR TO THE FAILURE. THE VEHICLE WAS DESTROYED. THE FAILURE MILEAGE WAS UNKNOWN.

Jan 15, 2021

THE TRANSMISSION WENT OUT THERE ARE 3 INTERNAL FAULTS

Jan 7, 2021 Fire

DRIVING ON INTERSTATE CHECK ENGINE LIGHT CAME ON THEN MESSAGE BOARD READ CAR IS OVERHEATED AND TO PULL OVER AND CAR SHUT DOWN, THEN THE TEMP GAUGE SHOT UP TO H. FINALLY CAME TO A COMPLETE STOP & CAR WAS SMOKING, OPENED THE HOOD AND SAW FLAMES, POURED WATER ON IT CALLED 911... APPARENTLY COOLLANT LEAKED OUT AND CAUSED THE TURBO TO GET HOT AND STARTED A FIRE.

Mileage: 116,883

Jan 7, 2021

MY 2014 FORD ESCAPE JUST HAD ENGINE LIGHTS COMING ON AND OVERHEATED AND JUST QUIT RUNNING.

Mileage: 80,000

Jan 5, 2021

THE VEHICLE RANDOMLY OVERHEATS AT TIMES AND SMOKES. NO MATTER THE AMOUNT OF COOLANT THAT'S IN THE TANK IT SEEMS LIKE IT'S NEVER FULL AND IT BURNS IT UP WITHIN MINUTES. THE VEHICLE CAN ONLY BE DRIVEN LESS THAN 8 MILES BEFORE IT STARTS SMOKING. WHEN DRIVING UPHILL SOMETIMES IT'LL SAY 'REDUCED POWER DUE TO OVERHEATING' EVEN THOUGH YOU JUST STARTED THE VEHICLE AND IT COULDN'T BE THAT HOT YET. THERE'S A RECALL ON THIS EXACT MODEL OF VEHICLE FOR THE SAME THING AND I BELIEVE MY VEHICLE WAS AFFECTED.

Mileage: 80,000

Dec 24, 2020

MY 2014 FORD ESCAPE IS HAVING THE SAME PROBLEM MANY AT HTTPS://WWW.CARPROBLEMZOO.COM/FORD/ESCAPE/2014/COOLANT-LEAKING-PROBLEMS.PHP ARE COMPLAINING OF. THE ENGINE COOLANT LIGHT KEEPS COMING ON. WENT TO FORD DEALERSHIP, THEY DID EXTENSIVE TESTING ON IT, SAID THERE WAS NO PROBLEM AND ONLY THAT THE ENGINE COOLANT SENSOR CAN BE SENSITIVE. TODAY, AS WITH THE OWNER COMPLAINTS, I WAS GOING UP A HILL, AND A RED ENGINE LIGHT CAME ON SAYING 'ENGINE TOO HOT, TURN OFF IMMEDIATELY AND PULL OVER' WELL I COULDN'T PULL OVER ON THE HILL SO WITHIN ONLY A FEW SECONDS, VEHICLE SHOOK, AND TURNED OFF LEAVING ME STUCK IN THE MIDDLE OF A HILL WITH NO ONE TO HELP. I CANNOT EVEN IMAGINE THIS HAPPENING ON THE FREEWAY LIKE OTHER OWNERS WITH THE SAME PROBLEM ARE HAVING! I'M SCARED TO DRIVE IT. LET ALONE TEACH MY DAUGHTER TO DRIVE ON IT! I THOUGHT I WAS BUYING HER A SAFE VEHICLE. I CHECKED VIA VIN NUMBER AND SHOWS ON OPEN RECALLS, YET, THIS IS THE EXACT SAME PROBLEM OTHER OWNERS ARE HAVING. THIS PROBLEM SHOULD BE RECALLED AND FIXED! PLEASE CONSIDER REVIEWING AND THANK YOU IN ADVANCE FOR YOUR HELP IN RESOLVING THIS ISSUE.

Mileage: 39,000

Dec 24, 2020

MY 2014 FORD ESCAPE ECOBOOST IS HAVING THE SAME PROBLEM MANY AT HTTPS://WWW.CARPROBLEMZOO.COM/FORD/ESCAPE/2014/COOLANT-LEAKING-PROBLEMS.PHP (SEE ATTACHMENT) ARE COMPLAINING ABOUT. THE ENGINE COOLANT LIGHT KEEPS COMING ON. WENT TO FORD DEALERSHIP, THEY DID EXTENSIVE TESTING ON IT, SAID THERE WAS NO PROBLEM AND ONLY THAT THE ENGINE COOLANT SENSOR CAN BE SENSITIVE. ENGINE COOLANT LIGHT GOES ON DAILY, YET LEVELS ARE OKAY. REMOVED CAP TO CHECK HEARD A HISSING NOISE AND THEN FLUID FROM OVERFLOW FLOWED IN AND NOT LOW. SO CANNOT ADD MORE COOLANT YET ENGINE LIGHT SAYS 'LOW ENGINE COOLANT' TODAY, AS WITH THE OWNER COMPLAINTS, I WAS GOING UP A HILL, AND A RED ENGINE LIGHT CAME ON SAYING 'ENGINE TOO HOT, TURN OFF IMMEDIATELY AND PULL OVER' WELL I COULDN'T PULL OVER ON THE HILL SO WITHIN ONLY A FEW SECONDS, VEHICLE SHOOK, AND TURNED OFF LEAVING ME STUCK/STRANDED IN THE MIDDLE OF A HILL WITH NO ONE TO HELP. WAITED TURNED ON AGAIN WAS ABLE TO GO MAYBE 2 FT, LIGHT CAME ON AGAIN, SHUT OFF VEHICLE AGAIN. IT IS ONLY 46 DEGREES OUT TODAY AND BARELY STARTED DRIVING WHEN THIS HAPPENED. I CANNOT EVEN IMAGINE THIS HAPPENING ON THE FREEWAY LIKE OTHER OWNERS WITH THE SAME PROBLEM ARE HAVING! I'M SCARED TO DRIVE IT. LET ALONE TEACH MY DAUGHTER TO DRIVE ON IT! I THOUGHT I WAS BUYING HER A SAFE VEHICLE. I CHECKED VIA VIN NUMBER AND SHOWS ON OPEN RECALLS, YET, THIS IS THE EXACT SAME PROBLEM OTHER OWNERS ARE HAVING. THIS PROBLEM SHOULD BE RECALLED AND FIXED! PLEASE CONSIDER REVIEWING AND THANK YOU IN ADVANCE FOR YOUR HELP IN RESOLVING THIS ISSUE.

Mileage: 39,000

Dec 24, 2020

WHAT CAN CAUSE MY 1.6L FORD ESCAPE TITANIUM 2014 TO BE HESITANT WHEN I PUSH DOWN ON GAS AND THEN SUDDENLY THE POWER KICS IN BACK AFTER ABOUT 5 SECONDS. IT LIKE ITS NOT GETTING ENOUGH GAS AT THE START! NO CHECK ENGINE ON - JC TAMPA FL

Mileage: 121,487

Dec 22, 2020

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE DRIVING AT VARIOUS SPEEDS, THE VEHICLE SHIFTED INTO LIMP MODE WITH A MESSAGE INDICATING CRITICAL OVERHEATING, SHUT-OFF VEHICLE BEING DISPLAYED. THE CONTACT COASTED TO THE SIDE OF THE ROADWAY AND SHUT-OFF THE VEHICLE. THE VEHICLE WAS RESTARTED BUT FAILED TO MOVE. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC AND WAS DIAGNOSED. THE CONTACT RETRIEVED DTC CODES: (P0219) ENGINE OVERSPEED CONDITION AND (P1299) CYLINDER HEAD OVERTEMPERATURE PROTECTION ACTIVE. THE CONTACT WAS ADVISED TO TAKE THE VEHICLE TO AN AUTHORIZED FORD DEALER. THE CONTACT WAS ALSO INFORMED OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE CONTACT CALLED LOVELAND FORD (999 E. EISENHOWER BLVD, LOVELAND, CO 80537, (970) 667-2220) TO INFORM THE DEALER OF THE FAILURE. THE DEALER INFORMED THE CONTACT THAT THE VIN WAS NOT INCLUDED. THE MANUFACTURER WAS CONTACTED AND REFERRED THE CONTACT TO NHTSA. THE FAILURE MILEAGE WAS APPROXIMATELY 97,755.

Mileage: 97,755

Dec 18, 2020

AFTER PURCHASING MY FORD MY TRANSMISSION WENT OUT WHILE DRIVING. I REPLACED IT AND A YEAR LATER HAD MY RECALL REPLACED FOR MY COOLANT SENSOR. WHILE THIS HAPPENED I HAD NO IDEA MY COOLANT LEVEL WAS SO LOW BECAUSE MY WARNING LIGHT NEVER CAME ON IN RETURN DAMAGED THE HOSE. SO I HAD TO SPEND $562 TO REPLACE THAT TO MAKE SURE THE RECALL WAS PUT ON CORRECTLY. WHEN I RETURNED TO PICK UP MY CAR I COULDN'T EVEN DRIVE IT OUT BECAUSE IT STARTED JERKING AND FEELS LIKE MY TRANSMISSION IS GOING OUT AGAIN. THIS 2014 FORD ESCAPE HAS SOME SERIOUS PROBLEMS WITH THE TRANSMISSION. NOT TO MENTION AFTER SO MANY MILES OF DRIVING I HAVE TO TAKE OUT MY FUSE TO RESET MY BLUETOOTH RADIO.

Dec 16, 2020

VEHICLE HAS BEEN DIAGNOSED AS LEAKING COOLANT INTO ONE OF THE CYLINDERS. IF LEFT UNREPAIRED, THERE IS A POSSIBILITY OF ENGINE FIRE. DEALER RECOMMENDED REPAIR IS TO REPLACE THE ENGINE, AT AN UNACCEPTABLY HIGH COST OF APPROXIMATELY $9000.

Mileage: 85,000

Dec 8, 2020

I OWN A 2014 FORD ESCAPE IT HAS 101,000 MILES ON IT. THE CAR HAS BEEN WELL MAINTAINED WITH ALL THE NORMAL MAINTENANCE DONE AT MILEAGE RECOMMENDED. I WAS ON THE INTERSTATE IN TRAFFIC WHEN ALL THE SUDDEN THE VEHICLE JUST SHUT OFF, WHICH LEFT ME IN THE MIDDLE OF THE INTERSTATE DUE TO THE BUMPER TO BUMPER TRAFFIC. I HAD THE VEHICLE TOWED TO SHOP AND COME TO FIND OUT THE TRANSMISSION WENT COMPLETELY OUT. CALLED THE FORD DEALERSHIP AND OF COURSE THE WARRANTY HAD JUST EXPIRED ON IT AND WAS TOLD THAT THEY WEREN'T AWARE OF THIS PROBLEM WITH THESE VEHICLES AND THERE WAS NOTHING THEY COULD DO ABOUT THIS PROBLEM. T THIS POINT IT WAS GOING TO COST ME OVER 5K TO HAVE EVERYTHING FIXED. COME TO FIND OUT FORD KNEW ABOUT THIS PROBLEM WITH THIS PARTICULAR YEAR MAKE AND MODEL OF THIS VEHICLE AND ARE PRETTY MUCH A JOKE. THIS PROBLEM SHOULD BE A RECALL GIVING THE FACT I STILL OWED MONEY FOR THIS VEHICLE.

Mileage: 101,000

Dec 6, 2020

MY CAR QUIT WORKING AND I HAVE BEEN TRYING TO GET IT FIXED SINCE 10/24. IT DEFINITELY SOUNDS LIKE THE RECALL ISSUE BUT FORD IS TELLING ME ITS NOT. THEY WANT TO CHARGE ME $5500 TO FIX IT BUT IT DEFINITELY SOUNDS LIKE A BUSHING ERROR.

Mileage: 90,000

Dec 4, 2020

IN FEB 2019 I HAD MY FORD ESCAPE SERVICED FOR AN ENGINE COOLANT RECALL (17S09). IN OCTOBER 2020 THE FORD DEALERSHIP FOUND MY ENGINE COOLANT LEAKING INTO THE CYLINDERS OF MY ENGINE. THIS IS A PROBLEM THAT SHOULD HAVE BEEN TAKEN CARE OF BY THE RECALL. THIS IS A FIRE HAZARD AND FORD CLAIMS THE REPAIR WILL BE $5,000. THEY CLAIM THAT THE RECALL WILL NOT COVER THE EXPENSE. I AM WRITING FOR FORD TO REOPEN RECALL 17S09. THIS IS A HUGE SAFETY HAZARD AND LIABILITY.

Nov 14, 2020

ENGINE KEEPS OVER HEATING BUT NO COOLANT LEAK WARNING LIKE KEEPS COMING ON SAYING ENGINE TEMP TO HIGH PULL OVER JUST GOT TRANSMISSION REPLACED BY FORD DEALERSHIP VEHICLE WAS TRAVELING AROUND 60MPH WHEN ENGINE TEMP WARNING LIGHT CAME ON AND WENT LIMP

Mileage: 92,470

Oct 21, 2020

THIS IS IN REGARDS TO RECALL 17V209000 FOR MY 2014 FORD ESCAPE. I HAD THIS FIXED IN 2019, BUT I WAS NOT HAPPY WITH THE DEALERSHIP'S SERVICE. FIRST OF ALL, MY CAR HAD BEEN OVERHEATING, AND I HAD TO ADD COOLANT CONSTANTLY, WHICH WAS A SYMPTOM OF THE RECALL ISSUE. I TOOK IT TO THE DEALERSHIP TO TAKE CARE OF THE RECALL, WHICH THEY SAID THEY DID, BUT THEY TOLD ME THE OVERHEATING WAS NOT CAUSED BY THE RECALL PROBLEM, BUT SOMETHING ELSE, SO IN ADDITION TO FIXING THE RECALL PROBLEM, THEY SAID THEY FIXED ANOTHER PROBLEM ASSOCIATED WITH THE OVERHEATING AND CHARGED ME $250. I DON'T BELIEVE THIS, AND I'M NOT EVEN SURE IF THEY FIXED THE RECALL PROBLEM, HOWEVER, THEY REPORTED THAT THEY DID, BUT THEY NEVER CALLED ME BACK TO HAVE IT INSTALLED. I BELIEVE THE RECALL ISSUE CAUSED A CRACKED CYLINDER BECAUSE LAST MONTH I HAD TO HAVE A NEW ENGINE (AT MY EXPENSE) INSTALLED. THIS CAR IS ONLY 6 YEARS OLD AND I HAVE KEPT CURRENT WITH PERIODIC OIL CHANGES AND CHECK-UPS. WHAT ARE MY OPTIONS WITH FILING A CLAIM, OR SOME KIND OF REPORT OR RECOURSE FOR THIS?

Mileage: 103,000

Oct 20, 2020

2014 FORD ESCAPE. CONSUMER WRITES IN REGARDS TO LOSS OF POWER WHILE DRIVING. *LD THE CONSUMER STATED WHILE DRIVING THE ENGINE WARNING LIGHT APPEARED ON THE DASHBOARD, THEN THE VEHICLE LOST POWER. THE NEXT MORNING, THE VEHICLE WAS TAKEN TO THE DEALER. NO CODES WERE FOUND. THE VEHICLE WAS NOT REPAIRED. *JS

Oct 17, 2020

MY ENGINE OVER HEATS. COOLANT LEAKS. I HAD IT SERVICED THROUGH FORD FOR THIS ISSUE, IMMEDIATELY AFTER THE CHECK ENGINE LIGHT CAME ON. THE LIGHT FOR COOLANT WAS STILL POPPING UP. MY CAR FLASHES 'TOO HOT TURN OFF IMMEDIATELY' DAILY.

Oct 16, 2020

THE COMMUNITY I LIVE IS LANDLOCKED (JUNEAU, ALASKA) AND THE ONE FORD DEALERSHIP CLOSED ITS DOORS A YEAR AND HALF LATER; SINCE THIS TIME THERE IS STILL NOT FORD DEALERSHIP OR AUTHORIZED FORD GARAGE IN THE JUNEAU AREA TO CORRECT THESE SIX RECALLED ITEMS - FORD TELLS MY I HAVE TO TAKE IT TO DEALER MYSELF, HOWEVER THE COST TO TRANSPORT THE 2014 ESCAPE WOULD COST IN THE THOUSANDS IN TRANSPORTATION COST. I'VE CALLED FORD SEVERAL TIMES OVER THE YEARS, AND REFUSED TO SEND TO SEND A TECHNICIAN OR OFFER A LOCAL REPAIR SHOP TO FIX THESE RECALLED ITEMS; SOME OF RECALLED ITEMS ARE PRETTY SERIOUS (POSSIBLE ENGINE FIRE, AND TRANSMISSION SLIPPING IN OR OUT GEAR). PLEASE HELP AS I TRY TO GET FORD TO FIX, BUT THEY OFFER NOTHING MORE EXPENSIVE COST TO ME FOR DEFECTIVE PRODUCT. THANK YOU, [XXX] INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TR

Mileage: 41,200

Oct 15, 2020

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE DRIVING AT AN UNDISCLOSED SPEED, THE CHECK ENGINE WARNING LIGHT ILLUMINATED WITH AN ENGINE FAULT MESSAGE DISPLAYED ON THE INSTRUMENT PANEL. ON SEVERAL OCCASIONS, THE VEHICLE LUNGED FORWARD INDEPENDENTLY. THE VEHICLE WAS TAKEN TO THE LOCAL DEALER ROCHESTER FORD LOCATED AT 8 CRAIN RD, ROCHESTER, NH 03867, WHO DIAGNOSED THAT THE MANIFOLD ABSOLUTE PRESSURE (MAP) SENSOR WAS DEFECTIVE. THE MAP SENSOR WAS REPLACED AND THE WIRING HARNESS WAS SPLICED TO REMEDY THE FAILURE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE AND THE CONTACT WAS INFORMED THAT THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 15V813000 (ELECTRICAL SYSTEM). THE CONTACT INDICATED THAT THE VEHICLE EXPERIENCED THE SAME FAILURE LISTED IN THE RECALL. THE FAILURE MILEAGE WAS 98,000.*JFT *DT*JB

Mileage: 98,000

Oct 14, 2020

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED WHILE DRIVING 65 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE VEHICLE WAS NOT DRIVABLE. THE VEHICLE WAS TOWED TO LOCAL DEALER GWINNETT PLACE FORD LOCATED AT 3230 SATELLITE BLVD, DULUTH, GA 30096, (404) 418-6877, WHERE IT WAS DIAGNOSED WITH NEEDING TRANSMISSION TO BE REPLACED. THE VEHICLE WAS REPAIRED HOWEVER, THE FAILURE RECURRED. UPON INVESTIGATION, THE CONTACT ASSOCIATED THE FAILURE WITH NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING) HOWEVER, THE VIN WAS NOT INCLUDED. THE CONTACT STATED SHE ATTEMPTED TO CONTACT MANUFACTURER BUT WAS UNABLE TO SPEAK TO A REPRESENTATIVE. THE FAILURE MILEAGE WAS APPROXIMATELY 120,000.

Mileage: 120,000

Oct 9, 2020

MY 2014 FORD ESCAPE IS STUCK IN PARK CAR WAS PARKED IN A PARKING LOT

Oct 3, 2020

COOLANT SYSTEM PROBLEM FOR MANY YEARS. ENGINE OVERHEATING WARNING COMES ON WHEN CAR IS STARTED. CYLINDER HEAD TEMPERATURE SENSOR CHANGED TWICE. LOSES COOLANT OVER TIME. THIS ISSUE HAS BEEN PREVALENT IN FORD ESCAPES FOR YEARS AND SOME VEHICLES WERE RECALLED. THIS VEHICLE HAS THE RECALL DESCRIBED ISSUES BUT WAS NOT LISTED FOR RECALL. NEED SYSTEM FIXED.

Mileage: 30,000

Sep 25, 2020

SMOKE WAS COMING OUT OF THE TAIL PIPE. TURBO WAS REPLACED. A FEW MONTHS LATER CAR WOULD NOT ACCELERATE PAST 20MPH. TRANSMISSION WAS REPLACED.

Mileage: 73,500

Sep 25, 2020

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE DRIVING AT AN UNDISCLOSED SPEED, THE CHECK ENGINE WARNING LIGHT ILLUMINATED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO STATED THAT THE HEAD GASKET BLEW AND THE HEAD GASKET NEEDED TO BE REPLACED. THE CONTACT REFERENCED NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING) HOWEVER, THE VIN WAS NOT INCLUDED. THE CONTACT CALLED THE GLOCKNER SOUTH POINT FORD DEALER LOCATED AT 155 CO RD 406, SOUTH POINT, OH 45680, AND WAS INFORMED THAT THE VEHICLE WAS NOT INCLUDED IN THE RECALL. THE MANUFACTURER WAS NOT MADE AWARE FO THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS APPROXIMATELY 166,000.

Mileage: 166,000

Sep 24, 2020

TOOK ESCAPE TO DEALER ON 08/26/20, ALL CHECKED OUT. SOMEONE HAD MARKED COOLANT RESEVOIR ON THE PAPER WORK DONE AT DEALER, WAS WRITTEN IN AND THEN IT WAS CROSSED OFF. FAST FOWARD 3 WEEKS AND DASH READ "TURN OFF ENGINE TOO HOT" TOOK TO DEALER NO OTHER MECHANIC HAS TOUCHED CAR AND THEY STATED THE RESEVOIR HAD LEAKED AND THAT THE ENGINE MOUNT WAS CORRODED. THEY TAKE NO RESPONSIBILITY FOR NOT TAKING ACTION ON A BROKEN RESEVOIR THAT CORRODED ENGINE MOUNT. THIS HAPPENED ON WHILE DRIVING 20 MINUETS ON THE FREEWAY.

Mileage: 20

Sep 17, 2020

I TOOK MY CAR TO A FORD DEALSHIP TO FOR A RECALL. THE RECALL WAS 17S09, A COOLANT LEVEL SENSOR INSTALLATION. WHEN I PICKED MY VEHICLE UP AND DROVE IT HOME, THE NEXT DAY MY CHECK ENGINE LIGHT CAME ON, SO I BROUGHT IT BACK. THEY THEN REPLACED A LEAKING COOLANT LINE TO DEGAS BOTTLE. A FEW DAYS LATER I TURNED ON MY VEHICLE TO GO SOMEWHERE AND BEFORE EVEN LEAVING MY BLOCK, MY CHECK ENGINE LIGHT CAME ON AGAIN AND INSTANTLY STARTED OVER HEATING. I WAS LUCKILY DOWN THE STREET FROM MY HOME SO I MANAGED TO GET IT BACK TO MY HOUSE, BUT I WAS AFRAID TO DRIVE IT SO I HAD IT TOWED TO THE DEALERSHIP FOR A THIRD TIME. THEY DIDN'T MAKE ANY NOTES ON THAT VISIT SO I'M NOT SURE WHAT HAPPENED BUT WHEN I PICKED IT UP THEY STATED I NEEDED TO PAY FOR SERVICES BECAUSE THEY NOTICED A LEAK IN MY HEATER HOSE AND THE SERVICE WAS GOING TO COST OVER $3000! MY CAR WAS PERFECTLY FINE BEFORE TAKING IT IN FOR A RECALL. I WISH I WOULD HAVE NEVER BROUGHT IT IN BECAUSE WHEN I TRIED TO MAKE A COMPLAINT ABOUT HOW MY CAR WAS SERVICED AND WHAT THEY DID TO IT, I HAD NO LUCK GETTING ANY HELP OR ASSISTANCE BUT I KNOW THE RECALL PUT MY CAR IN A WORSER CONDITION. MY VEHICLE HAD NEVER OVER HEATED BEFORE AND A FEW DAYS AFTER GETTING THIS RECALL IT OVER HEATED AS SOON AS I TURNED IT ON.

Mileage: 90,680

Sep 15, 2020

WHILE COASTING ON THE FREEWAY AT APPROXIMATELY 70MPH MY FORD ESCAPE STOPPED ACCELERATING. NO WARNING LIGHTS ILLUMINATED, SIMPLY THE ACCELERATOR STOPPED FUNCTIONING. ALL FLUID WERE OKAY AND NO OVERHEATING CONDITION WAS PRESENT. I WAS ABLE TO PULL OVER TO THE SHOULDER, SHUT OFF THE ENGINE AND AFTER A FEW MINUTES TURNED THE ENGINE BACK ON. I PRESSED ON THE ACCELERATOR AND THE CAR JERKED FORWARD. THE FORD SEEMED TO GO IN AND OUT OF GEAR. I ENDED UP TOWING THE VEHICLE HOME. I HAD THE TRANSMISSION SERVICED (NEW TRANSMISSION FLUID). FEW WEEKS LATER, SAME THING HAPPENED AGAIN (REPLACED THROTTLE BODY) WITH NOT CHECK ENGINE LIGHT OR FAULT CODE EVER COMING ON. THE SECOND TIME THIS OCCURRED, I WAS ALMOST INVOLVED IN A COLLISION DUE TO NOT BEING ABLE TO ACCELERATE. CAR DROVE AGAIN ON AND OFF. TOOK IT TO A TRANSMISSION SHOP AND WAS ADVISED THE TRANSMISSION WOULD NEED TO BE REBUILT. TRANSMISSION WAS REBUILT AND THE FORD SEEMS TO BE DRIVING MUCH BETTER, SHIFTING IS STILL NOT SMOOTH.

Mileage: 145,000

Sep 14, 2020

OUR 2014 FORD ESCAPE HAD A RECALL ON 02-15-18 FOR THE COOLANT SENSOR SYSTEM. REPAIR WAS DONE BUT DID NOT FIX THE PROBLEM. ENGINE HAS COOLANT LEAK CAUSING SMOKE IN THE EXHAUST SYSTEM AND LEAK UNDER THE HOOD. WE ARE AFRAID OF FIRE IN THE ENGINE COMPARTMENT AND IN THE CAR.ANYTIME WE START THIS VEHICLE OR DRIVE IT THIS HAPPENS.

Mileage: 92,000

Sep 12, 2020

MY 2014 FORD ESCAPE HAS OVERHEATED SOMETIME IN THE FALL OF 2019, DUE TO A LEAK IN THE COOLANT TANK, UNEXPECTEDLY SHUTTING OFF WHILE DRIVING ON A SMALL TOWN ROAD AT 40 MI/HR WITH CHILDREN IN THE BACK SEAT. I PAID FORD $600 TO REPLACE THE TANK. IN SEPTEMBER OF 2020, THE ENGINE OVERHEATED AGAIN, SUDDENLY SHUTTING OFF WHILE DRIVING 55 MI/HR ON A BUSY ROAD. I HAD CHILDREN IN THE CAR, WHEN THE ERROR OCCURRED AGAIN.THE TEMPERATURE GAUGE SHOWED NO SIGN OF OVERHEATING IN EITHER OCCURRENCE. THE ONLY MESSAGE I RECEIVED FROM THE DASH WAS "POWER REDUCED TO COOL ENGINE" ABOUT 3 SECONDS BEFORE THE CAR CAME TO A COMPLETE STOP. SMOKE APPEARED FROM UNDER THE HOOD IN BOTH INSTANCES. THE SECOND TIME AROUND, I ATTEMPTED TO REFILL THE COOLANT, WHICH LEAKED OUT ONTO THE GROUND. HOWEVER, THIS TIME THE LEAK DIDN'T APPEAR TO COME FROM THE COOLANT TANK, BUT RATHER THE ENGINE ITSELF. I RESEARCHED THE ISSUE AND IT TURNS OUT, MANY OF THE SAME YEAR AND MODEL CARS HAVE BEEN CATCHING ON FIRE AND/OR PRODUCING THE SAME ISSUE. THERE IS A RECALL FOR IT, BUT FORD TOLD ME THAT BASED ON MY VIN, MY CAR DIDN'T QUALIFY FOR THE RECALL. THEY ASKED ME PAY $3,000 REPLACE A BLOWN GASKET THAT WAS CAUSED BY THE SYSTEM OVER HEATING. OBVIOUSLY, THESE EXPENSIVE PARTS CONTINUE TO BREAK DUE TO A FAULTY ENGINE. YET, INSTEAD OF FIXING THE ROOT CAUSE, FORD MILKS ITS CUSTOMERS FOR HUNDREDS, EVEN THOUSANDS OF DOLLARS WORTH OF REPAIRS, KNOWING THE CAR WILL CONTINUE TO SHUT OFF AND CAUSE FINANCIAL, EVENTUALLY PHYSICAL HARM TO PEOPLE. MY QUESTION'S ARE: -HOW MUCH MORE MONEY DO I HAVE TO SPEND ON A FAULTY ENGINE THAT WILL CONTINUE TO SHUT OFF AND PUT MY AND MY FAMILY'S LIFE IN DANGER? -HOW CAN FORD REFUSE TO FIX A RECALL BASED ON VIN NUMBERS, IF THE ISSUE IS LIFE-THREATENING AND EXACTLY THE SAME AS THE RECALL ISSUE?

Mileage: 86,000

Sep 9, 2020

NHTSA CAMPAIGN ID: 17V209000 REPORT DATE: MAR 26, 2017 VEHICLES AFFECTED: 208584 THE DEALERSHIP DID NOT COMPLETE A RECALL REPAIR ON MY VEHICLE. THE CYLINDER HEAD CRACKED AND COOLANT HAS ENTERED THE MOTOR. LEAKS OIL, THE OIL MAY CONTACT A HOT ENGINE OR EXHAUST COMPONENT, INCREASING THE RISK OF A FIRE. MY ENGINE LIGHT IS ON, THE ENGINE FAULT ICON HAS ILLUMINATED. THE DEALERSHIP WANTS TO CHARGE ME $7,000 TO REPL;ACE THE ENGINE. THIS VEHICLE IS ONLY 6 YEARS NEW.

Mileage: 87,345

Sep 2, 2020

COOLANT IS LOW AND NEEDS TO BE REPLACED ON INSTRUMENT PANEL CAME ON ALONG WITH CHECK ENGINE LIGHT. THEN WHITE SMOKE STARTED COMING OUT OF EXHAUST FROM THE BACK AND CAR STARTED TO STALL. DIAGNOSTIC READER SAID THAT THERE WAS A MISFIRE IN COIL NUMBER 2.

Mileage: 10

Sep 2, 2020

IN 2014, I BOUGHT A NEW FORD ESCAPE FROM RHINEBECK FORD IN RHINEBECK NY. IT REMAINED IN PRISTINE CONDITION UNTIL ITS UNTIMELY 'DEATH' ON AUGUST 10, 2020. PRIOR TO AUGUST 10, IT WAS BACK AT THE DEALERSHIP APPROXIMATELY 15 TIMES TO ADDRESS SAFETY RECALLS. ON AUGUST 10 MY WIFE, SON AND NIECE BROKE DOWN IN THE MIDDLE OF THE ROAD. WE BROUGHT THE CAR TO RHINEBECK FORD. AFTER EXAMINING THE CAR, WE WERE TOLD THAT THE ENGINE AND CYLINDERS HAVE COOLANT IN THEM, AND THE TRANSMISSION IS FULL OF METAL FILINGS. BOTH OF THESE ISSUES COMBINED MEAN THAT THE CAR IS DISEASED; HOWEVER RHINEBECK FORD IS STILL IN THE PROCESS OF CREATING A COMPREHENSIVE LIST OF THE CAUSE OF DEATH. FORTUNATELY THESE DANGEROUS DEFECTS DID NOT RESULT IN INJURY TO MY FAMILY BUT THEY CERTAINLY DO REPRESENT A SERIOUS SAFETY RISK. ON AUGUST 10, THE CAR HAD APPROXIMATELY 108,000 MILES ON IT. I WAS SOLD A DEFECTIVE AND UNSAFE VEHICLE AND FORD MOTOR COMPANY IS NOT WILLING TO MAKE THIS RIGHT. I MADE NUMEROUS PHONE CALLS TO FORD CORPORATE OFFICES AND WAS TOLD THAT SINCE THE WARRANTY WAS EXPIRED AND THERE ARE NO ACTIVE RECALLS PERTAINING TO DEFECTIVE TRANSMISSIONS OR ENGINES THAT THEY WOULD NOT STAND BY THEIR PRODUCT.

Mileage: 108,000

Sep 1, 2020

MY CAR IS SPORADICALLY SPEWING ANTI-FREEZE FROM THE OVERFLOW TANK. I HAVE TAKEN IT TO 3 LOCAL MECHANICS AND 1 FORD DEALERSHIP AND NO ONE HAS BEEN ABLE TO FIND A REASON FOR THIS. I HAVE NOTICED THIS OCCURS IF I AM DRIVING AROUND FOR A LONG TIME WITH THE A/C OFF. THE LEAKING IS COMING FROM MY COOLANT OVERFLOW TANK'S AIR VENTILATION. ANTI-FREEZE DOES NOT LEAK OUT WHILST DRIVING THE VEHICLE, BUT ONLY WHEN I PARK AND SHUT IT OFF. THE MECHANICS HAVE DONE SEVERAL PRESSURE TESTS WHICH ALL CAME BACK NORMAL. DECEMBER 2019 MY COOLANT LIGHT CAME ON FOR THE FIRST TIME SINCE OWNING THE CAR FOR 2 YEARS AND I WAS NEEDING TO PUT A SMALL AMOUNT OF ANTI-FREEZE IN EVERY MONTH. SINCE JULY 2020 IT HAS BEEN OVERFLOWING AND LEAKING EVERY WEEK IT SEEMS. I WOULD AVERAGE I GO THROUGH 2-3 CUPS OF ANTI-FREEZE EVERY 1-2 WEEKS. WHEN PARKING AND TURNING OFF THE CAR THE OVERFLOW TANK HAS ANTI-FREEZE FILLED TO THE TOP, BUT NOT QUITE COMING OUT OF THE CAP. I AM ATTACHING SOME IMAGES OF MY OVERFLOW TANK.

Mileage: 75,000

Sep 1, 2020 Fire

TL* THE CONTACT OWNED A 2014 FORD ESCAPE. THE CONTACT STATED THAT ANTIFREEZE HAD BEEN LEAKING OUT OF HIS ENGINE AS HIS SERVICE ENGINE LIGHT HAD ILLUMINATED ON THE INSTRUMENT PANEL. THE CONTACT HAD TAKEN HIS VEHICLE TWICE TO AN INDEPENDENT MECHANIC AND WAS GIVEN VARIOUS REPORTS ON THE VEHICLE. THE CONTACT THEN TOOK THE VEHICLE TO CONWAY HEATON INC. (810 N 3RD ST, BARDSTOWN, KY 40004) WHERE HE WAS UNABLE TO PAY FOR A DIAGNOSIS AND STATED THAT HE HAD LINKED HIS FAILURE TO NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING) WHICH INCLUDED VIN. THE DEALER INFORMED HIM THAT THE RECALL HAD ALREADY BEEN PERFORMED PRIOR TO HIM OWNING THE VEHICLE, THE VEHICLE WAS THEN RETURNED TO THE CONTACT AND THE RECALL WAS NOT PERFORMED. WHILE DRIVING THE VEHICLE AT 60 MPH, HE NOTICED THAT THE TEMPERATURE GAUGE HAD BEEN RISING INDICATING THAT HIS VEHICLE WAS OVERHEATING. AS THE CONTACT ATTEMPTED TO PULL HE VEHICLE OVER, THE ENGINE FAULT SERVICE ENGINE NOW WARNING LIGHT HAD APPEARED ON THE INSTRUMENT PANEL. AS THE CONTACT EXITED HIS VEHICLE, HE OPENED HIS HOOD AND SAW A FLAME ARISE IN HIS ENGINE. THE CONTACT IMMEDIATELY CALLED THE AUTHORITIES AND AFTER 15 MINUTES OF WAITING FOR THE FIRE DEPARTMENT, THE ENTIRE VEHICLE BECAME ENGULFED IN FLAMES. ONCE THE FIRE DEPARTMENT ARRIVED, THE FIRE WAS EXTINGUISHED. THE VEHICLE WAS DESTROYED, NO INJURIES WERE REPORTED. THE VEHICLE WAS TOWED TO A LOCAL POLICE STATION WERE IN REMAINED IN THEIR POSSESSION. THE MANUFACTURER HAD BEEN NOTIFIED OF THE FAILURE AND THEY EXPLAINED TO HIM THAT THEY WOULD NOT BE ABLE TO REBUILD THE VEHICLE, THEY OFFERED NO FURTHER ASSISTANCE. THE VEHICLE WAS DESTROYED. THE FAILURE MILEAGE WAS APPROXIMATELY 108,000. VIN TOOL CONFIRMED PARTS DISTRIBUTION DISCONNECT.

Mileage: 108,000

Aug 27, 2020

I HAVE A 2014 FORD ESCAPE 1.6L ECOBOOST.THAT IS NOT RUNNING&FORD WILL NOT FIX NOR ADMIT THAT THERE ARE OTHER VEHICLE LIKE MINE.BEFORE THE COOLING RECALL CAME ABOUT MY VEHICLE OVER HEATED 2X.I CALLED FORD&THEY TOLD ME THERE WOULD BE A CHARGE TO FIND& FIX THE PROBLEM.FEW MONTHS LATER I WAS NOTIFIED OF THE RECALL.I TOOK MY VEHICLE INTO HALL FORD IN ELIZABETH CITY NC.FIRST THEY SAID THEY DID NOT KNOW WHAT NEEDED TO BE FIXED. THEN THE NEXT DAY THEY SAID THE PROBLEM HAD FIXED AFTER 24 HOURS OF HAVING THE VEHICLE. A YEAR LATER THEY RECALLED THE VEHICLE AGAIN FOR THE SAME THING&SAID THEY DID NOT FIX THE RIGHT THING. NOW AFTER 100,000 MILES THE VEHICLE SHIFTS OUT OF GEAR. FOR SAID THERE IS NO RECALL (BUT WITHOUT ACTUALLY LOOKING AT THE VEHICLE) THEY KNOW IT IS THE TRANSMISSION. THAT IT WILL COST $5,000 FOR A REMAN TRANSMISSION OR $7,000 FOR A NEW ONE. REMIND YOU THEY HAVE NOT LOOKED OVER THE VEHICLE AND THAT DOES NOT INCLUDE LABOR. THE VEHICLE POPS OUT OF GEAR AFTER NOT EVEN DRIVING IT FOR 5 MINUTES. IT IS THE 1.6LL 6 SPEED AUTOMATIC TRANSMISSION. I ASKED IF THERE WERE OTHER VEHICLES DOING THE SAME THING AND THEY REPLIED NO I WAS THE FIRST THEY HEARD OF. I SAID WELL HOW DO YOU KNOW IT IS THE TRANS.THEY REPLIED BECAUSE WE KNOW OUR VEHICLES. I ASKED IF IT COULD BE FROM THE CAR OVERHEATING 2X BEFORE THEY FIXED THE COOLING ISSUE.THEY SAID NO BECAUSE THEY KNOW THERE VEHICLES.I HAVE GOT 3 DIFFERENT PRICE QUOTES OVER THE PAST 6 MONTHS. THE FIRST QUOTE $2500 REMAN PLUS LABOR THEN 2500 FOR JUST TRAN TO 4-5K FOR REMAN TRANS NOT INCLUDING LABOR.THEY THEN ASKED IF I WOULD LIKE TO TRADE IN MY VEHICLE FOR SOMETHING THAT WAS RELIABLE. I ANSWERED NO BECAUSE MY CAR WAS PAID FOR. I SAID NO ONE CAN DRIVE IT LIKE THIS. THEY SAID THATS WHY YOU SHOULD BUY A NEW CAR.I STARTED DOING RESEARCH AND FOUND THAT MULTIPLE PEOPLE (HUNDREDS OF THOUSANDS)HAVE HAD THE SAME PROBLEM WITH THERE VEHICLE AS ME.

Mileage: 100,000

Aug 26, 2020

HAD THE COOLANT RESERVOIR CRACK TWICE, VEHICLE WAS STOPPED IMMEDIATELY AND THEN THE PART WAS REPLACED RIGHT AWAY. AFTER THE SECOND TIME I ASKED IF THIS WAS A COMMON ISSUE WITH THESE VEHICLES I WAS TOLD IT WAS AND THAT THEY ARE CONSTANTLY REORDERING THESE PARTS. NOT EVEN 2 MONTHS LATER I TOOK IT IS BECAUSE IT HAD A CHECK ENGINE LIGHT AND THEY CLAIMED IT WAS 2 BAD SENSORS, I TOOK IT IN TO GET REPAIRED AND THEN THEY TOLD ME MY MOTOR WAS SHOT.

Mileage: 90,000

Aug 25, 2020

I BOUGHT MY CAR IN NOVEMBER OF 2018, ALMOST IMMEDIATELY MY LOW COOLANT LIGHT WAS COMING ON OFTEN, I TOOK IT TO A MECHANIC AND THEY FOUND NO LEAKS SO I JUST CONTINUED TO ADD COOLANT WHEN IT CAME ON ABOUT EVERY 2 MONTHS. I WAS DRIVING FROM COLORADO TO OKLAHOMA ON MAY 26TH 2020 AND MY CHECK ENGINE LIGHT CAME ON I IMMEDIATELY TOOK IT TO A CERTIFIED FORD MECHANIC AND WAS TOLD I NEEDED A NEW TURBO CHARGER $2800. DRIVING FROM OKLAHOMA TO COLORADO ON JUNE 5TH 2020.MY CAR OVERHEATED, ONCE AGAIN I TOOK IT TO A FORD CERTIFIED MECHANIC AND WAS TOLD IT NEEDED A NEW THERMOSTAT AND 2 OTHER SENSORS, $1300. ON AUGUST 13TH MY CAR STARTED MAKING A LOUD GRINDING SOUND AS I WAS DRIVING ON THE HIGHWAY I DROVE 2HRS TO THE CLOSES FORD DEALERSHIP AND WAS TOLD I NEED A NEW ENGINE TO THE TUNE OF $8000. THIS VEHICLE IS WORTHLESS AND I AM SO FRUSTRATED WITH THIS WHOLE SITUATION. ONLY 109000 MILES

Mileage: 109,000

Aug 21, 2020

IT HAS BEEN A PROBLEM WITH 2014 FORD ESCAPES THAT THE TRANSMISSION FAILS AND ENGINE CYLINDER DEFECTS FROM THE LOUISVILLE ASSEMBLY PLANT IN LOUISVILLE, KENTUCKY. MY CAR WAS MANUFACTURED AT THIS PLANT DURING THE DATES OF THE DEFECTS IN 2013. THE DEFECTS EFFECTED THE 2014 ESCAPES. THE RECALL IS ON CARS FROM FEB 2013 THROUGH SEPT 2013. MY VECHILE WAS MANUFACTURED JUNE 2103 WHICH IS IN THE "RECALL DATES". I HAD TO REPLACE THE TRANSMISSION ON A CAR WITH LESS THAN 100,000 MILES AT THE COST OF $3,800 BECAUSE THE FORD DEALERSHIP SAID THAT "IT'S NOT UNDER WARRANTY OR RECALL". THE CAR NOW HAS A P304 CODE WHICH IS CYLINDER 4 DEFECT THAT IS A KNOW DEFECT OF THE CYLINDER HEAD. I CONTACTED FORD AND THEY "MAY LOOK AT IT" AND IF THERE ARE ENOUGH COMPLAINTS THEY "MAY DO A RECALL" ON MY VIN NUMBER. FORD "MAY REIMBURSE ME FOR THE TRANSMISSION THAT I PUT IN" THESE ARE KNOW DEFECTS FROM THIS MANUFACTURING PLANT WITH OTHER VINS GETTING REPAIRS. THE CAR WAS DRIVING ROUGH PRIOR TO THE TRANSMISSION BEING REPLACED WHICH WAS THE HEAD GEAR STARTING TO GO. I APPRECIATE YOUR TIME.

Mileage: 91,585

Aug 15, 2020

SIDE WALL OF CYLINDER CRACKED DUE TO AN UNCHECKED RECALL CAUSING COOLANT TO LEAK INTO CYLINDER. DAMAGING THE ENGINE WARRANTING THE WHOLE ENGINE BE REPLACED AT A COST OF AROUND $7000. THE VEHICLE WAS ALSO JUST OUT OF MILEAGE WARRANTY CAUSING THE OWNER TO PAY THE WHOLE BILL.

Mileage: 132,475

Aug 13, 2020

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 10 MPH, THE VEHICLE BEGAN TO JERK AND VIBRATE WHILE THE SPEED REDUCED INDEPENDENTLY. AFTER TURNING OFF AND RESTARTING THE VEHICLE, THE VEHICLE OPERATED AS DESIGNED HOWEVER, THE CHECK ENGINE WARNING LIGHT REMAINED ILLUMINATED. THE VEHICLE WAS TAKEN TO THE LOCAL DEALER PLANTATION FORD LOCATED AT 707 N. STATE RD 7, PLANTATION, FL 33317, WHO DIAGNOSED THAT THE THROTTLE BODY WAS DEFECTIVE AND NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE BUT NO ASSISTANCE WAS OFFERED. THE FAILURE MILEAGE WAS 89,800.

Mileage: 89,800

Aug 13, 2020

SERVICE ENGINE LIGHT CAME ON, I TURNED ON CAR TO TAKE TO MECHANIC AND THE CAR SHOOK BAD AND CHOKED ITSELF OUT. THIS HAPPENED TWICE. I LEFT SITTING FOR A DAY, DRIVE TO MECHANIC NEXT DAY, CAR STARTED NO PROBLEMS DRIVING. MECHANIC DIAGNOSIS FOLLOWS: - FOUND MISFIRE DTC, REMOVED SPARK PLUGS AND FOUND COOLANT INTRUSION IN CYLINDER 3 ITEM DESCRIPTION THIS IS THE ENTIRE PROCESS NEEDED TO EITHER REBUILD OR REPLACE THE VEHICLE'S ENGINE. THIS IS A PROCESS NEEDED WHEN THE VEHICLE'S ENGINE IS IN NEED OF SERIOUS REPAIR. REASON WITHOUT REPLACING OR REBUILDING A DAMAGED ENGINE, THE CAR WILL NOT BE ABLE TO FUNCTION AND WILL BE LEFT USELES

Mileage: 85,900

Aug 4, 2020

WE HAD THE COOLANR RECALL DONE HOPING IT WOULD FIX THE LEAKING COLLANT ISSUE BUT THINGS JUST GOT WORSE I HAVE NOT BEEN ABLE TO DRIVE MY CAR FOR MONTHS DEALER SAYS NEEDS NEW ENGINE

Mileage: 96,000

Aug 4, 2020

AS I WAS TRAVELING ON A CITY STREET AT 30MPH EVERYTHING SEEMED FINE. I STOPPED AT A RED LIGHT. WHILE STOPPED I SUDDENLY HEARD A KNOCKING SOUND NEAR THE FRONT OF THE VEHICLE. WHEN THE LIGHT TURNED GREEN I STARTED TO GO. THE VEHICLE SUDDENLY STALLED. PRIOR, THERE HAD BEEN NO CHECK ENGINE OR WARNING LIGHTS ON. THE VEHICLE WAS UP TO DATE ON ALL REQUIRED MAINTENANCE SERVICES. IT WOULD NOT RESTART. VEHICLES BEHIND ME SOUNDED THEIR HORNS IMMEDIATELY. I PUT MY 4WAY EMERGENCY FLASHERS ON. CALLED A TOW TRUCK. TOW ARRIVED 30 MINUTES LATER. MY VEHICLE AND ME WERE IN A VERY DANGEROUS SITUATION FOR 30 MINUTES, AS CARS AND TRUCKS HAD TO NEGOTIATE AROUND US AT A VERY BUSY CITY INTERSECTION. I WAS NEARLY STRUCK BY ANGRY MOTORISTS WHO WERE BURDENED BY MY BREAKDOWN. I WAS TOLD BY TWO REPAIR SHOPS THAT THERE WAS A CATASTOPHIC INTERNAL ENGINE FAILURE. THE EASIEST AND MOST COST EFFECTIVE PLAN WOULD BE TO REPLACE THE ENGINE. I HAD THE ENGINE REPLACED AT A COST OF $ 4164. THERE WAS 72649 MILES ON THE FAILED ENGINE.

Mileage: 72,663

Aug 3, 2020

ANTIFREEZE COOLANT CONTINUE TO BE LOW, CAR CENTER REPLACED A HOSE ON 1/20/20 FOR 200.00, THEN A WEEK LATER LOW COOLANT AGAIN THE CENTER ASSUME AIR POCKETS WAS THE REASON WITH NO COOLANT LEAKS 2/12/20. I KEPT REPLENISHING COOLANT, JUNE 3RD 2020 WHILE DRIVING ON HIGHWAY, THE TRANSMISSION FAILED, AND IT WAS REPLACE 6/10/20 FOR 4000.00. NOT EVEN ONE WEEK AFTER PICKING THE CAR UP THE LOW COOLANT WITH ENGINE LIGHT WITH ERROR CODES P0012 CAMSHAFT POSITION TIMING OVER-RETARDED BANK 1 AND P0303 CYLINDER 3 MISFIRE DETECTED. WHO IS GOING TO TAKE ON FIXING THIS CAR? I HAVE BEEN REPLACING PARTS AND REPLENISHING FLUIDS WITH NO RESOLUTION.

Mileage: 150,435

Jul 31, 2020

I PURCHASED A 2014 FORD ESCAPE SE 2L ECOBOOST. THE CAR STARTED TO OVERHEAT WHILE DRIVING AND IS LOSING COOLANT. THE VEHICLE WAS PRESSURE TESTED AND THERE ARE NO LEAKS. I TOOK THE CAR TO A FORD DEALERSHIP IN 2020 WITH LESS THAN 15,000 MILES ON THE ENGINE AND WAS TOLD THAT THE ENGINE NEEDS TO BE REPLACED WITH A REBUILT ENGINE FOR MORE THAN $9,000.00. AN ENTIRE ENGINE SHOULD NOT NEED TO BE REPLACED ON A VEHICLE WITH LESS THAN 15,000 MILES. THIS IS CLEARLY A FAULTY/DEFECTIVE ENGINE.

Mileage: 14,563

Jul 27, 2020

WHILE DRIVING I NOTICED THE CAR FELT LIKE IT WAS LOSING POWER, ALMOST LIKE RUNNING OUT OF GAS, THEN A SENSOR WENT OFF SAYING 'ENGINE FAULT SERVICE NOW', THEN I COULD REALLY FEEL THE CAR DRAGGING. I PULLED OVER AND COULD HEAR THE COOLANT BUBBLING, SO I WAITED TIL IT COOLED DOWN AND SAY THERE WASN'T MUCH THERE, I NOTICED A LEAK UNDER THE COOLANT AREA. I TOOK THE CAR IN TO A LOCAL MECHANIC AND WAS TOLD I NEEDED AN ENGINE FLUSH, I GOT THE FLUSH BUT SOON AFTER THE SAME ISSUE WAS REOCCURRING. RANDOMLY NOW IT WILL JUST LOSE POWER AND SENSOR WILL READ THE SAME THING, IT'S SCARY WITH YOUR FAMILY I'M THE CAR AND YOUR LOSING POWER. SO HERE I AM AGAIN BEING TOLD I NEED AN ENGINE FLUSH AGAIN WITHIN THE SAME YEAR. I HAVE SINCE REPLACED THE RESERVOIR BEING THAT IT WASN'T HOLDING COOLANT. WHEN I POUR COOLANT IN IT SEEMS LIKE THE ENGINE IS PULLING IT RIGHT OUT, I'M NOT SURE WHERE IT'S GOING BECAUSE IT'S NOT LEAKING OUT BUT IT'S GOING SOMEWHERE. I CALLED FORD AND WAS TOLD THIS WAS NOT A RECALL ON MY VIN, HOWEVER I HAVE READ MANY COMPLAINTS ON THIS SITE WITH THE SAME ISSUE. I'M HOPING TO CLEAR THIS UP SOME I CAN GET MY VEHICLE IN SAFE CONDITIONS FOR MY FAMILY, AND SO NO ONE GETS HURT.

Jul 15, 2020

2014 FORD ESCAPE WITH 85,000 MILES BEGAN TO ISSUE COOLANT LOW WARNING DESPITE HAVING JUST RECENTLY BEING FILLED RECENTLY. IT SHORTLY AFTER BEGAN TO OVERHEAT AND MISFIRE ON THE FREEWAY ON RAMP. I HAD IT TOWED TO AN INDEPENDENT MECHANIC WHO REGISTERED ABOUT 500 PPM OF EXHAUST GOING INTO THE COOLANT. HE DIAGNOSED IT AS A BROKEN HEAD GASKET AND THAT I POSSIBLE NEEDED AN ENTIRE ENGINE REPLACEMENT. HE ALSO NOTED THERE WAS NO LEAK IN OUR COOLANT.

Mileage: 85,000

Jul 10, 2020

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE REVERSING OUT OF HER DRIVEWAY, THE INSTRUMENT PANEL SHOWED THE ENGINE TEMPERATURE WAS HIGH AND THE VEHICLE STARTED TO JERK. THE CONTACT PULLED OVER AND RESTARTED THE VEHICLE AFTER A FEW MINUTES AND THE WARNING LIGHT DISAPPEARED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC TO BE DIAGNOSED. THE CONTACT WAS INFORMED THAT THE ENGINE TEMPERATURE SENSOR PROVIDED AN INCORRECT ENGINE TEMPERATURE READING. THE MECHANIC REFERRED THE CONTACT TO FAIRWAY FORD (2761 E STONE DR, KINGSPORT, TN 37660, 423-578-3600). THE CONTACT WAS INFORMED THAT THE VEHICLE WAS PREVIOUSLY REPAIRED UNDER NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE VEHICLE WAS REPAIRED AT THE CONTACT'S EXPENSE. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 83,333. *LN *BF THE CONSUMER STATED THERE WAS TRANSMISSION FAILURE AS WELL. *TR

Mileage: 83,333

Jun 25, 2020

IN 2017 I TOOK MY CAR IN TO GET SEVERAL RECALL ITEMS FIXED AND I WAS TOLD THERE WAS A COOLANT ISSUE BUT IT'S OKAY TO DRIVE AND JUST MONITOR THE COOLANT. EARLIER THIS YEAR THE ENGINE LIGHT STARTED TURNING ON AND I WOULD GET A "LOW COOLANT" MESSAGE. DUE TO COVID I DID NOT TAKE THE CAR IN IMMEDIATELY. I ENDED UP HAVING TO FILL THE COOLANT THREE TIMES IN ONE MONTH EVENTUALLY LEADING TO WHITE FUMES COMING OUT THE EXHAUST. WHEN MY CAR FINALLY STALLED IN THE MIDDLE OF AN INTERSECTION DUE TO "LOW COOLANT" (WHICH WE HAD REFILLED 5 DAYS PRIOR) I FINALLY TOOK THE CAR INTO FORD AND THEY IMMEDIATELY KNEW WHAT THE ISSUE WAS AS I PULLED UP SAYING THEY COULD "SMELL IT." SAID I WAS NOT ALLOWED TO DRIVE IT HOME AND IT WAS MOST LIKELY NEEDING TO RESULT IN A NEW ENGINE. IT WAS A COOLANT LEAK THAT COULD RESULT IN THE ENGINE OVERHEATING AND BREAKING DOWN, WHICH WAS TOO DANGEROUS FOR ME TO DRIVE. THE SERVICE GUY SAID THIS WAS ABOUT THE 20TH VEHICLE HE HAD TO DEAL WITH THIS ISSUE ON BUT SAID THEY WEREN'T GOING TO COVER IT. SAID THERE WAS A RECALL ON THIS ISSUE BUT ONLY FOR 2014 ESCAPES MANUFACTURED AT TWO LOCATIONS. I ASKED WHY THOSE TWO WHEN THIS ISSUE SEEMS TO BE HAPPENING WITH SEVERAL VEHICLES AND HE HAD NO ANSWERS. LUCKILY I HAD A WARRANTY THAT COVERED THE NEW $8000 ENGINE BUT WE WERE RESPONSIBLE FOR THE DEDUCTIBLE AND A MAJORITY OF THE RENTAL CAR. IT TOOK 8 WEEKS FOR THEM TO REPLACE THE ENGINE SO THE RENTAL WAS NOT CHEAP. *TR

Mileage: 75,000

Jun 22, 2020

BOUGHT THIS VEHICLE IN 2019 35000 MILES DROVE TO 54000 ,THEN THE DAUGHTER TOOK TO NEVADA WHERE THE LOW COOLANT CAME ON THEN THE VEHICLE TO STOP AND STRAND HER IN THE MIDDLE OF NOWHERE , HAD IT TOWED TO GALLAGHER FORD WHERE THEY INFORMED ME THE #3 CYLINDER HAD ANTI FREEZE IN AND I NEEDED A NEW ENGINE FORD WOULD NOT STAND BY THEIR MOTOR EVEN THOUGH AFTER INSTALLING USED MOTOR AND GETTING THE BILL RIGHT ON THE STATEMENT FROM FORD THIS IS A KNOWN PROBLEM WHERE IT STATES THESE ENGINES HAVE PROBLEMS LEAKING ANTI FREEZE INTO THE ENGINE PER THE PHOTO OF STATEMENT. *TR

Mileage: 54,000

Jun 16, 2020

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE DRIVING AT VARIOUS SPEEDS, THE LOW COOLANT LEVEL MESSAGE DISPLAYED ON THE INSTRUMENT PANEL. THE VEHICLE WAS TAKEN TO SEVERAL INDEPENDENT MECHANIC S HOWEVER, THE MECHANIC WAS UNABLE TO PROVIDE A CAUSE FOR THE FAILURE. THE VEHICLE WAS TAKEN TO JORDAN FORD (609 E. JEFFERSON BLVD, MISHAWAKA, IN 46545) AND THE CONTACT WAS INFORMED THAT ENGINE NEEDED TO BE REPAIRED DUE TO A FAILURE OF CYLINDER #3. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 60,900.

Mileage: 60,900

Jun 15, 2020

DUE TO FAULTY CRACKING COOLANT RESERVIORS THAT I HAVE REPLACED TWICE NOW, PART OF THE MOTOR HAS CRACKED AND NOT ONLY LEAKS OIL, BUT LEAKS COOLANT INTO MY ENGINE, WHERE THE ENGINE BURNS THE COOLANT. SO NOW MY MOTOR IS JUNK. I HAVE HAD NO RECALLS ON THIS VEHICLE BUT MULTIPLE ISSUES THAT FALL UNDER RECALLS FOR OTHER VEHICLES. REASSESSMENTS NEED TO BE MADE. *TR

Mileage: 90,000

Jun 15, 2020

ENGINE COOLANT LEAKED INTO THE 4TH ENGINE CYLINDER CAUSING THE SPARK PLUG TO SEIZE AND BREAK INSIDE THE CYLINDER. LEAK ALSO RUINED THE ENGINE AND NOW ENGINE NEEDS TO BE REPLACED. *TR

Mileage: 112,000

Jun 5, 2020

ENGINE AND ENGINE COOLING: THE VEHICLE STARTED AND DRIVEN WITH AN INSUFFICIENT LEVEL OF COOLANT WITHIN THE ENGINE COOLING SYSTEM, THE ENGINE OVERHEATS AND WILL NOT DRIVE. I FILLED THE COOLANT 50/50 RESERVOIR AT LEAST 2X A WEEK, I JUST BOUGHT MY CAR FROM A DEALERSHIP ON 04/15/2020. *TR

Jun 3, 2020

TRANSMISSION IS FAILING. I'M LITERALLY WAITING FOR IT TO DROP DEAD. WHEN DRIVING, THE VEHICLE HAS MULTIPLE HARD SHIFTS INTO DIFFERENT GEARS. THIS OCCURS NO MATTER WHAT GEAR IT GOES TOO. THE POWER ACTS LIKE IT WANTS TO GIVE UP AND ROCKS THE CAR BACK AND FORTH WHILE ACCELERATING AND SHIFTING GEARS. SOMETIMES THE SHIFT DOESN'T EVEN OCCUR. MOVE THE PRNDL LEVER TOO FAST FROM ANY SETTING, THE CAR MAKES A LOUD JERKING NOISE. ALSO WHEN PARKING ON ANY HILL WITH THE E-BRAKE ON, THE CAR MAKES A VERY LOUD NOISE SOUNDING LIKE THE BRAKES ARE GOING TO GIVEAWAY AND THE CAR MOVES. ITS BARELY NOTICEABLE, BUT I SAT IN THE CAR TO TEST IT , AND WHILE SITTING IN THE CAR YOU COULD TOTALLY TELL IT MOVED. IT DOES THIS 3 TIMES MINIMUM WHEN PARKED. *TR

Mileage: 87,000

Jun 2, 2020

FOR THE PAST 6 MONTHS (APPROXIMATELY) MY CAR HAS BEEN EXPERIENCING ANTIFREEZE LEAKS. MY VEHICLE HAS ROUGHLY 71,850 MILES AND IT IS A 2014 FORD ESCAPE. ABOUT ONCE A MONTH MY INFO LIGHTS COMES ON SIGNALING MY ENGINE COOLANT IS LOW. I HAVE TAKEN IT TO A COUPLE LOCATIONS AND NO ONE CAN FIND A LEAK. IN FEBRUARY THE MECHANIC SUGGESTED I REPLACE THE CAP IN CASE IT IS EVAPORATING. I REPLACED THE CAP END OF APRIL AND ONCE AGAIN IN MAY THE LIGHT CAN BACK ON. I FILL THE COOLANT TO THE MAX LINE, BUT AFTER A MONTH IT IS AT THE MIN LINE OR SOMETIMES LOWER. I SAW THERE ARE NO RECALLS ON MY VEHICLE, BUT THIS SEEMS TO BE A SERIOUS ISSUE AS MY CAR CAN FAIL WHILE I AM DRIVING AROUND WITH MY INFANT CHILD IN THE CAR. NO MECHANIC CAN SEEM TO HELP ME. *TR

May 19, 2020

PURCHASED 3/28/20, MILEAGE 78,277; 4/8/20 VEHICLE STALLED PULLING OUT OF DRIVEWAY AFTER WARNING LIGHT INDICATED "COOLANT LOW," "STOP SAFELY" - VEHICLE STOPPED ITSELF AND WOULD NOT RESTART; 4/9/20 LEFT VEHICLE AT FORD DEALER SERVICE DEPT.; 4/13/20 DIAGNOSED WITH BLOWN HEAD GASKET DUE TO COOLANT LEAKAGE, ENGINE REPLACEMENT REQUIRED; 4/23/20 INFORMED THAT ENGINE WAS ON BACK ORDER; 5/18/20 5 PM, (OVER 1 MONTH LATER) REPAIRS COMPLETED, PICKED UP FROM DEALERSHIP; DROVE APPROX 3 MI., STOPPED FOR 10 HRS; 5/19/20 3:30 AM, DROVE APPROX 10 MILES, STOPPED FOR 1/2 HR; DROVE OFF FROM 2ND STOP, VEHICLE STALLED WITHIN 3 MILES AFTER WARNING LIGHT INDICATED "COOLANT LOW," "STOP SAFELY," AND TEMP GAUGE MAXED OUT ON HOT, VEHICLE DIED AND WOULD NOT RESTART, LEAVING ME STRANDED ON THE SIDE OF A RURAL HIGHWAY AT 4 IN THE MORNING. OPENED HOOD JUST IN TIME TO SEE REMAINING COOLANT DRAINING FROM RESERVOIR. ALTHOUGH I HAVE A NEW, UNOPENED JUG OF COOLANT, LOCATION OF THE RESERVOIR REQUIRES A FUNNEL TO ADD COOLANT !!! - (CAR DOES NOT COME EQUIPPED WITH FUNNEL AND OWNER'S MANUAL FAILS TO MENTION THIS!) CAUGHT A RIDE WITH SHERIFF'S UNIT THAT JUST HAPPENED TO BE PASSING BY. 5/19/20 VEHICLE BEING TOWED BACK TO SERVICE DEPT.; CURRENT MILEAGE 79,079. *TR

Mileage: 79,079

May 19, 2020

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE ACCELERATING FROM A STOP, THE VEHICLE HESITATED AND SPUTTERED BEFORE DRIVING AS DESIGNED. DURING THE FAILURE, THE MESSAGE ENGINE FAULT DISPLAYED ON THE INSTRUMENT PANEL. THE CAUSE OF THE FAILURE WAS NOT DETERMINED. THE LOCAL DEALER PHIL LONG FORD LOCATED AT 7887 W TUFTS AVE, LITTLETON, CO 80123 AND MANUFACTURER WERE NOTIFIED OF THE FAILURE BUT NO ASSISTANCE WAS OFFERED. THE FAILURE MILEAGE WAS 65,000.

Mileage: 65,000

May 8, 2020

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE HER SON WAS DRIVING AT 40 MPH, SEVERAL UNKNOWN WARNING LIGHTS ILLUMINATED. THE CONTACT WAS INFORMED VIA AN APP ON HIS CELLPHONE TO PULL OVER AND STOP THE VEHICLE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE VEHICLE OVERHEATED AND CAUSED THE ENGINE TO CRACK. THE TECHNICIAN ALSO STATED THAT THE TRANSMISSION NEED TO BE REPAIRED. THE VEHICLE WAS TAKEN TO GENE MESSER FORD (6000 WEST 19TH, LUBBOCK, TX 79407, (806) 788-2222) WHERE THE TECHNICIAN CONFIRMED THAT THE ENGINE BLOCK WAS CRACKED AND NEEDED TO BE REPLACED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED HOWEVER, THE SAME DEALER REPURCHASED THE VEHICLE. THE FAILURE MILEAGE WAS APPROXIMATELY 80,000. *BF*JB

Mileage: 80,000

Apr 24, 2020

MY 2014 FORD IS LEAKING ENGINE COOLANT INTO MY ENGINE AS WELL AS OIL. WHICH IS CAUSING MY CAR TO DECREASE IN ACCELERATION AND HAS CAUSED MY CAR TO STALL ON CITY STREET. I TOOK MY CAR TO A FORD DEALERSHIP AND THEY MADE IT WORST BY NOT RECOGNIZING THAT THIS WAS A PROBLEM CONCERNING A RECALL ON FORD AND REFUSES TO FIX MY CAR.

Mileage: 103,013

Apr 11, 2020

1ST ISSUE IS THE CAR STALLS RANDOMLY AND WARNING STATES, 'SERVICE ENGINE SOON,' WITH NO CODES THROWN. IT HAS HAPPENED WHILE MOVING AND AT A STOP LIGHT. IT WILL START BACK UP AFTER SITTING FOR 5 MINUTES. HAPPENS EVERY COUPLE MONTHS. THE OTHER ISSUE IS THE TRANSMISSION SHUTTERS BETWEEN FIRST AND SECOND GEAR AND ALSO BETWEEN 2ND AND 3RD GEAR. DEALERSHIP CANNOT FIND ANY ISSUES FOR EITHER ISSUE.

Mileage: 60,000

Apr 1, 2020

MY 2014 FORD ESCAPE HAD A RECALL PERFORMED RECENTLY 17S09 COOLANT LEVEL SENSOR SYSTEM, BEFORE THIS RECALL WAS PERFORMED ON MY VEHICLE, MY VEHICLE WAS PERFECTLY FINE, I'VE ONLY HAD ISSUES WITH THE REAR DOOR LATCH, THAT WAS BROKEN ( ALSO A RECALL) AND FOR THIS REASON IS WHY MY VEHICLE WAS TAKEN TO THE FORD SERVICE DEPARTMENT. IT WAS THEN, WHEN THE SERVICE TECH RECOMMENDED TO HAVE THE COOLANT LEVEL SENSOR SYSTEM REPLACED PER THE RECALL. SINCE THEN, MY VEHICLE HAS NOT BEEN THE SAME, THE VEHICLE HAS BEEN BACK TO THE SERVICE DEPARTMENT WITH THE SAME ONGOING COMPLAINT ,THE ENGINE LIGHT RECENTLY CAME UP ALERTING THAT MY VEHICLE WAS OVERHEATING, THOU THE VEHICLE WAS SITTING IN MY WORK PARKING LOT FOR 10 HRS. THE VEHICLE WAS TAKEN BACK TO THE SERVICE DEPARTMENT, AND AFTER 2 DAYS, I WAS INFORMED THAT THE TECH FOUND COOLANT IN MY ENGINE, THEREFORE, MY VEHICLE WOULD NEED A NEW ENGINE. MY VEHICLE WAS PERFECTLY FINE BEFORE THE SERVICE DEPARTMENT BEGAN PERFORMING THE RECALL UPGRADES. THIS IS THE FAULT OF THE SERVICE DEPARTMENT FOR LACKING KNOWLEDGE ON HOW TO PROPERLY INSTALL THE RECALL COMPONENTS, FAILED TO MITIGATE FUTURE DAMAGE TO MY ENGINE. IN MY RESEARCH, I FOUND THAT FORD IS AWARE OF THIS ISSUE AND HAS FAILED TO PROPERLY COMPENSATE THE CONSUMER OR PROTECT THE CONSUMER FROM THIS LOSS.

Mileage: 88,700

Mar 12, 2020

MY 2014 FORD ESCAPE OVERHEATED AS A RESULT OF A CRACK IN THE COOLANT DEGAS BOTTLE. THERE WAS NO INDICATION OF LOW COOLANT LEVEL PRIOR TO THE INCIDENT. FORD REPLACED THE DEGAS BOTTLE TO CORRECT THE PROBLEM AND I PAID THE WARRANTY DEDUCTIBLE. UPON INVESTIGATION, I DISCOVERED RECALL 17S09 WHICH IS PERTINENT TO A LOW COOLANT WARNING SYSTEM ISSUE. ACCORDING TO THE DOCUMENT, MY 2014 FORD ESCAPE, BUILT IN LOUISVILLE IN MAY OF 2014 IS ONE OF THE AFFECTED VEHICLES. (PLEASE SEE ATTACHMENT) I HAVE TWO CONCERNS. FIRST AND FOREMOST, MY VEHICLE HAS EXPERIENCED OVERHEATING WITH ALMOST NO WARNING OF A LOW COOLANT CONDITION. I BELIEVE THERE SHOULD HAVE BEEN WARNING OF A LOW COOLANT SITUATION PRIOR TO THE EVENT, INDICATING THE CORRECTIONS TO THE SYSTEM PER 17S09 MAY BE NECESSARY TO PREVENT DAMAGE TO MY VEHICLE'S ENGINE. SECOND, I PAID FOR A REPAIR UNDER MY EXTENDED WARRANTY THAT SHOULD HAVE BEEN INCLUDED WITHIN THE SCOPE OF 17S09. THE FORD DEALERSHIP TOLD ME THEY CANNOT COMPLETE THIS RECALL UNLESS NOTIFIED BY FORD MOTOR COMPANY. CAN YOU PLEASE INVESTIGATE THIS CONCERN? MY EXTENDED WARRANTY WILL EXPIRE IN JUNE.

Mileage: 40,555

Mar 9, 2020

CAC TUBING, BAND CLAMP AROUND TURBO BURNED WITH INDICATIONS OF OIL LEAKS AT EXHAUST. NEED TURBO REPLACEMENT.

Mar 6, 2020

COOLANT LIGHT COMES ON THAN CAR SHUTS DOWN. NOT ABLE TO GO OR STEER

Mileage: 62,000

Mar 5, 2020

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE DRIVING AT 60 MPH, THE COOLANT GAUGE INDICATED THAT VEHICLE WAS RUNNING HOT. A WARNING LIGHT ALSO ILLUMINATED ON THE DASHBOARD INFORMING THE CONTACT TO PULL OVER. THE CONTACT PULLED OVER AND HAD THE VEHICLE TOWED TO SILL-TERHAR MOTORS SERVICE LOCATED AT (150 ALTER ST, BROOMFIELD, CO 80020) WHERE THE VEHICLE WAS DIAGNOSED WITH A DEFECTIVE COOLANT BLOCK. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE BUT OFFERED NO ASSISTANCE. THE FAILURE MILEAGE WAS 144,000.

Mileage: 144,000

Feb 25, 2020 Fire

VEHICLE CAUGHT FIRE SOMEWHERE IN THE ENGINE DUE TO A RECALL ISSUE (OVERHEATING OF THE ENGINE CYLINDER HEAD, ETC.). FORD METRO MOTORS AT #405 ESTATE ANNAS RETREAT, ST. THOMAS, VI 00802 DID NOT AND WON'T FIX THE VEHICLE WITHOUT PAYMENT FROM ME AS THE VEHICLE OWNER. THE VEHICLE HAS BEEN AT THAT ESTABLISHMENT SINCE JUNE 2019. I'VE BEEN SENT MULTIPLE ESTIMATES AND SERVICE REPORTS THAT ARE NOT FACTUAL AND THE ESTABLISHMENT DOES NOT WANT TO TAKE RESPONSIBILITY FOR THIS VEHICLE FIRE.

Mileage: 100,000

Feb 24, 2020

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE DRIVING AT 70 MPH, THE LOW COOLANT LEVEL WARNING LIGHT AND THE CHECK ENGINE WARNING LIGHT ILLUMINATED AND THE VEHICLE LOST MOTIVE POWER. THE CONTACT WAS ABLE TO RESTART THE VEHICLE HOWEVER, THE FAILURE PERSISTED. CHRIS AUFFENBERG LINCOLN LOCATED AT 5840 MO-100, WASHINGTON, MO 63090, WAS CONTACTED AND MADE AWARE OF THE FAILURE. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC TO BE DIAGNOSED. THE CONTACT WAS INFORMED THAT THE TRANSMISSION NEEDED TO BE REPLACED. THE VEHICLE WAS THEN TOWED TO A DIFFERENT INDEPENDENT MECHANIC AND REPAIRED. THE CONTACT STATED THAT THE FAILURE RECURRED AFTER THE VEHICLE WAS REPAIRED. THE CONTACT WAS THEN INFORMED THAT THE TRANSMISSION CONTROL MODULE SOFTWARE NEEDED TO BE UPDATED. THE CONTACT STATED THAT AFTER THE SOFTWARE UPDATE WAS PERFORMED, THE COOLANT WARNING LIGHT ILLUMINATED. THE CONTACT ALSO BECAME AWARE OF A COOLANT LEAK. THE VEHICLE WAS TAKEN BACK TO THE SAME DEALER WHERE THE MECHANIC REPLACED THE TRANSMISSION COOLER ASSEMBLY HOWEVER, THE FAILURE PERSISTED. THE MANUFACTURER WAS CONTACTED AND INFORMED OF THE FAILURE. THE FAILURE MILEAGE WAS 93,000.

Mileage: 93,000

Feb 23, 2020

WHILE DRIVING, MY VEHICLE SUDDENLY SHOWS A LOW COOLANT THAN ENGINE OVERHEAT MESSAGE. IT IMMEDIATELY BEGINS TO SHUT DOWN, SPEED RAPIDLY DECREASES AND POWER STEERING IS LOST. I MUST STOP THE CAR, PLACE IT IN PARK, SHUT IT OFF, WAIT A FEW MINUTES THAN RESTART IT. SERVICE ENGINE LIGHT REMAINS ON. THE VEHICLE WAS TRAVELING BETWEEN 55 AND 65 MPH ON THE MAJOR FREEWAY WHERE THE POSTED SPEED LIMIT IS UP TO 70 MPH, 3 LANES OF TRAFFIC. SINCE THE LOSS OF POWER IS IMMEDIATE AND I HAVE NO CONTROL OVER IT, I HAVE VERY LITTLE TIME TO GET OUT OF THE WAY OF OTHER VEHICLES BEFORE I AM IN CRAWL MODE. THE VEHICLE WAS JUST INTO THE DEALERSHIP FOR REPAIRS AND I WAS TOLD IT WAS FIXED. COOLANT IS NOT LOW, ENGINE HAD NOT OVERHEATED AND THERE IS NO WARNING THAT THERE IS AN ISSUE UNTIL 30 SECONDS BEFORE IT STARTS SHUTTING DOWN. HAS HAPPENED TWICE NOW AND IT WAS SUPPOSEDLY FIXED AFTER THE FIRST TIME. MY VEHICLE HAS NO OPEN RECALLS AND IT HAS BEEN INTO THE DEALERSHIP TWICE IN THE PAST 2 WEEKS WITH REGARDS TO THE OVERHEAT ISSUE.

Mileage: 81,000

Feb 21, 2020

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED WHILE SHE WAS DRIVING AT APPROXIMATELY 35 MPH, SHE HEARD AN ABNORMAL NOISE COMING FROM THE ENGINE. THE CONTACT STATED SHE MANAGED TO SAFELY PULL OVER THE VEHICLE AND WHEN SHE LIFTED THE HOOD SHE SAW WHITE SMOKE COMING FROM THE COOLANT. THE VEHICLE WAS TOWED TO A LOCAL MECHANIC. THE MECHANIC STATED THE VEHICLE DID NOT HAVE ANY COOLANT AND THAT CAUSED THE ENGINE TO OVER HEAT. HOWEVER A FEW DAYS LATER, THE VEHICLE WAS TOWED TO A LOCAL DEALER (SUTTON FORD 21315 CENTRAL AVE, MATTESON, IL 60443) FOR A DIAGNOSIS. THE DIAGNOSIS WAS DETERMINED THAT THE ENGINE WAS "LOCKED UP AND THE RECALL WAS NOT ASSOCIATED WITH THE FAILURE. THE CONTACT ALSO STATED THAT THE DEALER INFORMED HER IF A FULL DIAGNOSTIC EXAM WAS PERFORMED SHE WOULD BE RESPONSIBLE. THE VEHICLE PREVIOUSLY HAD A REPLACED ENGINE 13 MONTHS PRIOR. THE MANUFACTURER CONFIRMED THE INFORMATION THE DEALER STATED BUT OFFERED NO ASSISTANCE. THE APPROXIMATE FAILURE MILEAGE WAS 155,000.

Mileage: 155,000

Feb 20, 2020

DON'T RUNNING

Feb 15, 2020 Fire

DRIVING DOWN ROAD. CAR SAID ENGINE FAILURE PULLED OVER POPED THE HOOD AND ENGINE CAUGHT ON FIRE AND CAR BURNED TOTAL LOSS

Mileage: 3

Feb 15, 2020

CAR STALLS AFTER STARTING AND DRIVING A SHORT DISTANCE. WILL RESTART AND PERFORM OK. USUALLY HAPPENS AFTER CAR HAS BEEN DRIVEN THEN PARKED FOR A SHORT AMOUNT OF TIME (LIKE RUNNING INTO A STORE) THEN STALLS AFTER DRIVEN SHORT DISTANCE.

Mileage: 68,000

Feb 4, 2020 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THE VEHICLE THE CONTACT STATED THAT WHILE DRIVING AT 40 MPH IN 2017, THE VEHICLE LOST LEAKED COOLANT AND LOST POWER. THE CHECK ENGINE LIGHT ILLUMINATED. THE VEHICLE WAS PULLED OVER AND THE CONTACT NOTICED FIRE FROM THE ENGINE. THE CONTACT WENT TO LOOK FOR FIRE EXTINGUISHER AND WHEN HE CAME BACK, THE FIRE EXTINGUISHED BY ITSELF. THE VEHICLE WAS TOWED THE TROPHY FORD DEALER, LOCATED AT 288 HAROLD G CLARKE PKWY, FORSYTH, GA 31029 WHERE IT WAS DIAGNOSED THAT THE VEHICLE WAS OUT OF COOLANT. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND SENT INVESTIGATORS TO EVALUATE THE VEHICLE. THE ENGINE WAS REPLACED. THE CONTACT LATER RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING) THE VEHICLE WAS TAKEN TO THE FIVE STAR FORD LINCOLN OF WARNER ROBINS DEALER, LOCATED AT 900 RUSSELL PWKY, WARNER ROBINS, GA 31088 WHERE THE RECALL WAS REPAIRED. THE CONTACT STATED THAT WHEN THE VEHICLE WAS STARTED, THE VEHICLE SHOOK AND WAS TAKEN BACK THE DEALER WHO PERFORMED THE RECALL. THE TECHNICIAN DIAGNOSED 'A CATASTROPHIC ENGINE FAILURE' AND TOPPED THE COOLANT. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE ISSUE AND THE CONTACT WAS NOT CALLED BACK. THE FAILURE MILEAGE WAS APPROXIMATELY 58,000.

Mileage: 58,000

Feb 4, 2020

A LACK OF COOLANT CIRCULATION CAUSED THE ENGINE TO OVERHEAT, RESULTING IN A CRACKED CYLINDER HEAD. VEHICLE WAS IN MOTION IN A CITY. VEHICLE IS IN THE SHOP AND I JUST BOUGHT IT 1 YEAR AGO. I STILL OWE AND DO NOT HAVE THE MONEY TO REPAIR. I HAVE 2 SMALL CHILDREN AND OUR LIFE IS IN TURMOIL BECAUSE OF THIS.

Mileage: 86,000

Jan 24, 2020

THE AUTO CONTINUES TO STALL IN LOW IDLE

Mileage: 80,000

Jan 23, 2020

ENGINE COOLANT KEEPS EVAPORATING/LEAKING OUT

Jan 20, 2020

VEHICLE ENGINE STARTED TO REACH HIGH TEMPERATURE LEVELS WHILE DRIVING AND A NOTIFICATION TO STOP THE VEHICLE DUE TO HIGH TEMPERATURES. CAN ONLY DRIVE FOR 10-15 MINS BEFORE THIS HAPPENS. A PROFESSIONAL MECHANIC PERFORMED A DIAGNOSTIC TEST AND A RECALL CAME BACK FOR 2014 FORD ESCAPE - COOLANT LEVEL SENSOR SYSTEM INSTALLATION.IN THE AFFECTED VEHICLES, A LACK OF COOLANT CIRCULATION COULD CAUSE AN ENGINE TO OVERHEAT, RESULTING IN A CRACK IN THE CYLINDER HEAD. A CRACKED CYLINDER HEAD CAN RESULT IN A PRESSURIZED OIL LEAK. OIL THAT COMES INTO CONTACT WITH A HOT ENGINE SURFACE INCREASES THE RISK OF A FIRE IN THE ENGINE COMPARTMENT.

Mileage: 89,000

Jan 17, 2020

MY CAR HAD A CHECK ENGINE LIGHT COME ON WHEN I TURNED IT ON ONE DAY. IT WAS ON THE WEEKEND SO I HAD TO WAIT UNTIL MONDAY TO GET DIAGNOSTICS AT MY LOCAL DEALER. THE CAR STARTED TO RUN REALLY ROUGH AND WAS SLIPPING. I TOOK IT TO MY LOCAL FORD DEALER AND THEY TOLD ME THAT MY HEAD GASKET WAS BLOWN AND LEAKING ANTIFREEZE EVERYWHERE. I AM CURRENTLY AWAITING TO SEE IF THE HEAD IS CRACKED TO WHICH I'M TOLD IS COMMON WITH THIS ISSUE AND THIS CAR. THERE WAS A RECALL FOR THIS IN THE SAME YEAR MY CAR WAS MADE, HOWEVER, MY CAR WAS NOT INCLUDED INTO THIS RECALL IN IS NOW MY RESPONSIBILITY FINANCIALLY TO FIX THIS.

Mileage: 117,000

Jan 17, 2020 Fire

THE VEHICLE WAS BEING DRIVEN AND HAD ONLY BEEN STARTED AND MOVING FOR LESS THAN 5 MINUTES. NOTICED THAT WINDSHIELD WIPERS WOULD NOT SHUT OFF OR CHANGE SPEEDS, THEN NOTICED A SLIGHT ODOR IN CAR THAT INCREASINGLY STRENGTHENED. PHONED MY HUSBAND WHILE AT A STOP LIGHT, ODOR OF SOMETHING BURNING BECAME MUCH STRONGER, THEN NOTICED SMOKE COMING BETWEEN THE THE DRIVERS SIDE HOOD SEAM AND BETWEEN THE HOOD AND THE WINDSHIELD, THIS WAS IMMEDIATELY FOLLOWED BY NOTICABLE FLAME. I PUT THE VEHICLE IN PARK, TURNED ON HAZARD LIGHTS AND EXITED THE VEHICLE. LOCAL POLICE AND FIRE DEPARTMENT RESPONDED, BEGAN WITH SMALL FIRE EXTINGUISHERS, WITHOUT SUCCESS AND FIRE DEPARTMENT OPENED HOOD AND APPLIED WATER TO EXTINGUISH. THIS WAS ON A CITY STREET IN O'FALLON, MO. UNCERTAIN OF CAUSE, BUT AM NOW AWARE THAT FORD ISSUED A RECALL ON THIS MODEL (RECALL 17S09) AND BELIEVE THIS COULD BE A POSSIBILITY.

Mileage: 61,000

Jan 16, 2020

COOLANT DISAPPEARING

Mileage: 89,300

Jan 7, 2020

DRIVING OUR ESCAPE, WITH 58,800 MILES, ON A ROAD TRIP HAD CHECK ENGINE LIGHT COME ON. WE DROVE IT TO A CLOSE REPAIR SHOP AND FOUND OUT COOLANT LEAKED INTO HEAD GASKET #3 CAUSING OVER HEATING DAMAGE AND REPLACEMENT OF CYLINDER HEAD WOULD BE REQUIRED. FORD DEALER WOULD NOT HELP REPAIR OR REPLACE OR EVEN DIAGNOSE. RECALL FIX 17S09 (NHTSA 17V-209) DID NOT FIX THE POTENTIAL DANGER OR DAMAGE. THE COOLANT LEAK STILL HAPPENED CAUSING ENGINE FAILURE AND A WORTHLESS CAR AT 58,800 MILES.

Mileage: 58,800

Jan 7, 2020

MY BATTERY DIED. IT WAS JUMPED AND WORKING, BUT THE CAR WAS NOT DRIVABLE BECAUSE THE 'HOT ENGINE' MESSAGE WAS ON. IT WAS TOWED TO FIRESTONE. THEY PUT A NEW BATTERY IN, BUT THE 'HOT ENGINE ' LIGHT WAS STILL ON. I FOUND A RECALL ABOUT THE COOLANT SYSTEM ON THE INTERNET. 17S09. THE CAR WAS TOWED TO HUNTERSVILLE FORD DEALERSHIP. THEY HAVE HAD IT FOR 24 HOURS AND HAVE NOT CALLED OR RETURNED MY CALLS.

Mileage: 40,000

Jan 3, 2020

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING APPROXIMATELY 30 MPH, THE VEHICLE UNEXPECTEDLY DECELERATED. THE CONTACT OBSERVED SMOKE COMING FROM THE VEHICLE AND PULLED OFF THE ROAD. THE VEHICLE WAS TOWED TO TEAM FORD LINCOLN, INC. (1813 4TH AVE S, DENISON, IA 51442) WHERE IT WAS DIAGNOSED THAT THE CYLINDER HEAD HAD A CRACK. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED. THE CONTACT REFERENCED NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE). THE FAILURE MILEAGE WAS 104,000.

Mileage: 104,000

Dec 28, 2019

THE ENGINE SUDDENLY DOWN DIES WHILE DRIVING SEVERAL TIMES IN THE PAST FEW MONTHS.

Mileage: 20

Dec 27, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING AND PULLING INTO A PARKING SPOT, THE VEHICLE SHUT OFF AND WAS TOWED TO THE CONTACT'S HOME. THE FOLLOWING DAY, THE CONTACT ATTEMPTED TO DRIVE THE VEHICLE, BUT IT SHUT OFF AGAIN. THE VEHICLE WAS TAKEN TO CROSSROADS FORD OF PRINCE GEORGE (4500 WHITEHILL BLVD, PRINCE GEORGE, VA 23875, (877) 331-9405). THE CONTACT WAS ADVISED TO USE ROLLING STOPS TO AVOID THE VEHICLE SHUTTING OFF. THE VEHICLE SHUT OFF IN THE DEALER'S PARKING LOT. THE DEALER REPLACED THE OXYGEN SENSORS AFTER PERFORMING A SMALL TEST DRIVE. IT WAS DIAGNOSED THAT THE TRANSMISSION NEEDED TO BE REPLACED. THE VEHICLE REMAINED AT THE DEALER FOR ALMOST TWO WEEKS. THE TOTAL COST FOR THE REPAIRS WAS OVER $4,200. THE VEHICLE WAS CURRENTLY AT THE DEALER AWAITING REPAIRS. THE FAILURE MILEAGE WAS 79,000. THE VIN WAS INVALID.

Mileage: 79,000

Dec 20, 2019 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT INTERMITTENTLY SMELLED A BURNING ODOR COMING FROM THE VENTS INSIDE THE VEHICLE. WHILE THE VEHICLE WAS UNDERGOING AN INSPECTION, THE CONTACT WAS INFORMED THAT THE CHECK ENGINE WARNING INDICATOR WAS ILLUMINATED AND THE TURBO ENGINE WAS NOT READING THE CORRECT CODE, WHICH CAUSED THE VEHICLE TO FAIL INSPECTION. THE CONTACT CALLED HERB CHAMBERS FORD OF BRAINTREE (LOCATED AT 75 GRANITE STREET RTE 37, BRAINTREE, MA 021847, 781-848-1350) AND WAS INFORMED THAT THE VEHICLE WAS NOT INCLUDED IN A RECALL AND THEY WERE NOT SURE IF IT WAS INCLUDED IN A WARRANTY. THE VEHICLE HAD NOT BEEN DIAGNOSED OR REPAIRED BY THE DEALER. THE MANUFACTURER WAS NOT NOTIFIED. THE APPROXIMATE FAILURE MILEAGE WAS 80,000.

Mileage: 80,000

Dec 18, 2019 Fire

CURRENT ISSUE IS HEAD GASKET OVERHEATED AND BLEW. COOLANT IS INTERNALLY LEAKING INTO THE ENGINE. CAR BLOWS OUT A TON OF EXHAUST WHILE DRIVING AND HAS THE SMELL OF COOLANT IN IT. I CAN'T EVEN DRIVE ON THE HIGHWAY ANYMORE BECAUSE THE CAR OVERHEATS AND LIMITS MY SPEED TO 45 MPH. SOMETIMES I HAVE TO PULL OVER JUST TO LET IT COOL DOWN. EVERY TIME THE CAR STARTS UP IT VIBRATES SO MUCH THAT ITS QUITE ANNOYING. SOMETIMES THE CAR SHUTS OFF RIGHT AFTER I START IT IN THE MORNING, RIGHT AFTER A CRAZY BURST OF VIBRATION. A LITTLE OVER A MONTH AGO I STARTED MY CAR AND IT VIBRATED SO MUCH AND THEN SO MUCH OIL LEAKED FROM MY CAR, EXHAUST BLEW OUT DARK BLACK SMOG AND SMOKE WAS COMING FROM MY HOOD. CAR IS REALLY LOUD ON IDLE, NEVER BEEN IN A CAR SO LOUD WITH SO MUCH VIBRATION ALL THROUGHOUT THE CAR. CAR CONSTANTLY OVERHEATS AND HAS NO POWER WHEN DRIVING. CAR VIBRATES INSANELY WHEN I'M IDLE AT A RED LIGHT. CHECK ENGINE LIGHT GOES ON AND OFF EVERY OTHER DAY. MY MECHANIC HAS DONE RESEARCH ON THE CAR AND SAYS TO GET RID OF IT, IT'S NOT EVEN WORTH FIXING; HE SAYS YOU'LL END UP SPENDING JUST AS MUCH MONEY FIXING THIS IN THE LONG RUN THAN JUST BUYING A NEW CAR. MY MECHANIC SAID FIXING THE HEAD GASKET WONT SOLVE YOUR PROBLEM, YOU NEED AN ENTIRE NEW ENGINE AND CYLINDER BLOCK. WE'VE BEEN DOING A LOT OF RESEARCH ON THIS CAR/MODEL AND EVERYONE'S HAVING THE SAME ISSUES AND CAN'T REALLY GET DOWN TO THE BOTTOM LINE ON WHAT'S WRONG WITH THE VEHICLE. I'M CURIOUS IF EVERYONE HAS THE SAME PROBLEM WITH THIS CAR/MODEL THAT THERE'S NO MAJOR RECALL ON IT. INSTEAD PEOPLE ARE DRIVING AROUND WITH A LOUD CAR THAT CONSTANTLY VIBRATES, LEAKS COOLANT INTO THE ENGINE AND HAVING TO CONSTANTLY TAKE IT TO THE SHOP.

Mileage: 88,000

Dec 12, 2019 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE THE CONTACT'S HUSBAND WAS DRIVING 40 MPH, THE "ENGINE FAILURE" WARNING MESSAGE ILLUMINATED ON THE INSTRUMENT PANEL. THE DRIVER SMELLED AND OBSERVED SMOKE EMITTING FROM THE HOOD. A FIRE OCCURRED UNDER THE HOOD AND THE DRIVER WAS ABLE TO LOCATE A FIRE EXTINGUISHER AND PUT OUT THE FLAMES HIMSELF. THERE WERE NO WARNING INDICATORS ILLUMINATED. THE VEHICLE WAS NOT ABLE TO BE DRIVEN. THE VIN WAS INCLUDED IN NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE VEHICLE WAS TOWED TO SONJU ALL AMERICAN SUPERSTORE (LOCATED AT 893 SCENIC DR, TWO HARBORS, MN 55616, (218) 834-2101) WHERE IT WAS DIAGNOSED THAT THE ENGINE NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED. THE FAILURE MILEAGE WAS 73,589.

Mileage: 73,589

Nov 22, 2019

2 MONTHS AGO, MY CAR DIED IN AS I WAS EXITING THE INTERSTATE. TRANSMISSION ISSUES - REPAIRED AFTER 2 MONTHS. DROVE IT OUT OF TOWN AND SECOND DAY BEING OUT OF TOWN ENGINE LIGHT ON. BROUGHT IT BACK TO MECHANIC AND TRANSMISSION MECHANIC SAID THERE WAS NO TRANS CODE PRESENT, BUT FOLLOWING CODES PRESENT P1116 AND P0234. UNABLE TO DRIVE CAR AGAIN UNTIL LIGHT ENGINE LIGHT IS OFF AND THIS REPAIR IS OUT OF POCKET AGAIN.

Mileage: 104

Nov 21, 2019

ENGINE COOLANT LEVEL CONTINUES TO DROP IN RESERVOIR. VEHICLE WAS PURCHASED NEW AND MAINTAINED PER FORD. COOLANT HAS BEEN ADDED TWICE AT DEALERSHIP ALTHOUGH COOLANT SYSTEM IS REPUTEDLY SEALED. THIS VEHICLE WAS NOT UNDER FORD'S EARLIER RECALL. CAR IS USED IN NORMAL DRIVING CONDITIONS (HIGHWAY, AROUND TOWN).

Mileage: 80,700

Nov 12, 2019

MY 2014 FORD ESCAPE WITH THE 1.6L ECOBOOST HAS A SAFETY RECALL FOR CRACKING OF THE CYLINDER HEAD, THERE FIX FOR THIS ONLY TO PLACE A COOLANT SENSOR IN THE COOLANT RESERVOIR. SO I HAD THE RECALL INSTALLED, NOT LONG AFTER I STARED HAVING ISSUES WITH LOSSING COOLANT. NEXT IF STARED MISSING WELL I TOOK IT IN AND THE DEALER SAID "YOU HAVE A CRACKED ENGINE BLOCK" WHEN ASK TO PROVE THE BLOCK WAS CRACKED THEY COULD NOT, AND THE DEALER ALSO TOLD ME THAT, "THEY HAVE TO REPLACE THE ENGINE EVEN IF ITS ONLY A HEAD" SO FORD IS MAKING TO WHERE THE COSTUMER IS RESPONSABLE FOR REPLACING THE ENGINE. THEN AFTER I GOT MY CAR BACK 2 MONTHS LATER, MY STREERING HAD A CATCH OCCASIONALLY THEN STARTED LOCKING UP COMPLETELY AND HAPPEND TO BE STATIONARY OR VERY LOW SPEEDS WHEN IT DID LOCK UP. SO I TAKE IT BACK TO FORD DEALER AGAIN THEY SAY I HAVE TO PAY FOR EVERY THING SO WHEN I GO TO DO THE WORK MYSELF I DESCOVIORED THEY COMPLETLY LEFT OF THE SHROUD UNDER THE CAR THAT CHANNALS COLD AIR BETWEEN THE EXHUST AND ELECTRONIC STEERING GEAR. SO TOOK IT BACK AND MADE THE DEALER REPLACE THE PART. THE DEALER TOLD ME THIS IS A COMON PROBLEM. THIS IS DEFENTLEY A SAFETY ISSUE THAT NEEDS ADDRESSED!!!

Mileage: 98,000

Nov 11, 2019

MY VEHICLE STARTED TO OVERHEAT AND SMOKE UP. A MECHANIC LOOKED AT THE VEHICLE AND THOUGHT IT WAS THE VACUUM PUMP OR SOMETHING CLOSE TO THAT NAME. I CAN FILL UP MY COOLANT TO THE MAX LINE AND DRIVE AND BE EMPTY WITHIN MINUTES. THEN I NOTICED A RECALL FOR FORD ESCAPES CONCERNING A COOLANT PROBLEM AND I AM WORRIED. THIS VEHICLE IS BRAND NEW TO ME (ONLY 2 YEARS) AND STILL UNDER 6 YEARS OLD. I AM AFRAID THAT MY VEHICLE WILL COMBUST WITH MY KIDS IN IT. WE CANT FIND WHERE THE COOLANT IS COMING FROM AND ITS A REAL SCARE.

Mileage: 140,000

Nov 9, 2019

CAR STALLS AT IDLE ESPECIALLY AFTER PARKING THE VEHICLE, AND RESTARTING IT AFTER A FEW MINUTES. CHECK ENGINE LIGHT COMES ON. I PUT THE CAR IN PARK AND RESTART AND IT STALLS AGAIN. AFTER A FEW ATTEMPTS THE CAR STARTS AND DRIVES NORMALLY. THIS HAPPENS MOSTLY WHEN IN MOTION AT SLOW SPEEDS ON THE CITY STREET.

Nov 6, 2019

WHILE DRIVING THE VEHICLE AND TRAVELING ON A BUSY HIGHWAY THE VEHICLE WOULD NOT SHIFT INTO GEAR TO MOVE WITH TRAFFIC. VEHICLE LOST POWER. A FEW DAYS LATER ON ANOTHER BUSY HIGHWAY DRIVING APPROXIMATELY 60 MILES AN HOUR, THE COMPUTER READ TRANSMISSION FAILED. MY MILEAGE WAS 59,647 WHICH WAS UNDER THE 60,000 WARRANTY BUT OUT OF DATE. I PURCHASED THE CAR WITH 49,443 MILES ON 8/1/18. I IMMEDIATELY BROUGHT THE CAR TO SUNNY SIDE MOTORS A AUTHORIZED FORD DEALERSHIP AND HAD THE TRANSMISSION FAILED MESSAGE DIAGNOSIS DONE AT THE COST OF $159.95 TO FIND OUT THE REPAIR WOULD COST ME $2712.19 WHICH WOULD NOT BE COVER UNDER THE 60,000 MILE WARRANTY. THE TEST RETRIEVE CODE P1744 FOR TORQUE CONVERTER CLUTCH PERFORMED, PRESSURE DROPPING OUT OF SPEC WHEN WARM CHECKED FLUID CONDITION AND FOUND TORQUE CONVERTER CLUTCH DAMAGED CAUSING INTERNAL CONTAMINATION AND NEEDS INTERNAL REPAIRS. BEING A SINGLE WOMEN AT 72 YEARS OF AGE, AND BEING A SURVIVOR OF A NEAR FATAL ACCIDENT IN JANUARY OF 2018, WHICH TOOK ME 8 MONTHS TO GET BACK BEHIND A WHEEL OF A CAR I ONCE AGAIN FIND MYSELF FEELING UNSAFE DRIVING A CAR THAT JUST RANDOMLY LOSES POWER. AFTER READING MANY COMPLAINTS WITH THE SAME EXISTING PROBLEMS AS I AM EXPERIENCING I AM VERY CONCERNED WHY THIS PROBLEM HAS NOT BEEN A FACTORY RECALL. VERY UNSAFE WHEN DRIVING AND YOU LOSE POWER. HOPEFULLY A RECALL WILL BE ISSUED BASED ON THE MANY COMPLAINTS THAT HAVE BEEN PLACED. THE 1ST DEALERSHIP I VISITED IN WESTBOROUGH MA HAD A WAIT TIME OF 3 WEEKS TO DIAGNOSE THE PROBLEM.

Mileage: 59,600

Nov 4, 2019

AFTER STARTING IGNITION AND CAR IDOLS/DRIVEN HEAVY GAS/EMISSIONS SMELL FILLS CABIN WHEN USING HEAT/A/C OR DEFROST SYSTEMS. ENGINE LIGHT SOMETIMES GOES ON. CAR HAS 35,100 MI. TOOK CAR TO QUEENS NY FORD SERVICE CENTER 4 HOURS LATER $400 LATER, CHANGED CABIN FILTER AND SPRAYED FRAGRANCE ON IT. TOLD MUST USE CABIN RECYCLE AIR FUNCTION. FORD OWNERS MANUAL DOESNT SAY MUST USE AND IN NO OTHER CAR HAVE HAD TO MUST USE THIS FUNCTION. I HAVE A CASE# CAS24667125 AND APPT FOR 11/6/19. FORD BUILT THIS CAR TECH'S SHOULD KNOW HOW TO FIX THIS!

Mileage: 34,897

Nov 1, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 50 MPH, THE CONTACT NOTICED A MESSAGE ON THE INSTRUMENT PANEL, INDICATING "REDUCING POWER DUE TO OVERHEATING" AND ANOTHER UNKNOWN MESSAGE APPEARED. THE CONTACT STATED THAT THE TEMPERATURE GAUGE DID NOT SHOW THAT THE VEHICLE WAS OVERHEATING. THE CONTACT WAS ABLE TO PARK ON THE SIDE OF THE ROAD AND NOTICED SMOKE UNDER THE HOOD. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC AND THE CONTACT WAS INFORMED THAT THE VEHICLE DID NOT HAVE ANY OIL DUE TO A LEAK. THE CONTACT ASSOCIATED THE FAILURE WITH NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. A DEALER WAS NOT CONTACTED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 123,148.

Mileage: 123,148

Oct 29, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING, THE VEHICLE STALLED WITHOUT WARNING. THE CONTACT WAS ABLE TO COAST THE VEHICLE TO THE SIDE OF THE ROAD AND POWER OFF THE ENGINE. THE VEHICLE WAS RESTARTED, BUT FAILED TO DRIVE. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE TORQUE CONVERTOR PUMP SEAL WAS LEAKING DARK BROWN OIL WITH METAL FLUID INSIDE THE ENGINE. THE TECHNICIAN INFORMED THE CONTACT THAT THE VEHICLE'S SENSORS WOULD CAUSE THE ENGINE TO OVERHEAT AND CATCH FIRE. THE CONTACT STATED THAT THE TECHNICIAN REPAIRED THE LEAK, BUT THE COMPUTER SENSOR WAS NOT REPAIRED. THE CONTACT CALLED ANTELOPE VALLEY FORD (1155 AUTO MALL DR, LANCASTER, CA 93534, (888) 415-0959) AND WAS INFORMED THAT THE VEHICLE WAS NOT INCLUDED IN A RECALL. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 126,000.

Mileage: 126,000

Oct 28, 2019

EVERY TIME I GET GAS THE CAR HAVE TROUBLE STARTING BACK UP. THE VEHICLE ACCELERATE ON IT'S OWN WHILE DRIVING, AND RANDOMLY STOPS. TODAY 10/28/2019 I WAS ON THE EWAY GOING WEST OF 465 INDIANAPOLIS AND THE CAR SLOWED DOWN NSTOPPED BEFORE I CAN EVEN PULL OVER. I SAT THERE FOR 5 MINS CAR OFF AND IT TURNED BACK ON. I HAVE TO SHUT THE CAR OFF N START BACK UP. ENGINE LIGHT BATTERY AND TRANS LIGHT HAVE ALL CAME ON AMD IT SHUTS OFF AND COME BACK ON LIKE NOTHING EVER HAPPENED YET AUTO SHOPS CAN NOT FIND A DIAGNOSTIC FOR THE PROBLEM. THIS IS AN ONGOING ISSUE AND I HAVE ONLY HAD THIS CAR FOR A MONTH

Mileage: 120,000

Oct 27, 2019

WHILE CAR IS IN MOTION OUR 2014 FORD ESCAPE STALLS. WE TURN THE KEY OFF, TURN IT BACK IN AND IT WILL SOMETIMES RUN FOR A BIT BEFORE STALLING AGAIN AND SOMETIMES STALL IMMEDIATELY. CURRENTLY THIS HAS HAPPENED ON CITY STREETS AND PARKING LOTS. ONCE WHILE TURNING. OTHERS GOING STRAIGHT. LUCKILY WE HAVE NOT HAD THIS HAPPEN ON THE INTERSTATE YET.

Mileage: 1

Oct 12, 2019

VEHICLE WAS STATIONARY. NOTICED FLUID ON A HOSE UNDER THE FRONT PASSENGER SIDE WHILE PERFORMING AN OIL CHANGE. ALSO OBSERVED THE FLUID POOLING AND DISCOLORING UNDERSIDE OF ENGINE. BROUGHT VEHICLE TO LOUISBURG FORD. SERVICE TEAM INFORMED ME THAT THE TURBO HAD FAILED AND NEEDED TO BE REPLACED. COOLANT ALSO APPEARS LOW WITHOUT EXPLANATION. JUST BOUGHT VEHICLE USED FROM LOUISBURG WITH 74,000 MILES IN FEBRUARY 2019. NOW 86,000 MILES.

Mileage: 86,000

Oct 11, 2019

WHILE DRIVING THE CAR EXHIBITS AN ENGINE HIGH HEAR AND ENTERS SAFE MODE AND RAPIDLY DECELERATING. THIS HAPPENED ONCE AND WAS DIAGNOSED BY THE DEALER AS A BAD PART FROM A PREVIOUS RECALL 17S09. IT OCCURRED AGAIN JUST RECENTLY AND WAS SUPPOSEDLY REPAIRED (COOLANT HOSE PROBLEMS) AND DID IT AGAIN IMMEDIATELY AFTER LEAVING THE DEALER SERVICE DEPARTMENT. IN BOTH CASES THE VEHICLE WAS TRAVELING AT 50 MPH ON A BUSY ROAD AND WE WERE LUCKY TO EXIT THE ROAD TO A SAFE AREA. THE ORIGINAL RECALL WAS RELATED TO ENGINE FIRES BUT THIS IS ANOTHER SAFETY HAZARD. IT IS ALSO POSSIBLE THAT THE RECALL ACTION BY FORD IS INADEQUATE TO CORRECT THE CONDITION.

Mileage: 28,800

Oct 10, 2019

MY 2014 FORD ESCAPE WITH CLOSE TO 69K MILES ON IT STARTED RUNNING ROUGH, FELT AND SOUNDED LIKE IT HAD TO DO WITH TIMING IS THE VEHICLE. CHECK ENGINE LIGHT CAME ON DAYS LATER AND AROUND THE SAME TIME NOTICED LOW COOLANT ALERTS. TOPPED OFF COOLANT BUT ALSO NOTICED COOLANT WOULD BE RETURNED TO RESERVOIR WHEN REMOVING THE CAP TO REFILL. CAR CONTINUES TO RUN ROUGH SO I TAKE IT IN TO MY LOCAL MECHANIC. CODE COMES BACK SAYING IT'S A COIL PACKAGE. REPAIRS ARE MADE, CAR RUNS GREAT AND CHECK ENGINE LIGHT IS OFF. A DAY LATER THE LIGHT COMES BACK ON AND SO DOES THE LOW COOLANT WARNING. TOP OFF COOLANT AND DECIDE TO TAKE IT INTO A DEALER. I DO MY RESEARCH ONLINE AND FIND THIS IS IS QUITE A COMMON PROBLEM WITH THESE VEHICLES. DEALER TELLS ME I HAVE A COOLANT LEAK IN CYLINDER 3 MUCH LIKE OTHER REPORTS I READ. THEY CLAIM IT'S A DIFFERENT ISSUE FROM THE COOLANT RECALL FORD ISSUED. I HAVE A HARD TIME BELIEVING THIS IS THE CASE AND AM MINDBLOWN FORD DOESN'T HAVE A REMEDY FOR THIS ISSUE.

Mileage: 68,023

Oct 10, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). WHILE DRIVING 70 MPH, THERE WAS AN AUDIBLE NOTIFICATION STATING THAT THE VEHICLE WAS OVERHEATING. THE VEHICLE WAS COASTED TO A COMPLETE STOP ON THE SIDE OF THE ROAD. THE CONTACT ALSO DETECTED OIL LEAKING FROM THE VEHICLE. MAC HAIK FORD OF GEORGETOWN (7201 N INTERSTATE HWY 35, GEORGETOWN, TX 78626, (512) 930-3673) WAS CONTACTED AND STATED THAT THE NEXT AVAILABLE APPOINTMENT WAS IN A MONTH. THE VEHICLE WAS NOT TAKEN TO A DEALER OR INDEPENDENT MECHANIC FOR DIAGNOSTIC TESTING OR REPAIRS. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 43,375.

Mileage: 43,375

Sep 26, 2019

TRANSMISSION WOULD NOT GO INTO GEAR CAR WOULD NOT GO FORWARDS.

Mileage: 156,000

Sep 26, 2019

I HAVE ALREADY FILED A COMPLAINT REGARDING THE COOLANT LIGHT SENSOR THAT KEPT COMING ON WHEN THERE WAS COOLANT IN THE CAR. LESS THAN ONE WEEK AFTER PAYING TO HAVE THE SENSOR REPLACED, MY ENGINE LIGHT CAME ON FOR A CYLINDER 2 MISFIRE. SO NOW I AM BEING TOLD THIS IS A CRACKED HEAD GASKET. I HAVE OWNED THIS CAR FOR ONE MONTH AND IT HAS LESS THAN 100,000 MILES. THIS IS THE EXACT PROBLEM LISTED IN THE FORD RECALL 17S09 AND THIS VEHICLE WAS MADE AT THE PLANT ASSOCIATED WITH THE RECALL DURING THE TIMEFRAME. THE EXPENSE OF THIS REPAIR NEEDS TO BE PAID FOR BY FORD. IT IS EXPENSIVE AND NOW MY CAR IS NOT SAFE TO DRIVE.

Mileage: 92,500

Sep 24, 2019

IN LINE AT A FAST FOOD DRIVE THROUGH, CHECK ENGINE LIGHT AND TEMPERATURE GAUGE CAME ON. SHUT VEHICLE DOWN AND THEN DROVE TO THE DEALERSHIP, HAD A CYLINDER 3 MISFIRE AND LOW COOLANT. AFTER NUMEROUS TESTS I AM TOLD THAT MY ENGINE IS CONSUMING COOLANT AND THAT IT WILL NEED TO REPLACED.I WAS ALSO TOLD THAT THIS IS A COMMON AND KNOWN ISSUE AMONG MY VEHICLE/ENGINE TYPE YET NO RECALL HAS BEEN ISSUED.

Mileage: 58,000

Sep 23, 2019

THE CAR KEEP GIVING ME A MESSAGE THAT IS OVERHEATING, THEN THE AC START BLOWING HOT AIR BUT THE CAR IS NOT HOT. WITHIN 3 MINUTES THE MESSAGING AWAY THE AC START WORKING LIKE NOTHING HAPPENED. ALSO THE TRANSMISSION SEEMS NOT TO CHANGE AT ALL WHEN THIS IS HAPPENING TO THE CAR.

Mileage: 114

Sep 18, 2019

I'LL BE DRIVING, THE IT WILL STOP AND THROW UP THE OIL LIGHT, BATTERY LIGHT AND THE AIRBAG LIGHT. I TOOK IT TO THE FORD DEALERSHIP ON 122ND ST IN PORTLAND, THEY SAID THEY COULDN'T FIND ANYTHING WRONG BECAUSE IT WASN'T THROWING ANY CODES. NOW I'M SITTING ON THE SIDE OF THE ROAD AND THE ERROR CODE SAYS ENGINE FAULT SERVICE NOW. I'VE HAD REGULAR MAINTENANCE ON THE CAR SO NOT SURE WHY THIS IS HAPPENING. CARS/SUVS SHOULDN'T JUST STOP WORKING WHILE YOU'RE DRIVING THEM.

Mileage: 1

Sep 16, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING APPROXIMATELY 35 MPH, THE LOW COOLANT WARNING INDICATOR ILLUMINATED CONTINUOUSLY. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THERE WAS COOLANT IN THE VEHICLE. THE CONTACT WAS ABLE TO DRIVE THE VEHICLE; HOWEVER, THE FAILURE PERSISTED. THE VEHICLE DISPLAYED AN OVERHEATING MESSAGE, WHICH CAUSED THE VEHICLE TO STALL. THE VEHICLE WAS UNABLE TO RESTART. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THERE WAS AIR IN THE COOLANT LINE. THE VEHICLE WAS REPAIRED, BUT THE FAILURE PERSISTED A WEEK LATER. THE VEHICLE WAS TAKEN BACK TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE COOLANT WAS LOW IN THE VEHICLE AND WAS BURNING ETERNALLY; HOWEVER, THERE WAS NO LEAK. THE CONTACT WAS INFORMED TO TAKE THE VEHICLE TO A FORD DEALER. THE VEHICLE WAS NOT REPAIRED. THE VEHICLE WAS TAKEN TO ANOTHER INDEPENDENT MECHANIC WHO STATED THAT THE FAILURE WAS DUE TO A RECALL. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE AND INFORMED THE CONTACT THAT THE VIN WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE DEALER WAS NOT CONTACTED. THE APPROXIMATE FAILURE MILEAGE WAS 94,000.

Mileage: 94,000

Sep 10, 2019

THE VEHICLE WAS STATIONARY AND HAD NOT BEEN DRIVEN FOR MORE THAN 3 HOURS. I PUSHED THE REMOTE START AND THE CAR STARTED, BUT IT SHUT OFF ALMOST IMMEDIATELY. THE SHUT DOWN WAS DUE TO OVERHEATING. THE ENGINE WAS COOL AND THE COOLANT WAS TEPID AT BEST. THIS IS NOT AN OVERHEATING ISSUE. THE CAR WILL NOT RUN ON MORE THAN 2 CYLINDERS. THIS IS THE SECOND TIME THIS HAS HAPPENED SINCE THE RECALL FOR THE COOLANT SENSOR. THE CAR HAD TO BE TOWED TO THE DEALER WHERE I WAS CHARGED TO DIAGNOSE THE ISSUE. THIS SHOULD BE NO CHARGE SINCE IT WAS RECALLED FOR THE OVERHEATING ISSUE. THIS OVERHEATING HAS CAUSED MY TRANSMISSION AND TORQUE CONVERTER TO FAIL AS WELL. THE COST OF THE TRANSMISSION SHOULD BE REIMBURSED BY FORD SINCE THEY HAVE KNOW ABOUT THE OVERHEATING ISSUE FOR A LONG TIME NOW.

Mileage: 125,000

Sep 9, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE THE CONTACT'S WIFE WAS DRIVING APPROXIMATELY 35 MPH, AN ABNORMAL NOISE WAS HEARD FROM THE FRONT END OF THE VEHICLE. ALSO, THE CHECK ENGINE WARNING INDICATOR ILLUMINATED CONTINUOUSLY WHILE THE VEHICLE WAS HOT. THE CONTACT MENTIONED THAT THE INDICATOR DID NOT ILLUMINATE WHILE THE VEHICLE WAS COOL. THERE WERE ALSO OTHER MULTIPLE UNKNOWN INDICATORS THAT ILLUMINATED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE COOLANT VALVE NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. SAYVILLE FORD (5686 SUNRISE HWY, SAYVILLE, NY 11782, (855) 561-1191) WAS CONTACTED AND STATED THAT THERE WERE NO RECALLS FOR THE FAILURE. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 48,620.

Mileage: 48,620

Sep 4, 2019

FORD 1.6L ECO-BOOST FAILURE. FORD KNOWS ABOUT THIS (NOT MINE, BUT THE ONGOING PROBLEMS). MY CAR HAS ONLY 74K MILES AND GREAT MAINTENANCE. THE VEHICLE OVERHEATED FOR A MOMENT. 2 WEEKS LATER, COOLANT FROM EXHAUST, BLOWN HEAD GASKET, WARPED HEAD. THIS IS A KNOWN PROBLEM WITH THE FORD 1.6L ECO-BOOST TURBO. FORD DUMPED THE ENGINE. OTHER COUNTRIES HAVE FORCED RECALLS (UK). THE NHTSA SHOULD DO THE SAME. THE SITUATION IS DRAMATIC AND CAN CAUSE MAJOR COLLISIONS.

Mileage: 74,000

Sep 2, 2019

THE CAR WAS STATIONARY. RECALL ISSUE WITH THE COOLANT RESERVOIR. BROKE TWICE AND COVERED BUT THIRD TIME NO WARNING. ENGINE NOW IS CRACKED DUE TO THE LACK OF COOLANT. I HAVE A COOLANT INTRUSION IN THE MOTOR AND IT NEEDS TO BE REPLACED. FORD WON'T COVER IT BECAUSE THE RECALL WARRANTY HAS EXPIRED PER THE DEALER AND THEIR CUSTOMER SERVICE NUMBER.

Mileage: 107,012

Aug 28, 2019

ON 1/17/18 MILEAGE 47120 I BROUGHT THE VEHICLE TO OUR LOCAL FORD DEALER AND THEY REPAIRED THE VEHICLE UNDER WARRANTY DUE TO RECALL 17S09. HOWEVER, ON 8/5/2019 MILEAGE 62,500 THE VEHICLE WAS RUNNING ROUGH AND THE CHECK ENGINE LIGHT CAME ON. LONG STORY SHORT, THE VEHICLE WAS TOWED TO ANOTHER FORD DEALER WHERE THEY DETERMINED THE VEHICLE HAD A CRACKED CYLINDER, THE EXACT SAME CONDITION THAT 17S09 WAS SUPPOSED TO FIX. WHILE I DID NOT SUFFER A SAFETY INCIDENT IN THIS CASE, MY CONCERN IS THAT THE VEHICLE WAS NOT REPAIRED CORRECTLY UNDER THE ORIGINAL RECALL, AND THUS THERE MAY STILL BE A SAFETY ISSUE THAT MAY AFFECT OTHERS.

Mileage: 62,500

Aug 26, 2019

VEHICLE NEEDS "NEW ENGINE" AS DIAGNOSED BY TAPPER FORD DEALERSHIP, PAW PAW MI. WAS TOLD THE "BLOCK" WAS BAD AFTER "COOLANT LEAKED INTO ENGINE" FROM HEAD GASKET CRACKED. THIS VEHICLE HAS A RECALL STATING "LOCALIZED OVERHEATING OF THE ENGINE CYLINDER HEAD MAY CAUSE THE CYLINDER HEAD TO CRACK". THIS VEHICLE WAS AT STAND STILL IN TRAFFIC JAM ON HIGHWAY7/25/19 WARNING SOUNDS AND MESSAGE APPEARED ON DASHBOARD OF VEHICLE STATING TO PULL OVER DUE TO ENGINE OVERHEATING. VEHICLE WAS DRIVEN 1 MORE MILE TO HIGHWAY EXIT, PULLED INTO GAS STATION AT EXIT, HOOD OPENED TO SHOW NO COOLANT PRESENT IN TANK. VEHICLE ALLOWED TO COOL FOR 30MIN, PLACED APPROPRIATE AMOUNT OF ORANGE COOLANT IN TANK AS INSTRUCTED TO BY MANUAL AND DROVE CARE ANOTHER HOUR WITHOUT ISSUE. NEXT MORNING COOLANT TANK CHECKED AND NOTED NO COOLANT PRESENT, AGAIN PLACED APPROPRIATE AMOUNT IN TANK AS MANUAL STATES, DROVE VEHICLE ANOTHER HOUR. COOLANT LEVEL CHECKED FOR NEXT FEW DAYS AND HAD NO ISSUE. COOLANT LEVEL CHECK PRIOR TO DRIVING VEHICLE HOME FROM NORTHERN MICHIGAN, AGAIN NONE PRESENT IN TANK, AGAIN ADDED APPROPRIATE AMOUNT OF COOLANT, DROVE HOME APPROX. 350MILES WITHOUT ISSUE. NEXT MORNING (SUNDAY, AUGUST 4TH, 2019) STARTED SUV, ENTIRE VEHICLE WAS SHAKING, LARGE AMOUNT OF WHITE THICK EXHAUST PRESENT, SWEET SMELLING. VEHICLE BROUGHT TO LOCAL MECHANIC, STATED HEAD GASKET NEEDED REPLACED AND STATED A RECALL WAS OUT FOR AN ISSUE WITH A SENSOR THAT COULD MALFUNCTION AND CAUSE THIS DAMAGE. VEHICLE WAS TOWED TO TAPPER FORD DEALERSHIP IN PAW, PAW MI FOR FURTHER EVALUATION. THIS DEALERSHIP TOLD US THAT AN ENTIRE NEW ENGINE WAS NEEDED AND WOULD NOT BE COVERED BY FORD. THE PROBLEMS WITH THE ENGINE OF THIS VEHICLE IS DUE TO THE RECALL STATED ABOVE. HOW CAN FORD REFUSE TO FIX THIS PROBLEM AT A COST TO THEM? WAS GIVEN A PHONE QUOTE OF "$8,000.00" FOR THE NEW ENGINE. I DO HAVE A VIDEO OF THE WHITE THICK EXHAUST.

Mileage: 87,500

Aug 26, 2019

I PURCHASED 2014 FORD ESCAPE SE WITH BRANDED TITLE FROM CAR AUCTION. AFTER RECEIVING CAR FROM TOW TRUCK, I STARTED CAR ON MY DRIVE, FEW MINUTES LATER VISIBLE SMOKE START COMING FROM THE ENGINE, AND I ALSO NOTICED OVERHEAT FROM ENGINE. I STOP THE ENGINE. NEXT DAY I STARTED CAR, AND EXPERIENCED SAME PROBLEM. I CONTACTED TWO RIVERS FORD - MT JULIET, TN. FORD SERVICE DEPARTMENT ASKED ME TO BRING CAR IN THEIR SERVICE. THEY CHECKED CAR, AND COMMUNICATED FORD MOTOR AND FORD LEGAL SERVICE WHETHER TO FULL FILL RECALL PROCEDURES FOR BRANDED TITLE CAR. AFTER 20 DAYS, THEY CALLED ME. THEIR DECISION IS NOT TO FULFILL RECALL. THEY SAID FORD WARRANTIES NOT COVER BRANDED TITLE CARS. CAR IS NOT SAFE TO DRIVE. AND MY CAR PROBLEM SEEMS PRIMARY RELATED TO RECALL ISSUE. ENGINE OBVIOUSLY EXPERIENCED OVERHEAT BEFORE SINCE PLASTICS OVER THE ENGINE WAS MELTED.

Mileage: 67,000

Aug 22, 2019

COOLANT CONSTANTLY LEAKING AND ENGINE GETTING VERY HOT, CURRENTLY PUTTING COOLANT IN DAILY

Mileage: 79,850

Aug 21, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT THE VEHICLE TENDED TO OVERHEAT. THE COOLANT SENSOR WAS REPLACED BY AN INDEPENDENT MECHANIC, BUT THE FAILURE RECURRED. THE DEALER AND MANUFACTURER WERE NOT NOTIFIED OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 126,000.

Mileage: 126,000

Aug 20, 2019

TRANSMISSION HAS A HARD SHIFT FROM TIME TO TIME MAKING IT FEEL LIKE THE ENGINE IS JUST GOING TO FALL OUT. IT DOES NOT HAPPEN DURING A SPECIFIC OCCURRENCE BUT IT SEEMS AS IF THE TRANSMISSION IS DELAYED GOING GEAR TO GEAR WETHER IT BE FROM PARK TO REVERSE TO DRIVE, OR FROM GEARS 1-5

Mileage: 35,000

Aug 20, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT THE CHECK ENGINE WARNING INDICATOR ILLUMINATED. THE VEHICLE WAS TAKEN TO ELDER FORD OF TAMPA (9560 N FLORIDA AVE, TAMPA, FL 33612), BUT THEY DID NOT HAVE ANY APPOINTMENTS AVAILABLE FOR TWO WEEKS. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT A NEW SPARK PLUG AND COIL WERE NEEDED. THE VEHICLE WAS REPAIRED. TWO WEEKS LATER, THE CHECK ENGINE WARNING INDICATOR ILLUMINATED AGAIN. THE VEHICLE WAS TAKEN BACK TO THE DEALER WHERE IT WAS DIAGNOSED THAT THE HEAD GASKET FAILED AND NEEDED REPLACEMENT. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURES. THE APPROXIMATE FAILURE MILEAGE WAS 47,726.

Mileage: 47,726

Aug 19, 2019

MY CAR COOLANT IS ALWAYS LEAKING HAVE TO FILL OUT AND FIX MOST OF THE TIME. THE TRANSMISSION WAS SUDDENLY FAILED EVEN ONLY 80000K MILEAGE AND SERVICE CENTER FOR REPLACEMENT COST IS $6000.THAT'S REALLY RIDICULOUS.

Mileage: 80,000

Aug 15, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. AFTER RESTARTING THE VEHICLE, "ENGINE OVERHEATING' DISPLAYED ON THE INSTRUMENT PANEL, ALTHOUGH THE ENGINE HAD NOT WARMED UP AND THE VEHICLE SPEED WOULD NOT EXCEED 5 MPH. THE VEHICLE WAS TOWED TO LONG LEWIS FORD (2091 ALABAMA 14, PRATVILLE, AL) TO BE DIAGNOSED, BUT THE CAUSE OF THE FAILURE WAS NOT DETERMINED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE CONTACT INDICATED THAT THE VEHICLE WAS PREVIOUSLY SERVICED PER NHTSA CAMPAIGN NUMBER: 17V209000(ENGINE); HOWEVER, THE FAILURE RECURRED. THE FAILURE MILEAGE WAS 72,999.

Mileage: 72,999

Aug 14, 2019

MY CAR WAS OVERHEATING SO I TOOK IT INTO THE SHOP AND THEY SAID IT WAS THE THERMOSTAT SO I REPLACED THE THERMOSTAT AND IT'S STILL KEPT OVERHEATING SO I TOOK IT BACK IN THEY RAN A TEST IN THE HEADS WERE BLOWN SO THEY HAD TO REPLACE THE HEADS WELL FROM WHAT I UNDERSTAND THAT THIS IS A COMMON PROBLEM WITH MY YEAR OF VEHICLE AND THE FORD ESCAPES BECAUSE THERE WAS ANOTHER FORD ESCAPE WITH THE SAME ISSUE AND THEY HAD TO REPLACE THE HEADS ON IT I FEEL LIKE IT SHOULD BE RECALLED BECAUSE IT IS A COMMON PROBLEM AND I THINK FORD IS AWARE OF IT I DON'T HAVE THE MONEY TO REPLACE A HEAD ON MY VEHICLE IT'S A 2014 IT SHOULDN'T EVEN NEED THE HEADS REPLACED IT LOOK LIKE IT BELONGS TO

Mileage: 154,000

Aug 12, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 45 MPH, THE VEHICLE DECELERATED AND WHITE SMOKE APPEARED FROM THE EXHAUST. THE CONTACT PULLED THE VEHICLE OVER UNTIL THE SMOKE SUBSIDED. WHEN THE CONTACT TURNED OFF THE VEHICLE, IT COULD NOT BE RESTARTED. THE VEHICLE WAS TAKEN TO BILL KAY FORD (14633 S CICEROS, MIDLOTHIAN, IL 60445, (708) 388-3000) WHERE IT WAS DIAGNOSED THAT A NEW ENGINE WAS NEEDED. THE DEALER STATED THAT THE WARRANTY WAS EXPIRED; THEREFORE, THEY DID NOT ASSIST. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 78,000. THE VIN WAS UNKNOWN.

Mileage: 78,000

Aug 12, 2019 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED WHILE DRIVING 50 MPH, WHEN HE NOTICED THE TEMPERATURE GAUGE INCREASE. THE CONTACT STATED NO WARNING LIGHTS WERE ILLUMINATED. THE CONTACT STATED HE HEARD AN ABNORMAL NOISE FROM THE ENGINE AND SAW SMOKE EXITING FROM THE HOOD. THE CONTACT PULLED THE VEHICLE ON THE SIDE OF THE ROAD AND LET THE ENGINE COOL FOR 15 MINUTES BEFORE CONTINUING DRIVING, BUT AFTER 20 MINUTES THE FAILURE OCCURRED AGAIN. THE VEHICLE WAS TAKEN TO LOCAL DEALER BOZEMAN FORD LINCOLN LOCATED AT 2900 N 19TH AVE, BOZEMAN, MT 59718, (406) 587-1221, WHERE HE WAS MADE AWARE OF THE FAILURE. THE CONTACT STATED THE DEALER SET UP AN APPOINTMENT FOR NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING) REPAIRS WITH IN A WEEK. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED AS OF YET. THE MANUFACTURER HAD NOT BEEN INFORMED OF FAILURE. THE FAILURE MILEAGE WAS 112,000.

Mileage: 112,000

Aug 12, 2019

THIS VEHICLE SHOULD HAVE BEEN INCLUDED IN A 2017 SAFETY RECALL RELATED TO OVERHEATING AND COOLANT LEAKS, BUT IT WAS NOT. IN FEBRUARY 2019, IT OVERHEATED WITH LITTLE WARNING ON THE FREEWAY, BLOWING A HOLE IN THE MOTOR (AT 62K MILES). FORD REJECTED REQUEST FOR ASSISTANCE, SO REPAIR WAS DONE BY INDEPENDENT MECHANIC (MOTOR REPLACED). THREE MONTHS LATER, DURING FREEWAY DRIVE, MESSAGE APPEARED SEVERAL TIMES STATING POWER WAS BEING CUT TO KEEP ENGINE FROM OVERHEATING (NO INDICATION ENGINE ACTUALLY WAS OVERHEATING). ULTIMATELY, MESSAGE APPEARED WARNING TO PULL OFF THE ROAD IMMEDIATELY. OVERHEATED ENGINE COMPLETELY MELTED A BRACKET. MECHANIC IDENTIFIED A BURNT-OUT SENSOR BUT COULD NOT SAY WHY IT HAPPENED. I SECURED TWO DEALERSHIP DIAGNOSTICS. FIRST CONDUCTED COMPREHENSIVE DIAGNOSTIC AND CONCLUDED A WASTE GATE WAS STUCK OPEN; NO MENTION OF DAMAGED SENSOR. SECOND SAID THE DEGAS BOTTLE WAS CRACKED AND DECLINED TO PERFORM PRESSURE TEST; NO MENTION OF DAMAGED SENSOR OR WASTE GATE ISSUE. I CANNOT AFFORD ALL THESE RANDOM REPAIRS AND IN ANY CASE, DO NOT FEEL THIS CAR CAN BE PUT INTO A SAFE CONDITION FOR DRIVING.

Mileage: 68,000

Aug 5, 2019

HAD RECALL DONE AT DEALERSHIP TO PREVENT VEHICLE FIRE DUE TO WARPED HEADS ON ENGINE BECAUSE NO SENSOR TO TELL YOU LOW ON COOLANT. CAR HAS OVER 100,000 ON IT NEVER HAD A PROBLEM. NOW AFTER RECALL WORK IS DONE CAR IS SHUTTING DOWN IN TRAFFIC SAYING ENGINE OVERHEATING. BROUGHT TO FORD DEALERSHIP AND WAS TOLD THERE IS ALOT OF THESE COMING IN. WAS TOLD DEALERSHIP IS A MONTH BEHIND ON ENGINE WORK. DEALERSHIP HAD FOR 7 DAYS KEPT SAYING THEY WERE GOING TO LOOK AT IT TOMORROW TO DIAGNOSE. THEY WOULD CALL BACK AND SAY ANOTHER DAY. WHEN TO PICK UP AND THEY SAID NOT UNDER WARRANTY WOULD BE ALOT OF MONEY TO FIX. THIS IS MY DAUGHTERS CAR AND IT IS SHUTTING DOWN ON FREEWAYS AND SIDE ROADS. NOT GOOD. DANGEROUS. SOUNDS LIKE DEFECTIVE ENGINE

Mileage: 104,000

Jul 26, 2019

MY FORD GAVE OFF EXHAUST SMELL FROM TIME TO TIME AND OCCASIONALLY THE ENGINE LIGHT MAY COME ON. BUT DEALERSHIP DID NOT FIND ANY PROBLEMS RECENTLY, THE ENGINE LIGHT CAME ON AND I DROVE MY CARD TO THE NEAREST FORDS DEALERSHIP BUT, NEEDED TO SCHEDULE AN APPOINTMENT. ADVISED COULD DRIVE HOME IF NO UNUSUAL SOUNDS. ENGINE LIGHT WENT OFF BEFORE APPOINTMENT, SO I CANCELED. 2-3 WEEKS LATER ENGINE LIGHT, CAME BACK ON WITH SMELL OF FUMES. I SCHEDULED AN APPOINTMENT. THE DAY OF THE APPOINTMENT, I STARTED THE CAR AND COOLANT LIGHT ALSO CAME ON AT START WITH THE SMELL OF FUMES. FEELING UNEASY DRIVING THE CAR, I HAD 2014 FORD ESCAPE TOWED TO THE DEALERSHIP THAT I FREQUENT AND DESCRIBE ENGINE LIGHT AND COOLANT LIGHT CAME ON DURING START, WITH A LOUD HUMMING NOISE. SINCE I HAD ALREADY SCHEDULED TO GET THE WORKS SYNTHETIC OIL CHANGE AND VEHICLE MAINTENANCE ON THE SAME DAY, I ALSO REQUESTED DIAGNOSTIC TESTING. THE CAR WAS KEPT OVERNIGHT. THERE IS ONLY 47746 MILES ON THE VEHICLE AND TOO MANY ISSUES. I WAS ADVISED THE CAR HAD MISFIRED CODES AND OVERHEAT CODES. PRESSURED TESTED COOLANT PULLED THE SPARK PLUG, FOUND COOLANT IN A CYLINDER. THE CAR NEEDS A HEAD GASKET. CAR SMOKED DURING COLD START AND EXHAUST SMELLS LIKE COOLANT. MY CAR WAS PREVIOUSLY RECALLED FOR A DOOR HATCH AND OVERHEATING.. I HAVE TAKEN THE CAR TO THE DEALERSHIP SEVERAL TIMES BEFORE FOR ENGINE LIGHT, BUT, VEHICLE CHECK-UP ALWAYS SEEMS TO RESOLVE THE ISSUE. ON ONE OCCASION, REQUESTED OIL CHANGE AND VEHICLE INSPECTION, WHEN ALMOST A QUARTER OF A MILE FROM HOME ALL OF THE DASHBOARD LIGHTS CAME ON. HAD THE CAR TOWED BACK TO THE DEALERSHIP, THE ISSUE SEEMED TO BE RESOLVED.

Mileage: 47,746

Jul 23, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. AFTER STARTING THE VEHICLE, THE CONTACT NOTICED THAT THE ENGINE WAS IDLING ROUGHLY, THE CHECK ENGINE INDICATOR ILLUMINATED, AND WHITE SMOKE WAS COMING FROM THE EXHAUST. THE VEHICLE WAS TAKEN TO KEY FORD (422 US-1, YORK, MAINE) WHERE IT WAS DIAGNOSED THAT THE HEAD GASKET WAS FAULTY AND DAMAGED THE ENGINE. THE ENGINE NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE CONTACT INDICATED THAT THE VEHICLE WAS PREVIOUSLY SERVICED PER NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE MANUFACTURER WAS NOTIFIED, BUT NO ASSISTANCE WAS OFFERED. THE FAILURE MILEAGE WAS 118,000.

Mileage: 118,000

Jul 23, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 65 MPH, THE TEMPERATURE GAUGE INCREASED TO HIGH IN A SHORT AMOUNT OF TIME. THE CONTACT STATED THAT AN UNKNOWN MESSAGE APPEARED ON THE INSTRUMENT PANEL WHEN THE FAILURE OCCURRED. THE CONTACT ASSOCIATED THE FAILURE WITH NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE COOLANT TEMPERATE SENSOR FAILED. THE CONTACT STATED THAT THE VEHICLE WAS REPAIRED, BUT THE FAILURE CONTINUED. THE CONTACT CALLED LITHIA FORD LINCOLN OF ROSEBURG (LOCATED AT 1650 NE STEPHENS ST, ROSEBURG, OR 97470, (541) 537-4643) TO NOTIFY THEM OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS 104,000.

Mileage: 104,000

Jul 21, 2019

UPON BEGINNING. TO MOVE FORWARD (PULLING INTO TRAFFIC) THE ENGINE WILL SOMETIMES STALL(CUT OFF) . OTHER TIMES IT WILL BEGIN TO RUN VERY ROUGH SOMETIMES CAUSING ITHE ENGINE TO STALL. ALTHOUGH THIS VEHICLE DOES NOT SEEM TO BE PART OF RECALL # 14S30 OR #14S20 THE CONDITIONS ARE VERY SIMILAR TO THESE REPORTS.

Mileage: 61,342

Jul 18, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT THE MOTOR BLOCK CRACKED. DEWEY FORD (3055 SE DELAWARE AVE, ANKENY, IA 50021, (515) 963-9575) CONFIRMED THAT THE MOTOR BLOCK WAS CRACKED AND ADMITTED THAT THE 1.6 LITER MOTORS HAVE HAD MANY ISSUES WITH THE BLOCKS CRACKING. THE MANUFACTURER STATED THAT THERE WAS NO RECALL; THEREFORE, THEY COULD NOT ASSIST WITH THE REPAIRS. THE MANUFACTURER REFERRED THE CONTACT TO NHTSA. THE FAILURE MILEAGE WAS 80,000. THE VIN WAS UNKNOWN.

Mileage: 80,000

Jul 18, 2019

AT 85,000 MILES, I GET A CHECK ENGINE LIGHT UPON START UP AND IT SPUTTERS. IT GOES ON AND OFF AS I AM DRIVING. I BRING IT TO THE DEALERSHIP, AND THEY TELL ME IT'S THE #3 COIL AND CHANGE THAT AND GIVE ME A NEW SET OF SPARK PLUGS. PROBLEM IS, THEY SAID THE WARRANTY WAS ONLY GOOD FOR A TOTAL OF 60,000 MILES. I HAVE NO WARRANTY. THE COST IS $350. FINE, I PAID IT, TOOK IT HOME AND START LOOKING FOR ANOTHER FORD BECAUSE I NEED ONE WITH A WARRANTY. I LOOK THROUGH MY ORIGINAL PAPERWORK AND THE FINE PRINT SAYS THE EXPIRATION IS THE TOTAL OF 60,000 NOT AN ADDITIONAL. MY BAD FOR TRUSTING WHAT THE F&I PERSON TOLD ME INSTEAD OF READING THE CONTRACT. WE GO ON VACATION, LEAVE THE ESCAPE HOME AND FIRST DAY BACK AT WORK THE ENGINE LIGHT COMES ON, PLUS A NEW LIGHT WHILE I AM DRIVING TELLING ME THE ENGINE COOLANT IS LOW AND TO SERVICE IT SOON. I CALL MY SERVICE ADVISER, HE ASKED IF THE TEMPERATURE IS HIGH AND IT WAS NOT. HE SAID TO DRIVE IT TO THEM, AND THEY WILL LOOK AT IT. I GET A CALL LATER THAT DAY SAYING THAT THE ENGINE BLOCK IS CRACKED, AND I NEED $5,300 TO GET A NEW BLOCK OR $6,500 TO GET A NEW ENGINE. HE ALSO EXPLAINED THAT THE 1.9L TURBO ESCAPES ARE EXPERIENCING A LOT OF ISSUES AND HE HAS 2 AT THE DEALERSHIP RIGHT NOW WITH THE SAME PROBLEM.

Mileage: 85,000

Jul 18, 2019

I PURCHASED MY 2014 FORD ESCAPE ECOBOOST BRAND NEW, SOLE OWNER. I HAVE BEEN HAVING ISSUES WITH LOSING COOLANT FOR APPROX 2 YEARS AND TAKING IT BACK AND FORTH TO THE FORD DEALER. THE DEALER RAN MULTIPLE TESTS ON MULTIPLE OCCASIONS AND FOUND NOTHING, EVEN CALLING IT "ONE OF THOSE FORD MYSTERIES". TODAY, 7/18/19 ON THE WAY TO WORK, MY SUV LOST THE ABILITY TO ACCELERATE. I WAS STOPPED AT A TRAFFIC LIGHT AND WHEN THE LIGHT CHANGED AND I HIT THE GAS, MY SUV BARELY MOVED. AFTER APPROX 10 SECS, MY SUV JERKED AND ACCELERATED TO AN ALMOST NORMAL SPEED. THAT LASTED ONLY FOR A FEW SECONDS, WHEN IT STARTED TO BARELY MOVE AGAIN. I WAS ABLE TO DRIVE SLOWLY TO THE SIDE OF THE ROAD, OUT OF TRAFFIC. THERE I WAITED FOR A TOW TRUCK, WHO TOOK THE SUV TO THE FORD DEALER. I HAVE GOTTEN ALL MY MAINTENANCE AND OIL CHANGES DONE AT THE FORD DEALER SINCE I PURCHASED THE CAR, SO OF COURSE I'M SHOCKED TO HEAR THAT AFTER ONLY 77,000 MILES, I HAVE A TRANSMISSION FAILURE. I'M EVEN MORE SHOCKED TO FIND ENDLESS COMPLAINTS ONLINE ABOUT THE SAME ISSUES AND FORD HAS DONE NOTHING. I OWNED MY PREVIOUS CAR FOR 13 YEARS, WITH NO MAJOR ISSUES. IT WAS STILL RUNNING WHEN I PURCHASED MY FORD ESCSPE. I CAN'T AFFORD TO PAY THOUSANDS OF DOLLARS TO FIX A MAJOR ISSUE THAT SHOULDN'T HAVE FAILED WITHIN 5 YEARS. THIS IS SAD AND FORD SHOULD BE ASHAMED THAT THEY ARE STEALING, BY PUTTING OUT SUCH A POOR PRODUCT TO THE WORKING CLASS PEOPLE AND REFUSING TO TAKE ACCOUNTABILITY.

Mileage: 77,000

Jul 17, 2019

MY CAR IS THROWING P0303 CODE CYLINDER 3 MISFIRE AND ALSO LOOSING ENGINE COOLANT. CAR HAS GONE INTO LIMP MODE. THERE WAS A RECALL BUT IT DIDN'T FIX THE ISSUE. THERE ARE SEVERAL FORUMS WITH MANY PEOPLE HAVING THE SAME PROBLEM WITH MECHANICS TELLING THEM THAT ITS A HEAD GASKET ISSUE AND THEY NEED A NEW ENGINE. MY CAR HAS 109,000 MILES. WE REPLACED THE SPARK PLUGS AND SWITCHED THE COILS TO SEE IF THE MISFIRE WOULD SWITCH AND IT HASN'T. WE HAVE DRAINED AND REFILLED THE COOLANT AND IT IS STILL LOOSING BUT NO VISIBLE LEAKS. CAR SOMETIMES STARTS ROUGH.

Jul 16, 2019

WHILE DRIVING TO WORK THE CAR LOST POWER SUDDENLY. THE CAR THEN SUDDENLY ACCELERATED ON ITS OWN AND LOST POWER. THE CAR BECAME IMMOBILE AFTER JUST A FEW MINUTES OF THE INITIAL PROBLEM THE CAR WAS STUCK ON THE ROAD UNTIL HELP COULD ARRIVE TO LOVE IT OFF THE ROAD WHERE IT CAME TO A STOP. THE CAR WAS ON A COUNTY ROAD, IN MOTION, WITH NO PRE INDICATION OF ISSUE. THE CARS TRANSMISSION IS BELIEVED BAD FROM THIS EVENT AND THE CAR CAN NOT BE DRIVEN OR MOVED UNDER ITS OWN POWER.

Mileage: 140,000

Jul 16, 2019

COOLANT ISSUES SIMILAR TO THOSE INCLUDED IN THE PART 573 SAFETY RECALL 17V-209, THOUGH MY VEHICLE WAS MANUFACTURED A FEW WEEKS LATER AND NOT INCLUDED IN THAT RECALL, AS WELL AS ELECTRICAL ISSUES THAT WERE SIMILAR TO OTHER RECALLS THAT DIDN'T INCLUDE MY VIN. IN JUNE 2019, IT STARTED WITH THE VEHICLE NOT TURNING ON OR SHIFTING OUT OF PARK INTERMITTENTLY.. WORK WAS PERFORMED AND THEN A WEEK LATER P0303 CYLINDER MISFIRE.. AGAIN WORK WAS COMPLETED, THE CODE CAME BACK, AND NOW FORD IS RECOMMENDING REPLACING THE ENGINE BUT WILL NOT COVER THE COSTS DUE TO BEING 5 YEARS AND IN EXCESS OF 60K MILES. TOOK FOR 2ND OPINION AND RAN OUT OF COOLANT AND OVERHEATED LESS THAN 5 MILES AWAY FROM FORD DEALERSHIP, EVEN THOUGH THEY JUST REPLACED THE COOLANT OVERFLOW TANK AND FILLED IT.. CONTINUES NEED COOLANT EVERY FEW MILES. SEEMS CRAZY THAT A VEHICLE THAT STAYED ON TOP OF ROUTINE MAINTENANCE AND HAS NOT BEEN INVOLVED IN AN ACCIDENT OR EXCESSIVE CONDITIONS WOULD NEED A NEW ENGINE AT LESS THAN 94K MILES AND IS THE CONSUMER'S RESPONSIBILITY TO FOOT THE BILL. I'VE ALREADY SPENT ALMOST $3K ON THIS ISSUE AND FORD VERBALLY TOLD ME JUST THE ENGINE WOULD BE AROUND $7-8K WITHOUT LABOR. THEY ALSO HAD THEIR SALES DEPARTMENT CALL ME AND OFFER TO "TAKE A COUPLE HUNDRED OFF A NEW VEHICLE" FOR MY CURRENT ONE. VERY DISHEARTENING TO HEAR THAT WHEN I'VE TAKEN CARE OF THE VEHICLE AS THE SOLE OWNER, LESS A FEW RECOMMENDED TIRE ROTATIONS.

Mileage: 92,000

Jul 12, 2019

10/16/18 AT 94201 MILES: VEHICLE HAD COOLENT SYSTEM RECALL DONE. 11/19/18 AT 96375 MILES: VEHICLE WOULD NOT START. IT COMPLETELY SHUT DOWN DUE TO LOW COOLENT/ OVER HEATING CODES. HAD TO BE TOWED TO DEALERSHIP. 12/6/18 AT 97874 MILES: VEHICLE HAD POWER REDUCED TO APPROX 15 MILES PER HOUR. TAKEN TO DEALERSHIP AGAIN WITH LOW COOLENT CODES. 06/04/19 AT 107000 MILES: CHECK ENGINE LIGHT CAME ON. OWNER ADDED COOLENT PRIOR TO TAKING BACK TO DEALERSHIP. DEALERSHIP DID CAMERA DIAGNOSIS OF COOLENT IN THE PISTONS. UPON TAKING ENGINE APART FOUND A DEFECTIVE SCRATCH LINE THAT CROSSES OVER THE PISTON TO THE COOLENT PACK. FORD CLAIMING IT IS NOT COVERED BY RECALL, THEREFORE NOT COVERED AT ALL..

Mileage: 96,375

Jul 9, 2019

WHEN IDLING THE VEHICLE SHAKES REALLY BAD. GOING DOWN THE ROAD EVERYTHING IS FINE. AS SOON AS YOU STOP IT STARTS SHAKING AGAIN. IT DOESN'T MATTER IF THE AC IS ON OR OFF. OCCASIONALLY THERE IS HESITATION WHEN GIVING IT GAS AND TRYING TO MOVE. SOMETIMES IT WON'T GO FROM REVERSE TO DRIVE SMOOTHLY.

Mileage: 77,000

Jul 4, 2019

TRANSMISSION FAULT SERVICE NOW LIGHT HAS CAME ON. THE CAR NO LONGER SHIFTS GEARS WHILE DRIVING. PREVIOUSLY, THE CAR WOULD SHIFT VERY HARD, ROCKING THE VEHICLE WHILE DRIVING, STALLING, THEN GOING BACK TO ACCELERATION.

Mileage: 66,500

Jul 3, 2019

MY 2014 FORD ESCAPE WAS EFFECTED BY A RECALL ISSUE IN NOVEMBER 2018, THE ENGINE OVERHEATS CAUSING THE COOLANT CONTAINER TO CRACK AND LEAK. I PAID $175 TO REPLACE THE COOLANT CONTAINER IN JUNE 2018. HOWEVER IN NOVEMBER 2018 MY CAR COMPLETELY TURNED OFF WHILE DRIVING ON BUSY CITY STREET AT STOP LIGHT AND SMOKE STARTED COMING IN THROUGH THE VENTS AND THE ENGINE CAUGHT ON FIRE. WE NEVER RECEIVED NOTICE OF A RECALL UNTIL AFTER THIS INCIDENT OCCURED. AFTER 30 DAYS FORD FINALLY ACCEPTED RESPONSIBILITY AND PAID $9500 TO REPLACE THE DAMAGE. THE VEHICLE PROBABLY SHOULD HAVE BEEN TOTALLED. THE DAY I GOT IT BACK FROM THE DEALERSHIP I HAD NOTICED A CHANGE IN THE TRANSMISSION. I MADE THE DEALERSHIP AWARE BUT THEY SAID THEY DIDN'T NOTICE A DIFFERENCE. MY TRANSMISSION COMPLETELY DIED 4 MONTHS LATER WHILE DRIVING AND I HAVE BEEN TRYING TO GET AHOLD OF SOMEONE FROM FORD CORPORATION SINCE, IT HAS BEEN WAITING AT A DIFFERENT FORD DEALERSHIP FOR A MONTH AND A HALF AGO. TODAY WE FINALLY RECEIVED A CALL FROM THE FORD GOODWILL DEPARTMENT OFFERING $1200 OFF THE TOTAL COST OF OVER $5200. UNFORTUNATELY WE CANNOT AFFORD THE $4000 AND THEY WILL NOT PAY ANYTHING OF WE DECIDE TO HAD A USED TRANSMISSION PUT IN. THEY WILL NOT GIVE US A PHONE NUMBER OR EMAIL TO FORD LEGAL JUST A FAX. SOMEONE DID TELL US ON FRIDAY THEY WERE TRANSFERRING OUR CASE TO LEGAL AND WOULD CALL THE DEALERSHIP AND US ON MONDAY BUT THEY DID NOT AND THE PERSON I TALKED TO TODAY SAYS THERE IS NO RECORD OF US SPEAKING TO ANYONE FRIDAY OR ANYTHING BEING TRANSFERRED TO LEGAL. IT HAS BEEN IMPOSSIBLE TO GET ANY INFORMATION FROM ANYONE AND WE ARE UNSURE WHAT WE SHOULD DO. I HAVE A WARRANTY FROM THE WORK DONE IN NOVEMBER REGARDING THE RECALL ISSUE BUT FORD IS SAYING THIS IS UNRELATED AND WILL NOT BE COVERED, BUT ALSO WILL NOT TEAR APART THE TRANSMISSION TO DETERMINE THE ACTUAL CAUSE DUE TO THE LABOR COST UNLESS WE PAY FOR THAT AS WELL.

Mileage: 93,000

Jul 2, 2019

VEHICLE WILL STOP RUNNING WHILE IN MOTION WITHOUT WARNING. ALSO GIVES OFF HEAVY EXHAUST SMELL. THERE IS ONLY 100K MILES ON IT. IT IS DUE TO A COOLANT LEAK INTO THE CYLINDER 3 CAUSING A GASKET TO BLOW (SEE ATTACHMENT FOR INVOICE AND DETAILS). WE WERE TOLD BY THE CAR SHOP THAT THIS HAS HAPPENED TO AT LEAST 5 OTHER FORD ESCAPE OWNERS (WE AREN'T IN A HEAVILY POPULATED AREA, SO THIS IS SIGNIFICANT). CAR IS NOT SAFE TO DRIVE DUE TO HIGH RISK OF BECOMING STRANDED, WHICH IS NOT SAFE DUE TO TRAFFIC, CHILDREN ON BOARD, HOT WEATHER, AND SO ON.

Mileage: 100,000

Jun 25, 2019

VEHICLE IS OVERHEATING. COOLANT LEVEL STAYS LOW EVEN AFTER REFILLING. NO VISIBLE LEAKS.

Mileage: 79,000

Jun 18, 2019

ON MAY 13, 2019 TOOK MY CAR TO WORLD FORD TO FIX DOOR RECALL, AS I WAS THERE WAS TOLD I NEEDED BRAKE AND TRANSMISSION FLUID REPLACED. AFTER I GOT MY CAR BACK I WAS SITTING IDLE AND MY TEMP GAUGE WHEN TO HIGH TURN OFF ENGINE SAFELY. I CHECKED THE COOLANT LEVEL IT WAS LOW ADDED WATER. I DIDN'T HAVE TO DO THIS EVERY DAY. ON MAY 31ST, CHECK ENGINE LIGHT CAME ON, MY HUSBAND CHECKED THE DIP STICK WHICH HAD NO OIL ON IT. I HAD THE CAR TOWED TO WORLD FORD, WHO STATED I NEEDED A NEW ENGINE BECAUSE I HAD METAL SHAVINGS IN MY ENGINE AND OIL ALL OVER MY CAR FROM AN OIL LEAK. THEY TOLD ME IT WAS THE PEOPLE WHO CHANGE MY OIL LAST, I SPOKE WITH THAT COMPANY AND HAVE HAD BOTH THE OWNERS GO TO WORLD FORD, WHO HAS YET TO RETURN EITHER OF THEIR PHONE CALLS. I HAVE PICTURES OF OIL UNDERNEATH MY CAR, WHICH IN TURN HAS ALL STEMMED FROM MY COOLANT BEING LOW AND OVERHEATING MY ENGINE THAT HAS CAUSED AN OIL LEAK. I CALLED FORD AND WAS TOLD THEY HAVE NO RESOURCES TO FIX MY CAR AND I CAN PAY FOR IT AND IF THEY DO COME UP WITH A PROGRAM I MIGHT BE ABLE TO BE REIMBURSED. WORLD FORD CALLED ME ON JUNE 14TH AND SAID THEY FIXED THE COOLANT RECALL, BUT NO ONE IS FIXING MY ENGINE SO I CAN COME GET THE CAR. THIS IS ABSOLUTELY RIDICULOUS THAT BECAUSE OF THEIR FAULTY ENGINEERING I HAVE BEEN WITHOUT A CAR FOR 3 WEEKS.

Mileage: 67,000

Jun 13, 2019

THE CAR BEGAN TO OVERHEAT ONE MORNING WHILE IT WAS BEING DRIVEN ON A CITY STREET ABOUT 45-50 MPH. THE CAR HAD BEEN PARKED OVERNIGHT FOR 8-10 HOURS BEFORE BEING DRIVEN. THERE WERE NO VISIBLE SIGNS OF LEAKING COOLANT WHERE THE CAR HAD BEEN PARKED. WHEN COOLANT WAS ADDED AFTER THE CAR HAD COOLED OFF IT POURED OUT THE BOTTOM OF THE CAR. IT WAS TAKEN TO A MECHANIC AND THERE WAS A LEAK/HOLE IN THE COOLANT TANK.

Mileage: 100,000

Jun 12, 2019

I BEGAN LOSING COOLANT AFTER TAKING MY CAR IN FOR COOLANT LEVEL SENSOR RECALL. I ADDED WATER A FEW TIMES BEFORE I DECIDED NOT TO DRIVE IT ANYMORE. COULDN'T FIGURE OUT WHAT WAS HAPPENING TO MY 5 YEAR OLD LESS THAN 50,OOO MILE CAR. COULDN'T SEE ANY LEAK ON THE GROUND, DECIDED TO CHECK OIL, DIP STICK CAME BACK WITH WATER IN THE OIL. HAD IT TOWED TO FORD AND MY ENGINE IS BLOWN, WATER ALL IN TH ENGINE

Mileage: 40,550

Jun 10, 2019

MARCH OF 2018 ENGINE STARTING TICKING, TOOK IT IN FOR OIL CHANGE AND ASKED THEM TO LOOK AT IT. GOT IT BACK THE NEXT DAY, THEY TOLD ME IT WAS THE ALTERNATOR TICKING AND IT WAS NORMAL. NOVEMBER OF 2018 TOOK MY CAR BACK IN FOR TIRE, TOLD THEM ABOUT THE TICKING AGAIN AND SAID IT WASN'T THE ALTERNATOR, SOMETHING IN THE ENGINE IS TICKING AND NOW IT IDLES ROUGH. THE PUT NEW TIRES ON IT DID A 60,000 MILE ENGINE PERFORMANCE (I ONLY HAD 50,000 MILES ON IT) FEBRUARY 2019, I WAS GETTING ON THE EXPRESSWAY AND IT STARTED SHAKING, THE RPM'S JUMPED TO 5 AND BACK DOWN TO 2 THEM BACK UP TO 5 OR 6 AND THE CAR WOULD NOT MAINTAIN SPEED. TOOK THE CAR TO BRONDE'S FORD, THEY TOLD ME I BLEW THE ENGINE. PAID TO HAVE THE SHORT BLOCK REPLACED, GOT THE CAR BACK 2 WEEKS LATER, NO MORE TICKING. DROVE MY CAR FOR 4 WEEKS AND ON MY WAY TO WORK ON US223, 55MPH, MY CAR STARTED VIBRATING AGAIN AND MY ENGINE LIGHT WAS FLASHING. I TURNED AROUND, TOOK THE CAR BACK TO BRONDE'S AGAIN. THEY HAD THE CAR FOR 4 WEEKS THIS TIME. REPLACED THE SHORT BLOCK AND HEAD GASKET AGAIN. BOTH TIMES IT WAS CYLINDER 4 IN MY ENGINE. THIS TIME I HAD MY CAR FOR 13 DAYS. I WAS GETTING ON THE EXPRESSWAY 23 NORTH AND BARELY GOT GOING AND THE CAR DID A LITTLE HESITATION. I LOOKED OVER AT THE PANEL AND THE ENGINE LIGHT WAS FLASHING AGAIN. I PULLED OFF THE VERY NEXT EXIT AND THE CAR WAS SMOKING SO BAD, I THOUGHT IT WAS GOING TO CATCH ON FIRE. PULLED OFF AND CALLED BRONDE'S TO SEND A TOW TRUCK. I COULD SMELL A SWEET SMELL AND KNOW I BLEW A HEAD GASKET AGAIN. BRONDE'S SENT A CAR HAULER AND LOADED IT UP. HE TURNED THE KEY AND IT READ ENGINE FAILURE FAILURE FAILURE. IN 14 1/2 WEEKS I HAVE HAD MY CAR IN 3X FOR A BLOWN ENGINE. I AM STILL MAKING PAYMENTS ON THIS CAR AND IT IS JUNK.

Mileage: 58,000

Jun 5, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 65 MPH, THE TRANSMISSION FAULT SERVICE NOW WARNING MESSAGE APPEARED ON THE INSTRUMENT PANEL. THE VEHICLE WAS TAKEN TO LUNDGREN FORD (LOCATED AT 900 OLD HWY 53, EVELETH, MN 55734, (800) 954-0323) WHERE IT WAS DIAGNOSED THAT THE TRANSMISSION NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED. THE FAILURE MILEAGE WAS 91,000. THE VIN WAS UNKNOWN.

Mileage: 91,000

May 24, 2019

WHILE DRIVING ABOUT 45 MPH ON A CITY STREET, THE CAR BEGAN TO FLASH WARNING SIGNALS STATING TO PULL OVER IMMEDIATELY. WHEN I LOOKED AT THE TEMPERATURE GAUGE IT WAS ALL THE WAY ON HOT, BUT HAD NOT STARTED SMOKING YET. THE DEALERSHIP STATED THAT THE HEAD GASKET FAILED WHICH RESULTED IN THE OVERHEATING. THE CAR WAS BOUGHT CERTIFIED PRE-OWNED FROM A FORD DEALERSHIP IN 2017, AND I HAVE ALREADY HAD TO REPLACE THE TRANSMISSION, A COOLANT LEAKAGE PROBLEM, BRAND NEW BRAKES, NEW TIRES DUE TO "WEAR AND TEAR," AND NOW THIS. MY COMMUTE HOME FROM WORK TAKES ABOUT AN HOUR ON A HIGHWAY THEN CITY STREET, AND WHILE ON THE HIGHWAY THE CAR GAVE NO SIGNAL TO THE RISING TEMPERATURE. WHILE ON THE CITY STREET I WAS AT A RED LIGHT, AND ONCE I STARTED TO DRIVE AGAIN THE CAR THEN FLASHED TO PULL OVER AND THE ENGINE LIGHT CAME ON. LOOKING AT THE PROBLEMS OTHER FORD ESCAPE 2014 CAR OWNERS HAVE HAD, AND THE RECALLS THAT OCCURRED BEFORE MY CAR, IT SEEMS THAT THIS ENGINE PROBLEM IS BEING EXPERIENCED AMONGST OTHERS, AND COULD BE DUE TO THE COOLANT RECALL THAT OCCURRED IN APRIL OF 2017. PERSONALLY, I BOUGHT MY CAR IN SEPTEMBER OF 2017 AND WAS UNAWARE OF SUCH RECALL.

Mileage: 71,000

May 24, 2019

THE CAR'S ENGINE WILL CUT OFF, LIGHTS AND ELECTRICITY WILL STAY ON, BUT THE ENGINE WILL CUT OUT WHILE DRIVING. ACCELERATION IS LOST, AND CANNOT START MOVING AGAIN UNTIL THE CAR IS PUT IN PARK, TURNED OFF, AND TURNED BACK ON. THIS IS WHILE THE CAR IS IN MOTION. THIS HAS HAPPENED AT 30 MPH AND SLOWER, AS WELL AS 55 MPH. THE CAR WILL GIVE AN ENGINE FAULT OR ENGINE FAILURE AND BEGIN JERKING. THIS HAPPENS ON THE HIGHWAY AND CITY STREETS. THE MOST RECENT TIME, THE CAR BEGAN JERKING AFTER TURNING AND COULD NOT STAY ON FOR LONGER THAN 10 SECONDS BEFORE SHUTTING OFF. THIS HAS HAPPENED AT LEAST 6-10 TIMES, AND ALMOST CAUSED CAR ACCIDENTS. MULTIPLE PARTS HAVE BEEN REPLACED, AND THE ISSUE STILL HAPPENS.

Mileage: 34,000

May 22, 2019 Fire

TL* THE CONTACT OWNED A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 60 MPH, SMOKE WAS SEEN IN THE REAR VIEW MIRROR AND THE DASHBOARD LIGHTS HAD SHUT OFF. AFTER STOPPING THE VEHICLE, IT WAS DISCOVERED THAT FLAMES WERE PRESENT UNDER THE HOOD. THE FIRE DEPARTMENT WAS CALLED TO THE SCENE AND EXTINGUISHED THE FLAMES. DURING THE INCIDENT THE VEHICLE WAS DESTROYED AND TOWED AWAY. A FIRE REPORT WAS TAKEN AT THE SCENE. THE CAUSE OF THE FAILURE WAS NOT DETERMINED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE CONTACT STATED THAT THE VEHICLE WAS SERVICED FOR NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE) THREE WEEKS PRIOR TO THE FAILURE AT PRATER FORD (704 S WALL ST, CALHOUN, GA 30701). THE FAILURE MILEAGE WAS 140,000.

Mileage: 140,000

May 17, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 75 MPH, THE VEHICLE STALLED. THE CONTACT PULLED OVER, DISCONNECTED AND RECONNECTED THE BATTERY, AND RESTARTED THE VEHICLE. THERE WERE NO WARNING INDICATORS ILLUMINATED. THE DEALER WAS NOT CONTACTED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE FAILURE MILEAGE WAS 53,000.

Mileage: 53,000

May 16, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING APPROXIMATELY 40 MPH, THE VEHICLE OVERHEATED AND STALLED. IN ADDITION, THE CHECK ENGINE WARNING INDICATOR ILLUMINATED. THE VEHICLE WAS TOWED TO BARBEE'S FREEWAY FORD (4471 E EVANS AVE, DENVER, CO 80222) WHERE IT WAS DIAGNOSED THAT THE COOLING SYSTEM SENSOR FAILED AND NEEDED REPLACEMENT. THE CONTACT RECEIVED A RECALL NOTIFICATION FOR NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING) IN APRIL OF 2019. THE VEHICLE WAS REPAIRED IN 2018 PER AN INTERIM REPAIR, BUT THE FAILURE RECURRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 89,000.

Mileage: 89,000

May 7, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT THE CHECK ENGINE INDICATOR KEPT RANDOMLY FLASHING AND THE VEHICLE WAS RUNNING HOT. AN INDEPENDENT MECHANIC PROVIDED A COOLANT PRESSURE CHECK AND FOUND COOLANT IN THE RESERVOIR. THE MECHANIC STATED THAT THE HEAD GASKET WAS CRACKED AND THE COMPRESSION SENSOR MAY NEED TO BE REPLACED. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE DEALER (NORTH BAY FORD, 1999 SOQUEL AVE, SANTA CRUZ, CA 95062, (831) 457-5858) REPAIRED THE VEHICLE, BUT THE FAILURE RECURRED THE NEXT DAY. THE CONTACT ALSO STATED THAT THE THERMOSTAT WAS NOT REGULATING THE HEAT AND THE COOLANT LEVEL WAS FLUCTUATING. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 40,992. *BF *TR

Mileage: 40,992

Apr 29, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT THE VEHICLE WAS LEAKING ANTIFREEZE. THE VEHICLE WAS TAKEN TO VIVA AUTO GROUP (414 EXECUTIVE CENTER BLVD, EL PASO, TEXAS 79902, (915) 834-6200), BUT THE PART WAS NOT AVAILABLE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING); HOWEVER, THE PART NEEDED FOR THE REPAIR WAS NOT AVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE CONTACT CALLED GALPIN FORD (LOCATED AT 15505 ROSCOE BLVD, NORTH HILLS, CA 91343, (818) 787-3800) AND WAS INFORMED THAT THE PART WAS NOT AVAILABLE. THE MANUFACTURER WAS NOTIFIED AND STATED THAT THE PART WOULD BECOME AVAILABLE IN DECEMBER OF 2018. THE APPROXIMATE FAILURE MILEAGE WAS 71,000. PARTS DISTRIBUTION DISCONNECT.

Mileage: 71,000

Apr 24, 2019

MY CAR WAS SERVICED FOR THE COOLANT RELATED RECALL. LESS THAN A MONTH LATER THE LOW COOLANT LIGHT CAME ON AND I BROUGHT THE VEHICLE BACK IN FOR SERVICE. THEY DIDN'T SEE A LEAK AND BELIEVED THERE MUST HAVE BEEN AN AIR BUBBLE IN THE SYSTEM THAT WORKED ITSELF OUT AND ADDED MORE COOLANT. LESS THAN A MONTH AFTER THAT THE LOW COOLANT LIGHT CAME BACK ON AGAIN AND I BROUGHT THE VEHICLE IN TO BE SERVICED. THEY DETERMINED THAT THERE'S AN INTERNAL LEAK AND COOLANT HAD BEEN LEAKING INTO THE ENGINE. THEY HAVE RECOMMENDED REPLACING THE ENGINE AND SAY THAT THIS ISSUE IS DIFFERENT THAN THE COOLANT RELATED RECALL THAT MY CAR HAD BEEN ORIGINALLY SERVICED FOR. THIS CAR IS A 2014 WITH LESS THAN 100K MILES ON IT. IT SHOULD NOT NEED A NEW ENGINE.

Mileage: 90,000

Apr 23, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT AFTER SHUTTING OFF THE ENGINE, THE VEHICLE FAILED TO RESTART. ALSO, THE GEAR SHIFTER FAILED TO ENGAGE IN REVERSE OR DRIVE AND CAUSED THE VEHICLE TO STALL. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO STATED THAT THE VEHICLE MIGHT BE EXPERIENCING GEAR SHIFTER FAILURE. THE DEALER AND MANUFACTURER WERE NOT CONTACTED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 56,000.

Mileage: 56,000

Apr 23, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT THE AIR CONDITIONER AND HEATER BLEW OUT INSULATION INSIDE THE VEHICLE THROUGH THE VENTS. ADDITIONALLY, THE PUSH TO START BUTTON FAILED TO WORK AND AN ABNORMAL NOISE WAS HEARD. THERE WERE NO WARNING INDICATORS ILLUMINATED. THE LOCAL DEALER WAS NOT CONTACTED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC, BUT NO ASSISTANCE WAS PROVIDED. THE MANUFACTURER WAS CONTACTED AND REFERRED THE CONTACT TO NHTSA. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE FAILURE MILEAGE WAS 49,000.

Mileage: 49,000

Apr 23, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING APPROXIMATELY 55 MPH, THE CHECK ENGINE AND ENGINE OVERHEATING WARNING INDICATORS ILLUMINATED ON THE INSTRUMENT PANEL. THERE WAS NO COOLANT LEAK; HOWEVER, THE CONTACT TOPPED OFF THE COOLANT ON THOSE OCCASIONS ANYWAY. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). A DEALER WAS NOT CONTACTED. THE MANUFACTURER WAS NOTIFIED. THE APPROXIMATE FAILURE MILEAGE WAS 80,000.

Mileage: 80,000

Apr 17, 2019

MY CAR OVER HEATED WHILE DRIVING. SO I PULLED OVER AND LET IT COOL DOWN. I THEN TOOK IT TO THE SHOP AND I WAS TOLD I NEEDED A NEW CYLINDER HEAD WHEN ASKED WHY IT OVER HEATED THEY REFEREED TO THE COOLANT SYSTEM BUT DIDN'T KNOW WHY THE COOLANT WAS GETTING THERE. AFTER DOING SOME RESEARCH ONLINE THE WAY THEY EXPLAINED EVERYTHING SEEMS VERY SIMILAR TO THE RECALL NUMBER 17V209000 OR FORD RECALL NUMBER 17S09

Mileage: 65,000

Apr 9, 2019

LOW COOLANT LIGHT APPEARED. HAD OIL CHANGED/FLUIDS TOPPED. A WEEK LATER, COOLANT LIGHT APPEARED AND CHECK ENGINE LIGHT CAME ON. TOOK IT BACK TO PLACE THAT CHANGED MY OIL. COOLANT WAS NOT LOW. THEY USED A DIAGNOSTIC CODE READER THAT INDICATED CYLINDER 2 HAD MISFIRED 3 TIMES (I WAS UNAWARE). A FEW DAYS LATER, TOOK IT TO HAVE CHECKED (FIRESTONE). THEY USED A DIAGNOSTIC CODE THAT SAID THE SAME THING BUT ONE OF THE MECHANICS RELATED HE HAD JUST FIXED A FORD ESCAPE HAVING THE SAME ISSUE AND THAT THEY HAD THEN FIGURED OUT THERE WAS A RECALL FOR THE PROBLEM. FORD SAYS MY VIN IS NOT INCLUDED IN THE RECALL. THERE HAS BEEN NO LEAK NOTED THIS ENTIRE TIME. THE ENGINE LIGHT WENT OFF. I DROVE IT APPROXIMATELY 25 MINUTES, WENT IN TO A BUSINESS FOR 2 HOURS, CAME BACK OUT AND STARTED THE CAR, PULLED OUT OF THE PARKING LOT AND SAW THE CHECK ENGINE LIGHT AND A MESSAGE THAT THE ENGINE WAS OVERHEATING AND PULL OVER SAFELY (WHICH I DID IMMEDIATELY). THERE WAS NO OBVIOUS SIGN THAT THE ENGINE WAS OVERHEATING (STEAM, ODOR, LEAKING, ETC). THE VEHICLE WOULD ONLY START, BUT WOULD NOT ACCELERATE AT ALL. HAD IT TOWED TO JOHNSON CITY FORD WHICH TOLD ME THAT THEY WOULD HAVE TO DROP THE ENGINE TO DETERMINE THE CAUSE ($1700) AND THAT THE TOTAL REPAIR JOB WOULD COST BETWEEN $3500-$7000+ DEPENDING ON THE CAUSE AND DAMAGE (MAY HAVE TO HAVE A NEW MOTOR!). HE THEN TOLD ME IT WOULD BE ABOUT 3 +WEEKS BEFORE THEY COULD REPAIR IT SINCE THERE ARE 5 JUST LIKE IT WAITING TO BE SERVICED! I QUESTIONED HIM ABOUT THIS. HE RELATED THAT THERE WERE 5 FORD ESCAPES WITH A COOLANT LOW/OVERHEATING ISSUE CURRENTLY IN THEIR SHOP. MY VEHICLE WAS BOUGHT BRAND NEW. IT IS GARAGE KEPT AND SERVICED REGULARLY. I DO NOT UNDERSTAND HOW A VEHICLE THAT IS WELL-KEPT AND HAS UNDER 90,000 MILES CAN SUDDENLY, WITHOUT WARNING OR REASON, HAVE THIS KIND OF ISSUE? WHY HASN'T THERE BEEN A RECALL ON THIS ISSUE?

Mileage: 88,000

Apr 5, 2019

A WEEK AFTER PURCHASING 2/21/2017. THE ESCAPE STARTING RUNNING HOT THEN IT SHUT DOWN THE CAR ACCELERATION . TOOK IT BACK BECAUSE IT UNDER THE FACTORY WARRANTY, THEY SAID THE HEAD GASKET WERE BLOWN AND LEAKING COOLANT INTO THE ENGINE. MIND YOU IT ONLY RAN HOT FOR ONE MINUTE. THEY REPAIRED IT. A YEAR LATER IN FEBRUARY BEFORE MY BIRTHDAY 2/26- I SAY 2/19. THE TRANSMISSION WENT OUT, THEY REPAIRED THAT. A RECALL ON OWN COOLANT VALVE WAS FIXED BY DEALER. NOW IN THE BEGINNING OF MARCH THE WATER PUMP AND ENGINE PROBLEM HAS COME BACK. IF FILL THIS MODEL OF 2014 FORD ESCAPE IS A LEMON AND I SHOULD BE COMPENSATED FOR ALL MY INCONVENIENCE. IT BEEN NOTHING BUT A MONEY DRAIN AND THE DEALERSHIP IS ROBBING ME. I TOOK IT UP THERE TO SEE IF THEY COULD REPAIR THE PROBLEM, BUT THEY SAID MY WARRANTY HAS EXPIRED. THE TOLD ME THE WATER PUMP NEEDED TO BE FIX AND IT WILL COST $1,300 AND THAT I HAVE TO PAY THAT BEFORE THE CAN LOOK AT HEAD GASKET. TO MUCH TO PAY AND THERE CHARGING A SERVICE FEE WHICH IS OK BUT THE NEVER SAID ANYTHING ABOUT A STORAGE FEE. I HAD A TRIP SCHEDULE FOR DOMINICAN REPUBLIC. SHE TOLD ME THEY LEFT A MESSAGE DAYS AFTER BUT NEVER RECEIVED IT. I ASKED IF THEY CAN WAVE THE STORAGE FEE AND I'LL PAY THE REST BUT WAS TOLD THEY CAN'T DO SO. I ASKED TO SPEAK WITH THE MANAGER AND WAS TOLD HE WON'T BE BACK UNTIL MONDAY AND IT FRIDAY. CALLED CORPORATE THEY WERE NO HELP AT ALL. FORD MOTOR COMPANY IS THE WORST CAR COMPANY AND THEY DO NOT HELP THERE CUSTOMERS. POOR CUSTOMER SERVICE AND NO SOLUTION TO A PROBLEM THAT THEY NO THIS CAR IS KNOWN FOR. I'LL BE TAKING LEGAL ACTION IN A CIVIL SUIT AGAINST FORD. THANK YOU FOR LISTENING AND IF ANYONE HAS A SOLUTION PLEASE CONTACT ME. THANK YOU. ( I WILL NEVER THINK FORD FIRST- YOUR LAST). THEY WANT $160.00 FOR STORAGE.

Apr 4, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. ON SEVERAL OCCASIONS, WHILE DRIVING 10-45 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE CONTACT WAS ABLE TO RESTART THE VEHICLE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC TO BE DIAGNOSED, BUT THE MECHANIC WAS UNABLE TO RETRIEVE A FAULT CODE. THE VEHICLE WAS NOT REPAIRED. CLONINGER FORD (LOCATED AT 1241 US HWY 70 SE, HICKORY, NC 28602, (828) 615-8653) WAS CALLED AND THE CONTACT WAS INFORMED THAT THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 14V495000 (ELECTRICAL SYSTEM). THE FAILURE RECURRED APPROXIMATELY 8-10 TIMES. THE MANUFACTURER WAS NOTIFIED. THE APPROXIMATE FAILURE MILEAGE WAS 35,000.

Mileage: 35,000

Apr 4, 2019

SHORTLY AFTER STARTING THE CAR (ON A COOL FALL DAY) A WARNING CAME ON THE DASH SAYING "STOP IMMEDIATELY, ENGINE OVERHEATING". THIS CAUSED THE CAR TO LIMIT MY ABILITY TO DRIVE THEREFORE I HAD O SLOWLY STOP AT CURBSIDE OF HIGHWAY. I CHECKED THE COOLANT WHICH WAS BASICALLY GONE. WHICH DIDN'T SEEM RIGHT ESPECIALLY SINCE I HAD JUST PURCHASED THE CAR TWO MONTHS PRIOR. ADDITIONALLY, THE ENGINE WASN'T SMOKING OR VISIBLY SHOWING SIGNS OF OVERHEATING. WHEN I TOOK IT TO THE SHOP THEY WERE NOT ABLE TO IDENTIFY ANY ISSUES. THERE WERE NO POOLS OF LIQUID UNDERNEATH THE CAR THAT WOULD INDICATE A LEAK. HOWEVER, THE ISSUE GOT WORSE AND I HAVE HAD TO FILL THE COOLANT TANK EVERY OTHER WEEK. TOOK THE ESCAPE INTO THE DEALERSHIP, THEY SAID IT WOULD BE A HOSE LEAK AND THE COOLANT NEEDED TO BE FLUSHED FOR 800 DOLLARS. I DIDN'T HAVE THE MONEY, SO TOOK IT TO ANOTHER SHOP. THAT SHOP RAN TESTS BUT COULDN'T FIND A LEAK IN THE HOSING SYSTEM NOR COULD THEY SEE SIGNS OF COOLANT ON OTHER PARTS OF THE ENGINE. MY CAR CONTINUED TO SUCK DOWN COOLANT FOR NO APPARENT REASON UNTIL FINALLY THE TIMING BELT BROKE.

Apr 3, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 45 MPH, THE CHECK ENGINE WARNING INDICATOR ILLUMINATED AND THE VEHICLE STARTED TO OVERHEAT. THE VEHICLE WAS TAKEN TO FORD MOTOR CREDIT COMPANY (LOCATED AT 9009 CAROTHERS PKWY, FRANKLIN, TN 37067, (800) 727-7000) AND WAS INFORMED THAT THE CYLINDER HEAD WAS FRACTURED AND THE ENGINE NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE VEHICLE WAS INCLUDED IN NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING), BUT THE PART WAS NOT AVAILABLE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE DEALER WAS NOT CONTACTED. THE APPROXIMATE FAILURE MILEAGE WAS 36,000. PARTS DISTRIBUTION DISCONNECT.

Mileage: 36,000

Mar 23, 2019

OUR 2014 FORD ESCAPE WAS RECENTLY UNDER REPAIR FOR THE JAN 2018 COOLANT RECALL. IT WAS COMPLETED ON MAR 15, 2019. ON MAR 16, 2019. OUR VEHICLE HAD DRIVEN ON THE FREEWAY FOR 3 HRS FOR A DISTANCE OF 200 MILES AND UPON EXITING THE FREEWAY AND STOPPING AT A STOPLIGHT. MY VEHICLE STOPPED MOVING AND MANAGED TO GET IT ONTO A GAS STATION PARKING LOT.. I HAD IT TOWED THE NEAREST CAR DEALERSHIP AND THEY HAD DIAGNOSED IT AND CAME BACK WITH THE TRANSMISSION AND COOLANT BEING THE ISSUE. THEY ARE CURRENTLY WANTING TO CHARGE US A LARGE AMOUNT OF MONEY TO FOX THE REPAIRS AND TRANSMISSION. I NOTICED THAT THERE IS A RECALL FOR THE TRANSMISSION AS OF SEPT 2018. NO RECALL MESSAGE HAS BEEN SENT OUT YET. HOWEVER. I BELIEVE MY VEHICLE IS AFFECTED AS IT WOULD MAKE AN UNUSUAL SOUND FROM TIME TO TIME WHEN SHIFTING FROM PARK, REVERSE, OR DRIVE AS IF IT GOT STUCK. I WOULD LOVE TO HAVE SOMEONE FROM THE FORD ASSIST ME WITH THIS BECAUSE IT DOESNT MAKE SENSE FOR ME TO DEAL WITH THIS IF THIS HAS BEEN A DISCOVERED ISSUE. PLEASE ASSIST ME IN THIS MATTER. THANK YOU.

Mileage: 93,300

Mar 21, 2019

VEHICLE HAD A RECALL FOR COOLANT SENSOR FIXED IN 01/2018. SINCE THEN COOLANT HAS RUN LOW, BEEN CHECKED NUMEROUS TIMES, HAD HOSES REPLACED, SEVERAL DIAGNOSTIC TESTS LOOKING FOR PROBLEMS, CAR HAS SINCE OVERHEATED, AND IS NOW IN NEED OF A NEW ENGINE BECAUSE OF COOLANT SYSTEM PROBLEM NOT FIXED BY A SENSOR ALERTING YOU TO A LEVEL OF FLUID. NO LEAK EXISTS SO COOLING FLUID IS WORKING ITS WAY THROUGH THE ENGINE SYSTEM SOME OTHER WAY. THE PROBLEM HAS PERSISTED FOR NEARLY 7 MONTHS NOW. THE VEHICLE RAN EMERGENCY MESSAGES ON THE DASH MERE MINUTES AFTER STARTING STATING THAT THE ENGINE WAS OVERHEATING AND TO IMMEDIATELY EXIT THE VEHICLE.

Mileage: 58,000

Mar 18, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 35 MPH, THE CHECK ENGINE WARNING INDICATOR ILLUMINATED AND THE COOLANT LEVEL WAS LOW. THE CONTACT DROVE THE VEHICLE TO SAM LEMAN FORD (LOCATED AT 1508 MORRISSEY DR, BLOOMINGTON, IL 6170, (309) 663-1331) WHERE IT WAS DIAGNOSED THAT THE COOLANT BYPASS VALVE NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS CONTACTED AND DID NOT ASSIST. THE FAILURE MILEAGE WAS 49,000.

Mileage: 49,000

Mar 14, 2019

MANUFACTURER NAME : FORD MOTOR COMPANY NHTSA RECALL NO. / MFR RECALL NO. : 17V-209 / 17S09 RECALL SUBJECT : ENGINE CYLINDER HEAD MAY LEAK OIL WHEN SITTING AT A STOP LIGHT, A MESSAGE CAME UP ON MY MESSAGE BOARD "SERVICE ENGINE NOW". THE VEHICLE STARTED TO SHUDDER AND THEN SMOKE CAME OUT FROM UNDER MY HOOD. I TURNED THE VEHICLE OFF IMMEDIATELY, WHILE STILL SITTING AT THE LIGHT, AND GOT OUT. THE VEHICLE WAS INSPECTED BY A FORD DEALERSHIP AND STATED THE HEAD NEEDED TO BE REPLACED DUE TO A CRACKED CYLINDER HEAD WITH AN ESTIMATED OF $3500.00. I DID NOT RECEIVE NOTICE OF THE RECALL REFERENCED ABOVE. MY VEHICLE HAS BEEN "LOSING" COOLANT, WHICH I HAD BEEN REFILLING QUITE OFTEN WITH NO VISIBLE LEAKS OR PUDDLES. IF I HAD KNOWN OF THE RECALL THIS COULD HAVE BEEN PREVENTED. DUE TO AN ISSUE BY THE MANUFACTURER, I AM NOW SOMEHOW RESPONSIBLE TO FIX THEIR PROBLEM. THIS HAS HAPPENED ON MANY OTHER VEHICLES AND SHOULD BE CORRECTED BY THE COMPANY. I AM THANKFUL I DID NOT HAVE MY YOUNG DAUGHTER WITH ME AT THE TIME.

Mileage: 150,000

Mar 13, 2019

THERE WAS A RECALL ON THE COOLANT SYSTEM, TO ADD A SENSOR DUE TO FORD HAVING CARS BLOWING MOTORS. AFTER THIS RECALL WAS DONE, I HAD THE CAR IN THE GARAGE ON AND OFF FOR OVER A MONTH, TO FIND OUT THAT TH COOLANT WAS LEAKING INTO THE NUMBER 4 CYLINDER. SO, THEY REPLACE THE MOTOR, NOT SURE ABOUT THE HEADS. THEN WITH IN WEEKS TROUBLE WITH THE TRANSMISSION.

Mileage: 39,000

Mar 10, 2019

CAR OCCASIONALLY DIED AT STOP LIGHTS, SIGNS AND ONCE ON THE EXIT RAMP WHILE EXITING A HIGHWAY. OCCASIONAL TO OFTEN ROUGH RUNNING ESPECIALLY AT LOW SPEED AND ODD SHIFTS FROM THE TRANSMISSION. SURGING IN THE ENGINE WHILE AT HIGHWAY SPEED AND WHEN SLOWING TO STOP. ENGINE FAULT MESSAGE WOULD COME UP IN DISPLAY AND I TOOK A PICTURE, SHOWED IT TO SERVICE MANAGER WITH NO SUCCESS. COMPUTER WOULD NOT STORE CODES WHEN THESE PROBLEMS OCCURRED SO ON 4 SEPARATE TRIPS TO THE DEALERSHIP I WAS TOLD THERE WAS NOTHING THAT COULD BE DONE AND TO CONTINUE TO DRIVE IT AND BRING IT IN IF IT HAPPENED AGAIN. VEHICLE FINALLY DIED AND CHECK ENGINE LIGHT CAME ON AND STAYED ON. HAD IT TOWED TO THE DEALERSHIP AND A SIGNAL RETURN FOR MAP WIRING PROBLEM WAS DIAGNOSED AND REPAIRED. AFTER SOME READING I BELIEVE THERE HAVE BEEN SERVICE ADVISORIES AND POSSIBLY A RECALL FOR CERTAIN VIN'S. I TOLD THE DEALERSHIP I DID NOT FEEL SAFE DRIVING THE VEHICLE WITH THE PROBLEMS IT WAS HAVING BUT IT MADE NO DIFFERENCE.

Mileage: 49,000

Mar 6, 2019 Fire

I WAS DRIVING DOWN THE HIGHWAY AT A NORMAL RATE OF SPEED (65), AS BY VEHICLE BEGAN TO STALL OUT. THE CAR STOPPED DRIVING RIGHT ON THE HIGHWAY, AND I WAS BARELY ABLE TO PULL IT TO THE SHOULDER WITHOUT GETTING HIT BY OTHER CARS. ONCE I PULLED TO THE SHOULDER, THE CAR BEGAN SMOKING. SMOKE QUICKLY FILLED THE INSIDE OF THE VEHICLE. BEFORE I COULD ROLL ALL THE WINDOWS DOWN, THE ENGINE HAD BURST INTO FLAMES.

Mileage: 70,000

Mar 6, 2019 Fire

TL* THE CONTACT OWNED A 2014 FORD ESCAPE. WHILE DRIVING APPROXIMATELY 50 MPH, THE "SERVICE THE ENGINE" INDICATOR ILLUMINATED. THE VEHICLE WAS PULLED OVER TO THE SIDE OF THE ROAD. THE CONTACT EXITED THE VEHICLE AND NOTICED FLAMES UNDERNEATH THE HOOD. THE CONTACT CALLED 911 AND TWO POLICE VEHICLES AND A FIRE TRUCK IMMEDIATELY ARRIVED AT THE SCENE. THE FIRE DEPARTMENT EXTINGUISHED THE FIRE. A POLICE REPORT AND A FIRE REPORT WERE FILED. THE VEHICLE WAS COMPLETELY DESTROYED AND TOWED TO A TOW YARD. THERE WERE NO INJURIES. THE DEALER WAS NOT CALLED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND DID NOT ASSIST. THE CONTACT WAS UNAWARE OF NHTSA CAMPAIGN NUMBERS: 17V209000 (ENGINE AND ENGINE COOLING) AND 18V471000 (POWER TRAIN). THE FAILURE MILEAGE WAS APPROXIMATELY 75,000. PARTS DISTRIBUTION DISCONNECT.

Mileage: 75,000

Mar 5, 2019

MY 2014 FORD ESCAPE, WITH A 1.6L GTDI ECOBOOST ENGINE, BUILT IN LOUISVILLE, KY IN MARCH 2014 LEAKS ENGINE COOLANT. I PURCHASED THIS VEHICLE ON JUNE 6, 2014. I HAVE PUT MY VIN INTO THE NHTSA NATIONAL RECALL SITE AND IT SAYS MY CAR IS NOT RECALLED. HOWEVER, FORD SAFETY RECALL 17S09 SUPPLEMENTAL #1, DATED DECEMBER 13, 2017, AND NHTSA CAMPAIGN NUMBER 17V209, AFFECTING 230,000 2014 ESCAPES CLEARLY STATES THAT MY VEHICLE, MANUFACTURED IN MARCH 2014, SHOULD BE IN THE RECALL SINCE IT WAS BUILT IN LOUISVILLE BETWEEN FEB 13, 2013 AND SEPT 2, 2014, THE RECALL TIMELINE. MY CAR, LEAKING ENGINE COOLANT, IS EXACTLY THAT DESCRIBED IN FORD SAFETY RECALL 17S09. IN THE PAST 10 WEEKS OR SO I HAVE NOTICED COOLANT ON MY GARAGE FLOOR AND HAVE FILLED THE COOLANT RESERVOIR AT LEAST 8 TIMES. AT ONE TIME THE HEATER DID NOT WORK AND THE RESERVOIR WAS NEARLY EMPTY. I AM CONCERNED ABOUT THE POSSIBILITY OF AN OVERHEATED ENGINE CAUSING THE CYLINDER TO CRACK AND SPEW OIL RESULTING IN A POSSIBLE ENGINE FIRE. I CURRENTLY HAVE APPROXIMATELY 39,000 MILES ON THIS VEHICLE. IF THIS VEHICLE VIN IS NOT RECALLED, I CERTAINLY WOULD LIKE A DETAILED ANSWER WHY IT IS NOT SINCE IT MEETS ALL THE PARAMETERS OF SAFETY RECALL 17S09 SUPPLEMENTAL #1 AND NHTSA CAMPAIGN NUMBER 17V209. THANK YOU.

Feb 28, 2019

CAR LOSSES ALL POWER WHILE ACCELERATING OVER 40 MPH. GETTING ON THE HIGHWAY IS THE WORST. MOTOR WILL REV UP ALMOST REDLINING BEFORE SLAMMING INTO A RANDOM GEAR WITH AGAIN NO POWER SO I'M NOT GAINING ANY SPEED. JUST RPMS ARE SCREAMING LIKE I'M IN NEUTRAL. IT'S VERY UNSETTLING TO HAVE MY CAR PRACTICALLY STOPPING IN THE HIGHWAY.

Mileage: 64,000

Feb 25, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE REVERSING OUT OF THE DRIVEWAY, THE VEHICLE STALLED WITHOUT WARNING. THE CONTACT HAD TO TURN THE VEHICLE OFF AND BACK ON FOR IT TO OPERATE. THE DEALER WAS NOT CONTACTED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND INFORMED THE CONTACT TO CALL NHTSA TO FILE A COMPLAINT. THE FAILURE MILEAGE WAS 57,000.

Mileage: 57,000

Feb 15, 2019 Fire

ON MY WAY TO WORK THIS MORNING I WAS IN MOTION WHEN ALL OF THE SUDDEN ALL THE LIGHTS IN MY CAR CAME ON A MESSAGE CAME UP THAT SAID SERVICE ENGINE NOW THE CAR WOULD NOT GO AT ALL AS I TURNED OFF OF THE HIGHWAY ONTO A CITY STREET I NOTICED THE CAR SMOKING I GOT OUT TO LOOKIF THERE WAS FIRE THERE WAS I GOT MY 3 CHILDREN OUT OF THE BACKSEAT AND GOT AWAY FROM THE CAR I WATCHED AS MY CAR BURNT TO THE GROUND.

Mileage: 100,000

Feb 14, 2019

PURGE VALVE FAILURE. PURGE VALVE WAS EXPERIENCING A LEAK AND REQUIRED REPLACMENT. CAR WOULD SHUT OFF ON ROAD WHEN IDLING. MECHANIC NOTED HE HAS SEEN SIMILAR ISSUES IN OTHER FORD ESCAPES, AND EVEN NOTED THE PART IS IDENTICAL TO THE PURGE VALVE THAT HAS BEEN RECALLED ON THE FORD FOCUS.

Mileage: 60,000

Feb 13, 2019

"TAKATA RECALL". MY VEHICLE HAS LOST 2 TANKS OF ANTIFREEZE IN 3 MONTHS. IT IS NOT LEAKING ONTO THE GROUND, BECAUSE THERE ARE NO DRIPS OR PUDDLES EVER VISIBLE UNDER THE VEHICLE. OTHER 2014 FORD ESCAPES WERE RECALLED FOR THIS SAME THING, WHICH COULD ULTIMATELY CAUSE A FIRE. MY PARTICULAR VEHICLE WAS NOT INCLUDED IN THE RECALL, BUT IS HAVING THE SAME ISSUE, AND DEALERSHIPS WON'T FIX IT AS A RECALL. MUST MY VEHICLE CATCH ON FIRE BEFORE SOMETHING IS DONE!!

Mileage: 89,000

Feb 13, 2019

FORD HAD A RECALL ON THE 2014 FORD ESCAPE IN TWOTHOUSAND 17 FOR AN ENGINE COOLANT SENSOR I BOUGHT THE CAR SIX MONTHS AGO THE RECALL WAS FIXED BY THE OLD OWNER AT A FORD DEALERSHIP NOW THAT THE CAR BELONGS TO ME THE SENSOR IS BAD AGAIN NOW I'M STUCK PAYING FOR A BAD SENSOR I BELIEVE THE SENSOR WAS DEFECTIVE AND SO DOES MECHANIC WHY SHOULD I HAVE TO PAY FOR IT DEFECTIVE PART FORD IS NO HELP

Mileage: 127,000

Feb 8, 2019

I BOUGHT MY CAR IN FEBRUARY 2017. SOON AFTER PURCHASING THIS (USED) I BEGAN LOSING ENGINE COOLANT RAPIDLY AND MY CAR WOULD NOT GET WARM WHEN I HAD THE HEAT ON. ALSO, BLUE SMOKE WOULD COME FROM THE EXHAUST. I HAVE TAKEN TO MY BROTHER-IN-LAW FOR A LOOK-OVER AND THEY SAID THIS LOOKS LIKE A LEMON CAR. WELL, UPON RESEARCH, I SEE A RECALL WHICH MATCHES A LOT OF THE SYMPTOMS OF MY CARS ISSUES, BUT NO RECALL HAS BEEN ISSUED ON MY VIN. I BELIEVE THAT WHATEVER IS GOING ON WITH MY CAR IS A DIRECT RESULT OF THE SAME ISSUE BEING RECALLED AND I NEED THIS INVESTIGATED AS SOON AS POSSIBLE.

Feb 4, 2019

THERE WAS A LEAK FROM THE RADIATOR FLUID INTO THE ENGINE BLOCK THAT RESULTED IN A BLOWN HEAD GASKET. THERE WAS NO WARN LIGHT SUGGESTING THAT THE COOLANT LEVEL WAS LOW, WHICH MAY HAVE PREVENTED THE PROBLEM. THERE HAS BEEN A FACTORY RECALL FOR THIS EXACT SITUATION ON THE EXACT SAME MAKE MODEL AND YEAR OF MY VEHICLE, BUT SOMEHOW MY VEHICLE WAS NOT INCLUDED. PLEASE SEE ATTACHED RECALL LETTER FROM FORD'S SITE. THIS IS MY ONLY CAR I HAVE SAVED UP TO GET AND REPAIRS OF THE HEAD GASKET WOULD BE $3000. HOWEVER, FORD WILL NOT REPAIR IT BECAUSE THEY SAID THEY CAN NOT GUARANTEE THE REPAIR DUE TO THE ISSUE WITH THE LEAK. THEY HAVE SEEN THIS SEVERAL TIMES. THEY WILL ONLY DO A FULL ENGINE REBUILD OR REPLACEMENT FOR $8000 BECAUSE THEY ADMIT THAT THIS IS A FACTORY DEFECT. THE VEHICLE IS CURRENTLY AT THE SHAWNEE MISSION FORD (11501 SHAWNEE MISSION PKWY. SHAWNEE, KS 66203) IN DESPERATE NEED OF A RECALL. THIS HAPPEN WHILE DRIVING DOWN INTERSTATE 35 FROM OMAHA TO KANSAS CITY

Mileage: 65,000

Feb 2, 2019

THIS CAR HAS HAD 13 RECALLS SINCE MANUFACTURED FOR DIFFERENT MECHANICAL AND SAFETY ISSUES SOME EVEN RESULTING IN SPONTANEOUS ERUPTION OF FIRE TO THE ENGINE BAY. WHILE REPLACING MY BATTERY THE DELEARAHIP NOTIFIED ME OF SEVERAL RECALLS THAT REQUIRED ATTENTION, SO I HAD THEM REPLACE EACH ITEM THAT HAD BEEN RECALLED, ONE OF WHICH WAS A SENSOR WITHIN THE TRANSMISSION. AFTER I TOOK THE VEHICLE TO HAVE IT REPLACED SUBSEQUENTLY, MAYBE 6 MONTHS LATER I HAD DRIVING ISSUES WHILE OPERATING IT ON THE EXPRESSWAY. THE VEHICLE WOULD GO IN AND OUT OF GEAR WHILE DRIVING AND I COULD NOT CONTROL THE SPEED OF THE VEHICLE. THIS OCCURRED THE ENTIRE DRIVE HOME TO THE POINT WHERE I HAD TO DRIVE WITH HAZARD LIGHTS ON SO THAT I WOULD NOT GET REAR ENDED FOR HAVING INTERMITTENT SPEED/DRIVING ISSUES. THE CAR WOULD LITERALLY OVER REV THE THE ENGINE AS IF I WAS FLOORING THE PEDAL WHEN I WASN'T EVEN TOUCH THE GAS AT ALL. THE SENSOR LITERALLY TOOK CONTROL OF THE ENGINE AS IF IT WAS DRIVING ITSELF. I DIDN'T DRIVE IT UNTIL THE NEXT MORNING THEN THE NEXT DAY, THE ONLY WAY TO DRIVE IT WAS IF I SLOWLY TRANSITIONED SPEEDS. I HAD TO TAKE THE VEHICLE TO HAVE THE SAME SENSOR REPLACED. AFTER REPLACING THE SENSOR IT STILLS SEEMS TO NEED TO BE DRIVEN SLOWER THAN WHEN I FIRST BOUGHT IT OR IT MIGHT BREAK AGAIN. THIS IS A SAFETY HAZARD. I'M AFRAID TO DRIVE THE VEHICLE WITH MY DAUGHTER IN IT DUE TO THE FACT THAT I MIGHT HAVE MECHANICAL ISSUES WHILE DRIVING AGAIN & BE ON THE HIGHWAY TO HAVE A HIGH SPEED COLLISION WITH A TODDLER WOULD KILL ONE OR BOTH OF US. THIS MODEL IN PARTICULAR HAS HAD MORE RECALLS THAN ANY CAR I'VE EVER HAD OR EVEN HEARD OF HAVING. I HAVE TO CONTINUE MAKING PAYMENTS ON IT DUE TO MY NEGATIVE EQUITY YET IT ISN'T RELIABLE ENOUGH TO GET ME TO WORK EVERYDAY. FORD NEEDS TO REPLACE THIS MODEL FOR ALL OWNERS.

Mileage: 113,000

Feb 1, 2019

RECALLED 17S09 REPAIRED, MAY 2018. COOLANT LIGHT ON HOT, EVERYTHING LOCKED DOWN. VEHICLE STATIONARY, REMOTE USED TO START CAR.

Jan 31, 2019

RECALL PERFORMED (17S09) COOLANT SENSOR UPGRADE. THE NEW SENSOR BUT THE VEHICLE IN (LIMP MODE) CAN NOT DRIVE IT EVEN THOUGH THE COOLANT LEVEL WAS IN THE NORMAL OPERATING LEVEL. THE MECHANIC INDICATED THAT A LEAK IN THE TOP HOSE WAS THE ISSUE AND THAT THERE WAS A REDESIGN OF A KNOWN ISSUE.LUCKY THE VEHICLE WAS PARKED AND HAD TO BE TOWED BACK TO THE DEALERSHIP.

Mileage: 38,000

Jan 31, 2019 Fire

ENGINE FIRE DRIVING ON A HIGHWAY THE CAR ENGINE STOPPED AND I COASTED TO THE RIGHT SHOULDER. I MADE PHONE CALLS FOR HELP AND ASSISTANCE. THE NYSDOT, HIGHWAY EMERGENCY LOCAL PATROL (HELP) TRUCK PULLED AFTER ABOUT 15-20 MINUTES AFTER STOPPING. THE HELP OPERATOR LOOKED INSIDE THE ENGINE AND SAW THAT THE COOLANT RESERVOIR WAS LOW AND OFFERED TO PUT SOME COOLANT IN MY VEHICLE FROM A SUPPLY IN HIS TRUCK. THEN HE HAD ME RUN THE ENGINE IN IDLE ON THE SIDE OF THE ROAD. THE CAR SEEMED TO RUN FINE. IN AN EFFORT TO GET THE CAR OFF OF THE HIGHWAY AND TO GET SOME MORE COOLANT, I DROVE THE CAR TO THE PARKING LOT OF A LOCAL STORE APPROXIMATELY 1.5 MILES. WHEN I PULLED INTO THE PARKING LOT, THE CAR WAS STEAMING UP AGAIN SO I PARKED IT OUT A WAYS FROM THE STORE. I NOTICED THAT THE SMOKE WAS A BIT BLACK AND THICK, SO I OPENED THE HOOD AND SAW THE PLASTIC ENGINE COVER WAS ON FIRE. I STARTED THROWING SNOW ON IT WHEN SOMEONE CAME BY WITH A FIRE EXTINGUISHER, SO I USED IT TO PUT THE FIRE OUT. A TOW TRUCK DRIVER TOOK THE VEHICLE TO THE CLOSEST FORD DEALER ABOUT 1 MILE FROM THE PARKING LOT.

Mileage: 96,000

Jan 31, 2019

ON JAN 29TH DRIVING DOWN THE STREET AND OUT OF KNOW WHERE CAR STARTS STALLING AND THEN SMOKE AND THEN THE 💡 CAME ON SAYING ENGINE OVERHEATING..... I LEFT UP THE HOOD THE CONTAINER FILLED ..... PARKED CAR AND NEVER GOT BACK IN SMOKE WAS POURING OUT OF THE HOOD.... IN THE MIDDLE IF HARBSON AND ARGAMINO..... MR MY DAUGHTER 1MONTH OLD GRANDSON AND NEICE. ... THE MOST SCARIEST THING EVER IN MY LIFE....

Mileage: 59,000

Jan 30, 2019

OVER THE COURSE OF 1 YEAR, VEHICLE IN THE SHOP 9 TIMES FOR 109 DAYS. ON 7-6-2017- CAR WOULD NOT ACCELERATE & LOW POWER LIGHT ON. 8-23-2017- VEHICLE OVERHEATING, GOES IN TO LIMP MODE, HIGH TEMPERATURE GAUGE GOES UP. 12-26-2017-TOWED IN AS CAR WOULD NOT START. COOLANT LEAK, QUICK CONNECTOR TO HEATER CORE AND BYPASS VALVE LEAKING. 2-27-2018- CHECK ENGINE LIGHT ON, CYLINDER MISFIRE, CYLINDER HEAD HIGH TEMPERATURE, LOW ENGINE COOLANT, COOLANT LEVEL SENSOR 3-16-18- COOLANT LIGHT COMES ON, FOUND UPPER COOLANT HOSE LEAK , CHECK ENGINE LIGHT ON 3-19-18- TOWED IN- LOW COOLANT AND TEMPERATURE LIGHT ON, NO HEAT , VEHICLE SHUTS OFF. 4-4-18- COOLANT LEVEL LOW LIGHT ON.WATER PUMP WAS LEAKING. 4-19-18- CHECK ENGINE LIGHT ON. TECHNICIAN VERIFIED SES LIGHT ON, FOUND MISFIRECODES &COOLANT CODE BUT COOLANT WAS FULL, WAS ADVISED TO STOP BACK IN 2 WEEKS TO CHECK COOLANT. CALLED FORD CERTIFIED GARAGE AT THE 2 WEEK DATE & WAS TOLD THEY WERE TOO BUSY TO BRING VEHICLE IN FOR A CHECK. 5-14-2018- CHECK ENGINE LIGHT ON--ENGINE MISFIRING, REMOVED SPARK PLUGS AND COLIS TO BORESOPE ENGINE, FOUND COOLANT IN CYLINDER 1, REMOVED CYLINDER HEAD FOR FURTHER INSPECTION, MAP SENSOR CONTAMINATED, FOUND CYLINDER HEAD POROSITY, LIKELY DUE TO OVERHEATING .MY TOTAL IN REPAIRS AND TOWING: $4000+ IN ONE YEAR. FEEL ALL ISSUES WERE RELATED TO RECALL 17V209000 REGARDING THE ENGINE AND ENGINE COOLING, WHICH STATED IF THE VEHICLE IS STARTED AND DRIVEN WITH AN INSUFFICIENT LEVEL OF COOLANT WITHIN THE SYSTEM, THE ENGINE CYLINDER HEAD MAY OVERHEAT AND CRACK:

Mileage: 67,000

Jan 22, 2019

PURGE VALVE FAIL, FAILS TO START PROPERLY AFTER FILLING FUEL TANK.WAS STALLING AFTER STARTING AND ENGINE CHECK LIGHT COMES ON. BAD SMELL FROM EXHAUST.

Mileage: 51,496

Jan 22, 2019

ENGINE LIGHT CAME ON ONE DAY THEN WENT OFF THE NEXT DAY. A WEEK LATER WENT TO GET ROUTINE OIL CHANGE AND WAS NOTIFIED OF OIL IN COOLANT AND POSSIBLE HEAD GASKET CRACKED AS WELL. THEY RECOMMENDED TAKE IT TO MECHANIC NEXT DOOR. APPARENTLY THE ENGINE CYLINDER HEAD OVERHEATED AND CRACKED. OIL LEAKED INTO OTHER SYSTEMS IN ENGINE CONTAMINATED VALVES, INTAKES, SPARK PLUGS ETC. COULD HAVE COMBUSTED CAUSING FIRE AT ANY MOMENT. MECHANIC TOLD US TO HAVE IT TOWED TO FORD NOT SAFE TO DRIVE 3 MILES. GOT CAR FIXED AT FORD DEALERSHIP FOR $3551.09. THE FOLLOWING WEEK WE RECEIVED A RECALL NOTICE FOR OUR OTHER 2014 FORD ESCAPE BUILT IN SAME LOUISVILLE FACTORY A FEW WEEKS EARLIER THAN THE JUST REPAIRED ESCAPE. GOT THE RECALL ADDRESSED ON THAT VEHICLE BUT FORD SAYS THE VIN FOR THE ONE I JUST PAID FOR HAS NOT BEEN IDENTIFIED FOR THE RECALL! REALLY???

Mileage: 71,240

Jan 21, 2019

ENGINE STALLS FOR NO APPARENT REASON. VEHICLE WAS STATIONARY AT TRAFFIC LIGHT. LAST TIME WAS SATURDAY 1/19/2019

Mileage: 60,000

Jan 21, 2019

WHILE STANDING STILL OR DRIVING UNDER 30 MPH,EXHAUST FUMES ENTER VEHICLE WITH FRESH AIR INDICATED ON SWITCH,SET TO RECIRCULATE, AIR SWITCH CHANGES BY ITSELF AND ALLOWS FUMES INTO CAR.

Mileage: 60,000

Jan 15, 2019

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING APPROXIMATELY 30 MINUTES AT 30 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE CONTACT TOOK THE VEHICLE TO TASCA FORD SEEKONK (200 FALL RIVER AVE, SEEKONK, MA 02771, (800)-737-0435) WHERE IT WAS DIAGNOSED THAT THE FUEL PUMP SYSTEM FAILED AND NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED, BUT THE FAILURE RECURRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND STATED THAT THE VIN WAS NOT INCLUDED IN A RECALL. THE FAILURE MILEAGE WAS 28,000.

Mileage: 28,000

Jan 14, 2019 Fire

JANUARY 9, 2019 AT 10:39PM MY 2014 FORD ESCAPE CAUGHT ON FIRE. DRIVING DOWN INTERSTATE 81, GOING SPEED LIMIT 70 MPH, VEHICLE SHUT OFF AND SAID "SERVICE ENGINE NOW". STEERING AND BRAKES DID NOT LOCK UP BUT THE VEHICLE LOST RPMS AND WAS NOT RUNNING AS I PULLED OVER TO THE RIGHT HAND SHOULDER, I WAS IN THE LEFT HAND LANE WHEN MY VEHICLE SHUT OFF. AS I STOPPED, I PUT VEHICLE IN PARK AND TURNED KEY OFF, ALL WHILE IT SAID "SERVICE ENGINE NOW". I TURNED MY HAZARDS ON AND GOT OUT MY PHONE TO CALL SOMEONE FOR HELP. AS I LOOKED UP I SEEN FLAMES COMING FROM THE WINDSHIELD WIPER AREA AND SMOKE IN FRONT OF MY LIGHTS, I GRABBED MY WORK BAG AND JUMPED OUT OF THE VEHICLE, JUMPED ACROSS THE GUARD RAIL, AND IMMEDIATELY CALLED 911 FROM A SAFE DISTANCE. IN APPROXIMATELY 6-9 MINUTES THE ENTIRE FRONT END OF MY VEHICLE WAS ENGULFED IN FLAMES AS I WAS ON THE PHONE WITH 911. TOOK RESPONDERS ABOUT 15 TO 20 MINUTES TO ARRIVE AND TO PUT OUT THE FIRE. AS SOON AS RESPONDERS FINALLY SHOWED, I COULD HEAR BOTH TIRES EXPLODE A FEW MINUTES APART FROM EACH OTHER. ONCE FIRE WAS SAFELY PUT OUT, THE ENTIRE FRONT END OF MY VEHICLE WAS MELTED AND THE INSIDE AS WELL WAS BEYOND RECOGNIZABLE. I WAS TOLD MY VEHICLE IS TOTALLED, OBVIOUSLY, AND I GOT A TOW TO TAKE VEHICLE TO MY HOUSE WHERE THE 2014 FORD ESCAPE IS SITTING IN MY YARD. I FIGURED MY INSURANCE COMPANY MIGHT COME LOOK AT IT BUT THEY DIDN'T BECAUSE ALL I HAD WAS LIABILITY ON IT. I DID NOT KNOW UNTIL A COUPLE DAYS LATER THERE WAS IN FACT A RECALL ON MY VEHICLE, DUE TO RISK OF ENGINE FIRE.

Mileage: 197,000

Jan 14, 2019

A RECALL WAS INITIATED FOR MY CAR FOR LOCALIZED OVERHEATING IN ENGINE CYLINDER CAUSING CYLINDER HEAD TO CRACK, AND PRESSURIZED OIL LEAKS THAT CAN RESULT IN A FIRE IN THE ENGINE COMPARTMENT. I INITIALLY BROUGHT MY CAR IN FOR MY ENGINE OVERHEATING WHERE MY CAR WAS GIVING ME A WARNING SIGN TO PULL OVER AND IMMEDIATELY TURN OFF MY CAR. THEY REPLACED THE COOLANT HOSE. TWO MONTHS LATER THE SAME ISSUE OCCURRED AND THEY THEN REPLACED THE COOLANT TANK. FAST FORWARD ONE YEAR AND THE ISSUE BEGAN TO HAPPEN ONCE AGAIN. I TOOK MY CAR BACK IN AND THE COOLANT TANK WAS REPLACED FOR THE SECOND TIME IN MAY OF 2018. I HAD NO ISSUES UNTIL DECEMBER OF 2018 WHERE ONCE AGAIN THE CAR GAVE ME THE SAME WARNING SIGN AND ONCE AGAIN NEEDS THE COOLANT HOSE REPLACED DUE TO IT LEAKING. THEY HAVE TOLD ME I AM RESPONSIBLE FOR REPLACING THIS ON MY OWN AND PAYING FOR IT. EACH TIME I HAVE BEEN DRIVING WHEN THIS ISSUE OCCURS AND I HAVE TO IMMEDIATELY PULL OVER AND TURN MY CAR OFF TO AVOID FURTHER DAMAGE AS WELL AND I CANNOT DRIVE MY CAR FOR NUMEROUS DAYS WHILE I WAIT FOR THEM TO REPAIR IT. I WANT TO FIGURE OUT A SOLUTION MOVING FORWARD BECAUSE CLEARLY THIS CAR IS NOT BEING FIXED EVEN WHEN I TAKE IT IN OVER AND OVER AGAIN.

Mileage: 42,109

Jan 11, 2019

ON 02/06/208 TOOK VEHICLE TO HERITAGE FORD VT FOR COOLANT LEVEL SENSOR RECALL . RECALL WAS PERFORMED . ON 03/20/2018 VEHICLE WAS TOWED BACK TO HERITAGE FORD VT DUE TO RECALL PERFORMED INCORRECTLY REPAIR WAS COMPLETE. 04/19/2018 VEHICLE TOWED BACK TO HERITAGE FORD VT RECALL DONE INCORRECTLY RESULTING IN REMANUFACTURED ENGINE REPLACE. VEHICLE WAS TOWED BACK TO HERITAGE FORD 05/16/2018,06/19/2018,07/09/2018,09/07/2018 DUE TO VEHICLE OVERHEATING CAUSING POSSIBLE COOLANT TO LEAK INTO ENGINE . ON 10/30/2018 VEHICLE OVERHEATED HERITAGE FORD VT SUPERVISOR AND MECHANIC VIDEO RECORDED POURING COOLANT INTO VEHICLE AND DRIVING AWAY POSSIBLY CAUSING MORE DAMAGE TO OIL AND ENGINE .11/30/2018 VEHICLE RETURNED TO HERITAGE FORD VT DUE TO OVERHEAT COOLANT POSSIBILITY CAUSING A BREAKDOWN OF OIL AND DAMAGE TO ENGINE . HERITAGE FORD VT REPLACED COOLANT SENSOR IMPROPERLY. HERITAGE FORD VT IS NOW CLAIMING NO RESPONSIBILITY FOR THIS ACTION, STATING, IN ORDER FOR THIS VEHICLE TO BE REPAIRED I THE CUSTOMER WILL HAVE TO PURCHASE A NEW ENGINE DUE TO HERITAGE FORD VT NEGLIGENCE OF REPLACING A COOLANT SENSOR CORRECTLY.I FEEL AS THE CUSTOMER THIS VEHICLE IS,WAS A SAFETY ISSUE DUE TO THE NEGLIGENCE OF HERITAGE FORD VT .

Mileage: 44,459

Jan 7, 2019

MY CAR KEPT SHUTTING OFF ON ME AND I TOOK IT TO MY DEALER AND THEY SAID THE COOLANT WAS LEAKING INTO MY CYLINDER HEAD AND I NEEDED A NEW ENGINE. I SEE ON HERE THAT THERE ARE MULTIPLE RECALLS FOR THIS MODEL DEALING WITH THE COOLANT LEAKING. HOWEVER, THE DEALER CALLED FORD AND WAS TOLD IT WAS NOT COVERED. MY CAR IS ONLY 4 YEARS OLD AND I NEED A COMPLETE NEW ENGINE FOR $9,000 DOLLARS. I'M NOT SURE WHO TO COMPLAIN TO OR HOW TO GET THIS HANDLED BUT I DON'T HAVE $9K LAYING AROUND. I WORK TWO JOBS AS IT IS AND I CAN'T AFFORD IT.

Mileage: 98,000

Jan 7, 2019

WHILE DRIVING THE CAR USUALLY GOING UP A HILL THE TEMPERATURE GAUGE QUICKLY GOES UP AND SHOWS THE CAR IS OVERHEATING AND ALL KINDS OF WARNINGS SOUNDS AND VISUAL NOTICES GO OFF TELLING ME TO STOP THE CAR AND PARK SAFELY. THIS HAS HAPPENED 3 TIMES. THE LAST TIME THIS HAPPENED 2 DAYS AGO I COULD PUT THE CAR INTO GEAR BUT IT WOULD NOT ENGAGE AND GO FORWARD OR BACKWARD AND I HAD TO COAST TO A STOP AND PULL OVER TO THE SIDE OF THE ROAD AND HAVE IT TOWED.

Mileage: 58,000

Dec 17, 2018

MY FORD ESCAPE IS OVERHEATING. WHILE DRIVING THE DISPLAY PANEL READ: SPEED REDUCED TO LOWER ENGINE TEMPERATURE. AFTER RESEARCHING I REALIZED THAT THIS PROBLEM WAS PART OF AN EARLIER RECALL. I CONTACTED FORD AND WAS TOLD THAT MY VIN WAS NOT INCLUDED IN THAT RECALL.

Mileage: 67,000

Dec 14, 2018

FORMULA FORD PREFORMED SEVERAL RECALLS ON MY 2014 FORD ESCAPE ON OCTOBER 31 2018. ONE RECALL IN PARTICULAR WAS ON THE COOLANT SYSTEM IN MY CAR, IT TOOK THEM A COUPLE DAYS TO PREFORM NEEDED RECALLS. A WEEK OR TWO AFTER MY CAR HAVING THE RECALLS DONE TO IT A COOLANT LOW SERVICE SOON WARNING LIGHT CAME ON MY DASH. I CALLED FORMULA FORD SERVICE AND WAS TOLD TO TRY AN PUT COOLANT IN IT AND SEE IF THAT REMEDIED THE PROBLEM. I DID AND THE LIGHT WENT OUT BUT IN ANOTHER WEEK OR SO THE LIGHT CAME BACK ON I CALLED FORMULA FORD SERVICE AGAIN TO HAVE MY CAR LOOKED AT AND THEY WERE NOT ABLE TO SCHEDULE ME UNTIL 12/13/18 ON 12/7/18 MY CAR BECAME INOPERABLE. I HAD IT TOWED INTO FORMULA FORD UNDER MY ROAD SIDE ASSISTANCE THROUGH MY INSURANCE, AFTER THEIR INSPECTION OF THE CAR I WAS TOLD ON MONDAY 12/10 THAT IT HAD A BLOWN HEAD GASKET DUE TO OVER HEATING BUT IT HAD NOTHING TO DO WITH THE RECALL THEY PREFORMED ON MY COOLANT SYSTEM, EVEN THOUGH MY CAR RAN FINE PRIOR TO BRINGING IT TO THIS SHOP.

Mileage: 68,000

Dec 11, 2018 Fire

THE VEHICLE STALLED WHILE DRIVING DOWN A RURAL HIGHWAY. A SUDDEN JERK WAS FELT AND THEN 'ENGINE FAILURE' APPEARED ON THE DISPLAY. THE CAR BEGAN TO SMOKE AND WITHIN SECONDS THE ENGINE COMPARTMENT WAS FULLY ENGULFED. IT WAS LATER LEARNED THAT THIS VEHICLE HAD A RECALL RELATED TO A DEFECT THAT HAS CAUSED SEVERAL SIMILAR CASES. THIS RECALL NOTICE WAS NEVER RECEIVED BY US, THEREFORE WENT UNFIXED. THIS VEHICLE HAS BEEN WORKED ON BY A CERTIFIED FORD DEALERSHIP SINCE THE RECALL AND THE RECALL WENT UNNOTICED THERE AS WELL.

Mileage: 60,000

Dec 6, 2018

I HAVE A BLOWN HEAD GASKET WHICH RESULTED FROM A LEAK FROM THE RADIATOR INTO THE MANIFOLD. THERE WAS NO LOW FLUID LIGHT THAT WARNED OF THE LEAK WHICH WOULD HAVE PREVENTED THIS DEFECTIVE FLAW.THIS PROBLEM EXACTLY FITS THE RECALL 17V209000 (SEE ATTACHED) FOR EXACTLY THE MAKE, MODEL, YEAR, ENGINE, ETC. OF MY VEHICLE, BUT FOR SOME REASON MY VEHICLE WAS NOT INCLUDED. I BROUGHT THE VEHICLE TO 2 MECHANICS AND THEY BELIEVE 100% THAT IT SHOULD INCLUDE MY VEHICLE AND ARE NOT SURE WHY ITS INCLUDED. PLEASE REVIEW AND PLEASE TRY TO ADD MY VEHICLE TO THE RECALL LIST

Mileage: 145,000

Dec 5, 2018

VEHICLE STALLS IN THE MIDDLE OF THE DRIVE AND ENGINE OIL SYMBOL AND BATTERY SIGNS POP UP ON THE DASHBOARD. TURN OFF THE CAR AND ON AGAIN TO RESOLVE THE ISSUE. THIS IS A SAFETY ISSUE WITH ONCOMING TRAFFIC. THIS STARTS OCCURRING ON MY CARS ONCE THE CAR HAS 60,000 MILES. CANNOT REPRODUCE THIS ISSUE. BATTERY AND ALTERNATOR ARE VERIFIED AND THEY ARE GOOD CONDITION.

Mileage: 60,050

Dec 5, 2018

KEEP LOOSING COOLANT AND RESULTED TO DAMAGING CYLINDER HEAD AND FORD DOES NOT WANT TO FIX THE PROBLEM DESPITE THE RECALL. THEY SAY RECALL THEY MADE IS TO PREVENT THE PREVENTIVE.

Mileage: 71,000

Dec 4, 2018

COOLANT LEAK. NO SENSOR WARNING LIGHT. NO RECALL NOTICE. MESSAGE STATED CAR WAS OVERHEATING WHILE IDLING IN A DRIVE-THRU. ADDED COOLANT. SEVERAL MONTHS LATER, SAME SITUATION, DIFFERENT DRIVE-THRU. COOLANT ADDED.

Mileage: 84,500

Dec 4, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE THE VEHICLE WAS AT A COMPLETE STOP, THE ENGINE TEMPERATURE AND ENGINE COOLING WARNING INDICATORS ILLUMINATED. THE VEHICLE WAS TAKEN TO GWINNETT PLACE FORD (3230 SATELLITE BLVD, DULUTH, GA 30096, 404-418-6877), BUT WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 48,064.

Mileage: 48,064

Nov 29, 2018

ENGINE STALLED DURING HIGHWAY CRUISE(70 MPH), LOST ALL THROTTLE RESPONSE. LIGHTING, BRAKE, STEERING WORKED FINE. COOLANT LEAKAGE WAS OBSERVED UNDER THE HOOD AFTER PARKING. AFTER THE VEHICLE WAS TOWED TO A FORD DEALER, SERVICE PEOPLE REPORTED ENGINE WIRINGS WERE BURNED OUT DUE TO FIRE.

Mileage: 850,000

Nov 28, 2018

TRANSMISSION DOES NOT SHIFT PROPERLY. ENGINE IS MAKING RATTLING NOISE WHEN RUNNING.

Mileage: 78,000

Nov 28, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE DEALER (GALLIGHER FORD, 650 30TH ST, ELKO, NV 8980, 775-738-3147) WAS CONTACTED AND CONFIRMED THAT THE PARTS WERE NOT AVAILABLE FOR THE RECALL REMEDY. THE MANUFACTURER WAS NOT NOTIFIED. THE CONTACT HAD NOT EXPERIENCED A FAILURE. PARTS DISTRIBUTION DISCONNECT.

Nov 26, 2018

WHILE HAVING TO REPLACE THE COOLANT AT LEAST TWICE A WEEK AND AFTER HAVING 2 RECALL REPAIRS COMPLETED ON THE COOLANT SYSTEM, THEN AFTER 10000 MILES AFTER THE RECALL REPAIRS WERE COMPLETED, IE REPLACE OVERFLOW BOTTLE, SENSORS, ETC. THE CAR STILL IS LOSING COOLANT AND NOW THE "ENGINE HAS REACHED HIGH TEMP PLEASE STOP CAR SAFELY". WARNING IS SHOWING ON PANEL AND THE CAR WILL GO INTO DRIVE BUT WILL NOT MOVE. THE CAR HAD NOT BEEN DRIVEN WHEN THIS "WARNING" OCCURRED IN MY DRIVEWAY, THERE WAS NO WAY ENGINE COULD HAVE OVERHEATED AS IT HAD NOT BEEN DRIVEN. THIS WOULD APPEAR TO BE A DEFECT IN THE RECALL REPAIRS THAT WERE DONE OR THAT THERE IS ANOTHER PROBLEM.. I HAVE THE CAR CURRENTLY AT THE DEALERSHIP AND AM TOLD THAT IT COULD TAKE UP TO 3 WEEKS FOR REPAIRS.

Mileage: 105,450

Nov 26, 2018

I HAVE HAD 3 RELATED ISSUES SO FAR WITH THE ENGINE COOLANT IN MY CAR - RESULTING NOW WITH A LEAK THAT IS ALLOWING COOLANT FLUID ONTO OTHER PARTS OF THE ENGINE. MY VEHICLE WAS RUNNING WITH NO ISSUES WHEN ONE DAY IT STARTED BUT IMMEDIATELY BEEPED WARNING THAT THE ENGINE TEMP. WAS TOO HOT & TO SAFELY STOP THE CAR IMMEDIATELY. THE ENGINE TEMP. GAUGE WAS IN THE MAX POSITION, BUT IT WAS A MILD DAY & THERE IS NO WAY THE ENGINE WOULD NATURALLY HAVE STARTED THAT HOT. IN ADDITION, THE CAR WOULDN'T GO. I COULD SHIFT INTO DRIVE & IT WOULD ROLL FORWARD BUT THERE WAS NO GOING OTHER THAN ROLLING. I TRIED LETTING IT SIT & RE-STARTING, BUT THE SAME ERROR CAME UP, THE ENGINE SHUTTERED/VIBRATED A LITTLE, & STAYED IN THAT SAFETY MODE. I HAD A REPAIR SHOP TOW IT & THEY THOUGHT IT WAS A BAD SENSOR SENDING INCORRECT SIGNALS THAT THE ENGINE WAS OVERHEATING SO THEY ORDERED THE PART & REPLACED IT. SOON AFTER, THE LOW COOLANT WARNING LIT UP, BUT THE SHOP HAD JUST CHECKED THE COOLANT WHEN THEY REPLACED THE SENSOR. A FEW MONTH'S LATER NOW ON A 22 DEGREE MORNING AFTER MY CAR WAS PARKED ALL NIGHT I REMOTE STARTED AND LET IT IDLE FOR A FEW MIN THEN GOT IN & HIT FULL-START, IT GAVE ME THE SAME ERROR MESSAGE (ENGINE WAS OVERHEATED) & WOULDN'T DRIVE. I HAD TO TOW IT TO FORD DEALERSHIP AFTER I GOOGLED THE PROBLEM & NOTICED THAT NOT ONLY THERE ARE SIMILAR COMPLAINTS BUT ALSO THE 2013 FORD ESCAPE 1.6L GTDI FROM TN PLANT WAS RECALLED FOR COOLANT LEAKS CAUSING FIRES! I HAVE SAME JUST 1 YEAR NEWER PLUS OTHER ARTICLES ACTUALLY SAID THE 2014 MODEL WAS INCLUDED WITH THE RECALL. BUT, DEALER TOLD ME THERE WAS NO RECALL FOR MINE SO I HAVE TO PAY TO FIX THE PROBLEM... THEY'RE NOW SAYING ENGINE COOLANT LIQUID WAS FOUND OUTSIDE THE CHAMBER ON THE SENSORS & THEY WANT TO CHARGE ME $560 + $119 DIAGNOSTIC FEE. THIS IS A DEFECT THAT I SHOULDN'T HAVE TO PAY FOR (AGAIN), & IS ALSO A SAFETY HAZARD. PLEASE HELP INVESTIGATE!

Mileage: 58,000

Nov 24, 2018

FAILURE AT 80,000 MILES, HOWEVER THE ENGINE WAS REPLACED WITH A NEW ENGINE AT 76,000 DUE TO PROBLEMS FROM THE COOLANT RECALL; THIS TIME THE VEHICLE WOULD STALL WHEN COMING TO A STOP OR WHILE DRIVING. COMPUTER SCREEN WOULD SHOW "SYSTEM SHUTTING DOWN"; VEHICLE WOULD GO INTO "LIMP" MODE, REDUCE SPEED AND CAR WOULD SHUT OFF WITHOUT NOTICE. VEHICLE WAS TOWED IN AFTER ISSUE OCCURING 4X IN A 2 MILE DRIVE. VEHICLE WAS TOWED IN. ADVISED BY THE DEALERSHIP THAT THEY COULD NOT DUPLICATE THE PROBLEM. AFTER 30 DAYS THEY RETURNED THE CAR WITH 75 MILES TEST DRIVEN AND SHOWED THAT THE TECH RESET THE COMPUTER MODULE PRIOR TO DUPLICATING THE ISSUE. THE SERVICE MANAGER HAD ME "RESET" THE VEHICLE BY DRIVING IT. WHILE DRIVING 55MPH THE ISSUE REOCCURRED AT 100 MILES AFTER THE SYSTEM RESET. THE VEHICLE WOULD NOT RESTART AND WAS TOWED INTO THE DEALERSHIP. AFTER A WEEK THEY WERE ABLE TO DUPLICATE "SOME" BUT NOT ALL OF THE ISSUES. AFTER SPEAKING WITH THE GENERAL MANAGER OF THE DEALERSHIP THEY DECIDED TO PURCHASE THE VEHICLE BACK BY PAYING OFF THE EXISTING LOAN IN EXCHANGE FOR PURCHASING A 2018 FORD ESCAPE.

Mileage: 80,000

Nov 23, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 65 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE CONTACT WAS ABLE TO RESTART THE VEHICLE AFTER SEVERAL ATTEMPTS. THE VEHICLE WAS TAKEN TO RUSH TRUCK CENTER ORLANDO (LOCATED AT 2350 DIVERSIFIED WAY, ORLANDO, FL 32804, (407) 581-8000) WHERE IT WAS DIAGNOSED THAT THE PURGE VALVE NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED. THE APPROXIMATE FAILURE MILEAGE WAS 150,000.

Mileage: 150,000

Nov 15, 2018

HIGH ENGINE TEMP, PULL OVER SAFELY MESSAGE FLASHES ON DISPLAY AND ENGINE LIGHT COMES ON. CAR STARTED RUNNING ROUGH. FORTUNATELY WAS JUST PULLING OUT OF MY DRIVEWAY AND DIDN'T GET OVER 5 MPH. I BACKED UP INTO GARAGE, TURNED OFF CAR. STARTED IT AGAIN AND WHEN I GOT TO SAME SPOT (APPROXIMATELY 1/8 MILE) THE SAME WARNINGS POPPED UP. TOWED TO DEALER UPON THEIR ADVISE. NOW THEY ARE TELLING ME, AFTER HAVING THE CAR FOR 6 DAYS, THAT IT'S EITHER THE HEAD GASKET OR BLOCK CRACKED DUE TO COOLANT BEING LOW. THEY TESTED COOLANT AND CONFIRMED IT IS LEAKING INTERNALLY. NOTE - I DID HAVE THE RECALL RELATED TO THE ISSUE PERFORMED IN FEBRUARY 2018. NOW, WITH ONLY 1 MONTH LEFT ON ORIGINAL WARRANTY BUT AT 61,500 MILES (SO OVER BY A SMIDGE), FORD WILL NOT REPAIR CAR. IF THE RECALL WAS PERFORMED BUT THE CAR EXHIBITED THE PROBLEM ANYWAYS, NO MATTER HOW FAR IT WAS DRIVEN SINCE THEN, THAT TELLS ME THAT THE RECALL SOLUTION DID NOT WORK.

Mileage: 61,500

Nov 15, 2018

THIS IS NOW THE 4TH TIME MY CAR HAS STALLED ON THE ROAD WITHOUT WARNING. THEY'VE ALL REVOLVED AROUND SOME TYPE OF ELECTRICAL FAILURE THAT EITHER CAUSED THE VEHICLE NOT TO START, OVERHEAT OR LOSE POWER ALL TOGETHER AND COME TO A COMPLETE STOP. THREE TIMES THIS HAPPENED WHILE ON THE HIGHWAY AND ONCE ON SURFACE STREETS. IN THIS MOST RECENT ONE. SOME OF THE REPAIRS WERE COVERED UNDER A RECALL BUT THERE'S SOMETHING ABOUT THIS MODEL THAT IS JUST WRONG. I HAD A FORD EXPLORER FOR OVER 10 YEARS AND 200,000 MILES AND IT NEVER BROKE DOWN ON ME THE WAY THIS ONE HAS. I DO NOT FEEL SAFE WITH THIS CAR.

Mileage: 89,000

Nov 14, 2018 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT THE INSTRUMENT PANEL INDICATORS ILLUMINATED AND SMOKE APPEARED UNDER THE HOOD. THE VEHICLE WAS PULLED OVER AND THE CONTACT DISCOVERED THAT COOLANT WAS LEAKING. THE CONTACT LET THE VEHICLE COOL OFF AND ADDED MORE COOLANT. THE VEHICLE WAS TOWED TO COCONUT POINT FORD (22400 S TAMIAMI TRAIL, ESTERO, FL 33928, (888) 859-1976) WHERE IT WAS DIAGNOSED THAT COOLANT LEAKED OUT FROM A DEFECTIVE UNKNOWN PART THAT WAS NOT COVERED UNDER THE EXTENDED WARRANTY. THE MANUFACTURER STATED THAT THERE WAS NO RECALL ON THE VEHICLE AND WOULD OPEN A CASE TO SEE IF THEY COULD PROVIDE ASSISTANCE TOWARDS THE REPAIR COSTS SINCE THE WARRANTY HAD JUST EXPIRED. THE FAILURE MILEAGE WAS 67,000.

Mileage: 67,000

Nov 14, 2018 Fire

ON 10/28/2018 AROUND 10:30AM I WAS DRIVING TO CHURCH WITH MY FAMILY. WHILE STOPPING AT AN INTERSECTION OF NORTH ROUTE 88 AND 837 IN MONONGAHELA, PA, I NOTICED THAT THERE WAS SMOKE COMING OUT OF THE HEATING VENTS. THEN AS I TRIED TO ACCELERATE, THE CAR SHUT DOWN. SO, I WAS ABLE TO PUSH THE CAR TO A NEARBY PARKING LOT TO INVESTIGATE THE PROBLEM. AFTER I EVACUATED MY FAMILY FROM THE CAR, I OPENED THE HOOD AND THE SMOKE PROGRESSED TO A FIRE, WHICH I CALLED 911 AND THE FIRE DEPARTMENT ARRIVED AND EXTINGUISHED IT. THEN A TOW TRUCK WAS CALLED AND TOWED MY VEHICLE TO LENZI SERVICE STATION IN MONONGAHELA, PA. AFTER REPORTING THIS TO THE INSURANCE COMPANY, THE INSURANCE INVESTIGATOR DETERMINED THAT IT WAS AN EXHAUST FIRE OCCURRED DUE TO AN UNSEEN OIL LEAK. I REPORTED THE INCIDENT TO FORD ON 10/29/2018, BUT HAVE YET TO HEAR FROM THEM. THE INSURANCE COMPANY, WHICH IS USAA, HAS AGREED TO BUY OUT THE REST OF MY PAYMENT AND TOLD ME THAT I CAN GO AND BUY A NEW CAR.

Mileage: 110,310

Nov 13, 2018 Fire

WHILE ON HIGHWAY. RPM SCDROPPED TO 0. ALL LIGHTS ON DASH LIT UP. SMELL BURNING. CAR STOPPED WORKING ROLLED TO SIDE OF HIGHWAY EXIT RAMP. TOWED TO KUHLMANNS'S AUTOMOTIVE ON MERIDENRD WOLCOTT CT 06716

Mileage: 53,000

Nov 5, 2018

FORD FIXED A RECALL ON MY CAR REGARDING THE COOLANT SENSOR AND MY CAR HASN'T BEEN RIGHT EVER SINCE. SAME DAY THAT I BROUGHT IT HOME THE COOLANT SENSOR SAID COOLANT LEVEL LOW EVEN THOUGH THEY HAD JUST FILLED IT UP AND THERE WAS PLENTY OF COOLANT IN THE CAR. YESTERDAY ON MY WAY HOME FROM WORK MY CAR OVER HEATED AND, LIGHTS ON THE DASH SAID FOR ME TO PULL OVER SAFELY AS SOON AS POSSIBLE. THE CAR AUTOMATICALLY SLOWED DOWN TO BARELY 5MILES/HOUR ON IT OWN, IT WOULD NOT ACCELERATE. NOW THE CAR IS NOT DRIVABLE AS IT OVERHEATS WITHIN 30 SECONDS OF STARTING THE CAR UP. DEALERSHIPS NEAR ME WILL NOT SERVICE MY CAR FOR ANOTHER 2 WEEKS AND THEY DON'T HAVE A LOANER CAR THAT I CAN USE IN THE MEANTIME, AND ON TOP OF THAT IT'S GOING TO HAVE TO BE TOWED TO THE DEALERSHIP BECAUSE IT'S NON-DRIVABLE. ACCORDING TO THE DIAGNOSTICS RAN ON IT THE CODE THAT CAME UP WAS - P1299.

Mileage: 89,400

Nov 5, 2018

THIS IS THE SECOND TIME THIS VEHICLE HAS EXPERIENCED THIS ISSUE. THE CAR LOSES COOLANT FLUID, THEN OVERHEATS. THE MANUFACTURER HAS INSTALLED A SENSOR THAT REPORTS THE FLUID LEVEL CONDITION, BUT HAS NOT ADDRESSED THE CAUSE OF THE FLUID LOSS. AS A RESULT, THE HEAD REQUIRES REPLACING, OR THE VEHICLE NEEDS A NEW ENGINE. THE CAR ALSO HAS A CHANCE FOR AN UNDER-HOOD FIRE. THE MANUFACTURER, FORD, IS NEGLIGENT.

Mileage: 80,000

Oct 31, 2018 Fire

TL* THE CONTACT OWNED A 2014 FORD ESCAPE. THE CONTACT STATED THAT A RECALL NOTICED WAS RECEIVED UNDER CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING), THE VEHICLE WAS TAKEN TO COLONIAL FORD DEALER (120 FEDERAL RD # 126, DANBURY, CT 06811, (203) 748-3503) WHERE THE RECALL WAS COMPLETED. THE CONTACT STATED THAT THE COOLANT WARNING LIGHT ILLUMINATED, THE VEHICLE WAS TAKEN BACK TO COLONIAL FORD DEALER, AND IT WAS DIAGNOSED THAT A POOR PIN FIT CORRECTION #48802 P2560 NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. THE CONTACT STATED THAT WHILE THE DRIVER WAS DRIVING AT 20 MPH, THE COOLANT WARNING LIGHT ILLUMINATED, AND THE VEHICLE STALLED BUT WAS ABLE TO COAST TO THE SIDE OF THE ROAD. THE DRIVER NOTICED SMOKE WAS COMING FROM UNDER THE HOOD THEN FLAMES APPEARED. THE VEHICLE CAUGHT ON FIRE. THE FIRE DEPARTMENT EXTINGUISHED THE FIRE. A POLICE REPORT WAS FILED. THE VEHICLE WAS TOWED TO A TOW LOT AND DESTROYED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE 52,000.

Mileage: 52,000

Oct 30, 2018

1.6L ECOBOOST ENGINE IS BURNING COOLANT THROUGH THE COMBUSTION CHAMBER (HEADS). THIS CAUSES CAR TO LOSE COOLANT, MISFIRE, AND OVERHEAT. RECALL 17S09 WOULD SEEM TO ADDRESS THIS ISSUE. MY VEHICLE, THAT MEETS ALL OF THE PARAMETERS OF THE RECALL TO INCLUDE VEHICLE MODEL, MAKE, YEAR, ENGINE SIZE, FACTORY OF ASSEMBLY, DATE OF ASSEMBLY, ETC., IS NOT INCLUDED IN THE RECALL. FORD IS UNWILLING TO RECTIFY.

Mileage: 3

Oct 30, 2018 Fire

COOLANT LEVEL SENSOR SYSTEM INSTALLATION ,NHTSA RECALL NUMBER: 17V209,DAUGHTER HAD WENT TO GROCERY STORE WITH A FRIEND,HAD TURNED OFF VEHICLE AND EXITED IT, WAS HELPING FRIEND CARRY GROCERIES TO APARTMENT,WHEN WENT TO GOT BACK TO CAR IT WAS ON FIRE UNDER THE HOOD,CALLED FIRE DEPARTMENT ,FIRE DEPARTMENT CAME AND EXTINGUISHED THE FIRE,VEHICLE WAS TOWED AND IS BEING INVESTIGATED BY FIRE MARSHAL

Mileage: 53,000

Oct 29, 2018

I PREVIOUSLY FILED A REPORT DUE TO THE ENGINE COOLANT LOW LIGHT COMING ON. TOOK CAR TO THE DEALER WHERE THEY RAN TEST AND DISCOVERED COOLANT HAD LEAKED INTO THE ENGINE AND OIL AND THAT THE ENGINE WOULD HAVE TO BE REPLACED. QUOTED A PRICE OF $6,400+/- WHEN THEY PULLED THE ENGINE THEY REMOVED THE TURBO FOR RE-USE. UPON REMOVAL OF THE TURBO, BEARINGS AND SHROUDS OF METAL FEEL OUT. I WAS TOLD THAT THERE WAS CATASTROPHIC FAILURE AND THAT THE BEARINGS AND METAL HAD EXPLODED INTO THE ALUMINUM ENGINE BLOCK CAUSING A CRACK AND ALLOWING COOLANT INTO THE ENGINE AND OIL. I'M STILL WAITING ON THE REPAIR TO BE COMPLETED, AND KNOW THE COST APPEARS TO BE AROUND $7,500+/-. STILL HAVEN'T HEARD BACK FROM FORD. THIS COULD HAVE BEEN BAD OF THE ENGINE SHUT DOWN WHILE DRIVING.

Mileage: 95,000

Oct 25, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 55 MPH, THE ENGINE WARNING INDICATOR ILLUMINATED AND THE VEHICLE STALLED. THE VEHICLE WAS TOWED TO BLUE SPRINGS FORD (3200 NW SOUTH OUTER RD, BLUE SPRINGS, MO 64015, 816-229-4400) WHERE IT WAS DIAGNOSED THAT THE ENGINE BLOCK HAD FRACTURED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE AND ADVISED THE CONTACT TO CALL NHTSA. THE FAILURE MILEAGE WAS APPROXIMATELY 74,947.

Mileage: 74,947

Oct 24, 2018

ENGINE COOLANT LOW LIGHT CAME ON. CHECKED RESERVE AND IT WAS LOW. VEHICLE HAD JUST BEEN SERVICED 2,000 MILES EARLIER. I ADDED COOLANT THE NEXT DAY. I DISCOVERED OIL ON THE FLOOR. TOOK CAR TO FORD AND THEY DID PRESSURE AND DYE TESTS. THEY WOULD COOLANT IN THE OIL. THEY SAID THIS WAS NOT PART OF THE COOLANT/CRACKED BLOCK, POTENTIAL FIRE RECALL. OUT CAR IS SERVICED EVERY 5,000 MILES. DUE TO THE COOLANT CONTAMINATION OF THE ALUMINUM ENGINE, FORD STATED THE THE ENGINE WOULD REQUIRE REPLACEMENT AT $6,200+. THE DEALER HAD ME SPEAK TO FORD CUSTOMER CARE WHICH I DID. I GOOGLED ONLINE AND THERE APPEARS TO BE A NUMBER OF SIMILAR INCIDENTS. THE VEHICLE HAS APPROXIMATELY 95,000 MILES. A PROPERLY SERVICED ENGINE SHOULDN'T FAIL THAT SOON. THE SCOPE OF THE FORD RECALL SHOULD BE EXPANDED TO COVER ENGINE COOLANT LOSS AND ENGINE CONTAMINATION. FURTHER DRIVING COULD HAVE RESULTED IN THE ENGINE SEIZING UP WHILE DRIVING.

Mileage: 95,000

Oct 22, 2018

I PURCHASED A 2014 FORD ESCAPE FROM BEST FORD IN NASHUA, NH BACK IN JULY OF 2014. I STARTED TO HEAR ABOUT RECALLS ON THE ESCAPE BECAUSE OF ISSUES WITH COOLANT LEVELS LEADING TO CRACKED BLOCKS & POTENTIAL FIRES. I STARTED KEEPING AN EYE ON MY COOLANT LEVELS. I STARTED TO NOTICE THAT IT WAS RUNNING LOW & I FOUND MYSELF TOPPING OFF THE COOLANT ON A REGULAR BASIS. I CALLED FORD & EXPLAINED TO THEM THAT I WAS HAVING ISSUES WITH COOLANT LEVELS AS STATED IN MANY RECALLS, I ASKED IF MY CAR WOULD BE ADDED TO THE RECALL. THEY TOLD ME MY CAR WOULDN'T FALL UNDER THE RECALL BECAUSE THE RECALL PERTAINED ONLY TO CERTAIN ENGINES THAT CAME FROM A CERTAIN PLANT. THAT IS INCORRECT. A COUPLE OF WEEKS AGO MY CAR STARTED ACTING UP. I TOOK IT TO A LOCAL MECHANIC BUT HE SAID I SHOULD GO DIRECTLY TO FORD WITH MY CAR. I TOOK MY VEHICLE TO IPSWICH FORD. ONCE THEY STARTED TO DIG INTO THE ISSUES WITH MY CAR, THEY REALIZED THAT THE MOTOR WAS JUNK BUT ALSO THAT MY VEHICLE WAS NOT UNDER RECALL OR WARRANTY. THEY STOPPED WORKING ON THE CAR BECAUSE IT WOULD HAVE COST ME HUNDREDS OF DOLLARS TO FIND OUT WHAT THEY ALREADY KNEW, THAT THE ENGINE WAS JUNK. BY THEM STOPPING THE WORK, THEY WERE ABLE TO PUT THE MOTOR BACK TOGETHER SO I COULD DRIVE IT TEMPORARILY. IF THEY CONTINUED, I WOULD HAVE BEEN TAKING THE CAR OUT OF THE SERVICE CENTER ON A FLAT BED. THE SERVICE MANAGER AT IPSWICH FORD ALSO TOLD ME THAT THE ISSUE WITH THESE MOTORS IS NOT ONLY FROM A CERTAIN PLANT BUT THAT ALL ECOBOOST MOTORS HAVE ISSUES. HE SAID THAT FORD WAS GIVING THEM AN ALLOWANCE YEARLY TO HELP PEOPLE WITH ENGINE ISSUES. HE INFORMED THAT FORD HAS NOW CUT-OFF ANY ALLOWANCES & THAT IF THE CAR ISN'T ON A RECALL OR HAS THE EXTENDED WARRANTY, THE CUSTOMER IS LEFT OUT IN THE COLD. I NEED TO KNOW IF THERE IS ANYTHING THAT CAN BE DONE FOR ME IN MY SITUATION. CAN I BE ADDED TO THE RECALL, DO I HAVE ANY OTHER AVENUES TO GET COMPENSATION FROM FORD

Mileage: 97,000

Oct 22, 2018 Fire

WHILE DRIVING UPHILL ON I-80 ON A COOL DAY IN OCTOBER, SPEED LIMIT 65MPH, OUT OF NO WHERE, MY 2014 ESCAPE ILLUMINATED THE CHECK ENGINE LIGHT, IMMEDIATELY FOLLOWED BY AN "ENGINE TEMP HIGH, PLEASE STOP SAFELY" ON THE SCREEN. I HAD NEVER SEEN EITHER OF THESE WARNINGS BEFORE SO I IMMEDIATELY PULLED OVER TO THE SIDE OF THE HIGHWAY AND TURNED OFF THE ENGINE AS IT BEGAN SMOKING FROM UNDER THE HOOD. AT THIS TIME THE OIL WARNING LIGHT ILLUMINATED RED - WITHIN APPROX. 60 SECONDS, THE ENGINE MADE A LOUD POPPING NOISE AND EXPLODED INTO FLAMES. I QUICKLY EVACUATED THE VEHICLE AND RAN DOWN THE HIGHWAY, WITHIN MINUTES THE ENTIRE CAR WAS IN FLAMES AND WAS LATER RULED A TOTAL LOSS. THIS VEHICLE HAD BEEN SERVICED BY THE HYUNDAI DEALERSHIP IT WAS PURCHASED FROM 6 DAYS PRIOR AND WAS GIVEN A "CLEAN BILL OF HEALTH" BY THE MECHANICS.

Mileage: 85,000

Oct 18, 2018

WHILE TRAVELING AT APPROXIMATELY 60MPH, AT APPROXIMATELY 52K MILES, MY 2014 FORD ESCAPE SUDDENLY OVERHEATED AND PRESENTED A WARNING TO PULL OVER AND STOP THE CAR. MY COOLANT LEVEL HAD DROPPED BELOW THE MINIMUM AND MY CAR OVERHEATED. I ADDED WATER FOR THE SYSTEM AND HAD MY CAR TAKEN TO A LOCAL SHOP WHO REPLACED THE THERMOSTAT AS WELL AS COOLANT OVERFLOW SYSTEM. ADDITIONALLY THE CHECK ENGINE LIGHT ILLUMINATED AFTER OVERHEATING. ONCE "FIXED" AND LESS THAN 5000 MILES LATER (APPROXIMATELY 56K), MY CAR OVERHEATED AGAIN. THE COOLANT LEVELS WERE LOW, WITH NO WARNING OF LOW COOLANT SYSTEM EVER DISPLAYED UNTIL I RECEIVED THE WARNING (AGAIN GOING APPROXIMATELY 60 MPH) TO PULL OVER AND SHUT DOWN OVERHEATED ENGINE. THE CHECK ENGINE LIGHT WAS ILLUMINATED AND I BROUGHT THE CAR TO SHOP AGAIN. DIAGNOSTIC OF CODE READ POTENTIALLY FAULTY THERMOSTAT (WHICH I HAD REPLACED LESS THAN 5000 MILES BEFORE) OR LOW COOLANT (AGAIN JUST FILLED). I DECIDED NOT TO ACTION (EXCEPT STANDARD OIL CHANGE DUE) AND THE CHECK ENGINE LIGHT WENT OFF ON ITS OWN. NOW AT 56,800 MY CAR HAD THE CHECK ENGINE LIGHT RE-ILLUMINATED AND NOW IS BLINKING THAT I HAVE LOW OIL PRESSURE (LESS THAN 2000 MILES SINCE OIL CHANGE). TAKING TO SERVICE THIS AFTERNOON FOR DIAGNOSTIC. VERY SIMILAR TO ISSUES DOCUMENTED IN OTHER 2014 ESCAPES UNDER RECALL 17S09- HOWEVER, MY PARTICULAR VIN IS NOT CONSIDERED INCLUDED, DESPITE BUILD AT LOUIVILLE, KY IN APRIL 2014. THEREFORE, NO RECALL SERVICE OF COOLANT SENSOR CAN BE PROVIDED.

Mileage: 52,000

Oct 10, 2018

COOLANT RECOVERY CRACKED DUE TO ENGINE HEAT WITHOUT THERMOSTAT INDICATING HIGH ENGINE TEMPERATURE.

Mileage: 79,000

Oct 10, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING APPROXIMATELY 55 MPH, THE TRANSMISSION FAILED. THE CONTACT DEPRESSED THE ACCELERATOR PEDAL AND THE RPMS INCREASED RAPIDLY. THE CONTACT WAS UNABLE TO ACCELERATE BEYOND 55 MPH. THE CONTACT PULLED THE VEHICLE OVER TO THE SIDE OF THE ROAD AND WAS ABLE TO RESTART THE VEHICLE AND DRIVE AWAY. FOLSOM LAKE FORD (12755 FOLSOM BLVD, FOLSOM, CALIFORNIA, (916) 353-2040) DIAGNOSED THAT THE COOLANT LEVEL SENSOR SYSTEM WAS FAULTY. THE DEALER ALSO STATED THAT THE TRANSMISSION WAS FAULTY AND NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE CONTACT REFERENCED NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE FAILURE MILEAGE WAS 80,853.

Mileage: 80,853

Oct 10, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING VARIOUS SPEEDS, THE ENGINE COOLANT AND CHECK ENGINE INDICATORS ILLUMINATED ON SEVERAL OCCASIONS. THE CONTACT STATED THAT THE ENGINE COOLANT WAS REPLACED, BUT THE INDICATORS REMAINED ILLUMINATED. AN INDEPENDENT MECHANIC FOUND A DIAGNOSTIC TROUBLE CODE FOR THE CYLINDER 2 MISFIRE AND STATED THAT THE ENGINE WAS FAULTY AND NEEDED TO BE REPLACED DUE TO A BLOWN HEADGASKET. MIRACLE FORD (1394 NASHVILLE PIKE, GALLATIN, TENNESSEE 37066, (615) 452-5267) WAS MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED BY THE DEALER. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND REFERRED THE CONTACT TO NHTSA. IN ADDITION, THE MANUFACTURER STATED THAT THERE WERE NO RECALLS OR SERVICE WARRANTY PROGRAMS ON THE VEHICLE. THE FAILURE MILEAGE WAS 118,571.

Mileage: 118,571

Oct 9, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING AT AN UNKNOWN SPEED, THE ENGINE MADE A LOUD POPPING NOISE AND THE CHECK ENGINE WARNING INDICATOR ILLUMINATED. THE VEHICLE WAS TAKEN TO WAYNE FORD (444 US-46, WAYNE, NJ 07470) WHERE IT WAS DIAGNOSED THAT THE ENGINE NEEDED TO BE REPLACED BECAUSE IT INGESTED COOLANT. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE CONTACT STATED THAT THE VEHICLE WAS REPAIRED PER NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE APPROXIMATE FAILURE MILEAGE WAS 75,000.

Mileage: 75,000

Oct 8, 2018

I WAS PARKED IN A LARGE PARKING LOT OF A GROCERY STORE. WHEN LEAVING MY VEHICLE WAS BEING PUT INTO DRIVE, TRANSMISSION WENT INTO REVERSE AND SHIFTER WAS IN PARK. THE KEY WAS ABLE TO BE REMOVED BUT UNABLE TO KEEP CAR SECURE W/O LEAVING PARKING BRAKE ON. THERE WAS NO WAY TO CRANK THE CAR SINCE IT WAS NOT IN PARK. CAR WAS COMPLETELY NON WORKING. MY VEHICLE HAD TO BE LEFT IN THE PARKING LOT AND TOWED TO A DEALERSHIP FOR REPAIRS. IN SITTING IN THE PARKING LOT, WITH A NON-FUNCTIONING CAR WAITING FOR A TOW TRUCK, I SEARCHED ONLINE AND FOUND THE EXACT DESCRIPTION OF WHAT WAS GOING ON UNDER RECALL 18S20. INFORMED THE DEALERSHIP OF THIS WHEN THE CAR WAS DELIVERED TO THEM. THAT WAS THE ONLY PART THAT WAS FIXED, SINCE IT WAS THE ONLY FAULTY PART. FORD REFUSED TO PAY FOR THE REPAIRS SINCE, APPARENTLY, MY CAR WAS MANUFACTURED AT A DIFFERENT PLANT. SAME MAKE, MODEL, ETC. SAME PART, OTHERS ARE PAID FOR, JUST NOT MINE. FORD WAS NOT WILLING TO COMPENSATE BECAUSE THE VIN WAS NOT IN THE SYSTEM FOR THIS RECALL AT THE TIME OF MY REPAIRS. THIS WAS A SAFETY ISSUE AND LOT OF WASTED TIME, SERVICES AND MONEY. IF I HAD KNOWN AND BEEN INFORMED OF THIS I COULD HAVE HAD IT FIXED PRIOR TO A BREAKDOWN AND WOULD NOT HAVE HAD TO HAVE MY CHILDREN WITH ME, IN A HOT CAR, IN A BUSY PARKING LOT VERY UPSET. UNNECESSARY STRESS FOR SURE.

Mileage: 96,000

Oct 8, 2018

COOLANT OVERFLOW TANK IS LEAKING RESULTING IN LOW LEVELS OF COOLANT. COOLANT WAS NOTICED UNDER THE CAR AT 3 SEPARATE OCCASIONS. NOTICED A RECALL INCLUDING 2014 FORD ESCAPES WITH 1.6 LITER TURBOCHARGED 4 CYLINDER ENGINE HOWEVER MY VIN WAS NOT INCLUDED AND I FEEL IT SHOULD HAVE BEEN INCLUDED. RECALL STATES THAT LOW LEVELS OF COOLANT CAN CAUSE THE HEAD TO CRACK LEADING TO AN ENGINE FIRE.

Mileage: 31,854

Oct 6, 2018

TRUCK STALLS WHILE DRIVING, AND WON'T START BACK UP. IVE HAD IT TOWED TWICE ALREADY FOR THE SAME PROBLEM ALSO HAD IT TOWED TO A MECHANIC SHOP WHERE THEY COULDN'T FIND ANYTHING WRONG WITH IT BESIDES SAYING IT SEEMED TO BE A GLTCH INSIDE THE COMPUTER. CHECK ENGINE LIGHT ILLUMINATES READING CODE P0109. WHEN IT STALLS IT GIVES NO WARNING AND NO INDICATIONS THAT THERE'S A PROBLEM WHICH CAN LEAD TO A DANGEROUS SITUATION.

Mileage: 72,000

Oct 4, 2018

2014 ESCAPE RECALLED TO FIX COOLANT LEAK. 6 MONTHS LATER THE COOLANT IS LEAKING AND WARPED THE HEAD GASKET. HAD THE VEHICLE TOWED TO FORD, THEY ARE TRYING TO DENY RESPONSIBILITY, DESPITE THE SERVICE DEPARTMENT DIRECTLY STATING ON MY INVOICE "ENGINE COOLANT LEAK CAUSED HEAD GASKET TO WARP." MY CAR HAS BEEN AT THE DEALERSHIP FOR 15 DAYS AND THEY STILL HAVE NOT WORKED ON IT BECAUSE THEY ARE ARGUING WHO IS RESPONSIBLE WITH MY WARRANTY COMPANY. IT SEEMS LIKE A LOT OF PEOPLE ARE EXPERIENCING THE SAME POOR WORKMANSHIP. I AM NOW CONTACTING AN ATTORNEY, WITH ALL THESE CASES WE MAY HAVE A CLASS ACTION SUIT AGAINST FORD.

Mileage: 74,000

Oct 3, 2018

I HAVE HAD TO REPLACE MY BATTERY TWICE IN THIS CAR ALREADY, IT CONTINUOUSLY SHOWS CORROSION ON THE BATTERY TERMINALS. I HAVE BEEN TOLD THAT IT APPEARS THAT THERE IS SOMETHING THAT IS CONSTANTLY PULLING ENERGY BUT THERE IS NOTHING LEFT ON AND NO ADDED EXTRAS AT ANYTIME.

Oct 2, 2018

AFTER DRIVING APPROX. 1/2 MILE ON A VERY BUSY CITY STREET AT MORNING RUSH HOUR, GOING APPROX 35 MPH, I STARTED COASTING DOWNHILL. SCREEN INDICATED HIGH ENGINE TEMPERATURE, ENGINE IMMEDIATELY STARTED TO STALL MAKING IT HARD TO MANEUVER THE VEHICLE. MESSAGE INDICATED TO PULL OVER & SHUT OFF ENGINE. TEMP GAUGE WAS ALL THE WAY IN THE RED. HAD VEHICLE TOWED TO DEALERSHIP FOR DIAGNOSTIC.

Mileage: 72,000

Sep 30, 2018 Fire

I WAS DRIVING MY CAR SOUTHBOUND ON I75 AND MY ENGINE BURST INTO FLAMES, LUCKY MY BROTHER WAS BEHIND ME AND COULD SEE THE FIRST UNDER THE CAR AND CALLED ME TO TELL ME TO PULL OVER AND GET OUT RIGHT AWAY. I GOT OUT AND THE CAR BURNT UP ON THE SIDE OF THE ROAD.

Mileage: 144,000

Sep 30, 2018

17S09 COOLING SYSTEM RECALL PERFROMED IN FEB 2018 VEHICLE HAS HAD NUMEROUS TRIPS BACK TO MULTIPLE FORD DEALERSHIPS FOLLWOING HIGH TEMPERATURE LIGHT COMING ON. THE ENGINE HAS BEEN REPLACED A HOSE REPLACED, COOLING FAN RELAY REPLACED. CURRENTLY THE CAR IS AT A DEALER WHO IS NOW SAYING THE INSTRUMENT PANEL CLUSTER IS THE PROBLEM BUT IS NOW ATTEMPTING TO CHARGE ME $750, THIS CAR HAD NO ISSUES PRIOR TO THE RECALL. FORD DOES NOT SEEM TO KNOW HOW TO FIX THESE PROBLEMS AND NOW I AM ABOUT TO BE ON THE HOOK FOR THEM. I SHOULD'T HAVE TO PAY TO BE THEIR GUINEA PIG. THEY HAVE LEFT MY CAR UNSAFE AND UNRELIABLE.

Mileage: 80,000

Sep 26, 2018

MY CAR WITH ONLY 34,000 MILES OVERHEATED DRIVING ON THE HIGHWAY. I TAKE MY CAR FOR FOR OIL CHANGES AND SERVICE REGULARLY. THERE WAS NO INDICATION OF A PROBLEM UNTIL THIS HAPPENED. MY MECHANIC SAID I WAS LOW ON COOLANT AND AFTER FURTHER TESTING SAID I HAD A LEAK. HE THEN TOLD ME THAT THERE WAS A RECALL ON 2014 FORD ESCAPES FOR THIS EXACT PROBLEM. FORD'S NUMBER FOR THIS RECALL IS 17S09. I CALLED MY FORD DEALER AND WAS TOLD THAT EVEN TOUGH MY CAR WAS HAVING THE SAME ISSUE MY PARTICULAR CAR WAS NOT PART OF THE RECALL AND I WOULD HAVE TO PAY TO HAVE THE CAR FIXED. THINKING THIS WAS OUTRAGEOUS I CALLED FORD DIRECTLY. THEY AS WELL TOLD ME THE SAME THING. AFTER FURTHER RESEARCH I SEE THAT I AM NOT THE ONLY 2014 FORD ESCAPE OWNER THAT HAS BEEN TOLD THAT ALTHOUGH THEY HAVE THIS SAME SAFETY ISSUE OUR VEHICLE IS NOT INCLUDED IN THE RECALL. I BELIEVE FURTHER INVESTIGATION NEEDS TO BE DONE AND MORE CARS INCLUDED IN THIS RECALL.

Mileage: 34,000

Sep 26, 2018

THE VEHICLE COMPLETELY STALLED IN THE MIDDLE OF DRIVING AFTER A LEAK RECALL WAS MADE. WE TOOK THE CAR AND HAD THE NECESSARY RECALL DONE. HOWEVER THE ENGINE STALLED THE CAR AND NOW WE HAVE TO SHELL OUT $6,000 FOR A NEW ENGINE DUE TO A CRACKED BLOCK. SINCE WE ALREADY TOOK THE CAR TO GET A LEAK RECALL ISSUE FIXED, WE ARE AFRAID THE NEW ENGINE WILL GET OVERHEATED AGAIN AND THE CAR WILL STALL. ALSO, WE WOULD HAVE TO SHELL OUT MORE MONEY FOR ANOTHER ENGINE.

Mileage: 102,000

Sep 24, 2018

WHILE TRAVELING ON THE HIGHWAY, MY ENGINE SUDDENLY OVERHEATED AND I WAS GIVEN AN ALARM DISPLAYING THAT ITS OVERHEATING AND STOP SAFELY. WHEN OPENING MY LID, I FOUND THE COOLANT LEVEL HAD DROPPED BELOW MINIMUM. I HAD NO WARNING THAT MY COOLANT LEVEL WAS SUDDENLY LOW AND THE CAR HAD BEEN OPERATING FINE THE PREVIOUS DAY AND EARLIER IN THE MORNING. I ADDED WATER TO THE SYSTEM AND AFTER RETURNING THE CAR TO A SAFE TEMP, DROVE IT TO A STORE. THE CHECK ENGINE LIGHT CAME ON INSTANTLY AFTER THE HEATING ISSUE. FORD HAS A RECALL FOR THIS ISSUE INCLUDING 2014 FORD ESCAPE, HOWEVER MY VIN DOES NOT REGISTER AS BEING APPLICABLE TO THE RECALL (ALTHOUGH SEEMS LIKE IDENTICAL ISSUE.) THIS IS THE SECOND TIME BETWEEN 50-56000 MILES THIS SAME ISSUE HAS OCCURRED.

Mileage: 56,000

Sep 21, 2018

ENGINE COOLANT SENSOR FAULTY . BROUGHT TO THE DEALERSHIP 2 TIMES.

Mileage: 67,000

Sep 11, 2018

A DOZEN TIMES NOW WHEN WE START IT UP IT RUN REAL RUFF AND WILL LURCH, THE RPMS GO UP BUT NOT MPH BEING GAINED. I HAVE TO PULL OVER AND TURN IT OFF AND RESTART AND IT RUNS FINE. WE GET A MESSAGE THAT READS "ENGINE FAULT SERVICE NOW". WHEN WE TAKE IT TO THE DEALER THEY CAN'T FINE ANY ERRORS ON WHEN THEY HOOK IT UP TO THEIR COMPUTER. THIS HAS HAPPENED MULTIPLE TIMES WITHIN THE LAST WEEK AND OVER THE ALMOST 4 YEARS I'VE OWNED THE CAR. I WAS DRIVING IT ON A CITY STREET AND HAD JUST BACKED OUT OF MY DRIVE WAY, OTHER TIMES IT'S HAPPENED HAS BEEN ON CITY STREETS SHORTLY AFTER PULLING FORWARD, AND THOSE TIMES I HAD NOT BACKED UP AT ALL PRIOR TO IT DOING IT. THIS MORNING WHEN IT HAPPENED I ALMOST HAD SOMEONE REAR-END ME BECAUSE MY CAR WOULD NOT GET ABOVE 5MPH. I HAD DRIVEN ABOUT A BLOCK FROM MY HOME BEFORE THE ERROR MESSAGE CAME ON AND WAS FORCED TO PULL OVER. THANKFULLY I WASN'T ON THE HIGHWAY YET.

Mileage: 140,000

Sep 10, 2018 Fire

ON 13 AUGUST 2018 MY FIANCE WAS DRIVING TO OUR NEW HOME WE'RE BUYING WHEN SMOKE STARTED COMING OUT OF THE ENGINE COMPARTMENT. I TOLD HER TO PULL OVER AND GRAB HER PURSE AND GET AWAY FROM THE VEHICLE. BY NOW FLAMES WERE COMING FROM THE ENGINE COMPARTMENT. LUCKILY SHE HAD CRACKED OPEN THE DOOR BEFORE STOPPING BECAUSE BEFORE SHE STOPPED ALL THE DOORS AUTOMATICALLY LOCKED AND COULD NOT BE OPENED. I HAD ARRIVED AT THE SCENE AND THE CARS FRONT END HAD VIRTUALLY MELTED WITHIN 5 MINUTES. IF MY FIANCE HAD NOT CRACKED OPENED THE DOOR SHE MOST ASSUREDLY WOULD HAVE BURNED TO DEATH. IF I HAD BEEN DRIVING I WOULD DEFINITELY HAVE HAD A DIFFICULT TIME ESCAPING AS I AM A DISABLED VETERAN WITH SEVERAL MOBILITY PROBLEMS. OUR CAR WAS LESS THAN 4 YEARS OLD WITH ONLY 64000 MILES ON IT. WE NEVER EXPECTED WE MIGHT POSSIBLY BE INJURED OR DIE FROM A NEWER VEHICLE. I REALLY HOPE THAT FORD MOTOR COMPANY WASN'T AWARE OF THIS ISSUE AS WE NEVER RECEIVED ANY NOTICE OF ANY PROBLEMS WHATSOEVER WITH THIS VEHICLE.

Mileage: 64,400

Sep 7, 2018

VEHICLE ERRATICALLY DISPLAYS OVERHEATING VISUAL AND AUDIBLE ALARM DURING MOTION OR STATIONARY. AFTER VEHICLE IS TURNED OFF FOR A FEW SECONDS, ALARMS GO OFF AND TEMPERATURE GAGE RETURNS TO NORMAL OPERATING TEMPERATURE. CHECK ENGINE LIGHT ON FOR A WHILE, THEN OFF, THEN BACK ON. DROVE TO FORD DEALER FOR SERVICE (DIDN'T NOTICE ANY PERFORMANCE ISSUES), AND THEY STATE THAT THE ENGINE NEEDS TO BE REPLACED, BECAUSE OF A CRACK IN THE COOLANT RESEVOIR, AND COOLANT IS GETTING INTO CYLINDER #3. I DON'T KNOW HOW THESE ARE RELATED. I HAVE NEVER NOTICED A COOLANT LEAK OR STEAM/SMOKE IN THE EXHAUST.

Mileage: 119,000

Sep 4, 2018

I TOOK MY CAR IN TO THE DEALER DUE TO COOLANT BEING LOW. THE COOLANT LEAKED INTO THE ENGINE AND MY GASKET HAD TO BE REPLACED. THERE ARE SEVERAL ARTICLES IN WHICH FORD ADMITS THERE ARE ENGINE PROBLEMS UP TO AND INCLUDING FIRE. I WAS ABLE TO MITIGATE DAMAGE BY GETTING THE CAR IN EARLY. THE DEALER CALLED FORD, I CALLED THE FORD CARES LINE AND MY CLAIM WAS DECLINED. THIS IS A KNOWN PROBLEM. I HAVE WRITTEN TO FORD, NO REPLY

Aug 24, 2018

2 ACTIVE RECALLS-NO TIMEFRAME OF WHEN IT WILL BE REMEDIED. ADDITIONALLY, VEHICLE DIES WHEN PUT INTO D FROM R. VEHICLE HAS 52K MILES, WELL MAINTAINED, SHELL FUEL IS USED. THIS HAPPENS WHEN BACKING UP AND PUTTING INTO DRIVE. VEHICLE WAS IN MOTION.

Mileage: 52,000

Aug 22, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 45 MPH, THE VEHICLE EMITTED AN ABNORMAL ANTI-FREEZE ODOR AND EXPERIENCED A LOSS OF ENGINE POWER. THE FAILURE OCCURRED WITHOUT WARNING. THE VEHICLE WAS TOWED TO DAVE SINCLAIR LINCOLN ST. PETERS (4760 N SERVICE RD, ST PETERS, MO 63376) WHERE IT WAS DIAGNOSED THAT THE CYLINDER HEAD WAS CRACKED AND NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE CONTACT STATED THAT A SIMILAR FAILURE OCCURRED ONE YEAR PRIOR AND THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 94,000.

Mileage: 94,000

Aug 21, 2018

COOLANT LEAK INTO CYLINDER #3 & 4 RESULTING IN NECESSARY ENGINE REPLACEMENT AT 64K MILES. ONLY SERVICE ISSUE TO DATE ON VEHICLE WAS A DEFECTIVE WATER PUMP & COOLANT SENSOR AT JUST UNDER 60K MILES. WHILE DRIVING 'LOW COOLANT' LIGHT SUDDENLY CAME ON, CHECKED COOLANT WHICH WAS VERY LOW, FILLED AND TOOK TO DEALER LESS THAN 2 MILES AWAY. VEHICLE WAS NOT INCLUDED ON THE LAST COOLANT LEAK RECALL ALTHOUGH VERY SIMILAR ISSUE AND BUILT DURING THE SAME TIME PERIOD AT LOUISVILLE PLANT.

Mileage: 64,000

Aug 21, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT THE VEHICLE WAS TAKEN TO FELIX SABATES FORD LINCOLN (7601 SOUTH BLVD, CHARLOTTE, NC) TO BE REPAIRED PER NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE DEALER'S REPRESENTATIVE TOOK THE CONTACT'S KEYS AND DECLARED THE VEHICLE TO BE A ROAD HAZARD DUE TO THE ENGINE. THE VEHICLE WAS REPAIRED, BUT THE DEALER REFUSED TO RETURN THE VEHICLE DUE TO ADDITIONAL DAMAGES CAUSED BY OIL LEAKING INTO THE COOLANT. THE CONTACT REQUESTED DOCUMENTATION, BUT THE CONTACT REFUSED DUE TO THE DAMAGES BEING ATTRIBUTED TO THE RECALL. THE MANUFACTURER WAS NOTIFIED AND PROVIDED THE CONTACT WITH AN ESTIMATE OF THE DAMAGES AND REQUESTED THAT THE DEALER PROVIDE DOCUMENTATION. THE FAILURE MILEAGE WAS APPROXIMATELY 69,000.

Mileage: 69,000

Aug 16, 2018

MY VIN IS HAVING THE EXACT SAME COOLING ISSUES AS RECALL. DEALER STAES MY VIN IS NOT AFFECTED ALTHOUGH THE IT BROKE IN THE EXACT FASHION AS THE FORD RECALL 17V209000. THE VEHICLE OVERHEATED AND IS LOSING COOLANT SLOWLY. CAR OVERHEATED AND HAD TO PULL OVER.

Mileage: 182,000

Aug 9, 2018

2014 ESCAPE WAS TAKEN TO THE DEALERSHIP FOR A COOLANT LEAK. DEALER FOUND THAT THE COOLANT BYPASS SOLENOID WAS LEAKING AS WELL AS THE ENGINE COOLANT TEMPERATURE SENSOR WAS FAULTY. BOTH ITEMS WERE REPLACED. BILL WAS $566. FORD HAD A RECALL ON OVER 200000 ESCAPES IN THE 2013 AND SOME 2014 ESCAPES. I CALLED THE FORD COMPANY AND FOUND OUT THAT MY ESCAPE WAS NOT COVERED UNDER THERE ALL. SAID TO THEM THAT OVER 200000 ESCAPES WERE RECALLED FOR THE SAME EXACT PROBLEM AND THEY SAID TO BAD THE VIN NUMBER IS NOT ON THE RECALL LIST.

Aug 6, 2018

WE ADVISED THE LOCAL FORD DEALER THAT THE ENGINE WAS RUNNING ROUGH DURING START UP BUT THEN TURNED NORMAL, SLIGHT SMELL OF ANTI FREEZE BUT NO OVER HEATING OR CHANGE IN TEMPERATURE GAUGE, HAD PREVIOUSLY TAKE THE CAN IN FOR THE HEAT SENSOR / LOW COOLANT RECALL, WAS TOLD TO DRIVE CAR TO DEALER. AFTER ARRIVAL AND FURTHER INSPECTION WE WERE ADVISED THAT THE ENGINE WAS WARPED, HEAD WARPED AND NEEDED A NEW ENGINE. BOTH DEALER AND FORD AND AFTER MARKET WARRANTY BLAMED US FOR DRIVING 5 MILES ON LOCAL ROADS TO DEALER AND THEREFORE THEY WOULD NOT COVER THE PROBLEM.

Mileage: 82,000

Jul 29, 2018

POSTING DATE: JULY-29, 2018 (SUNDAY) VEHICLE : 2014 FORD ESCAPE TITANIUM 4X4 (4-CYLINDER TURBO ENGINE, AUTOMATIC TRANSMISSION) VEHICLE LOSES TRANSMISSION POWER. THREE WEEKS AGO I CAME OUT OF A FREEWAY AND TRIED TO MAKE A RIGHT TURN ON A FAST MOVING LOCAL ROAD. I MADE THE TURN AND PRESSED THE ACCELERATOR BUT THE CAR WOULD NOT MOVE. THE ENGINE REVVED UP BUT THERE WAS NO MOTION. I HAD TO IMMEDIATELY TURN ON THE HAZARD FLASH LIGHTS TO WARN APPROACHING VEHICLES BEHIND. FINALLY I PRESSED THE ACCELERATOR "SLOWLY" AND THE CAR DID MOVE AND PICK UP SPEED. THERE WERE NO FURTHER ISSUES THAT DAY. I HAD SENSED "BUMPY GEAR SHIFTS" AND "JERKY ACCELERATIONS" EVEN BEFORE THE ABOVE INCIDENT. I INSTINCTIVELY "KNEW" THAT THINGS WERE NOT RIGHT BUT DID NOT KNOW EXACTLY WHAT IT WAS. TWO DAYS AGO MY WIFE CALLED ME AT WORK AND SAID THAT AFTER BACKING OUT FROM THE GARAGE, THE CAR WAS NOT PICKING UP SPEED. THE "CHECK ENGINE" LIGHT HAD ALSO COME UP. SHE SOMEHOW LIMPED SLOWLY BACK INTO THE GARAGE. WHEN I RETURNED HOME, I TRIED IT TOO. I FOUND THAT ONLY THE "REAR DRIVE" WAS WORKING. THE "FORWARD DRIVE" HARDLY WORKED. OFTEN WHILE IN "DRIVE" MODE, THE CAR ROLLED BACKWARDS ON OUR MILDLY SLOPED DRIVEWAY! USING "THE LOWEST GEAR" I SOMEHOW PUT IT BACK INTO THE GARAGE. YESTERDAY I GOT IT TOWED TO THE NEAREST FORD DEALERSHIP. BEING A SATURDAY, THEY COULD NOT DO ANYTHING MORE. THEY SAID THEY WILL LOOK INTO IT TOMORROW (MONDAY). I CONSIDER THIS TO BE A MAJOR SAFETY ISSUE. I AM LUCKY THAT I DID NOT LOSE COMPLETE POWER ON THE FREEWAY AND NOTHING BAD HAS HAPPENED SO FAR TO ME OR MY WIFE. READING ABOUT OTHERS' EXPERIENCES ON THE INTERNET ON THE SAME MODEL YEAR VEHICLE, IT SEEMS THAT THEY MIGHT HAVE FACED MUCH MORE DANGEROUS SITUATIONS. PLEASE INVESTIGATE THIS PROBLEM SERIOUSLY AND NOTIFY THE VEHICLE MANUFACTURER.

Mileage: 74,000

Jul 29, 2018

ENGINE STALLS. - 1.6 L. - I HAVE TAKEN THIS CAR TO THE BOB TOMES FORD DEALERSHIP IN MCKINNEY, TEXAS FOR THIS PROBLEM AT LEAST TWICE SINCE I BOUGHT IT NEW AND THEY TOLD ME BOTH TIMES THAT THERE WAS NOTHING WRONG AND THAT THE ENGINE WAS OPERATING PER SPECIFICATIONS. IT IS STILL STALLING AND REALLY SCARES ME WHEN IT DOES. IN MY OPINION IT IS UNSAFE. I NOTICED YOUR ARTICLE ABOUT THE 2013 FORD ESCAPES IN THE DALLAS MORNING NEWS. *TR

Mileage: 50,100

Jul 23, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING APPROXIMATELY 40 MPH, THE VEHICLE SUDDENLY SHUT OFF AND COULD NOT BE RESTARTED. THE VEHICLE WAS TOWED TO THE CONTACT'S RESIDENCE. THE CAUSE OF THE FAILURE WAS NOT DETERMINED. THE LOCAL DEALER (JOHN BLEAKLEY FORD INC, 870 HWY 6 THORNTON RD, LITHIA SPRINGS, GA) WAS NOTIFIED OF THE FAILURE. THE MANUFACTURER WAS NOT NOTIFIED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE FAILURE MILEAGE WAS 85,000.

Mileage: 85,000

Jul 23, 2018

2014 FORD ESCAPE 4X2 OVERFLOW COOLANT TANK CAUSING COOLANT TO LEAK. 230,000 CARS HAVE BEEN REPAIRED BY FORD BUT THEY WILL NOT REPAIR MINE WITHOUT A $230+COST. FOR SOME UNKNOWN REASON MY SERIAL NUMBER IS NOT COVERED. LACK OF COOLANT LEADS TO OVERHEATING AND CRACKED HEAD GASKET. THE CAR DID REDUCE POWER AND SOUND A PULL OVER IMMEDIATELY WARNING ON 2 OCCASIONS. THE CAR HAS 55,000 MILES.

Mileage: 55,000

Jul 14, 2018

SUMMARY: IN OCTOBER 2018 I TOOK THE VEHICLE IN FOR RECALL 17S09/NHTSA17V-209 TO HAVE THE SENSORS PUT ON. THEN MARCH 2018 I TOOK VERHICLE IN FOR PARTS TO REPAIR THE LEAK.. HOWEVER AFTER THE PARTS WERE PUT ON THE VEHICLE HAD TO GO BACK BECAUSE THE COOLANT LIGHT CAME ON ABOUT LATE MAY. THE DEALERSHIP WAS VERY NICE AT LOOKING AT AND RESOLVING THE PROBLEM. THEN IN JUNE THE LIGHT CAME ON AGAIN AND THE COOLANT WAS LOW. DEALER CHECK. THEY DISCOVERED THE COOLANT LEAKING BACK INTO THE ENGINE. THIS WAS NOT A PROBLEM UNTIL THIS RECALL WAS DONE. I ATTEMPTED TO ESCALATE THIS THROUGH FORD CARES AND OBVIOUSLY THEY DON'T. THE ONLY RESPONSE I HAVE IS - THIS IS NOT RELATED TO THE RECALL. PLUS THEY CONTINUED TO TELL ME I DO NOT HAVE ANY WARRANTY LEFT ON THIS VEHICLE WHICH I AM WELL OF AWARE OF. THE RECALL SPECIFCALLY STATES THE LEAK WILL CAUSE A CRACK IN THE CYLYINDERS. THAT IS EXACTLY WHAT HAPPENED. WE COMPLIED WITH EVERYTHING FORD ASKED OF US REGARDING THIS RECALL.

Mileage: 64,000

Jul 11, 2018

IN JAN 2018 I TOOK THE VEHICLE IN FOR RECALL 17S09/NHTSA17V-209 TO HAVE THE SENSORS PUT ON. INITIALLY THE DEALER DID NOT HAVE THE PARTS, THE PART WERE PUT ON IN FEB. HOWEVER AFTER THE PARTS WERE PUT ON THE VEHICLE HAD TO GO BACK BECAUSE HE COOLANT LIGHT CAME ON ABOUT LATE APRIL. THE DEALERSHIP WAS VERY NICE AT LOOKING AT AND RESOLVING THE PROBLEM. THEN IN JUNE THE LIGHT CAME ON AGAIN AND THE COOLANT WAS LOW. NO SIGNS OF LEAKAGE AND I WAS HESITANT TO REPLACE SO I HAD THE DEALER CHECK. THEY DISCOVERED THE COOLANT LEAKING BACK INTO THE ENGINE. THIS WAS NOT A PROBLEM UNTIL THIS RECALL WAS DONE. I ATTEMPTED TO ESCALATE THIS THROUGH FORD CARES AND OBVIOUSLY THEY DON'T. THE ONLY RESPONSE I HAVE IS - THIS IS NOT RELATED TO THE RECALL. I AM A SINGLE MOM, IN A RENTAL AND NOW REPAIRS OF OVER 4K.

Mileage: 60,000

Jul 1, 2018

MY SON'S CAR, SAYS ENGINE OVERHEATING AND COMPLETELY DISABLES THE CARS ENGINE TO WHERE IT WILL STOP YOU MID DRIVING. SMOKE CAME FROM UNDER THE HOOD OF THE CAR. TOOK IT IN AND HAD A DIAGNOSTIC TEST AND NOTHING SHOWED UP. COOLANT LEVEL FINE AND OIL LEVEL FINE. CAR MECHANIC COULDN'T FINE ANYTHING WRONG. THIS CONTINUES TO HAPPEN. WE DON'T KNOW WHAT TO DO? MY SON GETS SCARED TO DRIVE THE CAR TO SCHOOL AND WORK, BUT WHAT REALLY SCARY IS HE DRIVES IN 55 MILE PER HOUR ROADS TO GET TO SCHOOL AND WORK AND THE CAR ENGINE WILL HESITATE WILL HE IS DRIVING AND THEN STOP ON HIM. CARS BEHIND HIM DON'T UNDERSTAND WHAT IS GOING ON AND HUNK AT HIM. HE HAS NO SHOULDER TO PULL OVER ON THE ROADS. WHAT IS GOING ON WITH FORD, ESCAPE 2014 ENGINE OVER HEATING?????????????????????????

Mileage: 44,000

Jun 13, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STARTED THE VEHICLE REMOTELY FOR APPROXIMATELY FIVE MINUTES. WHEN THE CONTACT ATTEMPTED TO DRIVE, THE MESSAGE CENTER DISPLAYED "ENGINE OVERHEATED". THE VEHICLE HAD TO BE TOWED TO THE DEALER (MAC HAIK FORD PASADENA, 4242 EAST SAM HOUSTON PARKWAY S, PASADENA, TEXAS 77505) WHERE IT WAS AWAITING DIAGNOSTIC TESTING AND REPAIRS. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 72,000. THE VIN WAS NOT AVAILABLE.

Mileage: 72,000

Jun 12, 2018 Fire

TL* THE CONTACT OWNED A 2014 FORD ESCAPE. WHILE DRIVING AT LOW SPEEDS, FLAMES WERE SEEN UNDER THE HOOD OF THE VEHICLE. THE ORIGIN OF THE FIRE WAS DETERMINED TO BE THE ENGINE COMPARTMENT. THE FIRE DEPARTMENT WAS CALLED AND EXTINGUISHED THE FIRE. A POLICE REPORT WAS FILED. THERE WERE NO INJURIES SUSTAINED. THE VEHICLE WAS TOWED TO A TOW LOT AND DEEMED DESTROYED. THE DEALER (CAVENAUGH FORD LINCOLN, LLC, 2000 E HIGHLAND DR., JONESBORO, AR 72401, (870) 972-8000) WAS NOTIFIED, BUT THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 100,000. *TT COOLANT LEVEL SENSOR SYSTEM RECALL#17509 UPDATED 9/25/18*JB

Mileage: 100,000

Jun 11, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT NOTICED STEAM EMERGING FROM THE HOOD AND AN ABNORMAL ODOR OF ANTI-FREEZE. THERE WERE NO WARNING INDICATORS ILLUMINATED. THE CONTACT VERIFIED THAT THE ANTI-FREEZE RESERVE TANK WAS CRACKED. THE LOCAL DEALER WAS NOT CONTACTED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS 63,900.

Mileage: 63,900

Jun 6, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE OPERATING THE VEHICLE, THE TEMPERATURE GAUGE INDICATED THAT THE ENGINE WAS OVERHEATED AND THE MESSAGE "HOT TEMPERATURE" WAS DISPLAYED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC AND IT WAS DIAGNOSED THAT THE WATER PUMP LEAKED AND THE COOLANT RESERVOIR WAS CRACKED. AFTER REPAIRING THE VEHICLE, THE ENGINE IMMEDIATELY OVERHEATED AND IT WAS DISCOVERED THAT THE ENGINE CYLINDER HEAD WAS ALSO CRACKED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE, BUT NO ASSISTANCE WAS OFFERED. THE CONTACT WAS INFORMED THAT THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING), ALTHOUGH THE VEHICLE EXPERIENCED THE SAME FAILURE AS LISTED IN THE RECALL. THE FAILURE MILEAGE WAS 118,346.

Mileage: 118,346

May 10, 2018

AFTER THE RECALL WITH THE AIR CONDITION I STILL HAS SOME PROBLEM AND NOW MY CAR IS MAKING A VERY STRANGE NOICE IN FRONT WHEN I DRIVE MORE THE 40 SOMETIMES I'M NOT GETTING COLD HAIR

May 1, 2018

THE VEHICLE'S GEAR SHIFT CABLE "BREAKS" LEAVING THE VEHICLE INOPERABLE UNABLE TO GO INTO GEAR, DRIVE OR REVERSE. THE VEHICLE DRIVE OK THEN PARKED. THE VEHICLE WAS PARKED IN A PUBLIC GARAGE WHEN I NOTICED THAT THE VEHICLE WOULD NOT GO INTO GEAR.

Mileage: 62,000

Apr 23, 2018 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 35 MPH, THE CONTACT NOTICED SMOKE UNDER THE HOOD OF THE VEHICLE. THE CONTACT WAS ABLE TO EXTINGUISH THE FIRE. THE FIRE DEPARTMENT WAS CONTACTED AND A FIRE REPORT WAS FILED. THERE WERE NO INJURIES SUSTAINED. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHERE IT WAS AWAITING INSPECTION. THE DEALER AND MANUFACTURER WERE NOT NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 53,000.

Mileage: 53,000

Apr 13, 2018

WHILE IN MOTION ON THE INTERSTATE DOING 75 MPH MY CAR STARTED MAKING A TICKING SOUND. I WASN'T SURE WHAT IT WAS AT THE TIME BUT I KNEW IT WAS GOOD. WHILE GETTING OFF THE EXIT I NOTICED MY BREAKS WERE GOING OUT. THEY WERE VERY HARD TO PUSH DOWN AND IT BARELY MADE MY CAR STOP. I TOOK IT TO A NEW BY PLACE THAT WAS ABLE TO READ SOME CODES. MY CHECK ENGINE LIGHT HAD COME ON AND THE CODES CAME UP AS CAM SHAFT POSITION SENSOR. I REPLACED THE SENSOR AND IT DID NOT FIX THE PROBLEM. I THEN TOOK MY CAR TO THE FORD DEALERSHIP WHERE I LIVE. AT THIS POINT IT HAD DIED TWICE ON THE INTERSTATE AND STILL MADE A HORRIBLE TICKING SOUND. THE DEALERSHIP TOLD ME THAT MY VACUUM PUMP HAD COME LOOSE AND THE BOLT HAD GOTTEN METAL IN MY ENGINE WHICH DESTROYED MY ENGINE. THERE WERE NO WARNING SIGNS WHEN THIS HAPPENED AND IT HAPPENED VERY FAST. MY CAR STARTED FINE THAT DAY AND DRIVE FINE UP UNTIL THE INCIDENT. THIS IS A BIG SAFETY CONCERN AND I'VE READ SEVERAL OF PEOPLE WHO HAD THIS SAME ISSUE. I AM NOW HAVING TO REPLACE THE ENGINE AND THE TURBO OF MY CAR OUT OF POCKET.

Mileage: 73,100

Apr 12, 2018 Fire

I WAS DRIVING MY 2014 FORD ESCAPE FOR ABOUT 10 MIN. ON WHITNEY MILL RRD. IN ONTARIO COUNTY NEW YORK. WHEN I GOT AN ALERT ON MY DASH BOARD. IT SAID ENGINE OVER HEATING PULL OVER ( OR SOMETHING ALONG THOSE LINES) I LOOK DOWN AT THE TEMPETURE GAGE AS I WAS PULLING OVER. THE NEEDLE WAS IN PERFECT POSITION BETWEEN HOT AND COLD. AFTER I STOOPED ( ABOUT 30 SECONDS AT T HE MOST) I GOT OUT, OPEN THE HOOD AND SAW FLAMES COMING UP IN THE BACK OF THE ENGINE BETWEEN THE ENGINE AND FIREWALL. I INSTRUCTED MY WIFE TO GET HERSELF AND THE DOG OUT OF THE VEHICLE. THEN I BEGAN THROWING SNOW ONTO THE AREA WHERE THE FIRE WAS COMING FROM. IN MY OPINION KEEPING THE FIRE CONTAINED. THE FIRE DEPARTMENT EVENTUALLY SHOW UP ( GUESSING 15 MIN.) THEY TOOK OVER FROM THAT POINT. SPRAYED FIRE EXTINGUISHER ON THE ENGINE AND REMOVE PIECES OF THE ENGINE COMPARTMENT TO GET A BETTER LOOK AT THE FIRE AND MAKE SURE IT WAS OUT. THEN A TOW TRUCK CAME AND TOOK IT AWAY.

Mileage: 50,000

Mar 28, 2018 Fire

I WAS DRIVING UP THE INTERSTATE AFTER WORK AND WHILE I WAS DRIVING I BEGAN TO NOTICE SMOKE. I LOOKED AROUND AND REALIZED IT WAS MY CAR. I PULLED OVER TO THE SIDE AND MY CAR STARTED FLASHING EVERYTHING ON THE DASH PANEL WAS RED AND FLASHING ENGINE FAILURE. I CUT THE CAR OFF AND THEN WENT TO TRY AND POP THE HOOD, I COULDN'T GET IT OPENED AND I LOOKED DOWN AND BEGAN TO SEE FLAMES. I CALLED 911 AND MY CAR ENGULFED IN FLAMES. I HAD A RECALL ON MY CAR FOR A PROBLEM WITH THE ENGINE CYLINDER HEAD SAYING THAT IT COULD CAUSE AN ENGINE FIRE IF OILS WERE TO GET OUT AND HIT A HOT SURFACE. I GOT MY RECALL FIXED AND THEN MY CAR CAUGHT ON FIRE A FEW WEEKS LATER.

Mileage: 74,000

Mar 26, 2018 Fire

TL* THE CONTACT OWNED A 2014 FORD ESCAPE. THE CONTACT STATED THAT WHILE AT A STOP, THE "HIGH TEMPERATURE TURN OFF ENGINE" LIGHT ILLUMINATED. THE CONTACT IMMEDIATELY TURNED THE ENGINE OFF AND EXIT THE VEHICLE. THE CONTACT SAW FLAMES SHOOTING OUT FROM UNDERNEATH THE HOOD. THE CONTACT CALLED 911 AND BEFORE THE POLICE AND THE FIRE TRUCK ARRIVED AT THE SCENE, THE VEHICLE BLEW UP. THE FIRE DEPARTMENT EXTINGUISHED THE FIRE. A POLICE AND FIRE REPORT WERE FILED. THERE WAS NO INJURY, THE DEALER WAS NOT CONTACTED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND PROVIDED THE CONTACT WITH A CASE NUMBER. THE VEHICLE WAS DESTROYED AND TOWED TO THE INSURANCE COMPANY'S TOW YARD. ADDITIONALLY, THE CONTACT STATED THAT HE DID NOT RECEIVE THE NOTIFICATION OF THE NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING).THE FAILURE MILEAGE WAS ABOUT 80,000.

Mileage: 80,000

Mar 19, 2018

THE CAR CONSUMES COOLANT AT A RATE OF ABOUT 3-4 QUARTS IN THE 5 MONTHS I'VE OWNED IT. I NOTICED IT WHILE CHANGING THE OIL. I AM AWARE THAT OTHER VINS FROM MY CAR'S MODEL YEAR AND ENGINE STYLE ARE ELIGIBLE FOR A RECALL CONCERNING THIS ISSUE, WHICH CAN CAUSE THE ENGINE TO CATCH FIRE. (RECALL CODE 17V209) I AM UNCLEAR AS TO WHY MY VIN IS NOT ON THE RECALL LIST, WHEN IT WAS MADE IN THE SAME FACTORY, WITHIN THE IDENTIFIED TIMEFRAME, WITH THE SAME ENGINE, AND EXHIBITING THE SAME DANGEROUS PROBLEM.

Mileage: 96,000

Mar 15, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING VARIOUS SPEEDS, THE HEATER FAILED TO OPERATE. THE CONTACT NOTICED THAT THE COOLANT SYSTEM WAS VERY LOW AND, AFTER BEING REFILLED, THE COOLANT WAS BACK LOW. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE THE DIAGNOSIS WAS UNDETERMINED. THE CONTACT CALLED JOHN KENNEDY FORD-POTTSTOWN AT 1-888-696-4917 AND WAS INFORMED THAT THE VEHICLE WAS NOT INCLUDED IN A RECALL. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE AND INFORMED THE CONTACT THAT THE VEHICLE WAS NOT MANUFACTURED AT THE RIGHT TIME TO BE INCLUDED IN A RECALL. THE VIN WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE APPROXIMATE FAILURE MILEAGE WAS 75,000.

Mileage: 75,000

Mar 14, 2018

TAKATA RECALL, CONCERN REGARDING 2014 FORD ESCAPE WITH CONTINUAL "LOW ENGINE COOLANT" LIGHT RETURNING.

Mileage: 40,000

Mar 12, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING, THE CHECK COOLANT INDICATOR ILLUMINATED. THE VEHICLE WAS REMEDIED PER NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE VEHICLE WAS TAKEN TO POMPANO FORD LINCOLN (2741 N FEDERAL HWY, POMPANO BEACH, FL 33064) WHERE IT WAS DIAGNOSED THAT WATER DAMAGED THE ENGINE. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED AND INFORMED THE CONTACT THAT REPAIRS AND A LOANER VEHICLE WOULD BE FREE OF CHARGE. THE FAILURE MILEAGE WAS 34,000.

Mileage: 34,000

Mar 9, 2018

IT'S BEEN A YEAR ON THIS RECALL. WHAT'S THE HOLD UP? IS THERE A TRADE-IN PROGRAM TO GET A CAR WITHOUT A RECALL? MAR 27,2017 MANUFACTURER RECALL NUMBER17S09 NHTSA RECALL NUMBER17S09 RECALL STATUSRECALL INCOMPLETE, REMEDY NOT YET AVAILABLE

Mar 9, 2018

IT ONLY HAPPENS WHEN YOU DRIVE THE CAR FOR A WHILE (45+ MINUTES), TURN IT OFF, AND THEN START IT UP 15-45 MINUTES LATER. IT WILL START BUT THEN WITHIN THE FIRST 100 YARDS IT WILL GO SLUGGISH AND STALL. WHEN I TRY TO GIVE IT GAS THAT DOESN'T HELP. I HAVE TO TURN THE CAR OFF, PUT IT IN PARK AND START IT BACK UP. A FEW TIMES IT'S STALLED 3 TIMES IN A ROW. ONCE IT GETS GOING GOOD IT'S FINE. IT'S ALWAYS FINE IF IT'S BEEN OFF FOR A WHILE (FIRST THING IN THE MORNING OR STARTING AFTER WORK). EVENTUALLY THE SERVICE ENGINE LIGHT CAME ON, I TOOK IT TO A SHOP, A GUY DIAGNOSED IT, CHANGED OUT A SENSOR AND THE FUEL PUMP. IT DIDN'T HELP.

Mileage: 50,000

Mar 6, 2018

MY VEHICLE WAS OVERHEATED FOR ABOUT 3 TIMES AND I HAVE REPORTED IT TO THE FORD DEALERSHIP HERE IN AMERICAN SAMOA. I ALSO RECEIVED A RECALL NOTICE ABOUT THIS VEHICLE (SAFETY RECALL NOTICE 17S09). UP TO NOW, THE FORD DEALERSHIP HAVE NOT FIX THIS RECALL ISSUE AND I AND MY FAMILY ARE ALWAYS AT HIGHER DANGEROUS RISK DUE TO THIS UNRESOLVED RECALL. I HAVE PAID HUNDREDS OF DOLLARS TO THE DEALERSHIP FOR FIXING THE PROBLEM VIA OTHER REPLACEMENT PARTS AND STILL NOTHING DIRECTLY TO THE RECALL PART. THE RECALL PART IS THE ENGINE COOLANT.

Mileage: 92,000

Mar 5, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING VARIOUS SPEEDS, THE VEHICLE OVERHEATED AND THE CHECK ENGINE AND RADIATOR WARNING INDICATORS ILLUMINATED. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING); HOWEVER, THE PARTS TO DO THE REPAIR WERE UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. JIM CLICK FORD LINCOLN EAST TUCSON (6244 E 22ND ST, TUCSON AZ, 85711) WAS CONTACTED AND PERFORMED THE RECALL REPAIR. THE FAILURE RECURRED AND THE VEHICLE WAS TAKEN BACK TO THE DEALER. THE DEALER COULD NOT REPLICATE THE FAILURE. THE MANUFACTURER WAS NOTIFIED. THE FAILURE MILEAGE WAS 34,000. *TT

Mileage: 34,000

Feb 26, 2018

I HAVE HAD 2 PRIOR REPAIRS MADE DUE TO RECALLS. THE DOORS AND AN ENGINE PART. THE DEALERSHIP JUST REPAIRED A SENSOR ON MY CAR LAST WEEK. NOW MY CAR IS STALLING WHEN I FIRST START IT (STATIONARY) OR FEELS LIKE IT'S GOING TO STALL WHILE DRIVING AT A RATE OF 45 MPH. IT ONLY HAS 56K ON IT. I HAVE NOTICED ONGOING ISSUES WITH THE DOORS, BUT WILL ADVISE THE DEALERSHIP SINCE THEY FIXED THEM AS PART OF THE FIRST RECALL.

Mileage: 56,800

Feb 17, 2018

I TOOK THE CAR TO THE LOCAL FORD DEALER (JONES WEST FORD IN RENO NV) FOR RECALL 17V-209 WHICH IS RELATED TO OVERHEATING THAT CAN CAUSE THE CYLINDER HEAD TO CRACK AND MAY RESULT IN FIRE. THE SERVICE ADVISER INFORMED ME THAT IT HAD A CRACKED HEAD BASED ON THEIR EXPERTISE, LOW COOLANT AND AMOUNT OF HYDROCARBONS WHEN TESTED. THE ONLY SOLUTION IS A NEW MOTOR. WHEN ASKED ABOUT IT BEING COVERED UNDER THE RECALL, HE QUICKLY SAID IT WAS NOT AND THE REPAIR WOULD BE $8,000.00. I REPORTED THE INCIDENT TO THE FORD MOTOR COMPANY FOR FURTHER REVIEW. DURING THE SAME SERVICE VISIT, THE TECH PERFORMED RECALL 16S30 ON ALL DOOR LATCHES. THE NEXT DAY I FOUND THE PASSENGER SIDE DOOR WINDOW TO NOT BE OPERATING PROPERLY. KNOWING THAT THE TECH HAD TO ACCESS THE REPAIR FROM THE INSIDE OF THE DOOR PANEL, I ASKED THE DEALER TO TAKE CARE OF THE WINDOW. WHILE IN THE SERVICE SHOP FOR THE WINDOW, THE SERVICE ADVISER TOOK THE LIBERTY OF CHECKING THE MOTOR AGAIN. THIS TIME HE CLAIMS THE "MASTER MECHANIC" DIAGNOSED IT AND EVERYTHING IS FINE. THEY INSTALLED THE PART AFFECTED BY THE RECALL AND THIS TIME THEY TOPPED OFF THE COOLANT. I SUSPECT THE REASON FOR TAKING ANOTHER LOOK IS BASED ON MY COMPLAINT TO THE MOTOR COMPANY. I REALLY DON'T KNOW IF THE HEAD IS CRACKED OR NOT. THEY DIDN'T REMOVE IT FOR PROPER TESTING. BASED ON MY EXPERIENCE, I WOULD SAY THEY HAVE NO INTENTION ON GETTING INVOLVED IN SUCH AN EXTENSIVE REPAIR. THE DEALER EVEN FAILED AT THE DOOR LATCH. THEY SAID THE WINDOW FAILURE IS A COINCIDENCE AND TOOK NO RESPONSIBILITY. THE WINDOW IS STILL NOT WORKING. I WOULD HAVE DECLINED THE DOOR LATCH RECALL IF I KNEW I WOULD END UP WITH A WINDOW THAT DOESN'T WORK. IT WAS FINE BEFORE THEY OPENED THE DOOR PANEL TO INSTALL A NEW LATCH. I HOPE THERE IS SOMETHING YOU CAN DO TO HOLD THE DEALER AND THE MANUFACTURER ACCOUNTABLE TO DO THE RIGHT THING PER THE INTENTION OF THE SAFETY RECALL.

Feb 15, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING); HOWEVER, THE PARTS TO DO THE REPAIRS WERE UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE DEALER (AL WHITE FORD LINCOLN, 2002 HILLSBORO BLVD, MANCHESTER, TN 37355, (931) 728-2402) WAS CONTACTED AND CONFIRMED THAT THE PARTS WERE NOT AVAILABLE FOR THE RECALL REMEDY. THE MANUFACTURER WAS NOT MADE AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.

Feb 10, 2018 Fire

I STARTED MY VEHICLE YESTERDAY TO WARM UP AND ABOUT 5-10 MINUTES LATER HEARD A BIG BOOM, LOOKED OUT THE DOOR AND THE FRONT END OF MY ESCAPE WAS COMPLETELY ENGULFED IN FLAMES. I HAD SCHEDULED IT TO GET REPAIRED YESTERDAY MORNING, BUT WAS UNABLE TO MAKE IT AS WE RECEIVED A LOT OF SNOW AND SCHOOLS WERE CANCELLED AND SUCH. I HAD KNOWN OF THE RECALL SINCE LAST YEAR SINCE I ALREADY WAS INVOLVED IN ANOTHER RECALL WITH THE LATCH. I TRIED TO GET THEM TAKEN CARE OF AT THE SAME TIME, BUT THE REMEDY WAS NOT AVAILABLE AND WOULDN'T BE FOR SOME TIME. I RECEIVED A NOTICE DIRECTLY FROM FORD BETWEEN ONE AND TWO WEEKS AGO AND CALLED ZIEGLER IN ELKHART TO MAKE AN APPOINTMENT, BUT THEY WEREN'T AVAILABLE FOR ALMOST A WEEK. IT IS OBVIOUS THE DAMAGE WAS ALREADY DONE WITH MY CAR ANYWAY, CONSIDERING THE DESCRIPTION OF THE RECALL, WHICH A WHOLE PROCESS OF THE CYLINDER HEAD CRACKING, COOLANT LEAKING OUT AND THAT POTENTIALLY CAUSING A FIRE IN THE ENGINE COMPARTMENT. I AM THANKFUL THAT THE CAR WAS JUST WARMING UP IN OUR DRIVEWAY AND NEITHER MY KIDS NOR MYSELF WERE INSIDE. I AM ALSO GRATEFUL THAT OUR HOUSE DIDN'T CATCH FIRE AND JUST SUSTAINED SOME COSMETIC DAMAGE DUE TO THE HEAT. I DO NOT HAVE THE REPORT FROM THE FIRE DEPARTMENT YET, BUT THEY SAID IT WOULD BE AVAILABLE SOON. IT WAS THE PENN TOWNSHIP FIRE DEPT THAT RESPONDED AND I TALKED TO DURGAN SPINSKY WHOSE WORK NUMBER IS 5742555075 * (RECALL RELATED INCIDENT) TS

Mileage: 60,500

Feb 6, 2018 Fire

MY 2014 FORD ESCAPE CAUGHT ON FIRE WHILE STATIONARY AT MY SON'S ELEMENTARY SCHOOL. I WAS WAITING IN THE DROP OFF LANE AT MY SON'S SCHOOL WHEN MY SUV STARTED TO SMOKE FROM UNDERNEATH THE DASH, I TRIED TO MOVE THE VEHICLE OUT OF THE LANE SO I WOULD NOT BLOCK OTHER PARENTS FROM COMING INTO THE SCHOOL, AND IT WOULD NOT DRIVE, MORE SMOKE CAME INTO THE CAB AND I QUICKLY GOT MY SON OUT OF THE CAR AND AWAY. IT CONTINUED TO SMOKE, AND I REALIZED THE CAR WAS STILL RUNNING, I QUICKLY SHUT IT OFF. NO FLAMES WERE SEEN, AND I HAD NO REALIZED IT WAS ACTUALLY ON FIRE UNTIL WE HAD IT TOWED TO A GARAGE. OUR MECHANIC WAS THE ONE TO INFORM US OF AN OPEN RECALL OF THE ISSUE I HAD JUST EXPERIENCED. THIS HAPPENED ON DECEMBER 21, 2017. FORD HAS NOT BE HELPFUL WHAT-SO-EVER.

Mileage: 99,000

Feb 6, 2018

CAR PURCHASED 1/18/2014. SAFETY RECALL NOTICE 17S09/NHTSA RECALL 17V-209 RECEIVED 4/2017. PARTS WERE NOT AVAILABLE TILL 11/22/2017. BY THIS TIME, VEHICLE WAS OUT OF WARRANTY. COOLANT SEEPAGE WAS DUE TO PRESSURE FRACTURES WITHIN COOLANT TANK WALLS AND TANK NOT PART OF RECALL. THE "LOW LEVEL SENSOR" IS A NEEDED ADDITION BUT I FAR AS I CAN TELL, THE REPLACEMENT COOLANT TANK IF NOT AN IMPROVED TANK, WILL ALSO DEVELOP PRESSURE FRACTURES IN THE FUTURE. MAYBE FORD WILL HAVE A TANK FIX LATER.

Mileage: 54,835

Feb 5, 2018

MARCH 27, 2017 RECALL - NHTSA RECALL NUMBER 17S09 - COOLANT LEVEL SENSOR SYSTEM INSTALLATION - CONTINUE TO BE TOLD BY DEALERSHIPS THAT PARTS ARE BACK ORDERED - PROBLEM COULD CAUSE ENGINE FIRE - HOW LONG CAN THIS GO ON BEFORE FORD PROVIDES PARTS?

Feb 4, 2018 Fire

ON JANUARY 6, 2018, I DROVE HOME FROM MY JOB 10 MILES AWAY. WHEN I TOOK I-95, MY FORD ESCAPE 2014 TURN OFF AND CONTINUED MOVING IN THE MIDDLE LANE. I MANAGED TO REACH THE CENTRAL SEPARATOR UNTIL IT STOPPED COMPLETELY. WHEN I TRIED TO START THE CAR OVER, I FELT A BURNT SMELL, DUE TO THAT FACT I DECIDED TO LEAVE MY FORD SCAPE 2014 AND REALIZED THAT IT GOT SUDDENLY ON FIRE. AS A PROOF, THE INCIDENT WAS RECORDED BY THE LOCAL NEWSCAST. IT'S IMPERATIVE FOR ME A SOLUTION FROM FORD CONSIDERING THAT I STILL OWE 19.000.00 TO THE BANK.

Mileage: 3

Jan 26, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 10 MPH, THE VEHICLE STALLED WITHOUT WARNING AND THE GEAR SHIFTER WAS STUCK IN THE PARK POSITION. THE VEHICLE WAS TOWED TO A LOCAL DEALER (RANDALL FORD, 5500 ROGERS AVE, FORT SMITH, AR 72903), BUT WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS APPROXIMATELY 80,000.

Mileage: 80,000

Jan 25, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING); HOWEVER, THE PARTS TO DO THE REPAIR WERE UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE DEALER (LAKEVIEW FORD LINCOLN, 295 W DICKMAN RD, BATTLE CREEK, MI 49037) WAS CONTACTED AND CONFIRMED THAT THE PARTS WERE NOT AVAILABLE FOR THE RECALL REMEDY. THE MANUFACTURER WAS NOT CONTACTED. THE CONTACT HAD NOT EXPERIENCED A FAILURE. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.

Jan 18, 2018 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING APPROXIMATELY 35 MPH, THE VEHICLE DECELERATED AND THE SERVICE ENGINE WARNING INDICATOR ILLUMINATED. THE CONTACT NOTICED GRAY SMOKE UNDER THE HOOD. THE CONTACT SHUT THE VEHICLE OFF AND ATTEMPTED TO RESTART IT, BUT WAS UNSUCCESSFUL. THE CONTACT EXITED THE VEHICLE AND IT IGNITED IN FLAMES. THE FIRE DEPARTMENT EXTINGUISHED THE FIRE AND COULD NOT DETERMINE HOW IT STARTED. A POLICE REPORT WAS FILED AND THERE WERE NO INJURIES. THE VEHICLE WAS TOWED TO GREEN FORD (3800 W WENDOVER AVE, GREENSBORO, NC 27407) WHERE IT WAS DETERMINED THAT THE VEHICLE WAS TOO BURNT TO DETERMINE THE CAUSE OF THE FIRE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE CONTACT WAS UNAWARE THAT THE VIN WAS INCLUDED IN NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE APPROXIMATE FAILURE MILEAGE WAS 55,300. * (RECALL RELATED INCIDENT) TS

Mileage: 55,300

Jan 17, 2018 Fire

MY VEHICLE RAN LOW ON COOLANT ON 2 INSTANCES IN NOVEMBER 2017, WITH THE ENGINE TEMPERATURE RISING INTO THE RED ZONE WHILE DRIVING. BOTH TIMES I PULLED OVER, TURNED THE IGNITION OFF AND RESTATED, AND THE VEHICLE RAN FINE. I FILLED THE COOLANT RESERVOIR TOOK TO A LOCAL GARAGE, THEY COULD NOT FIND A CAUSE FOR THE LOW COOLANT (NO SIGN OF LEAK & IT PASSED A PRESSURE TEST). THEIR ADVICE WAS TO MONITOR THE COOLANT LEVEL AND IT THE PROBLEM OCCURRED AGAIN TO TAKE THE VEHICLE TO A DEALERSHIP. I EXPERIENCED NO FURTHER ISSUES UNTIL THE EVENING OF JAN. 7, 2018, WHEN MY ENGINE SUDDENLY LOST ACCELERATION AFTER DRIVING FOR ONLY 2 MILES. THE MAIN DASH DISPLAY SHOWED AN "ENGINE FAILURE" MESSAGE. I BRAKED TO A STOP AND LIGHT SMOKE BEGAN VENTING FROM UNDER THE HOOD. I TURNED THE IGNITION OFF, TOOK A PEEK IN THE ENGINE COMPARTMENT AND DISCOVERED A WORKING FIRE UNDERNEATH THE ENGINE BLOCK AND A SMELL OF OIL. THE LOCAL FIRE DEPARTMENT & SHERIFF PATROL RESPONDED, THE FIRE BURNED FOR APPROX. 1 & 1/2 MINUTES AND SELF EXTINGUISHED ONCE THE ENGINE COOLED DOWN. THE BOTTOM OF THE ENGINE COMPARTMENT WAS SPRAYED IN OIL, OIL DRIPPING ONTO THE ROAD. THE VEHICLE WAS NOT DRIVABLE, WOULD NOT RE-START AND WAS TOWED TO A LOCAL GARAGE. NUMEROUS ERROR CODES REPORTED, THE MECHANIC SAID I WOULD NEED TO TAKE IT TO A DEALERSHIP. THEN ON JAN. 11 2018 I RECEIVED A RECALL NOTICE FROM FORD FOR 17S09 - FIRE HAZARD FOR THE MAKE & MODEL OF VEHICLE. 2014 FORD ESCAPE, I PURCHASED IT USED IN 2015 AND CURRENTLY HAVE 75,000 MILES ON IT. MY VEHICLE IS NOW AT A FORD DEALERSHIP AND I AM WAITING FOR A REPORT OF WHAT DAMAGE OCCURRED AND CORRECTIVE ACTION. RECALL NOTICE, FIRE REPORT & POLICE REPORT ARE ATTACHED.

Mileage: 75,000

Jan 16, 2018 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT PREVIOUSLY RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17S090000 (ENGINE). THE PARTS TO DO THE REPAIR WERE UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. WHILE DRIVING AT UNKNOWN SPEEDS, THE CONTACT NOTICED AN ABNORMAL BURNING ODOR AND SMOKE APPEARED UNDER THE HOOD. THE VEHICLE CAUGHT FIRE. THE FOUR WHEEL DRIVE AND ENGINE SERVICE INDICATORS ILLUMINATED. THE AIR BAGS DID NOT DEPLOY. THERE WERE NO INJURIES DUE TO THE FIRE AND A POLICE REPORT WAS NOT FILED. THE FIRE DEPARTMENT WAS PRESENT DURING THE INCIDENT. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC. THE CONTACT CALLED APPLE FORD (8800 STANFORD BLVD, COLUMBIA, MD 21045) AND WAS ADVISED TO CALL THE INSURANCE COMPANY. THE MANUFACTURER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS APPROXIMATELY 29,000. * (RECALL RELATED INCIDENT) TS

Mileage: 29,000

Jan 15, 2018

WHILE PULLING INTO DRIVEWAY AT LOW SPEED ENGINE STARTED SURGING AND WOULD NOT SLOW. SHIFTING TRANSMISSION INTO NEUTRAL ALLOWED VEHICLE TO BE STOPPED. ENGINE CONTINUING SURGING UNTIL TURNED OFF. MECHANIC FOUND CODES P0011 INTAKE CAMSHAFT POSITION TIMING OVER-ADVANCED (BANK 1) AND P0016 CRAFTSHAFT POSITION - CAMSHAFT POSITION CORRELATION - BANK 1 SENSOR A. MECHANIC STATED IT WAS VERY UNUSUAL FOR SUCH PROBLEMS TO EXIST IN AN ENGINE AT ONLY 66,000 MILES.

Mileage: 66,333

Jan 15, 2018 Fire

WHILE DRIVING LAST WEEK ON THE HIGHWAY, THE CAR EXPERIENCED A LOSS OF POWER SOMEWHAT LIKE IT WAS DOWNSHIFTING AND THEN THE CHECK ENGINE LIGHT CAME ON WITHIN 5 MINUTES OF LEAVING OUR HOUSE. WE PULLED OVER AND THEN THE CARE STARTED ON FIRE

Mileage: 60,000

Jan 10, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING); HOWEVER, THE PARTS TO DO THE REPAIR WERE UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE CONTACT CALLED AUTONATION FORD EAST AT (440) 296-3020 (28825 EUCLID AVE, WICKLIFFE, OH 44092) WHERE IT WAS CONFIRMED THAT THE PARTS WERE NOT AVAILABLE FOR THE RECALL REMEDY. THE MANUFACTURER WAS NOT NOTIFIED. THE CONTACT STATED THAT THE ENGINE WARNING INDICATOR ILLUMINATED. THE FAILURE MILEAGE WAS UNKNOWN. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.

Jan 9, 2018

ENGINE LIGHT KEEPS ON AND OFF WITH NOT A REASON AND WHEN I BRING THE CAR FOR AN OILS CHANGE INTO THE DEALER THEY ARE SAYING THAT IS NOT IMPORTANT AND IT IS GOING OFF WHEN THE OIL IS CHANGED. I ALSO NOTICE THAT THE CAR IS VERY SHORT AFTER THE GENTLY BREAKDOWN. THE OTHER ISSUE IS THE UNEXPECTED ACCELERATION ITSELF, EVEN IF I DO NOT USE THE ACCELERATOR PEDAL. THIS HAPPENS ANYWHERE ANYHOW AND WHEN THE VEHICLE IS IN MOTION.

Mileage: 63,000

Jan 6, 2018

I RECEIVED A RECALL NOTICE IN APRIL 2017 FROM FORD (17S09). IN MY OPINION THIS RECALL HAS NOT BEEN REPAIRED IN A REASONABLE AMOUNT OF TIME. 9 MONTHS OF DRIVING A VEHICLE WITH A RISK OF STARTING AN ENGINE FIRE IS TO LONG. DOES FORD HAVE AN UPDATED TIME FRAME FOR THE REPAIR. NHTSA RECALL # 17V209

Jan 5, 2018

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 50 MPH, THE VEHICLE STALLED WITHOUT WARNING DURING ACCELERATION. THE VEHICLE WAS TAKEN TO CRESCENT FORD (100 OLD WINSTON RD, HIGH POINT, NC 27265) WHERE IT WAS DIAGNOSED THAT THE FUEL PUMP PRESSURE SENSOR NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED, BUT THE FAILURE RECURRED. THE MANUFACTURER WAS NOTIFIED OF THE ISSUE AND REFERRED THE CONTACT TO NHTSA. THE VIN WAS INVALID. THE FAILURE MILEAGE WAS 41,000.

Mileage: 41,000

Jan 2, 2018 Fire

TL* THE CONTACT OWNED A 2014 FORD ESCAPE. WHILE OPERATING THE VEHICLE, SMOKE WAS PRESENT INSIDE THE CABIN. THE DRIVER IMMEDIATELY PARKED AND EXITED THE VEHICLE. SMOKE AND FLAMES WERE PRESENT COMING FROM UNDER THE HOOD AND THE FRONT UNDERCARRIAGE OF THE VEHICLE. THE FIRE DEPARTMENT WAS CALLED TO THE SCENE AND EXTINGUISHED THE FLAMES. THE VEHICLE WAS DESTROYED. A FIRE REPORT WAS FILED. THERE WERE NO INJURIES. THE MANUFACTURER AND LOCAL DEALER WERE NOT NOTIFIED. THE FAILURE MILEAGE WAS 52,000.

Mileage: 52,000

Dec 29, 2017

WHEN CAN I EXPECT THIS RECALL #17S09 TO BE SETTLED BY FORD?

Dec 28, 2017 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. ON OCTOBER 18, 2017, THE VEHICLE WAS TAKEN TO A LOCAL DEALER (SAM SCISM FORD, 5019 FLAT RIVER RD, FARMINGTON, MO 63640) WHERE IT WAS DIAGNOSED THAT THE SENSORS FOR THE COOLANT LEVELS NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. WHILE DRIVING 20 MPH, SMOKE APPEARED THROUGH THE AIR VENTS AND THE VEHICLE CAUGHT FIRE. THERE WERE NO INJURIES. THE AIR BAGS DID NOT DEPLOY. A POLICE REPORT WAS FILED. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC. THE LOCAL DEALER WAS NOT CONTACTED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS APPROXIMATELY 91,000.

Mileage: 91,000

Dec 28, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17S09000 (ENGINE AND ENGINE COOLING); HOWEVER, THE PART TO DO THE REPAIR WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. SAN LEANDRO FORD IN SAN LEANDRO, CALIFORNIA WAS MADE AWARE OF THE RECALL AND STATED THAT THE PARTS WERE UNAVAILABLE. THE MANUFACTURER WAS NOT MADE AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.

Dec 22, 2017

3 YR/36,000 MILE WARRANTY RAN OUT 2/21/17, RECALL LETTER DATED 4/2017 RECALL NOTICE 17S09 -NHTSA RECALL 17V-209. VEHICLE CAN'T MAINTAIN COOLANT LEVEL, HAD VEHICLE TO DEALERSHIP TWICE, CAN'T GET PROBLEM RESOLVED. CAN'T DRIVE VEHICLE OUT OF TOWN FOR FEAR OF FIRE. CONVENIENTLY WARRANTY HAS RUN OUT AND NOW THIS.

Mileage: 35,000

Dec 19, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT THE VEHICLE LEAKED COOLANT. THE "EXTREME TEMPERATURE, ENGINE CATCH ON FIRE" WARNING MESSAGE ILLUMINATED AND THE ENGINE SHUT OFF. THE VEHICLE WAS TOWED TO THE DEALER (MARYSVILLE FORD IN MARYSVILLE, WASHINGTON, PHONE NUMBER: 360-386-1245) WHERE IT WAS DIAGNOSED THAT THE COOLANT LINE FROM THE RESERVOIR TO THE INTAKE MANIFOLD CRACKED. THE MANUFACTURER WAS CALLED, BUT THERE WAS NO RESPONSE. THE FAILURE WAS NOT REPAIRED. ADDITIONALLY, THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING); HOWEVER, THE PART TO DO THE REPAIR WAS UNAVAILABLE. THE VIN WAS NOT PROVIDED. THE FAILURE MILEAGE WAS APPROXIMATELY 79,000.

Mileage: 79,000

Dec 18, 2017

THERMOSTAT QUIT WORKING AT 37900 MILES. NO HEAT HERE IN DECEMBER IN LOUISVILLE, KY

Mileage: 37,500

Dec 15, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING); HOWEVER, THE PART TO DO THE REPAIR WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE DEALER (COLUMBIA FORD IN COLUMBIA, CT, 860-228-2886 CONFIRMED THAT THE PARTS WERE NOT AVAILABLE FOR THE RECALL REMEDY. THE MANUFACTURER WAS MADE AWARE OF THE ISSUE AND WAS NOT ABLE TO CONFIRM WHEN THE PARTS WERE TO BECOME AVAILABLE. THE CONTACT STATED THAT AN UNKNOWN WARNING INDICATOR ILLUMINATED, BUT CLEARED UP WHEN ENGINE COOLANT WAS ADDED. THE FAILURE MILEAGE WAS APPROXIMATELY 29,000. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.

Mileage: 29,000

Dec 14, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE PARTS TO DO THE REPAIR WERE UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. ELLSWORTH FORD (424 INDUSTRIAL ROAD, ELLSWORTH, WI) CONFIRMED THAT THE PARTS WERE NOT AVAILABLE FOR THE RECALL REMEDY. THE MANUFACTURER WAS MADE AWARE OF THE ISSUE AND WAS NOT ABLE TO CONFIRM WHEN THE PARTS WERE TO BECOME AVAILABLE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.

Dec 12, 2017

THE CAR SUDDENLY STALLS OUT. HAS BEEN FIXED ONCE ALREADY BUT HAS HAPPENED NUMEROUS TIMES SINE THE REPAIR. WOULD HAPPEN PULLING OUT OF DRIVEWAY OR THROUGH PARKING LOT UNTIL THIS LAST TIME. I MERGED ONTO A MAJOR FREEWAY AND WAS UP TO 75-80MPH AND THE CAR STALLED OUT, ALMOST HIT BY 2 SEMIS TRYING TO AVOID RE ENDING ME ON THE FREEEWAY. *TT CONSUMER STATED NEVER HAD A BRAKE FAILURE. ISSUE WAS ENGINE STALL. UPDATED 9/4/18*JB

Mileage: 83,500

Dec 11, 2017 Fire

I BROKE DOWN ON THE HIGHWAY WITH SMOKE COMING OUT OF THE ENGINE COMPARTMENT. I HAD IT TOWED TO GO AUTOMOTIVE TO ENSURE IT WAS NOT BECAUSE OF A FAULTY OIL CHANGE (I HAD HAD AN OIL CHANGE 3 DAYS EARLIER). IT WAS DETERMINED THAT IT WAS NOT DUE TO ANY PART OF THE OIL CHANGE, BUT THAT IT WAS DUE TO A RECALL FORD RELEASED IN APRIL 2017. PARTS HAVE STILL NOT BEEN RECEIVED AT MY LOCAL DEALERSHIP FOR REPAIRS. THE AUTOMOTIVE SHOP DROVE THE CAR UP AND DOWN THE ROAD SEVERAL TIMES AND THOUGHT IT WAS SAFE TO DRIVE TO FORD (ABOUT 3 MILES AWAY) TO DISCUSS THE RECALL. MY MOM WAS TAKING THE CAR WHILE MY DAD FOLLOWED BEHIND HER. SHE ONLY DROVE CITY ROADS, NO HIGHWAYS. LESS THAN A QUARTER MILE FROM THE FORD LOT, THE CAR STARTED TO SMOKE LITTLE, LIGHT COLORED WISPS. WHEN MY MOM ARRIVED AT FORD AND PARKED IT BECAME HEAVIER (BUT STILL LIGHT COLORED) SMOKE, AND WHEN SHE WENT IN TO GET AN ASSOCIATE THEY GOT OUTSIDE AND IT WAS ON FIRE. IT TOOK THE FIRE DEPARTMENT TO PUT THE FLAMES OUT.

Mileage: 30,500

Nov 28, 2017

FIRST THE WIRING HAD TO BE REPLACE, WEEK LATER CATALYIC CONVERTOR, WEEK LATER TRANSMISSION, CAR IS ONLY 4 YRS OLD

Nov 27, 2017 Fire

MY SON WAS DRIVING MY 2014 FORD ESCAPE ON THE STREET TO I-25 WHEN HE THOUGHT HE SMELLED SMOKE, THEN THE ENGINE FAILURE FLASHED ON THE SCREEN AND THE ENGINE TURNED ITSELF OFF. HE WAS ABLE TO MOVE THE VEHICLE TO A SAFE LOCATION THEN HE POPPED THE HOOD AND SAW FLAMES SO HE SHUT THE HOOD AND CALLED THE FIRE DEPARTMENT

Mileage: 70,485

Nov 15, 2017

I'VE BEEN HAVING ISSUES WITH MY CAR STALLING OUT. IT BEGAN ON 11/10/17 WHEN I STARTED THE CAR. I DROVE ABOUT 500 FEET PULLING UP TO A STOP SIGN AND THE CAR STALLED OUT BUT ALL ELECTRICAL STAYED ON (I.E. RADIO). I TURNED THE CAR BACK ON AND IT DROVE FINE FOR A WHILE. THE SAME THING HAPPENED AGAIN LATER ON THE SAME DAY. THE FOLLOWING DAY IT HAPPENED IN THE SAME WAY AS I WAS PULLING OUT OF A PARKING LOT. I TURNED IT BACK ON AND IT DROVE WELL FOR A WHILE. LATER THAT EVENING IT HAPPENED AGAIN ALSO PULLING OUT OF A PARKING LOT. I DID NOT DRIVE THE CAR AGAIN TILL THE FOLLOWING MORNING. THE CAR DROVE WELL FOR 2 DAYS. UNTIL TODAY 11/15/17. IT TURNED ON IN THE MORNING. I GOT TO MY DESTINATION. PARKED THE CAR. CAME BACK ABOUT A HALF HOUR LATER AND I WAS PULLING OUT OF THE PARKING LOT ONLY DRIVING ABOUT 500 FEET WHEN THE CAR STALLED OUT AGAIN. I TURNED THE CAR BACK ON IT DROVE TO MY NEXT DESTINATION ABOUT 40 MINUTES AWAY. IT DID NOT FEEL AS IF IT WAS RUNNING AS SMOOTHLY AS USUAL. I'M AFRAID TO DRIVE MY CAR AS I LIVE IN A CITY AND TAKE HIGHWAYS EVERYWHERE. I WOULD HATE FOR MY CAR TO STALL OUT IN THE MIDDLE OF THE HIGHWAY AND CAUSE MYSELF AND OTHERS TO GET IMMENSELY HURT.

Mileage: 56,000

Nov 10, 2017

I FIRST FAILED A STATE INSPECTION (9/14/17) DUE TO A SMALL EVAP LEAK. I FIRST WENT TO A LOCAL BUSINESS TO GET THAT AND AT THE SAME TIME, THE VEHICLE WOULD CUT OFF AS I WAS DRIVING. THE LOCAL BUSINESS CLAIMED TO HAVE FIXED THE EVAP LEAK (AFTER WAITING A WEEK FOR THE PART (10/13/17), BUT HAD NO IDEA ABOUT THE VEHICLE STALLING. I THEN TOOK THE VEHICLE TO A FORD DEALERSHIP (10/19/17), WHERE IT WAS FIRST TAKEN IN FOR A WEEK ONLY TO HAVE THE SAME REPAIR DONE WITH FORD TELLING ME THE FIRST REPAIR USED A FAULTY PART. DRIVING HOME (10/24/17), THE VEHICLE DID NOT STALL, BUT STILL SHOWED DRIVING ISSUES. THE VEHICLE THEN STALLED WHILE IN PARK IDLE. I RETURNED TO THE FORD DEALER (10/27/17) AND FOR ANOTHER WEEK, REPAIRS WERE MADE OR LOOKED UP BY A HELP LINE INDICATING THAT EVEN FORD WASN'T SURE OF THE PROBLEM. I GOT THE VEHICLE BACK AGAIN ANOTHER WEEK LATER (11/6/17) AND THE NEXT MORNING THE CHECK ENGINE LIGHT HAS COME BACK ON. THE VEHICLE HAS NOT STALLED, BUT IT HAS NOT RUN THE SAME SINCE SEPTEMBER. I DO NOT HAVE FULL CONFIDENCE IN THE VEHICLE, BUT CAN'T AFFORD TO KEEP PLAYING GUESS WHAT'S WRONG WITH FORD.

Mileage: 87,225

Nov 10, 2017 Fire

I WAS DRIVING ON THE HIGHWAY 1 1/2 MILES FROM MY HOME WHEN THE ENGINE CUT OUT. I WAS ABLE TO DRIFT TO THE SIDE OF THE HIGHWAY AND COME TO A STOP. I REMAINED IN THE CAR AND SMELLED BURNING. THERE WAS SMOKE COMING FROM THE ENGINE COMPARTMENT. AFTER A FEW MINUTES THE SMOKE STOPPED. THERE WERE NO TROUBLE/WARNING LIGHTS PRIOR TO THE ENGINE FAILURE. I ARRANGED TO BE TOWED TO OUR REGULAR MECHANIC. HE INFORMED ME THAT HE THOUGHT I SHOULD GET THE VEHICLE TO A FORD DEALERSHIP, AS THERE HAD BEEN A FIRE IN THE ENGINE COMPARTMENT AND THERE WAS A HIGH PROBABILITY THAT IT WAS RELATED TO A FORD RECALL 17S09. THE VEHICLE WAS TOWED TO A NEARBY FORD DEALERSHIP AND A DIAGNOSTIC WAS PERFORMED. THE SERVICE MANAGER ALSO SUSPECTED THAT IT WAS PART OF THE ISSUE ASSOCIATED WITH THE RECALL. HE OPENED A FORD "HOTLINE" CASE. A DAY OR SO LATER THE SERVICE MANAGER CALLED AND SAID THAT THEY DETERMINED THAT IT WAS NOT PART OF THE RECALL BECAUSE THE COOLANT SYSTEM HAD PASSED THEIR PRESSURE TEST AND THERE HAD NOT BEEN A COOLANT LEAK. HE ALSO DETERMINED THAT THERE WAS A CRACKED HEAD AND CRACKED MANIFOLD, AND THAT THE VEHICLE HAD LOST OIL THROUGH THE CRACKED HEAD. WHEN I INQUIRED AS TO WHY THE HEAD WOULD CRACK WHEN THE VEHICLE HAS REGULAR OIL CHANGES (THE MOST RECENT JUST 20 DAYS PRIOR) AND THE COOLANT SYSTEM WAS FULL HE DIDN'T HAVE AN ANSWER. AT THAT TIME HE SAID THE ENGINE WOULD COST CLOSE TO $5,000 TO REPAIR, BUT THAT HE COULDN'T GUARANTEE THAT IT WOULDN'T HAVE "OTHER ISSUES" RELATED TO THE DAMAGES IDENTIFIED. BECAUSE OF LIMITED SPACE HERE, I HAVE ATTACHED A FULL DESCRIPTION AS A PDF.

Mileage: 76,000

Nov 3, 2017

IN 2016, I HAD THE COOLANT SYSTEM REPAIRED/REPLACED DUE TO A LEAK. THIS WAS PRIOR TO THE RECALL. AFTER RECALL NOTICE WAS SENT I ATTEMPTED TO HAVE IT ADDRESSED TWICE AND TOLD BOTH TIMES THE PARTS WERE NOT AVAILABLE. ON 10/26/17 I GOT A NOTICE THAT MY ENGINE WAS ABOUT TO OVERHEAT AND FOUND THAT THE COOLANT TANK WAS EMPTY. I MADE AN APPOINTMENT FOR 10/30/2017. ON 10/29/17 I FILLED THE COOLANT TANK BEFORE DRIVING TO CHURCH AND AFTER 15-20 MILES RECEIVED AN ENGINE FAIL NOTICE, SMOKE COMING OUT OF THE ENGINE AND CAR WOULD NOT RESTART. COOLANT TANK WAS ALREADY EMPTY. CAR WAS TOWED TO BERGLUND FORD IN BEDFORD, VIRGINIA. TODAY IS 11/3/2017, NO DIAGNOSIS MADE, NO IDEA WHAT THE CAUSE OF ENGINE FAILURE IS AND WE WERE TOLD BY THE SERVICE DEPARTMENT THAT THEY HAD NO KNOWLEDGE OF THE RECALL REPORTING THIS TYPE OF INCIDENT. MULTIPLE ATTEMPTS TO CONTACT FORD MOTOR HAS BEEN FRUITLESS BECAUSE THE DEALER IS NOT COMMUNICATING WITH THEM.

Mileage: 88,000

Nov 3, 2017 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 60 MPH, SMOKE APPEARED UNDER THE HOOD. THE CONTACT PULLED OVER AND THE ENGINE COMPARTMENT BURST INTO FLAMES WITHOUT WARNING. THE FIRE DEPARTMENT EXTINGUISHED THE FIRE. A POLICE REPORT WAS NOT FILED. THERE WERE NO INJURIES. THE VEHICLE WAS TOWED TO A LOCAL DEALER (FLAMMER FORD, 3335 COMMERCIAL WAY, SPRING HILL, FL 34606). THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS 55,000. THE CONSUMER STATED THE MANUFACTURER OFFERED 11,000 FOR THE VEHICLE. THE CONSUMER DECLINED. THE CONSUMER REQUESTED TO BE PROVIDED A VEHICLE OF THE SAME MAKE, MODEL, AND YEAR. *JS *LN *CN

Mileage: 55,000

Nov 3, 2017

ON FEBRUARY 2017 I BROUGHT A 2014 FORD ESCAPE AT ABOUT 59 K MILES AND NOW IT HAS ABOUT 70K MILES ON IT. I WAS TOTALLY CLUELESS AS TO HOW UNSAFE THIS CAR WAS AND ALL OF THE NUMEROUS COMPLAINTS/ISSUES THAT CONSUMERS ARE HAVING WITH THIS CAR. ON 09/22/2017, THIS CAR TOTALLY BROKE DOWN. THIS CAR IS A SAFETY HAZARD AS I ALMOST GOT INTO AN ACCIDENT AS THE CAR WITHOUT MADE A LOUD NOISE, AND WITHOUT ANY WARNING JUST STOPPED/SHUT DOWN IN TRAFFIC. NONE OF THE SAFETY INDICATOR ALERTS WORKED IN THIS CAR SO I WAS CLUELESS THAT THE CARD HAD ANY ISSUES. I ONLY OWNED THIS CAR FOR ABOUT 6 MONTHS AT THE TIME AND IT WAS CLEARLY OUT OF WARRANTY. I HAD THE CAR TOWED ONLY TO FIND OUT THAT IT IS THE TRANSMISSION, BAD BATTERY, ABS ISSUES AND POSSIBLY AN ALTERNATOR. I WAS ALSO ADVISED THAT IT WAS AN ELECTRICAL ISSUES AND POSSIBLE A RECALL THAT IS WHY NO WARNINGS LIGHTS CAME ON TO LET ME KNOW IT WAS A PROBLEM. I REACHED OUT TO FORD WHO BASICALLY SAID SORRY WE DON'T CARE HAVE A NICE DAY. THIS CAR IS NOT SAFE AND SHOULD BE TAKEN OFF OF THE MARKET UNTIL FORD CAN GET THIS IN ORDER. I REALLY HOPE SOMEONE LOOK INTO THIS MATTER BEFORE SOMEONE LOSE THEIR LIFE.

Mileage: 70,000

Nov 1, 2017 Fire

MY DAUGHTER WAS DRIVING THE CAR ON A 2 LANE HIGHWAY, GOING STRAIGHT, AT HIGHWAY SPEED ( MY DAUGHTER GOTTEN ABOUT 3 MILES FROM HOME ) AND ENGINE FAULT LIGHT CAME ON, CAR SPUTTERED, SERVICE NOW LIGHT CAME ON AND IMMEDIATELY SMOKE STARTED TO COME INTO THE CAR. SHE PULLED OVER IMMEDIATELY AND RAN FROM CAR AND CALLED 911 THE CAR CAUGHT ON FIRE UNDER HOOD. THE FIRE WAS VERY LARGE AND TOTALED CAR. TIME FROM ENGINE FAULT LIGHT TO FIRE WAS APPROXIMATELY 30 SECONDS TO 45 SECONDS. THAT PART IS AN ESTIMATE. NOTIFIED FORD MOTOR CORP AND THEY GAVE ME A CLAIM NUMBER. CURRENTLY INSURANCE COMPANY HAS THE CAR BUT WILL PROBABLY MAKE A CLAIM TO FORD. IT WAS IN A COUPLE OF WEEKS BEFORE BECAUSE IT HAD THE SAME KIND OF SPUTTER. THEY ALSO WORKED ON 4 RECALLS AT THIS TIME. WHEN TALKING TO FMC, THE LADY STATED THAT FOR SOME REASON ONE RECALL IS STILL OPEN ALTHOUGH IT SHOWED THAT THE DEALERSHIP HAD DONE IT. SHE WASN'T SURE WHY THEY DIDN'T CLOSE IT.

Mileage: 120,000

Nov 1, 2017

MY ENGINE LIGHT COME ON I WENT TO THE AUTOZONE TO PUT IN THE MACHINE I AM HAVING PROBLEM WHIT THE TURBO. AND WHEN I LEAVE MY CAR DOOR OPEN TO CLEAN MY CAR MY ENGINE DIE COMPLETELY IT DOES THIS NUMERO TIME. I AM SINGLE MOM I WORK VERY HARD I PAY MY CAR NOTE ON TIME EVERY MONTH KNOW IS GETTING TO THE POINT THAT HOW I WILL FIX MY CAR I CANT EVEN AFFORD IT ALL I AM THINKING ABOUT THE CAR NOTE OR FIX THE CAR, PLEASE FORD HELP.

Oct 27, 2017

ENGINE COOLANT SENSOR RE-PROGRAM RECALL. THIS WAS CORRECTED OCTOBER 10, 2017 AT FORD DEALERSHIP IN BENSENVILLE, ILLINOIS. ALSO FOUR DOOR LATCHES WERE RECALL AND REPLACED AT SAME TIME.

Mileage: 39,899

Oct 27, 2017

PLEASE SEE ATTACHED PDF. IT IS THE LETTER I SENT TO FORD MOTOR COMPANY. MY COMPLAINT FOCUSES ON THE ENGINE OVERHEATING AND THE CONSTANT LOSS OF ENGINE COOLANT.

Mileage: 60,000

Oct 25, 2017 Fire

WAS DRIVING ON HIGHWAY APPROXIMATELY 65 MPH WHEN THE ENGINE FAULT CAME ON AND LOST POWER. PULLED TO SIDE OF ROAD AND BEGAN TO SEE SMOKE FROM ENGINE. FIRST THOUGHT WAS OVERHEATING OR SIMILAR. WITHIN MINUTES NOTICED FLAMES FROM UNDER HOOD NEAR WINDSHIELD. GOT OUT OF CAR AND WITHIN LESS THAN 5 MINUTES CAR WAS FULLY ENGULFED IN FLAMES. THIS WAS AN OBVIOUS ENGINE ISSUE AND NOT A MAINTAINANCE ISSUE. THIS WAS A FLEET VEHICLE PROPERLY MAINTAINED UNTIL I PURCHASED IT FROM THAT EMPLOYER 1 YEAR PRIOR.

Mileage: 100,000

Oct 19, 2017

MAR 27,2017 MANUFACTURER RECALL NUMBER: 17S09 NHTSA RECALL NUMBER: 17S09 RECALL STATUS: RECALL INCOMPLETE, REMEDY NOT YET AVAILABLE THIS CRITICAL SAFETY ISSUE SEEMS TO BE TAKING A LONG TIME TIME TO FIND AND IMPLEMENT A SOLUTION. I HAVE TO KEEP ADDING COOLANT AT LEAST ONCE A WEEK SINCE 08/26/2015. NO WATER IN THE OIL DURING RECOMMENDED OIL CHANGES. I WOULD LIKE TO BE DRIVING A SAFE VEHICLE NOT ONE THAT COULD POSSIBLY KILL ME. IS THIS SOMETHING THAT COULD BE COVERED UNDER THE LEMON LAW IN THE STATE OF TEXAS? I WOULD BE HAPPY TO SWAP IT FOR A DIFFERENT VEHICLE THAT DIDN'T HAVE THIS ISSUE. IF THE MANUFACTURER HAS FAILED OR IS UNABLE TO REMEDY THIS SAFETY RECALL FOR YOUR VEHICLE IN A TIMELY MANNER, PLEASE CONTACT THE NHTSA VEHICLE SAFETY HOTLINE AT: 1-888-327-4236 OR TTY: 1-800-424-9153 OR FILE AN ONLINE COMPLAINT WITH NHTSA. THIS IS WHY I AM FILING THIS COMPLAINT AS I FEEL FORD SHOULD HAVE A SOLUTION READY TO IMPLEMENT. BUT I HAVE AS YET NOT BEEN CONTACTED.

Oct 10, 2017

DRIVING MY 2014 ESCAPE TO WORK I WAS ON A 35 MPH STREET, AN ALERT WARNING CAME ON TELLING ME THE ENGINE WAS HOT AND TO SAFELY STOP VEHICLE. MY TEMPERATURE GAUGE NEEDLE WAS AT THE HOT. I PULLED OVER AND IT SLOWLY WENT BACK DOWN ENOUGH WHERE I GOT TO MY DESTINATION A MILE AWAY. WHEN CHECKED, MY COOLANT OVERFLOW WAS COMPLETELY EMPTY. I HAD SOMEONE TAKE ME TO PURCHASE THE CORRECT COOLANT AND REPLACED IT BEFORE STARTING THE VEHICLE. WHEN I RETURNED HOME AND CHECKED THE LEVEL, THE COOLANT WAS AGAIN LOW. THE ENGINE WAS EXTREMELY HOT TO THE TOUCH, INCLUDING THE HANDLE TO LATCH OPEN THE HOOD. I REMEMBERED A RECALL ON MY VEHICLE, 17S09/ NHTSA RECALL 17V-209, AND WAS WAITING FOR THE SECOND RECALL LETTER WHEN THE PARTS WERE GOING TO BE AVAILABLE FOR REPAIRS. IT STATED IF THE VEHICLE LEAKED COOLANT OR BECAME HOT, IT COULD CAUSE POSSIBLE OIL LEAK AND CRACK IN THE CYLINDER HEAD, AND EVEN FIRE! I CALLED BRUCE TITUS FORD IN PORT ORCHARD WASHINGTON AND THE SERVICE GUY TOLD ME NOT TO DRIVE IT AND IT WAS TOWED TO THE SERVICE DEPARTMENT. THEY DID TESTS AND FOUND THAT THAT ALERT MESSAGE OF VEHICLE GETTING HOT, ETC SHOWED BUT THEY DID A PRESSURE TEST AND SO ON AND COULD NOT SEE WHERE THE COOLANT WAS GOING. THEY TOLD ME THERE WERE STILL NO PARTS AVAILABLE FOR THE, (ENHANCEMENT TO THE COOLANT PROBLEM), NOT THE FIX! APPARENTLY THE RECALL SAYS THE ENHANCEMENT PART IS A SENSOR WHICH TELLS ME THE COOLANT IS GETTING LOW. SO WITHOUT IT BEING FIXED, I WAS TOLD TO COME GET THE VEHICLE AND KEEP REFILLING AS NEEDED! I WAS TOLD THEY COULD REPLACE THE COOLANT OVERFLOW BOTTLE BUT IT WAS NOT ONLY ON BACK ORDER, BUT WOULD COST ME $400! COOLANT IS LEAKING AT WORK AND IN DRIVEWAYS AND A HAZARD TO MINE AND OTHERS PETS! I'VE SPENT $40 ON COOLANT SO FAR AND CANT KEEP DOING THIS! I SHOULD NOT HAVE TO. ONLY 52,000 MILES, MY ONLY TRANSPORTATION, AND I'M STILL PAYING OUT $458 PAYMENTS AND INSURANCE!

Mileage: 52,000

Oct 8, 2017

10/7/17 APPROX 6:30 PM WHILE ENTERING ON RAMP ONTO FRWAY AT APPROX 35 MPH, DRIVING DIST OF LESS THAN 1/2 TO 3/4 MILE FROM LAST PARKED STOP, INDICATOR DASH MEMO OF "ENGINE TEMP HIGH PULL OVER SAFELY", NO INDICATION ON ENGINE TEMPERATURE GAUGE AS IT REGISTERED BELOW MID MARK. PULLLED OVER ON FRWAY INTO CLOSED LANES, TURNED OFF ENGINE. TURNED ON AGAIN TO ADVANCE 10 FT OUT OF WAY OF ONRAMP VEHICLES, TEMP GAUGE INDICATED "H", TURNED OFF ENGINE. CALLED FOR TOW, TECH COULD NOT START ENG, BATTERY DEAD. TOWED HOME (LESS THAN 2-4 MILES), ENGINE OFF WITH TICKING SOUND THAT COULD BE HEARD ACROSS GRILL. TODAY, 10/8/17 THIS AM CHECKED COOLANT AND EMPTY. NO INDICATION OF ENG RUNNING "HOT" OR NO FLUID LOW INDICATOR LIGHT/WARNING. THERE WAS NEVER ANY WARNING LIGHTS, ETC TIME DRIVING FROM 9/27/17 THRU 10/7/17.. *ON 9/27/17 I HAD ROUTINE OIL CHANGE, FLUIDS CHECKS W/RECEIPT OF DEALER PERFORMING ALL WORK AND CHECKS PRIOR TO A TRIP OF APPROX 346 MI EA WAY, TRAVELED APPROX 20 ADDITIONAL MI FROM 10/3/17-10/7/17 AND THERE WAS NO INDICATION OVERHTING OF ENGINE AND I HAD TO EXPECT COOLANT WAS FULL, NOT LOW AS IT WAS SERVICED APPROX 9 DAYS PRIOR. *ON 9/27/17 I ALSO SPECIFICALLY ASKED SERVICE REP AND TECH IF FLUIDS WERE CHECKED BOTH STATED YES,OKAY, ALSO INDICATED ON SERVICE RECEIPT.THEY PERFORM A COMPLETE CHECK OF FLUIDS, HOSES, ETC. TO KNOW IF FORD ESCAPES, 2014 OR OTHERS, HAVE HAD COMPLAINTS REGARDING OVERHEATING W/O WARNINGS AND/OR IF THERE IS A POSSIBILITY OF THIS FORD ENGINE HAVING A RECORD OF THESE PROBLEMS AND COMPLAINTS W/DEALER WHO DOES ALL ROUTINE MAINT ON MY VEHICLE AND ANY COMPLAINTS R/T BELL FORD, PHX SERDEPT REGARDING SAME ISSUE? READ FORDESCAPE.ORG THERE HAS BEEN A RECALL FOR ENGINES CATCH FIRE DUE TO OVERHTING/COOLANT, #17S09 IS IT VALID? I WILL BE ARRANGING TOWING FROM MY HOME TO DEALERSHIP MY VEHICLE&PERFORMED LAST MAINT&OIL CHANGE ON 9 /27/17: BELL FORD, PHXAZ 85023

Mileage: 51,500

Oct 5, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING UNKNOWN SPEEDS, THE VEHICLE OVERHEATED AND STALLED WITHOUT WARNING. THE VEHICLE WAS TAKEN TO BOMMARITO FORD (675 DUNN RD, HAZELWOOD, MO 63042) WHERE IT WAS DIAGNOSED THAT THE PRESSURE TEST PASSED AND THE VEHICLE WAS FUNCTIONING PROPERLY. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER OPENED CASE NUMBER: 13094886, BUT DID NOT OFFER ANY FURTHER ASSISTANCE. THE VIN WAS UNKNOWN. THE FAILURE MILEAGE WAS 138,000. *LN CONSUMER THINKS THE SENSOR FOR COOLANT SYSTEM WENT OUT GWING FALSE READINGS SO THE COOLANT FAN DID NOT COME ON. UPDATED 7/25/18*JB

Mileage: 138,000

Oct 2, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING); HOWEVER, THE PART NEEDED FOR THE REPAIR WAS NOT AVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE VEHICLE WAS TAKEN TO TASCA FORD (1300 PONTIAC AVE, CRANSTON, RI 02920, PHONE NUMBER: (401) 681-1300), BUT WAS NOT REPAIRED DUE TO LACK OF PARTS. THE MANUFACTURER WAS NOT CONTACTED. THE CONTACT HAD NOT EXPERIENCED A FAILURE. VIN TOOL CONFIRMS PARTS NOT AVAILABLE. UPDATED 12/13/2017 *LN CONSUMER STATED SHE WAS ADVISED PARTS NOT AVAILABLE UNTIL END OF YEAR 2017 UPDATED 7/24/18*JB *TR

Sep 28, 2017

RECALL 17S09 FOR ENGINE CYLINDER HEAD, POTENTIALLY LEADING TO CRACKS AND RESULTING IN OIL LEAKS. DEALERSHIP CYPRESS COAST FORD IN SEASIDE CA CONTINUES TO CLAIM THEY DO NOT HAVE THE PARTS TO RESOLVE THE RECALL. I CONSIDER THIS TO BE A HUGE SAFETY HAZARD AND SINCE I DRIVE MY CAR EVERYDAY I AM AT RISK BECAUSE THE DEALERSHIP HASN'T RESOLVED THE RECALL/ DEFECT.

Sep 18, 2017

I AM AWARE OF A RECALL FOR MY CAR WHICH CAN RESULT IN AN ENGINE FIRE DUE TO A CRACKED HEAD. WHEN I CHECK FOR A RESOLUTION ALL I SEE IS THAT FORD HAS A PLAN TO CORRECT.. BUT THERE HAS BEEN NO ACTION TAKEN TO IMPLEMENT THE REPAIR.. WHEN DO THEY HAVE TO START ACTING ON THE RECALL?

Mileage: 42,000

Sep 5, 2017

VEHICLE COMMONLY OVERHEATS, LOSS OF COOLANT. OVERHEATING OCCURS WHEN TRAVELING UPHILL AT GREATER THAN 40 MPH WITH AIR CONDITIONING ON, OR IN ANY GEAR WHEN ENGINE SPEED IS HELD ABOVE 3500 RPM AND AIR CONDITIONING IS ON. COOLANT LOSS OCCURS AT ABOUT 20 OZ PER 1000 MILES DRIVEN

Mileage: 106,000

Sep 1, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING); HOWEVER, THE PARTS TO DO THE REPAIR WERE UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE CONTACT CALLED SPANGLER MOTORS (LOCATED AT 5620 PA-405, MILTON, PA 17847 (570) 742-8725) AND WAS INFORMED THAT THE PARTS WERE NOT AVAILABLE FOR THE RECALL REMEDY. THE MANUFACTURER WAS NOTIFIED OF THE ISSUE AND WAS NOT ABLE TO CONFIRM WHEN THE PARTS WERE TO BECOME AVAILABLE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. VIN TOOL CONFIRMS PARTS NOT AVAILABLE. PARTS DISTRIBUTION DISCONNECT.

Aug 31, 2017

VEHICLE HAS STALLED WHILE IN MOTION ON NUMEROUS OCCASIONS, THIS HAS BEEN HAPPENING FOR OVER A YEAR. IF THE ENGINE IS TURNED OFF AND THEN TURNED BACK ON, IT WILL SOMETIMES RUN JUST FINE, OTHER TIMES IT WILL DRIVE FOR 5-10 MINUTES AND THEN DO THE SAME THING. IF IT SITS FOR A PERIOD OF TIME, IT WILL THEN DRIVE FINE. THE CHECK ENGINE LIGHT WILL OR WILL NOT COME ON WHEN IT DOES THIS. I HAVE HAD IT IN SEVERAL TIMES TO HAVE THIS CHECKED AND IT IS CURRENTLY IN THE SHOP HAVING THE THROTTLE BODY REPLACED TO THE TUNE OF ALMOST $900. ALL OF THESE INCIDENCES HAPPENED WHILE DRIVING ON A CITY STREET. PRIOR TO THE CAR ACTING UP, THE CAR HAD BEEN IN PARK IDLING FOR ABOUT 5 MINUTES. THE DATE LISTED BELOW IS THE MOST RECENT DATE THIS OCCURRED.

Mileage: 108,235

Aug 29, 2017 Fire

I WAS DRIVING ON A HIGHWAY WHEN AN ALERT APPEARED ON MY DASHBOARD: "ENGINE ERROR 1"--- AND, I NOTICED MY BATTERY LIGHT WAS ON. IMMEDIATELY, THE VEHICLE SLOWED, BUT I WAS ABLE TO EEK TO AN EXIT AND STOP ON THE SIDE OF THE FRONTAGE ROAD. I TURNED OFF THE VEHICLE. AS I CALLED FOR A TOW TRUCK, I NOTICED SMOKE SLOWLY WAFTING FROM BENEATH THE HOOD, NEAR THE WINDSHIELD...AND THEN I SPOTTED AN ORANGE FLAME. I QUICKLY EXITED THE VEHICLE AND CALLED 911. AFTER THE FIREMEN STOPPED THE FIRE, I SAW THE FRONT OF THE VEHICLE, ON THE DRIVER'S SIDE, HAD MELTED AWAY.

Mileage: 60,000

Aug 25, 2017

I BOUGHT THE VEHICLE BRAND NEW IN JULY 2013. IT WAS ONE OF THE FIRST 2014 ESCAPE MODELS MADE. AFTER A YEAR OF OWNING IT (2014), I TURNED THE VEHICLE ON ONE MORNING AND I RECEIVED AN ERROR MESSAGE STATING "ENGINE FAULT - SERVICE NOW". I PROCEEDED TO TURN THE CAR OFF, THEN BACK ON, AND THE MESSAGE WAS GONE. WHEN I TOOK IT IN TO THE DEALER FOR AN OIL CHANGE, I MENTIONED WHAT HAPPENED AND THEY SAID THEY COULDN'T DO ANYTHING UNLESS THE MESSAGE WAS STILL ON THERE. OVER THE NEXT COUPLE OF YEARS (2015-2016), I WOULD GET THE MESSAGE RANDOMLY, BUT IT WOULD GO AWAY AFTER I RESTARTED THE VEHICLE. THE DRIVING SEEMED TO BE THE SAME, SO IT DIDN'T CAUSE TOO MUCH CONCERN. IN THE LAST FEW MONTHS (2017), I HAVE NOTICED THE MESSAGE RETURNING "ENGINE FAULT - SERVICE NOW." WHEN I TOOK THE CAR IN FOR A RECALL, I MENTIONED THE ERROR AGAIN AND THEY WERE ABLE TO DETERMINE WHAT IT WAS - THEY NEEDED TO REPLACE THE WIRE SPLICE. WHAT CONCERNS ME IS THAT OTHER FORD ESCAPES HAVE BEEN RECALLED WITH THIS PROBLEM, AND I'VE BEEN DRIVING AROUND WITH A SAFETY ISSUE SINCE I PURCHASED IT IN 2013.

Mileage: 39,000

Aug 16, 2017

FORD MOTOR COMPANY ANNOUNCED A RECALL REGARDING LEAKING COOLANT, RESULTANT CRACKED CYLINDER HEADS, AND RESULTANT UNDERHOOD/VEHICLE FIRES, ON MARCH 27, 2017. THE MANUFACTURER'S AND NHTSA'S RECALL NUMBER IS 17S09. THIS IS A CRITICAL SAFETY ISSUE, AS VEHICLE FIRE'S ARE LIKELY TO RESULT IN INJURY AND OR DEATH. AS OF AUGUST 16, 2017, FORD HAS NOT MADE AVAILABLE ANY REMEDY WHATSOEVER FOR THIS ISSUE; FORD HAS FAILED TO TIMELY CORRECT THE PROBLEM. MOREOVER, FORD'S PROPOSED REMEDY, WHICH AGAIN IS NOT AVAILABLE 5 MONTHS AFTER ITS IDENTIFYING THE ISSUE, IS A COOLANT LEVEL SENSOR, WHICH DOES NOT ADDRESS AT ALL THE UNDERLYING ISSUE OF LEAKING COOLANT, AND THUS DOES NOTHING TO PREVENT THE RESULTANT VEHICLE/UNDERHOOD FIRES.

Aug 14, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. AFTER STARTING THE VEHICLE, A HIGH TEMPERATURE WARNING INDICATOR ILLUMINATED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE COOLANT IN THE VEHICLE WAS LEAKING. THE INDEPENDENT MECHANIC ADDED COOLANT AND THE LIGHT TURNED OFF. WHILE DRIVING HOME, THE CONTACT NOTICED LOW COOLANT LEVEL IN THE VEHICLE. THE CONTACT SPOKE WITH PREMIER FORD (2120 US-45, COLUMBUS, MS 39705) WHO STATED THAT THE VIN WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING), AND THE CONTACT WOULD NEED TO HAVE THE VEHICLE DIAGNOSED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND CONFIRMED THAT THE VIN WAS NOT INCLUDED; HOWEVER, THEY WOULD MAKE A NOTE OF THE INCIDENT AND INFORM NHTSA. THE APPROXIMATE FAILURE MILEAGE WAS 50,100.

Mileage: 50,100

Aug 14, 2017 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING VARIOUS SPEEDS, THE ENGINE OVERHEATED. THE CONTACT STOPPED THE VEHICLE AND ADDED COOLANT AND OIL. THE CONTACT ALSO NOTICED SMOKE COMING FROM THE TAILPIPE OF THE VEHICLE. AUTONATION FORD TORRANCE IN TORRANCE, CALIFORNIA WAS MADE AWARE OF THE FAILURE AND STATED THAT THEY WOULD INSPECT THE VEHICLE FOR THE SOURCE OF THE FAILURE. THE MANUFACTURER WAS NOT MADE AWARE OF THE ISSUE. THE CONTACT RECEIVED NHTSA CAMPAIGN NUMBER: 17S09000 (ENGINE). THE FAILURE MILEAGE WAS APPROXIMATELY 112,000.

Mileage: 112,000

Aug 3, 2017

MY 2014 FORD ESCAPE HAS A COOLANT LEAK. IT HAS OVERHEATED AT LEAST 3 TIME WITHOUT WARNING WHILE DRIVING ON THE HIGHWAY. AS A RESULT MY VEHICLE HAS SUSTAINED ENGINE DAMAGE. THERE IS A RECALL ASSOCIATED WITH THE COOLANT SYSTEM. I THINK FORD SHOULD REPLACE/ REPAIR THE ENGINE AT NO CHARGE. THEY DON'T AGREE.

Mileage: 45,000

Aug 2, 2017

VEHICLE SUDDENLY HESITATES AND STALLS WHILE DRIVING IT CREATING A SERIOUS SAFETY ISSUE.

Mileage: 43,000

Jul 30, 2017

MY FORD ESCAPE HAS BEEN HAVING OVERHEATING ISSUES FOR MONTHS. WHEN TAKEN TO THE DEALER THEY CLAIMED TO HAVE FIXED IT ONLY TO HAVE MADE IT WORSE AS THE CAR COMPLETELY SHUTS DOWN DUE TO OVERHEATING. THERE IS A RECALL REGARDING THIS EXACT ISSUE AND THEIR REPAIR IS A SENSOR TO WARN OF LOW COOLANT. THAT'S RIDICULOUS!!! THE PROBLEM LIES WITH THE COOLANT LEAKING. WHERE IS THE ACTUAL FIX FOR THAT??? A WARNING LIGHT DOESN'T FIX THE MANUFACTURING ISSUE OF LEAKING COOLANT. A 3 YEAR OLD CAR SHOULDN'T HAVE LEAKING PROBLEMS!!! WHILE IN MOTION, THE OVERHEATING SENSORS TURN ON AND THE CAR SHUTS OFF MAKING FOR A VERY DANGEROUS SITUATION. FORD PRETENDED THEY HAD NO IDEA ABOUT AN OVERHEATING ISSUE AND CHARGED ME $800 TO FIX IT AND YET, IT ACTUALLY FIXED NOTHING!!! STILL OVERHEATING, AND I'M STILL OUT $800 AND NO RESOLUTION IN SIGHT.

Mileage: 70,000

Jul 25, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBERS: 16V643000 (LATCHES/LOCKS/LINKAGES) AND 17V209000 (ENGINE AND ENGINE COOLING). THE PARTS WERE NOT AVAILABLE WITHIN A REASONABLE TIME FRAME TO SCHEDULE THE RECALL REPAIR. THE DEALER (FRONTIER FORD, 12610 THOMPSON RD, ANACORTES, WA 98221, (360) 293-3105) DID NOT GIVE A SPECIFIC DATE FOR WHEN THE PART WOULD BECOME AVAILABLE. THE MANUFACTURER WAS CONTACTED AND COULD NOT PROVIDE AN ESTIMATED DATE FOR WHEN THE VEHICLE WOULD RECEIVE THE RECALL REPAIR. IN ADDITION, THE VEHICLE WAS ALSO INCLUDED IN A MANUFACTURER CAMPAIGN FOR THE "SYNC WITH MY FORD, MY LINCOLN" TOUCH CAMPAIGN, WHICH COVERED ACCESSORY PROTOCOL INTERFACE MODULE APIM. THE CONTACT WAS NOT EXPERIENCING A FAILURE AND WAS WAITING FOR A RESPONSE FROM THE MANUFACTURER CONCERNING THE TWO RECALLS AND THE SERVICE CAMPAIGN. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.

Jul 24, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17S090000 (ENGINE AND ENGINE COOLING); HOWEVER, THE PART FOR THE RECALL REPAIR WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE CONTACT STATED THAT THE VEHICLE OVERHEATED ON DIFFERENT OCCASIONS. THE CONTACT TOOK THE VEHICLE TO THE LITHIA FORD DEALER WHERE IT WAS DIAGNOSED THAT THE COOLANT TANK AND THE SENSOR NEEDED TO BE REPLACED. THE COOLANT TANK WAS REPLACED; HOWEVER, THE RECALL REPAIR WAS NOT COMPLETED. THE MANUFACTURER INFORMED THE CONTACT THAT THE REMEDY WOULD NOT BE AVAILABLE AND THEY WERE NOT ABLE TO PROVIDE LOANER VEHICLES DUE TO NHTSA NOT AUTHORIZING THEM TO DO SO. THE APPROXIMATE FAILURE MILEAGE WAS 25,000. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.

Mileage: 25,000

Jul 24, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHEN THE CONTACT STARTED THE VEHICLE, THE ENGINE FAULT INDICATOR ILLUMINATED. THE CONTACT TURNED OFF AND RESTARTED THE ENGINE AND THE VEHICLE RETURNED TO NORMAL. THE VEHICLE WAS TAKEN TO THE DEALER (TASCA AUTOMOTIVE GROUP LOCATED AT 1300 PONTIAC AVE, CRANSTON, RI 02920; (800) 788-2114) WHERE IT WAS DIAGNOSED THAT THE BOOST AND MAT SENSOR NEEDED TO BE REPLACED. IN ADDITION, THE ENGINE SPLICES ALSO NEEDED TO BE SERVICED. THE VEHICLE WAS REPAIRED. A MONTH LATER, ON JULY 6, 2017 WHILE DRIVING 25 MPH, THE ENGINE FAULT INDICATOR ILLUMINATED. THE CONTACT TURNED OFF AND RESTARTED THE ENGINE AND THE VEHICLE RETURNED TO NORMAL. THE VEHICLE WAS TAKEN TO THE DEALER AGAIN WHERE IT WAS DIAGNOSED THAT THE ENGINE SPLICES NEEDED TO BE SERVICED. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS CONTACTED AT 800-241-3673 AND STATED THAT THE CONTACT NEEDED TO CALL NHTSA. THE APPROXIMATE FAILURE MILEAGE WAS 34,243.

Mileage: 34,243

Jul 17, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING VARIOUS SPEEDS OR ATTEMPTING TO ACCELERATE, THE VEHICLE JERKED WITHOUT WARNING AND FELT LIKE IT WOULD STALL. THE VEHICLE WAS NOT TAKEN TO A DEALER. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE CONTACT RECEIVED A RECALL NOTIFICATION FOR NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING); HOWEVER, THE REMEDY PART NEEDED FOR THE REPAIR WAS NOT AVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE DEALER AND MANUFACTURER WERE NOT CONTACTED. THE APPROXIMATE FAILURE MILEAGE WAS 60,000. VIN TOOLS CONFIRMS PARTS NOT AVAILABLE.

Mileage: 60,000

Jul 14, 2017

ON EACH COLD START, IN PARK, HEAVY PUFF OF BLUE SMOKE EMITS FROM EXHAUST. VEHICLE HAS 66,000 MILES ON IT AND HAS BEEN REGULARLY AND PROFESSIONALLY MAINTAINED. DEALER SERVICE ADVISER STATES INTERNAL OIL LEAK ONTO ENGINE HEAD, LIKELY REQUIRING ENGINE REPLACEMENT. I WOULD LIKE NHTSA TO INVESTIGATE TO EXPAND MODELS WITHIN CURRENT CAMPAIGN NUMBER 17V209000 AND/OR RESEARCH ADDITIONAL ISSUE WITH LEAKS IN CERTAIN FORD ENGINES. I HAVE NOT RECEIVED NOTICE FROM FORD MOTOR COMPANY THAT MY VEHICLE WAS INCLUDED IN CAMPAIGN NUMBER 17V209000, AND A VIN SEARCH ON THE NHTSA SITE CONFIRMED THAT THE VEHICLE WAS NOT SUBJECT TO SUCH RECALL; HOWEVER, I BELIEVE IT IS LIKELY THAT MY VEHICLE IS IN THE SAME DANGER AS THOSE LISTED IN THE ABOVE-REFERENCED NHTSA RECALL EITHER FOR THE REASONS STATED IN THE RECALL OR ADDITIONAL REASONS. THANK YOU.

Mileage: 66,000

Jul 7, 2017 Fire

WHILE MY DAUGHTER WAS DRIVING THE CAR LESS THAN 10 MINUTES FROM HOME AFTER JUST STARTING UP FOR THE MORNING IN JUNE 27, 2017 UNDER HOOD STARTED TO SMOKE, CAUGHT ON FIRE, AN EXPLOSION SOUND AND CAR BURNED UP . CAR HAD TO BE PUT OUT BY FIRE DEPARTMENT. TOTAL LOSS PER INSURANCE COMPANY . THIS CAR HAS A ENGINE FIRE RECALL AND I WAS TOLD RECALL WORK WAS DONE PRIOR TO SALE OF THE CAR TO ME BY FORD DEALER IN MAY 2017. HOWEVER I NOW FIND OUT THAT THE ACTUAL RECALL PART IS STILL NOT AVAILABLE FROM FORD AND THAT ONLY AN INSPECTION WAS DONE PRIOR TO SALE. NOT AN ACTUAL REPAIR. THE RECALL HAD TO DO WITH ENGINE FIRES ! MAYBE ALL THESE CARS NEED TO BE OF THE ROAD.

Mileage: 38,000

Jul 7, 2017

I HAVE AN ID# 10971972 THAT I GOT WHEN I CALLED NHTSA BACK IN APRIL, ALSO FILLED OUT A FORM & RETURNED TO WASHINGTON OFFICE IN JUNE THAT WAS MAILED TO ME BACK IN MAY - TOO MUCH TO EXPLAIN HERE, I WILL ATTACH A WORD DOC WITH DETAILED ISSUE INFO

Jul 5, 2017

WHILE PULLING OUT INTO TRAFFIC ON JULY 3, 2017, MOVING AT 30 MPH, THE ENGINE SUDDENLY LOST ALL POWER AND THE TRANSMISSION DOWNSHIFTED CAUSING THE CAR TO QUICKLY DECELERATE NEARLY CAUSING A REAR END COLLISION. THE ENGINE WARNING LIGHT INDICATED AN ENGINE FAULT REQUIRING IMMEDIATE SERVICE. THE ENGINE CONTINUED RUNNING BUT WITH HARDLY ANY ACCELERATION THEN LOSS OF POWER AND BUCKING. I PULLED TO SHOULDER AND WAS ABLE TO LIMP HOME ABOUT A MILE WITH ENGINE RUNNING ERRATICALLY ALL THE WAY. CALLED AAA AND HAD VEHICLE TOWED TO HAMMONASSET FORD IN MADISON CT FOR SERVICE ON JULY 4 2017. AWAITING RESPONSE FROM THEM AT THIS TIME.

Mileage: 41,000

Jun 29, 2017 Fire

TL* THE CONTACT OWNED A 2014 FORD ESCAPE. WHILE DRIVING APPROXIMATELY 55 MPH, FLAMES ERUPTED UNDERNEATH THE VEHICLE AND UNDER THE HOOD. THE VEHICLE WAS COASTED TO THE SIDE OF THE ROAD. THE DRIVER NOTICED FLAMES COMING FROM UNDER THE HOOD AND FROM THE ENGINE COMPARTMENT. THE FRONT OF THE VEHICLE BURST INTO FLAMES. THE FIRE DEPARTMENT EXTINGUISHED THE FIRE. A POLICE REPORT WAS FILED. THE VEHICLE WAS DESTROYED AND TOWED TO WATERFORD TOWING LOT. THE VIN WAS INCLUDED IN NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE MANUFACTURER AND THE DEALER WERE NOT MADE AWARE OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 65,000. THE VIN WAS NOT AVAILABLE. *LN *TR

Mileage: 65,000

Jun 8, 2017

"TAKATA RECALL"......I STOPPED BY 7-11 ATM TO GET SOME MONEY AND OTHER ITEMS...UPON RETURNING TO MY VEHICLE I NOTICED IT WOULD NOT START. THE DASHBOARD SAID IT WAS IN REVERSE EVEN THOUGH IT WAS IN PARK MODE. I SPEND APPROXIMATELY 3.5 HOURS ON THE PHONE WITH THE FORD MOTOR COMPANY TRYING TO GET SOME REAL HELP. AFTER NO SUCCESS, I WENT THRU THREE DIFFERENT CUSTOMER SERVICE REPS WHO WERE NOT KNOWLEDGEABLE ON HOW TO HANDLE A VEHICLE THAT WAS DISABLED, STUCK IN REVERSE AND WOULD NOT START. I ENDED UP CALLING AAA AND HAD IT TOWED TO MY OWN MECHANIC BECAUSE I CALLED THREE FORD DEALERSHIP STATED THAT IT WOULD BE AT LEAST 2-3 WEEKS BEFORE SOMEONE COULD CHECK OUT MY VEHICLE. IN ADDITION, THEY WERE NOT COOPERATIVE IN HELPING ME GET A RENTAL CAR EITHER AND STATED THEY WOULD NOT COVER THE COST OF RENTING A CAR. MY OWN MECHANIC WHO HAS SERVICED ALL MY VEHICLES AND THERE HAS NEVER BEEN AN ISSUE... ADVISED ME THAT THE BRAKE CABLE OR SOMETHING TO THAT EFFECT WAS BROKEN. I JUST DON'T UNDERSTAND HOW THAT IS POSSIBLE SINCE I JUST PURCHASED THE VEHICLE 10/2016. THIS IS THE SECOND TIME IN 9 MONTHS I'VE HAD ISSUES WITH FORD AND THEIR FAULTY PRODUCTS. APRIL 2017 FORD MOTORS SETTLED WITH ME OVER MY 2013 FORD FOCUS WHICH WAS IN AN OUT OF THE SHOP SINCE MARCH 2015. I'VE HAD TO GO THRU NUMEROUS AGENCIES TO GET ANY REAL HELP. I'VE SPOKEN WITH MY MECHANIC TODAY AND WAS GIVEN AN APPROX ESTIMATE OF $700 TO REPAIR AND MY CAR WON'T BE AVAILABLE UNTIL NEXT WEEK. IN ADDITION, IT'S COSTING $170 TO RENT A CAR TO GET BACK AND FORTH TO SCHOOL AND WORK UNTIL MONDAY. I AM LOOKING FOR FORD TO REIMBURSE ME FOR MY EXPENSES AND COST TO REPAIR MY VEHICLE. OR THE OTHER ALTERNATIVE IS TO BUY BACK THE VEHICLE. I WILL NEVER PURCHASE ANOTHER VEHICLE FROM FORD AGAIN.

Jun 6, 2017

TL* THE CONTACT'S HUSBAND OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE PART FOR THE REMEDY WAS UNAVAILABLE. WHILE THE CONTACT'S HUSBAND WAS AT A STOP, THE CONTACT NOTICED THAT COOLANT LEAKED ONTO THE GROUND. UPON INSPECTION, THE CONTACT NOTICED THAT RADIATOR FLUID WAS LEAKING AND THE RESERVOIR COOLANT CAP WAS CRACKED. THE VEHICLE WAS NOT TAKEN TO A DEALER OR DIAGNOSED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 19,000. UPDATED 08/24/17*LJ *CN

Mileage: 19,000

May 30, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBERS: 16V643000 (LATCHES/ LOCKS/LINKAGES) AND 17V209000 (ENGINE AND ENGINE COOLING); HOWEVER, THE PARTS FOR THE RECALL REPAIRS WERE UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIRS. THE MANUFACTURER WAS NOT MADE AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. PARTS DISTRIBUTION DISCONNECT AND VIN TOOL CONFIRMS PARTS NOT AVAILABLE. UPDATED 07/13/17*LJ *CN

May 27, 2017

MY CAR IS HAVING SAME EXACT ISSUES AS REPORTED IN RECALL #14S17 YET MY VIN IS NOT INCLUDED. MY VEHICLE IS CURRENTLY STILL IN GARAGE, GOING ON 2 WEEKS NOW, AND THEY JUST TOLD ME 6 OUR OF 7 PARTS ARE COVERED UNDER MY WARRANTY YET 1 PART, THE WIRING ASSEMBLY EC SENSOR IS NOT AND WILL BE $800 TO FIX. MY VEHICLE LITERALLY WOULD STALL WHILE DRIVING AND HAD SEVERE HESITATION AFTER I TURNED IT OFF AND BACK ON. HOW CAN MY VEHICLE IN THE SAME YEAR BE EXPERIENCING SAME ISSUES AS THE RECALL BUT NOT BE INCLUDED IN THE RECALL BECAUSE OF MY VIN # AND NOW I'M RESPONSIBLE FOR THE $800? WE WERE HEADED TO LITTLE WASHINGTON, PA AND THE WHOLE RIDE UP WAS A HESITATION EVERY ONCE IN A WHILE WHILE DRIVING DOWN THE ROAD. THEN AT ONE POINT THE CAR JUST STALLED WHILE DRIVING. TURNED OFF AND BACK ON AND AT A RED LIGHT INTERSECTION, HIT THE GAS TO GO AND WOULD NOT MOVE. TURNED OFF AND BACK ON AND TOOK AWHILE FOR THE CAR TO GO BUT THANKFULLY WE MADE IT HOME AND IMMEDIATELY CALLED FORD AND MADE APPT AT CLOSEST DEALER TO TAKE IT TO. 2 WEEKS LATER AND IT IS STILL THERE. THE JUST CALLED 3 DAYS AGO TO TELL BE ABOUT THE PARTS AND NOT COVERED. I THEN CALLED FORD BACK AND LEFT MY CELL PHONE # TO CONTACT ME BACK SINCE I WAS IN THE OFFICE THIS WEEK AND THEY CALLED AND LEFT A MESSAGE ON HOME PHONE EXPLAINING THAT PART WAS NOT COVERED UNDER WARRANTY. I AM NOT PLEASED AT ALL WITH THE DEALER FIRST OFF THAT TOOK SO LONG AND LACK OF COMMUNICATION OR FORD FOR JUST SAYING OH WELL SUCK IT UP AND PAY IT. I SEARCHED INTERNET AND SAW THIS RECALL THAT MATCHED MY CAR'S EXPERIENCES TO A "T".

Mileage: 55,300

May 27, 2017

FEBRUARY 2017, VEHICLE IN MOTION, 50 MPH & SUDDENLY ALARM/ENGINE LIGHT & TEMP GAUGE WENT CRAZY, VEHICLE STALLS OUT FROM OVERHEATING IN LEFT LANE OF 2 LN HWY. ABLE TO CRUISE TO SHOULDER. KNEW IT WAS AN ISSUE W/ RADIATOR OR COOLANT FROM THE SMELL & WARNING ON DASH. IN CLOSE PROXIMITY OF STORE WHERE FRIEND WORKS SO WAITED 45 MIN TO COOL& VEHICLE DID START. ABLE TO NURSE IT OVER TO THE PARKING LOT THAT WAS 5MIN AWAY, ENG LIGHT STAYED ON. TIME OF INCIDENT WAS 8:00 PM VIEWING ENGINE UNDER BETTER LIGHT,COOLANT WAS CRITICALLY LOW.PURCHASED COOLANT FROM STORE WHERE REFILLED RESERVOIR, WAITED UNTIL HE WAS OFF WORK, 9:20 PM, SO CAN FOLLOW ME HOME IN CASE I NEED MORE ASSISTANCE. ARRIVE AT MY HOME WITHOUT INCIDENT, ENGINE LIGHT ON. IN FOLLOWING DAYS, I MONITOR COOLANT FOR 2 WEEKS& FIGURE ITS AN ISOLATED INCIDENT. ENGINE LT REMAINS ON FOR 7 DAYS. AFTER 3WKS, NEED TO TOP OFF COOLANT AS IT DROPS UNDER FILL LINE. I PURCHASED THIS VEHICLE @19KMI & TIME OF INCIDENT HAD 35K MILES. FEELING IT IS A BIT UNUSUAL TO HAVE THESE ISSUES AT SUCH LOW MILEAGE BUT IM NO EXPERT,FIGURED SOMETHING THAT NEEDS TO BE MONITORED REG AS THE TEMP GAUGE READS NORMAL/NO ENGINE/WARNING LIGHT HAS BEEN ON SINCE. I RECEIVED IN APRIL-SAFETY RECALL17S09/17V-209. I READ THAT REPAIR NOT AVAILABLE UNTIL LATE 2017& I WILL BE NOTIFIED BY FORD WHEN TO SCHED.SERVICE APPT FOR COOLING SYS.UPGRADE. HAVE NOT RCVD ANY FURTHER NOTICE & HAVE HAD TO TOP OFF THE COOLANT ONCE AGAIN.LETTER STATES TO "MAINTAIN PROPER COOLANT LEVEL TO REDUCE RISK OF OVERHEATING THAT CAN LEAD TO A FIRE" AM I REDUCING RISK ONLY? NOT ELIMINATING THIS RISK? IDID SOME RESEARCH, LEADING ME TO THIS COMPLAINT. I'M FINANCING THIS VEHICLE FOR $380/MTH & VERY UNHAPPY WITH THIS SITUATION & AM NOT SURE OF MY OPTIONS IF THERE IS NO RESOLUTION YET. I DO NOT WANT TO BREAK DOWN IN TRAFFIC AGAIN IF THERE IS A RISK OF REPEATING THE INITIAL INCIDENT, OR WORSE.

Mileage: 35,000

May 17, 2017

"TAKATA RECALL" EVEN THOUGH I NO LONGER HAVE THE CAR, HAD THEM REPOSSESSED IT. I MADE VERY CLEAR WHEN BUYING I WANTED A CAR I WOULD HAVE NO PROBLEMS WITH. I HAH JUST FILLED MY TANK WITH GAS ON MY WAY TO SEE MY PAIN MED DOCTOR 80 MILES AWAY FUEL SYSTEM QUIT, AT STATION, THIS IS AN IN CLOSED SYSTEM NOT SUPPOSED TO GO OUT BECAUSE MY CAR WAS STILL IN SHOP I MISSED ANOTHER APPOINTMENT WITH THIS DR. WHICH RESULTED IN ME BEING PUT INTO WITHDRAWALS FROM MEDICATION, HAD I DRIVEN THERE ANY SYSTEM HAD GONE OUT I WOULD HAVE LOST CONTROL ON HIGHWAY 287 TOWARDS WICHITA FALLS TX WHICH IS EXTREMELY HEAVY TRAFFIC. TWO TIMES MY LIFE WAS PLACED IN DANGER BECAUSE OF A RECALL I WAS NOT INFORMED OF. NOW FORD WHAT'S ME TO PAY FOR WHAT THEY DIDN'T GET FROM AUCTION I'M NOT PAYING FOR A CAR THAT NEARLY GOT ME KILLED TWICE AND I DON'T THINK THEY SHOULD PUT THIS AGAINST MY CREDIT. I'M CONSIDERING SUING AS THEY COST ME MY DOCTOR, THROUGH ME INTO WITHDRAWALS WHICH AT THE TIME WAS LIFE THREATENING BECAUSE OF HEALTH, AND POSSIBLY LOSING CONTROL ON HIGHWAY AT 70 MILES WHICH COULD HAVE COST ME MY LIFE, NOW THERE IS ANOTHER RECALL ABOUT ENGINE FIRES. STATIONARY FAILURE WITH FAR REACHING CONSEQUENCES.

May 17, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT THE VEHICLE EXPERIENCED A COOLANT LEAK. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 17V209000(ENGINE AND ENGINE COOLING); HOWEVER, THE PARTS TO DO THE REPAIR WERE UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE DEALER CONFIRMED THAT THE PARTS WERE NOT AVAILABLE FOR THE RECALL REMEDY UNTIL OCTOBER. THE MANUFACTURER WAS NOT MADE AWARE OF THE ISSUE AND WAS NOT ABLE TO CONFIRM WHEN THE PARTS WOULD BE AVAILABLE. THE FAILURE MILEAGE WAS APPROXIMATELY 30,600. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.

Mileage: 30,600

May 16, 2017

ROUGHLY FOUR WEEKS AGO, I RECEIVED AN ALERT THAT MY CAR WAS OVERHEATING WHEN I WAS PARKED. I TOOK MY CAR IN TO FORD AND THEY TOLD ME THAT I NEED A NEW RESERVE BOTTLE AND CHARGED ME NEARLY $300. AT THIS POINT, THEY INSPECTED MY COOLANT SYSTEM AND TOPPED OFF MY COOLANT WHICH WAS LOW. TWO WEEKS LATER, I WAS GETTING ON THE FREEWAY AND I RECEIVED A SEVERE WARNING FOR OVER HEATING. MY CAR STARTED SHAKING AND AN ALARM WAS GOING OFF. I PULLED OFF THE FREEWAY TO OBSERVE THAT MY COOLANT BOTTLE WAS COMPLETELY EMPTY. I HAD MY CAR IN THE SHOP FOR NEARLY A WEEK BEFORE THEY DISCOVERED NOW THAT I NEED A NEW COOLANT BYPASS VALVE. I BELIEVE THAT FORD NEEDS TO EXPAND THEIR RECALL (17S09) TO INCLUDE THE ACTUAL ISSUE OF WHAT IS CAUSING THE LOCALIZED OVERHEATING, WHICH IS A LACK OF COOLANT FLOWING THROUGH THE ENGINE LEADING TO A CRACK IN THE CYLINDER HEAD. I HAVE TO SPEND NEARLY $900 TO FIX THIS PART ON A CAR BUILT IN 2014. FORD'S SOLUTION TO FIXING THE POSSIBLE CRACKED CYLINDER HEAD IS NOT TO ADDRESS THE ISSUE OF WHY THE COOLANT IS LEAKING, BUT TO INSTALL A SENSOR TO THEN MAKE OWNERS HAVE TO CONSTANTLY CHECK THEIR COOLANT SYSTEM. THIS IS NOT A FAIR SOLUTION TO THEIR PROBLEM. I DO NOT BELIEVE IT IS RIGHT TO MAKE OWNERS HAVE TO PAY FOR THE FAULTY COOLANT SYSTEM. THIS IS UNSAFE. MOST AVERAGE CONSUMERS ARE NOT MECHANICS AND WE SHOULD NOT BE SADDLED WITH HAVING TO CONSTANTLY MONITOR OUR COOLANT LEVELS BECAUSE FORD DEVELOPED A FAULTY COOLANT SYSTEM THAT COULD LEAD TO CYLINDER CRACKS THAT CAUSE ENGINE FIRES. I HAVE SPOKEN TO FORD CONSUMER RELATIONS AND THEY WERE NO HELP AT ALL. THEY COULD NOT EVEN EXPLAIN TO ME WHAT ITEMS THEY WOULD REIMBURSE FOR IN REGARD TO THIS RECALL. EVEN THOUGH THE RECALL LETTER STATES THEY WILL REIMBURSE FOR PREVIOUSLY PAID FOR COOLANT LEAK OR OVERHEATING REPAIR, THEY REFUSE TO ASSIST ME OR REIMBURSE ME FOR MY COOLANT AND OVERHEATING REPAIR. THIS IS NOT FAIR.

Mileage: 90,000

May 15, 2017

THE ENGINE OVERHEATING WARNING LIGHT CAME ON ABOUT TWO MILES DOWN THE ROAD WITH MODERATE DRIVING. PULLED OVER AND CHECKED THE COOLANT LEVEL AND IT IS LOW. ONE MONTH AGO, THE COOLANT LEVEL WAS CHECKED, IT WAS LOW AND IT WAS TOPPED OFF. THE COOLANT LEVEL SHOULD NOT GO DOWN IN ONE MONTH OF MODERATE DRIVING. ALSO, LOOKING UP INFO ON THE 2014 FORD ESCAPE, THERE IS A HISTORY OF COOLANT AND OVERHEATING ISSUES. THERE IS A DANGER OF FIRE OR THE ENGINE BLOCK CRACKING. FORD'S ANSWER WAS TO INSTALL A DETECTOR TO TELL CAR OWNER'S WHEN THE COOLANT LEVEL IS LOW. THIS IS UNACCEPTABLE. PLEASE DO SOMETHING.

Mileage: 67,000

May 15, 2017 Fire

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING VARIOUS SPEEDS, THE VEHICLE WOULD NOT ACCELERATE ABOVE 5 MPH AND THE RPMS MALFUNCTIONED BY INCREASING AND DECREASING RAPIDLY. THE CONTACT STATED THAT HEAVY WHITISH, BLUE SMOKE EMITTED FROM THE EXHAUST. THE CONTACT STATED THAT THE VEHICLE OVERHEATED ON FOUR OCCASIONS. IN ADDITION, THE CONTACT STATED THAT THERE WAS A RECALL INITIATED PER NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING) FOR THE EXACT SAME FAILURE, BUT THE VIN WAS NOT INCLUDED. THE VEHICLE WAS REPAIRED, BUT THE FAILURE RECURRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 54,000.

Mileage: 54,000

May 15, 2017 Fire

TL* THE CONTACT OWNED A 2014 FORD ESCAPE. WHILE DRIVING 55 MPH, THE VEHICLE LOST POWER AND THE STEERING WHEEL SEIZED. THE CONTACT COASTED THE VEHICLE TO THE SIDE OF THE ROAD AND NOTICED SMOKE UNDER THE HOOD. THE VEHICLE BURST INTO FLAMES AND THE CHECK ENGINE AND BATTERY WARNING INDICATORS ILLUMINATED. THE FIRE DEPARTMENT EXTINGUISHED THE FIRE AND A FIRE REPORT WAS FILED. THE VEHICLE WAS TOWED TO A TOWING LOT AND WAS DESTROYED. THE MANUFACTURER ADVISED THE CONTACT TO CALL HER INSURANCE COMPANY AND DID NOT OFFER FURTHER ASSISTANCE. THE APPROXIMATE FAILURE MILEAGE WAS 25,000.

Mileage: 25,000

May 11, 2017 Fire

TRAVELING AT HIGHWAY SPEED, THE ENGINE LOST POWER. PULLED OVER TO THE SIDE OF THE ROAD AND DISCOVERED THAT THE AIR CLEANER WAS ON FIRE. THE FIRE HAD BEEN BURNING LONG ENOUGH FOR PLASTIC TO BE INGESTED INTO THE COMBUSTION CHAMBERS. THERE WAS NO SERIOUS INVESTIGATION UNDERTAKEN AND THE CAUSE OF THE FIRE REMAINS UNKNOWN. ADDITIONALLY, FORD MOTOR COMPANY REFUSED TO FIX THE ENGINE UNDER THE TERMS OF THEIR WARRANTY.

Mileage: 43,000

May 11, 2017 Fire

RECEIVED RECALL 17S09 ONE WEEK STATING LOSS OF COOLANT COULD CAUSE CYLINDER HEAD TO CRACK AND OIL TO LEAK OUT ONTO EXHAUST MANIFOLD AND CATCH FIRE. THE VERY NEXT WEEK WHILE DRIVING ON A COUNTRY ROAD MY ESCAPE CAUGHT FIRE WHILE DRIVING. I WAS LUCKY TO HAVE DRINKS IN THE CAR TO BE ABLE TO GET THE FIRE OUT BEFORE THE FIRE DEPARTMENT GOT THERE. TOWED VEHICLE TO FORD SHOP AND CONTACTED FORD CUSTOMER CARE KNOWING THAT THEY ARE AWARE OF THIS PROBLEM AND THEY WILL NOT ASSIST ME IN REPAIRING VEHICLE. THE RECALL BASICALLY ONLY STATES ADDING A LOW COOLANT SENSOR WHICH IN REALLY WILL NOT HELP BECAUSE IF IT BECOMES LOW ON COOLANT THE HEAD IS ALREADY CRACKED AND DAMAGE IS ALREADY DONE. FURTHER MORE FORD KNOWING THEY HAVE THIS PROBLEM DOESN'T EVEN HAVE PARTS AVAILABLE UNTIL AT THE EARLIEST FALL OF 2017 SO MORE PEOPLE WILL BE HAVING CAR FIRES AND MAY NOT BE AS LUCKY AS I WAS TO WRITE THIS REPORT.

Mileage: 111,000

May 1, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBERS: 16V643000 (LATCHES/LOCKS/LINKAGES) AND 17V209000 (ENGINE AND ENGINE COOLING). THE PARTS TO DO THE REPAIR WERE UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIRS. THE DEALER STATED THAT THE PARTS WERE NOT AVAILABLE FOR THE RECALL REMEDY. THE MANUFACTURER WAS NOT MADE AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. VIN TOOL CONFIRMS PARTS NOT AVAILABLE. UPDATED 06/21/17*LJ UPDATED 10/19/2017*JS

Apr 28, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBERS: 17V209000 (ENGINE) AND 16V643000 (LATCHES/LOCKS/LINKAGES:DOORS:LATCH). THE PARTS TO DO THE REPAIR WERE UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER STATED THAT PARTS WOULD NOT BE AVAILABLE FOR NHTSA CAMPAIGN NUMBER: 17V209000 UNTIL OCTOBER. THE CONTACT WAS PLACED ON A WAITING LIST FOR NHTSA CAMPAIGN NUMBER 16V643000. THE CONTACT HAD NOT EXPERIENCED A FAILURE. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.

Apr 11, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE THE CONTACT WAS FILLING THE RESERVES, THE ANTI-FREEZE LEAKED OUT. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE WATER PUMP NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 60,000. UPDATED 06/01/17*LJ *CN

Mileage: 60,000

Apr 6, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING BETWEEN 60-65 MPH, THE CHECK ENGINE WARNING INDICATOR ILLUMINATED. THE VEHICLE WAS TAKEN TO THE DEALER TO BE DIAGNOSED. THE CONTACT WAS INFORMED THAT THERE WAS A FRACTURE TO THE ENGINE BLOCK, WHICH CAUSED THE ENGINE TO OVERHEAT, MISFIRE, AND OIL TO LEAK. THE CONTACT WAS ALSO INFORMED THAT THE ENGINE NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 17V209000 (ENGINE AND ENGINE COOLING). THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 68,000.

Mileage: 68,000

Apr 1, 2017 Fire

DECEMBER 3 2016 I WAS DRIVING DOWN THE ROAD ON HWY 111 AND THE ENGINE SHUT DOWN. I COASTED OVER TO THE SHOULDER OF THE ROAD AND PUT THE VEHICLE IN PARK. THE INSTRUMENT PANEL DISPLAYED ENGINE FAILURE, IMMEDIATE ATTENTION REQUIRED. SMOKE WAS COMING FROM UNDER THE HOOD. I GOT OUT OF THE VEHICLE AND RAISED THE HOOD AND FLAMES STARTED COMING FROM THE ENGINE AREA AND SPREAD VERY QUICKLY. I CALLED 911 TO PUT THE FIRE OUT. CAUSE OF FIRE IS UNKNOWN. A POLICE REPORT WAS FILLED OUT BUT I DON'T HAVE IT AT THIS TIME.

Mileage: 36,000

Mar 19, 2017 Fire

WAS DRIVING HOME FROM WORK ON THE INTERSTATE. ENGINE BEGAN TO JERK A BIT THEN WARNING MESSAGES APPEARED ON SCREEN. PULLED OVER TO SIDE OF ROAD. AFTER CAR STOPPED SMOKE BEGAN TO APPEAR FROM UNDER HOOD AND ENTERING CAB THROUGH THE VENTS. I OPENED THE WINDOW TO CLEAR THE SMOKE AND LOOKED FOR PHONE NUMBER TO ROADSIDE ASSISTANCE THINKING IT WAS ONLY A BELT THAT HAD MELTED OR BURNED. WITHIN A FEW MINUTES I BEGAN TO SEE FLAMES COMING FROM UNDER THE HOOD BY THE WINDSHIELD. I EXITED THE VEHICLE AND A SHERIFF'S DEPUTY HAPPENED TO BE PULLING IN BEHIND ME AFTER SEEING MY CAR IN DISTRESS. FIRE DEPARTMENT WAS CALLED. WITHIN FIVE TO TEN MINUTES THE ENGINE AREA OF THE VEHICLE WAS ENGULFED IN FLAMES. AFTER A SHORT INVESTIGATION ON THE SCENE THE FD BELIEVED THE CAUSE TO BE ELECTRICAL AND APPEARED TO HAVE BEGUN AND CAUSED THE MOST DAMAGE TO THE PASSENGER SIDE FRONT CORNER OF THE ENGINE.

Mileage: 68,800

Mar 8, 2017

ON MANY DIFFERENT TIMES MY CAR OVER HEATS. I IMMEDIATELY HAVE TO PARK N WAIT A WHILE FOR IT TO COOL DOWN.

Mileage: 1

Feb 23, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 25 MPH, A HISSING NOISE WAS DETECTED AND THE ENGINE STALLED. THE FAILURE RECURRED NUMEROUS TIMES. THE VEHICLE WAS TAKEN TO A DEALER WHERE THE FAILURE COULD NOT BE DETERMINED. THE VEHICLE WAS NOT REPAIRED. THE CONTACT ALSO SMELLED A HORRIBLE ODOR INSIDE THE VEHICLE WHEN THE FAILURE OCCURRED. THE CONTACT MENTIONED THAT THE FAILURE OCCURRED AFTER FUELING THE VEHICLE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE VIN WAS INVALID. THE FAILURE MILEAGE WAS APPROXIMATELY 49,000.

Mileage: 49,000

Feb 13, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT THERE WAS AN ABNORMAL ODOR EMITTING FROM THE AIR VENTS OF THE VEHICLE. EXHAUST FUMES ALSO ENTERED THE CABIN OF THE VEHICLE. THE DEALER WAS UNABLE TO DUPLICATE THE ODOR. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE ISSUE. THE APPROXIMATE FAILURE MILEAGE WAS 48,400. UPDATED 07/19/17*LJ *CN

Mileage: 48,400

Jan 26, 2017

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING VARIOUS SPEEDS, THE VEHICLE STALLED WITHOUT WARNING. THE VEHICLE WAS TAKEN TO THE DEALER, BUT WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 35,967.

Mileage: 35,967

Nov 28, 2016

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THAT THE VEHICLE EXPERIENCED A LOSS ENGINE POWER WHILE BEING OPERATED AT ANY SPEED. THE CHECK ENGINE AND SERVICE ENGINE SOON WARNING INDICATORS ILLUMINATED. THE VEHICLE WAS TAKEN TO THE DEALER WHERE IT WAS DIAGNOSED THAT THE VEHICLE NEEDED A TERMINAL KIT AND GROUND WIRING INSTALLED. THE VEHICLE WAS REPAIRED, BUT THE FAILURE RECURRED. THE VEHICLE WAS TAKEN TO THE DEALER APPROXIMATELY 6-8 TIMES. THE CONTACT REFERENCED NHTSA CAMPAIGN NUMBER: 14V495000 (ELECTRICAL SYSTEM), BUT THE VIN WAS NOT INCLUDED. THE MANUFACTURER WAS NOTIFIED. THE FAILURE MILEAGE WAS APPROXIMATELY 8,764.

Mileage: 8,764

Nov 21, 2016 Fire

FORD - 2014 FORD ESCAPE (BUILT IN 2013). THE CAR WAS PARKED IN THE PARKING LOT, TURNED OFF AND AN HOUR AND A HALF LATER I WAS NOTIFIED IT WAS ON FIRE. THE FIRE STARTED UNDER THE HOOD AND ACCORDING TO THE FIRE MARSHAL THE HEAVIEST DAMAGE WAS LOCATED NEAR THE AIR FILTER AND BATTERY. ENGINE COMPARTMENT WAS HEAVILY DAMAGED.

Mileage: 38,000

Nov 11, 2016

I DROVE 25 MILES IN TRAFFIC TO PICK UP MY KIDS FROM DAYCARE. WHEN I GOT THE KIDS IN THE CAR TO GO HOME AND THE CAR WAS IN MOTION TURNING LEFT ONTO A BUSY HIGHWAY TURN/MERGE LANE, ALL OF A SUDDEN MY CHECK ENGINE LIGHT CAME ON AND ENGINE TEMPERATURE GAUGE WENT ALL THE WAY UP. I PULLED OVER AND CHECKED MY COOLANT. THERE WAS SO MUCH PRESSURE WHEN I TURNED THE LID, I THOUGHT THE COOLANT TANK WAS GOING TO EXPLODE. THE TEMPERATURE IN MY CAR WENT DOWN AND I WAS ABLE TO MAKE IT TO A MECHANIC CLOSE BY. THEY SAID I NEEDED A NEW COOLANT BYPASS SOLENOID. IT WAS REPLACED AND THE CAR HAS SEEMED FINE. NOW, 1 MONTH LATER, IT IS LEAKING COOLANT. I READ ABOUT A RECALL FOR THE SAME THING WHERE CARS CAUGHT FIRE BUT MY MODEL YEAR IS NOT COVERED UNDER THE OLD RECALL. I BELIEVE FORD NEEDS TO EXPAND THE RECALL AS I DO NOT FEEL SAFE DRIVING THIS VEHICLE WITH MY TWO SMALL CHILDREN AND THE POSSIBILITY OF IT CATCHING ON FIRE! I HAVE 78000 MILES ON THE CAR AND WAS PURCHASED 7/28/2013.

Mileage: 77,000

Oct 17, 2016

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 10 MPH, THE VEHICLE STALLED WITHOUT WARNING. IN ADDITION, THE HOOD UNLATCHED INDEPENDENTLY AND FRACTURED THE WINDSHIELD OF THE VEHICLE. THE VEHICLE WAS REPAIRED, BUT THE FAILURE RECURRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 73,000.

Mileage: 73,000

Oct 6, 2016

MY MOTHER OWNS A 2014 FORD ESCAPE WITH THE 1.6L TURBOCHARGED ECOBOOST ENGINE. SHE NOTES THAT THE FUEL SENSORS IN THE CAR AREN'T INJECTING FUEL INTO THE ENGINE WHEN SHE ACCELERATES FROM A STOP, MEANING THE CAR WILL STICK IN NEUTRAL AND REV UNTIL IT KICKS BACK IN GEAR. SHE NOTES THAT THIS HAS HAPPENED MULTIPLE TIMES. WE HAD TAKEN IT TO KELLER BROS. FORD WHICH IS WHERE SHE PURCHASED IT, AND THEY COULDN'T COME UP WITH THE PROBLEM. SO THEN WE WENT TO NEW HOLLAND FORD, AND THEY WERE ABLE TO FIND THE PROBLEM. THE GUY EVEN SHOWED MY MOM HOW TO RESET THE FUEL SENSOR. BUT THE PROBLEM CAME BACK UP AGAIN. MY MOM, I, AND HER BOYFRIEND ARE AT THE POINT WHERE IF SOMETIME THE CAR HESITATES, AND SOMEONE HITS HER, SHE'S GOING TO BE KILLED. FORD, YOU NEED TO DO SOMETHING ABOUT THIS. I DON'T WANT MY MOTHER KILLED. SO RECALL THE ESCAPE 1.6L'S THAT HAVE THE PROBLEM AND COME UP WITH A SOLUTION.

Mileage: 24,000

Oct 3, 2016

THIS HAPPENED TWICE IN LESS THAN A MONTH. DRIVING THE FORD ESCAPE AT LOWER SPEEDS (LESS THAN 40 MPH) ON A CITY STREET DURING MORNING TRAFFIC HOURS. SUDDENLY HEARD A CONTINUOUS LOUD SOUND ON THE REAR RIGHT OF CAR. VEHICLE THEN LOST POWER. ENGINE SHUT DOWN. HAD TO PULL TO THE SHOULDER AND RESTART THE CAR. THEN IT WORKED FINE. THE DEALER COULD NOT FIND ANY ERROR CODES WHEN I TOOK IN FOR SERVICE. THE AIR CONDITIONER WAS ON. OUTSIDE TEMPERATURE WAS AROUND 70F. NOT RAINING.

Mileage: 38,500

Jun 24, 2016

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 10 MPH, THE CHECK ENGINE WARNING LIGHT ILLUMINATED AND THE ENGINE STARTED TO HESITATE. THE FAILURE RECURRED INTERMITTENTLY. THE VEHICLE WAS NOT DIAGNOSED NOR REPAIRED. THE VIN WAS EXCLUDED FROM NHTSA CAMPAIGN NUMBER: 14V495000 (ELECTRICAL SYSTEM). THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 32,300.

Mileage: 32,300

May 24, 2016

MY ESCAPE SUFFERED A CATASTROPHIC ENGINE FAILURE WHILE DRIVING. THE ENGINE FAILURE WHILE DRIVING ON AN INTERSTATE PRESENTS A CLEAR AND POTENTIAL LIFE THREATENING EVENT AS ALL POWER WAS SUDDENLY LOST. AT THE TIME OF ENGINE FAILURE I WAS TRAVELING AT ABOUT 35 MPH. THE VEHICLE WAS TOWED TO A LOCAL DEALERSHIP FOR REPAIRS. THE DEALERSHIP TOLD ME THAT THE ENGINE FAILURE WAS DUE TO THE AC COMPRESSOR LOCKING UP CREATING TENSION ON THE DRIVE BELTS THAT RESULTED IN SUDDEN LOSS OF POWER AND ENGINE SHUT DOWN. HAD THIS OCCURRED ON A MAJOR INTERSTATE HIGHWAY WITH SEMI TRUCKS BARRELING UPON YOU, THE RESULTS WOULD HAVE BEEN DEADLY. FORTUNATELY FOR ME THE FAILURE OCCURRED 1/2 MILE BEFORE ENTERING THE INTERSTATE. I HAVE SINCE LEARNED OTHER OWERS OF FORD PRODUCTS HAVE EXPERIENCED THE SAME THING. THIS IS A SERIOUS DESIGN FLAW THAT NEEDS TO BE FIXED IN THE INTEREST OF PUBLIC SAFETY. I PURCHASED THIS VEHICLE NEW AND IT CURRENTLY HAS LESS THAN 13,800 MILES ON THE ODOMETER.

Mileage: 13,664

Apr 7, 2016

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 50 MPH, THE VEHICLE STALLED AND THE CHECK ENGINE WARNING LIGHT ILLUMINATED INTERMITTENTLY. THE VEHICLE WAS RESTARTED AND TOWED TO THE DEALER WHERE IT WAS DIAGNOSED THAT THE WIRING HARNESS HAD A BAD CONNECTION. THE VEHICLE WAS REPAIRED AND THE TURBO CHARGE BOOST SENSOR AND AIR SENSOR WERE REPLACED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 46,000. THE VIN WAS UNAVAILABLE. UPDATED 05/20/16*LJ

Mileage: 46,000

Feb 19, 2016

JUST PURCHASED A CERTIFIED PRE-OWNED 2014 FORD ESCAPE SE. A YELLOW CHECK ENGINE LIGHT APPEAR. TROUBLE CODE P26B7 (DEALER SPECIFIC). IT LOOKS LIKE THERE HAVE BEEN NUMEROUS ISSUES WITH THE BYPASS COOLANT SOLENOID OR COOLANT LEAKS. ALSO, STEERING WHEEL CONTROLS ONLY OCCASIONALLY WORK.

Mileage: 62,600

Feb 2, 2016

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. THE CONTACT STATED THE VEHICLE WOULD STALL AFTER IDLING. THE CONTACT HAD TO WAIT THREE MINUTES THEN THE VEHICLE WOULD START NORMALLY. THE VEHICLE WAS DRIVEN TO THE DEALER AND THEY COULD NOT DUPLICATE THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 28,000.

Mileage: 28,000

Dec 23, 2015

A FEW MONTHS AGO, I HAD FILED A COMPLAINT ON THE 2014 FORD ESCAPE SE 1.6L TURBOCHARGED ECOBOOST WITH I-4WD MY MOTHER CURRENTLY OWNS. SHE HAD ACCELERATION PROBLEMS WITH THE CAR. AT A STOPLIGHT OR WHLE MOVING AT A DECENT PACE (ABOUT 20-40MPH), THE ENGINE WOULD SUDDENLY REV TOWARDS 4000-5000 AND NOT DROP INTO DRIVE. THIS HAD CONCERNED ME ALOT. MOM CALLED KELLER BROS. FORD HERE IN LITITZ, PENNSYLVANIA, AND SAID THAT SHE WILL HAVE TO TAKE HER CAR DOWN FOR A SOFTWARE UPDATE. THE UPDATE FIXED EVERYTHING. NO ACCELERATION PROBLEMS. AND SINCE THIS SOFTWARE UPDATE, I'VE NOTICED A HUGE DIFFERENCE. IT FEELS LIKE THERE IS MORE HORSES IN MY MOM'S CAR THAN THERE WAS BEFORE THE UPDATE. THE UPDATE HAPPENED 4-6 MONTHS AGO. I FEEL MUCH SAFER KNOWING THAT HER CAR WON'T END HER IN AN ACCIDENT. SHE CURRENTLY HAS OVER 16,000 MILES, AND SINCE THAT TIME FRAME, NO "DROP-OUTS" (< AS I CALL THEM) HAVE HAPPENED.

Mileage: 10,000

Dec 17, 2015

CAR STALLS. POWER TO ENGINE STOPS. ENGINE FAULT LIGHT COMES ON. HAVE TO PULL OVER TURN ENGINE OFF AND RESTART. THIS HAS HAPPENED ON HIWAY AT SPEED OF 75 AND ON ROAD SITTING AT LIGHT.

Mileage: 41,000

Nov 9, 2015

I EXPERIENCED ON THREE OCCASIONS THAT THIS VEHICLE MISFIRES, STUMBLES, SHUDDERS AND ALMOST SHUTS OFF UNDER HEAVY ACCELERATION WHILE ATTEMPTING TO MERGE ONTO A HIGHWAY.THE LAST TIME THIS PROBLEM OCCURRED I WAS FORCED TO PULL ONTO THE BREAKDOWN LANE AND ALMOST CAUSED AN ACCIDENT DUE TO HIGHWAY TRAFFIC TRAVELING AT 70 MPH AND MY INABILITY TO ATTAIN A SUITABLE MERGING SPEED. I HAVE FURTHER OBSERVED THAT THIS SITUATION HAS ONLY OCCURRED AND COULD BE REPLICATED DURING RAIN AND HIGH HUMIDITY. THIS PROBLEM IS A DEFINITE SAFETY HAZARD THAT NEEDS TO BE ADDRESSED!

Mileage: 10,500

Nov 3, 2015

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING 10 MPH, THE VEHICLE LOST POWER DUE TO AN ELECTRICAL FAILURE. THE VEHICLE WAS TAKEN TO A DEALER TO BE REPAIRED WHERE IT WAS DIAGNOSED THAT THE BCM CONNECTOR WAS DISCONNECTED. THE MANUFACTURER WAS MADE AWARE OF THE ISSUE. THE FAILURE MILEAGE WAS 22,000.

Oct 23, 2015

THE CAR IS BUCKING AND ALMOST STALLING WHEN I ACCELERATE. I'VE TAKEN IT TO TWO DIFFERENT DEALERS AND THEY CAN'T FIND ANYTHING. ONE DEALER TOLD ME THAT THIS WAS NORMAL, EVEN THOUGH I FOUND SIMILAR COMPLAINTS ONLINE.

Mileage: 60,000

Oct 21, 2015

IN MARCH 2015 CAR KEPT STALLING WHILE DRIVING AND WHILE STOPPED. BROUGHT TO DEALER WHO DIAGNOSED AS A PROBLEM WITH FUEL PUMP. AFTER A MONTH I GOT THE CAR BACK WITH REPLACED FUEL PUMP. AFTER THE FIX, CAR WOULD OFTEN HESITATE, SPUTTER AND SHAKE LIKE IT WAS ABOUT TO STALL. IN SEPTEMBER CAR KEPT STALLING ON START UP. BROUGHT TO DEALER WHO SAID CAR WAS "FINE" AND OPERATING AS DESIGNED. THEY COULDN'T DUPLICATE PROBLEM. CAR CONTINUES TO HESITATE, SPUTTER AND SHAKE. AGAIN YESTERDAY CAR STALLED OUT 3 TIMES AT START UP. DON'T FEEL SAFE DRIVING IT.

Mileage: 20,455

Jul 6, 2015

USES TO MUCH GAS,GAUGES ON DASH GO UP AND DOWN TO MUCH, EX, IT SAYS 150 MILES TIL E GO 8 MILES IT SAYS 126. PARK IT SAYS 163 MILES TO E , START CAR BACK UP IT SAYS 187 MILES TIL E. IT IS NEVER THE SAME. DEALER SAYS THEY REPLACED GAUGES BUT IT STILL DOING IT. I PUT 11GALLONS OF GAS IN IT WILL SAY 287 MILES TIL E GO 60 MILES IT SAYS 164 MILES TIL E GAS GAUGE GOES FROM FULL TO 1/2 TANK WHICH MEANS IT TOOK 7 GALLONS TO GO 60 MILES WHICH MEANS 8.5 MILES TO A GALLON.

Jun 20, 2015

"ENGINE FAULT SERVICE NOW LIGHT" CAME ON TWICE WITH "HILL START ASSIST NOT AVAILABLE" BOTH TIMES. AFTER STOPPING AT TRAFFIC LIGHT AND STEPPING ON GAS PEDAL, CAR WOULD NOT MOVE AND GAVE NO INDICATION IT HAD STALLED. ALL NORMAL LIGHTS WERE ON. I PUT CAR IN "PARK" AND RESTARTED. THIS HAS HAPPENED TWICE ON HILLS AND HAS DIED ON ME FOUR TIMES.

Mileage: 5,753

May 28, 2015

I WAS DRIVING ON THE HIGHWAY WHEN THE "ENGINE FAULT SERVICE NOW" WARNING LIGHT CAME ON. MY CAR THEN LOST POWER AND WENT INTO A "LIMP HOME" MODE. ONCE I SAFELY ARRIVED AT MY DESTINATION I TURNED OFF THE VEHICLE. ONCE IT WAS TURNED BACK ON, IT WAS FINE. I TOOK THIS INTO THE DEALERSHIP. THEY REPAIRED A RECALL AND ORDERED PARTS. IT TOOK A FEW DAYS FOR THE PARTS TO GET IN. DURING THAT TIME EVERY TIME I DROVE ON THE HIGHWAY THE CAR STARTED MAKING A KNOCKING NOISE AND THEN THE LIGHT WOULD COME BACK ON AND THE VEHICLE WOULD GO BACK INTO THAT LIMP HOME MODE. I WAS ALMOST REAR ENDED BY SEMIS AND OTHER VEHICLES AT FAST RATES OF SPEED DUE TO THIS ISSUE. I TOOK THE VEHICLE BACK IN FOR THEM TO INSTALL THE ORDERED PARTS. WHEN I GOT MY CAR BACK THE ISSUE CONTINUED, AND NOW MY CAR IS IN THE SHOP FOR THE 4TH TIME. THEY ARE WORKING WITH FORD ENGINEERS AND THEY ARE NOT HAVING LUCK FINDING THE ISSUE. I HAVE READ OF OTHER INDIVIDUALS HAVING THIS SAME ISSUE. IS IT GOING TO TAKE A FATALITY BEFORE SOMETHING IS DONE? I HAVE AN 8 MONTH OLD BABY, AND I BOUGHT A NEW CAR FOR SAFETY AND SECURITY - I DO NOT HAVE EITHER AT THIS TIME.

Mileage: 16,700

May 22, 2015

MOST RECENT AND TROUBLING INCIDENT WAS TRAVELLING DOWNHILL AROUND 30 MPH, NOT PRESSING GAS PEDAL, AND ENGINE RPMS ROSE TO OVER 4000 AND STAYED WITH THE ENGINE MAKING A DISTINCT NOISE THAT EVEN A 12 YEAR OLD NOTICED WAS NOT RIGHT. AFTER APPLYING BRAKE AND REACHING BOTTOM OF HILL, THE RPMS EVENTUALLY REDUCED. SO FAR THIS EXTREME CASE WAS A ONE TIME OCCURENCE, BUT SEEMS RELATED TO OTHER BEHAVIOR. DURING REGULAR IN-TOWN TRAVELLING THE ENGINE JUST DOES NOT SEEM TO CHANGE GEARS CORRECTLY OR SMOOTHLY. RPMS WILL REMAIN BETWEEN 2000-3000 REGARDLESS IF YOU ARE GOING 10 MPH OR 55 MPH, BUT PROBLEM IS NOT CONSISTENT. MULTIPLE TIMES WHEN PULLING OUT INTO TRAFFIC AND ALSO GOING INTO REVERSE, THE CAR ALMOST STALLS AND DOES NOT ACCELERATE AS QUICKLY AS IT SHOULD GIVEN THE PRESSURE ON THE GAS PEDAL. IT SEEMS AS IF ALL OF THESE TYPES OF ISSUES ARE RELATED TO THE SAME CORE PROBLEM WITH THE ENGINE/TRANSMISSION AND I SEE OTHER COMPLAINTS HERE SIMILIAR TO THIS. I'VE HAD THE CAR FOR 8 MONTHS AND IT SEEMS TO BE MORE FREQUENT AS TIME PASSES. THESE ISSUES ARE MUCH MORE NOTICABLE WITH DAILY DRIVING, BUT MY HUSBAND HAS NOTICED DURING THE FEW TIMES HE DRIVES THE CAR. HE SAYS IT IS JUST A "CLUNKY" DRIVING CAR, BUT CAR FEELS VERY UNRELIABLE WHEN DRIVEN ON A DAILY BASIS ESPECIALLY FOR THE PRICE.

Mileage: 14,000

Apr 30, 2015

WHILE PULLING OUT OF A PARKING LOT, THE A/C WAS TURNED ON. THERE WAS A GRINDING NOISE, SMOKE STARTING COMING UP FROM THE HOOD AND OUT THE WHEEL WELL, AND THE ENGINE STALLED OUT, LEAVING THE CAR IN HALF WAY OUT IN TRAFFIC. EACH TIME THE ENGINE WAS RESTARTED, IT STALLED OUT AGAIN RIGHT AWAY. FINALLY THE VEHICLE WAS PUSHED OUT OF THE ROAD AND INTO AN ADJACENT PARKING LOT FOR TOWING. THE DEALERSHIP SAYS THE COMPRESSOR BLEW AND SENT METAL SHRAPNEL THROUGHOUT THE HOOD, PENETRATING RUBBER HOSES AND BELTS, AND CAUSING THE CAR TO STOP RUNNING. *TR

Mileage: 9,100

Apr 29, 2015

I HAVE ISSUED A COMPLAINT ABOUT THREE AND A HALF MONTHS AGO. AGAIN, MY MOTHER IS STILL HAVING ACCELERATION PROBLEMS WITH HER CAR. ON APRIL 22ND, SHE STATED THAT SHE WAS GOING UP A HILL, AND THE CAR SUDDENLY STARTED REVVING TO 4000-5000RPM. AT ONE POINT, SHE SAID SHE LIGHTLY WENT ON THE GAS TO SEE IF THE FUEL WOULD KICK IN AND IT REVVED UP 500 RPM PAST THE REDLINE, AND STILL NO ACCELERATION. ONE DAY, MY MOM IS GOING TO END UP BEING REAR-ENDED WHEN THIS HAPPENS AND I WOULD NOT LIKE THAT TO HAPPEN. FORD ABSOLUTELY NEEDS TO DO SOMETHING ABOUT THIS. I'VE SCROLLED THROUGH ALL COMPLAINTS OF THIS MODEL YEAR AND I'VE SEEN THAT AT LEAST 50 PEOPLE ARE EXPERIENCING THESE PROBLEMS. FORD MUST FIX THIS (THAT MEANS ISSUE RECALLS!!!)!!!!! *TR

Mileage: 12,000

Mar 25, 2015

VEHICLE WOULD NOT START AFTER BEING PARKED FOR APPROXIMATELY ONE HOUR. TRIED SEVERAL TIMES TO START, HEADLIGHTS AND DASH LIGHTS WOULD ILLUMINATE, BUT THERE WAS NO INDICATION OF ANY POWER GOING TO ENGINE TO START. NO CLICKING (AS WITH A DEAD BATTERY - ALL LIGHTS WERE FUNCTIONING PROPERLY). WAITED 10 MINUTES AND IT STARTED. TURNED IT OFF BRIEFLY TO GO INSIDE TO TELL SHOP OWNER THAT CAR HAD STARTED. CAME BACK OUT, IT WOULD NOT START AGAIN. TRIED SEVERAL TIMES TO RESTART AND IT WOULD NOT. LEFT CAR WHERE PARKED AND CALLED A TOW TRUCK TO TAKE CAR TO DEALER IN THE MORNING. DEALER WAS UNABLE TO RECREATE THE PROBLEM AND WAS ABLE TO GET THE CAR TO START EACH TIME. I WAS TOLD THAT THERE WAS NOTHING THEY COULD DO AND TO PICK UP MY CAR. WHICH I DID. *TR

Mileage: 12,698

Mar 25, 2015

BACKED OUT OF DRIVEWAY, PUT CAR IN GEAR AND "ENGINE MALFUNCTION" WARNING BOX CAME UP ON DASHBOARD. PUT CAR IN NEUTRAL AND BACK INTO DRIVE. WARNING BOX DISAPPEARED, BUT EXCLAMATION POINT IN TRIANGLE WAS ON DASHBOARD. DEPRESSED GAS PEDAL AND CAR MOVED FORWARD VERY SLOWLY WITH HESITATION AND JERKING POWER SURGES. DROVE APPROXIMATELY 2-3 BLOCKS AS HESITATION, JERKING AND LACK OF POWER CONTINUED. WENT BACK HOME AND CALLED TOW TRUCK TO TAKE CAR TO DEALER. TACHOMETER WAS ERRATIC AND BOUNCING AROUND, WHEN CAR IDLED. CAR STARTED FINE SEVERAL TIMES, BUT WOULD NOT ACCELERATE OR RUN NORMALLY. DEALER VERIFIED COMPLAINT, AND REPAIRED AFFECTING WIRING. *TR

Mileage: 12,645

Mar 25, 2015

ONCE AGAIN VEHICLE WOULD NOT START AFTER BEING PARKED FOR OVER AN HOUR. TRIED SEVERAL TIMES TO START. ALL DASH LIGHTS AND HEADLIGHTS, RADIO, WINDOWS, ETC. WOULD FUNCTION, BUT NO INDICATION OF IGNITION WHEN KEY WAS TURNED. TRIED BOTH KEYS TO MAKE SURE IT WAS NOT A BAD KEY. NEITHER KEY WORKED. LEFT CAR WHERE PARKED OVERNIGHT AND RETURNED IN THE MORNING. CAR STARTED. CALLED DEALER AND IT WAS SUGGESTED THAT I DRIVE THE CAR IN, RATHER THAN HAVE IT TOWED IN. I DID. I LEFT THE CAR AT THE DEALER AND WAS INFORMED LATER THAT DAY THAT THEY HAD BEEN ABLE TO VERIFY MY COMPLIANT. THEY INDICATED THAT IT WAS A BUILD UP OF RESISTANCE IN A WIRE THEN THE ENGINE WAS HOT. IT WAS WRAPPED AND I WAS ASSURED THE I WOULD NO LONGER HAVE THE PROBLEM. I DID SOME RESEARCH AND FOUND THAT SOME 2013-14 FORD ESCAPES HAVE BEEN RECALLED FOR INSUFFICIENT COMPRESSION OF CASING AROUND THE WIRING, CAUSING EXACTLY THE PROBLEMS I HAVE BEEN HAVING. ALL THE POTENTIAL PROBLEMS LISTED IN THE RECALL, SHORT OF A POSSIBLE CRASH HAVE BEEN EXPERIENCED TO DATE! MY VEHICLE WAS MANUFACTURED AT ONE OF THE AFFECTED ASSEMBLY PLANTS DURING THE AFFECTED DATES. HOWEVER, THE RECALL INDICATES 2.0 LITER ENGINES. MINE IS A 1.6 LITER ENGINE. THEREFORE, DEALER SAID THEY COULD NOT DO ANYTHING FOR ME AND ASSURED ME THE PROBLEM HAD BEEN SOLVED. I REQUESTED THAT THE WIRING HARNESS BE REPLACED BECAUSE I FELT UNSAFE IN MY VEHICLE AND WAS AFRAID THAT IT WOULD STOP SUDDENLY AND I COULD CRASH. I WAS TOLD THAT REPAIR WAS NOT POSSIBLE, BECAUSE MY SPECIFIC VIN WAS NOT RECALLED. I WAS ASSURED THAT I SHOULD HAVE NO FURTHER PROBLEMS. I ACCEPTED THE RETURN OF MY VEHICLE, WITH THE ASSURANCE THAT IF IT HAPPENED AGAIN, WE WOULD ESCALATE MY REQUEST FOR REPLACEMENT OF THE WIRING HARNESS. THE DEALER HAD MY CAR FOR OVER A WEEK. *TR

Mileage: 12,790

Feb 16, 2015

WHILE ACCELERATING TO PASS A SLOWER VEHICLE THE ENGINE STARTED STUMBLING AND WENT INTO SOME TYPE OF LIMP MODE AND LOST POWER. I HAD TO RAPIDLY PULL BACK INTO THE SLOWER LANE TO AVOID HAVING CARS BEHIND ME REAR-END ME. I STOPPED THE CAR, TURNED IT OFF , AND WHEN I RESTARTED THE CAR THE PROBLEM WAS GONE. I TOOK THE VEHICLE TO A FORD DEALER BUT THEY STATED THERE WAS NO ERROR CODES STORED IN THE ECU SO THEY COULDN'T DIAGNOSE OR FIX THE PROBLEM. THEN A FEW MONTHS LATER IT HAPPENED AGAIN JUST LIKE BEFORE- I WAS PASSING A SLOWER VEHICLE AND SUDDENLY THE CAR WENT INTO A LIMP MODE AND I LOST POWER AND HAD TO QUICKLY PULL BACK INTO THE SLOW LANE TO AVOID HAVING CARS FROM BEHIND REAR-END ME. THIS TIME I HAD MY WIFE USE HER PHONE TO VIDEO THE ENGINE FAILURE LIGHTS ON THE DASH.AGAIN I HAD TO STOP MY CAR, TURN IT OFF, AND WHEN I RESTARTED THE CARS IT WAS OK. AND AGAIN I TOOK IT TO A DIFFERENT FORD DEALER, I SHOWED THEM THE VIDEO OF THE PROBLEM OCCURRING, BUT AGAIN THEY COULDN'T FIND AN ERROR CODE SO THEY SAID THEY COULD NOT FIX THE PROBLEM. MY WIFE IS AFRAID TO TAKE THIS CAR ON TRIPS BECAUSE SHE IS AFRAID THE PROBLEM WILL HAPPEN AGAIN AND SHE WILL BE REAR-ENDED. I DID SOME INTERNET RESEARCH ON THIS ISSUE AND THERE ARE NUMEROUS COMPLAINTS FROM OTHER DRIVERS DESCRIBING THE EXACT SAME PROBLEM. THE TWO FORD DEALERS WE TOOK THE CAR NEVER TOLD US THAT THIS IS A KNOWN PROBLEM AND THERE HAVE RECALLS FOR THE OLDER ESCAPES FOR THE SAME ISSUE. NHTSA CAN YOU HELP BEFORE SOMEONE GETS HURT. *TR

Mileage: 6,000

Feb 10, 2015

PULLING OUT OF MY DRIVEWAY, ENGINE DIES WITH NO WARNING. PUT INTO NEUTRAL TO RESTART. PULLING OUT OF DRIVEWAY ONTO THE HARDTOP ROAD, ENGINE DIES WITH NO WARNING. TRAVELING AT 20 MPH OR LESS. THIS HAS BEEN GOING ON FOR 2 MONTHS NOW. DOESN'T HAPPEN WHEN THE CAR GOES TO THE DEALERSHIP...CAN'T SEEM TO FIGURE OUT WHAT IS CAUSING IT. *TR

Mileage: 8,270

Feb 5, 2015

TL* THE CONTACT OWNS A 2014 FORD ESCAPE. WHILE DRIVING AT VARIOUS SPEEDS, THE VEHICLE FAILED TO ACCELERATE AND THE SERVICE ENGINE WARNING INDICATOR ILLUMINATED. THE FAILURE RECURRED ON SEVERAL OCCASIONS. THE VEHICLE WAS TAKEN TO A DEALER, BUT WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE ISSUE. THE FAILURE MILEAGE WAS 15,334.... UPDATED 06/30/15 *BF UPDATED 12/10/15 *JS

Mileage: 15,334

Oct 30, 2014

OUTSIDE TEMPERATURES WERE OVER 100F. VEHICLE CUTOFF - LOST ALL POWER AND WAS COASTING. SHIFTED TO NEUTRAL TO RESTART - WHICH IT DID. PULLED OFF THE HIGHWAY CALLED HERTZ ROADSIDE ASSISTANCE. VEHICLE CUTOFF AGAIN WHILE PARKED. DID NOT IMMEDIATELY RESTART. RESTARTED AFTER ABOUT 10 MINUTES. VEHICLE WAS TOWED BY HERTZ. *TR

Mileage: 35,548

Oct 25, 2014

WE LEASED A 2014 ESCAPE IN MARCH OF 2014. FROM THE START IT HAS A PROBLEM ON ACCELERATION, IT WILL HESITATE AND ALMOST STALL WHEN PULLING OUT INTO TRAFFIC. THE HESITATION IS SPORADIC AS AT TIMES IT IS OK. WE NOTICE AT LOW SPEEDS AROUND 20 30 MPH WHEN ACCELERATING IT BUCKS, WILL NOT TAKE GAS. AT TIMES IT HAS BECOME SO FRUSTRATING I WILL STOP THE CAR AND RE START IF TRAFFIC PERMITS. THIS COULD BE A VERY UNSAFE CONDITION AS WE NEVER KNOW WHEN IT WILL DO IT. IT DOES IT USUALLY WHEN IT IS COLD HOWEVER IT HAS DONE IT AFTER DRIVING FOR HOURS, STOP FOR 15 MINUTES AND IT DOES IT THEN TOO. WE HAVE TAKEN IT TO THE DEALERSHIP BUT IT NEVER HAPPENS THEN. THIS IS CONSTANT AND ANNOYING [XXX] INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TR

Mileage: 150

Oct 19, 2014

I WAS DRIVING ALONG WITH CRUISE CONTROL ON AT 73 MPH, WHEN I COULD NO LONGER ACCELERATE, MY ESCAPE JUST DIED WITH NO WARNING LIGHTS, STALL OUT OR ANYTHING. JUST AS IF SOMEONE TURNED IT OFF. I HAD TO COAST TO THE SIDE OF THE ROAD. I WAITED A FEW MINUTES AND TRIED TO START IT AGAIN WITH NO LUCK. WHEN I TURNED THE KEY OVER, IT SEEMED LIKE IT WANTED TO START BUT WAS NOT GETTING THE GAS TO. I TRIED 3 MORE TIME AND FINALLY CALLED FORD ROADSIDE ASSISTANCE AND HAD IT TOWED TO THE NEAREST FORD DEALERSHIP. I AM WAITING ON A REPLY (WITH NO LOANER ETC) THE REASON I BUY NEW IS FOR PEACE OF MIND. NOT EVEN , 10,000 MILES ON THE CAR AND IT BRAKES? WHAT GIVES. I HAVE ALREADY TAKEN IT BACK TO THE DEALER ONCE (THE DAY AFTER I BOUGHT IT) BECAUSE IT TRIES TO STALL WHEN SWITCHING FROM REVERSE TO DRIVE, BUT THE DEALER MADE SOME EXCUSE AND SAID TO WATCH AND SEE IF IT CONTINUES. I AM JUST GLAD THAT I WAS WITHIN CELL PHONE SIGNAL RANGE BECAUSE I HAD JUST NOT BEEN A FEW MINUTES BEFORE (SCARY). *TR

Mileage: 9,500

Aug 24, 2014

SATURDAY, JULY 12 AROUND 3:00 PM DRIVING 70 MPH ON US 23 N, JUST SOUTH OF NORTH TERRITORIAL ROAD NEAR ANN ARBOR. THE CAR SUDDENLY LOST POWER AND THE ENGINE STOPPED. DRIFTED TO THE SHOULDER IN VERY HEAVY TRAFFIC AND TRIED TO RESTART. STARTED AND RAN FOR 5 SECONDS AND THEN STALLED AGAIN. REPEATED SEVERAL TIMES WITH SAME RESULT. CALLED ROADSIDE ASSISTANCE NUMBER AND THEY SAID THEY WOULD SEND A TOW WITHIN 30 MINUTES. POLICE STOPPED AND ASKED IF WE NEEDED HELP. LEFT AFTER WE SAID TOW WAS COMING. A FOLLOWING CAR TOOK ALL BUT ONE PASSENGER TO A GAS STATION AT NORTH TERRITORIAL BECAUSE HEAVY 75 MPH TRAFFIC PASSING INCHES FROM THE DRIVER'S DOOR WAS FRIGHTENING AND DANGEROUS. TOW TRUCK TOOK CAR TO VARSITY FORD IN ANN ARBOR AND WE CONTINUED TO TRAVERSE CITY IN THE FOLLOWING CAR. *TR

Mileage: 5,500

Jul 28, 2014

2014 FORD ESCAPE SE AWD WITH 1.6 ECOBOOST ENGINE. INFREQUENTLY UPON FULL THROTTLE ACCELERATION THE ENGINE BOGS DOWN. WHILE THE ENGINE DOES NOT STALL, POWER DISAPPEARS AND THEN POWER/ACCELERATION REBUILDS. IT HAS OCCURRED TWICE IN 3 MONTHS. VEHICLE CURRENTLY HAS ~3000 MILES ON THE ODOMETER. I HAVE HEARD THAT AN INVESTIGATION IS UNDERWAY FOR WHAT SOUNDS LIKE A SIMILAR ISSUE WITH F150'S WITH A DIFFERENT ECOBOOST ENGINE - RELATED? *JS

Mileage: 1,500

Jul 7, 2014

THE VEHICLE STALLED WITH NO WARNING, WOULD NOT RESTART. HAVE HAD FOR 6 WEEKS. HAS BEEN AT DEALERSHIP AND THEY CANNOT IDENTIFY PROBLEM. 5 SENSORS ARE NOT COMMUNICATING FROM THE ENGINE. THEY HAVE CHANGED COMPUTER IT RESTARTED AND DIED AGAIN. FORD INSISTS THEY ARE GOING TO FIX IT AND ARE GOING TO FORCE ME TO TAKE IT BACK. *JS

Mileage: 1,185

Jul 1, 2014

WHILE DRIVING DOWN THE INTERSTATE AT 55 MPH IN HEAVY TRAFFIC, THE ENGINE SUDDENLY STARTED RUNNING EXTREMELY ROUGH, JERKING AND LURCHING, WHILE LOSING POWER. THE "ENGINE FAULT - SERVICE NOW" WARNING DISPLAY ILLUMINATED AND THE ENGINE STALLED OUT. PULLED TO THE SIDE OF THE INTERSTATE AND WAS ABLE TO RESTART THE VEHICLE AND DRIVE HOME WITH NO FURTHER PROBLEMS. *TR

Mileage: 1,152

May 21, 2014

WHILE DRIVING ON HIGHWAY I ACCIDENTALLY DEPRESSED THE KEYLESS START-STOP BUTTON. THE ENGINE SHUT OFF, POWER STEERING AND BRAKES WERE LOST AND ENGINE WOULD NOT RESTART BY PUSHING START-STOP BUTTON. I WAS ABLE TO SLOW CAR - WITH OTHER CARS CLOSE BEHIND- SHIFT GEAR SHIFT TO NEUTRAL AND APPLY BRAKE PEDAL SO THAT START-STOP BUTTON WOULD RESTART ENGINE. I HAVE HAD FORD DEALERSHIP CHECK KEYLESS START-STOP SYSTEM AND THEY INDICATE THAT SYSTEM WORKS AS IT SHOULD. START - STOP BUTTON IS LOCATED IN DRIVERS RIGHT KNEE AREA AND IS TWO INCHES FROM SIMILAR LOOKING CLIMATE CONTROL BUTTON. POWER STEERING AND BRAKES WERE LOST WITH ENGINE OFF AND CAR IN MOTION. I CONTACTED FORD MOTOR COMPANY AND THEY REFERRED US TO THE DEALERSHIP. THIS IS A DANGEROUS DESIGN FLAW. *TR

Mileage: 9,600

May 10, 2014

FOR THE FIRST INCIDENT, THE CAR'S WARNING LIGHT CAME ON AND SAID "ENGINE FAILURE - SERVICE IMMEDIATELY." I ATTEMPTED TO PROCEED TO THE DEALER FOR SERVICE BUT, BEFORE I MADE IT OFF OF OUR STREET, THE CAR BEGAN TO SHAKE AND SHUDDER VIOLENTLY, THEN DIED IN THE MIDDLE OF THE ROAD. I WAS ABLE TO GET IT TO COAST TO A SMALL PARKING AREA. AS IT WOULD NOT START AGAIN, IT REQUIRED A TOW TO THE DEALER. THE DEALER INFORMED ME THAT IT WAS A SENSOR ISSUE AND ENSURED THAT IT WAS REPAIRED AND WOULD NOT HAPPEN AGAIN. TODAY (MAY 10TH) A SIMILAR ISSUE OCCURRED, THOUGH THIS TIME IT WAS WHILE I WAS PULLING INTO TRAFFIC. AGAIN, THE SAME WARNING LIGHT CAME ON. I ATTEMPTED TO TURN AND GET THE CAR HOME BUT, BEFORE I COULD DO THIS, THE CAR BEGAN TO SHAKE AGAIN AND THE ENGINE LOST POWER. THIS REQUIRED ANOTHER TOW TO THE DEALERSHIP FOR REPAIR; THE VEHICLE IS PRESENTLY IN THE SHOP. *TR

Mileage: 4,000

Apr 7, 2014

VEHICLE STOPPED AT STOP SIGN. ENGINE DIED. MOVED GEAR SELECTOR FROM DRIVE TO PARK AND RESTARTED WITH NO FURTHER INCIDENT. *TR

Mileage: 367

Apr 4, 2014

I BOUGHT A NEW FORD ESCAPE IN FEBRUARY 2014. SINCE DAY ONE I HAVE NOTICED AN EXHAUST SMELL IN CABIN WHEN THE VEHICLE IS PUT INTO REVERSE AND OCCASIONALLY WHEN DRIVING AT LOW SPEEDS. SIMILAR TO WHAT OTHER CUSTOMER COMPLAINED. I WILL BRING THIS TO THE ATTENTION OF MY FORD DEALERSHIP WHEN IT GOES IN FOR MAINTENANCE SERVICE WHEN IT REACHES 10,000 MILES, BUT MAYBE SOONER TO HAVE IT LOOKED AT. *TR

Mileage: 1,000

Apr 1, 2014

LEASED THIS VEHICLE IN AUGUST, 2013. SINCE DAY ONE I HAVE NOTICED AN EXHAUST SMELL IN CABIN WHEN THE VEHICLE IS PUT INTO REVERSE AND OCCASIONALLY WHEN DRIVING AT LOW SPEEDS. I AM SENSITIVE TO ODORS IN GENERAL AND MY FAMILY MEMBERS ONLY SMELLED IT OCCASIONALLY, SO I DISREGARDED UNTIL RECENTLY THE ODORS ARE BECOMING STRONGER INSIDE THE CABIN AND NOT CLEARING WHEN WINDOWS ARE LOWERED TO AIR OUT. I WILL BRING THIS TO THE ATTENTION OF MY FORD DEALERSHIP WHEN IT GOES IN FOR MAINTENANCE SERVICE WHEN IT REACHES 10,000 MILES, BUT MAYBE SOONER TO HAVE IT LOOKED AT. *TR

Mileage: 12

Feb 9, 2014

WHEN THE VEHICLE IS BETWEEN 1400-1600 RPM IT STARTS TO VIBRATE AND DRIVES ROUGH. IS THIS USUAL? HAD IT TO TWO DIFFERENT DEALERSHIPS AND COMPLAINED TO FORD. NO SATISFACTION!! *TR

Mileage: 50