1993 FORD EXPLORER Engine And Engine Cooling Problems
67 complaints about Engine And Engine Cooling
High Severity Issue
This component has been associated with crashes, fires, or deaths.
This Problem Across All Years
All Engine And Engine Cooling Complaints (67)
TL* THE CONTACT OWNS A 1993 FORD EXPLORER. . AFTER THREE ATTEMPTS OF ATTEMPTING TO START THE VEHICLE, THE ENGINE MISFIRED. A BYSTANDER NEAR THE DRIVER-SIDE DOOR SUSTAINED INJURIES TO HER EYES, HAIR, AND UPPER PORTION OF HER BODY. SHE HAD TO BE TRANSPORTED TO THE HOSPITAL. THE VEHICLE WAS COMPLETELY DESTROYED. THE FAILURE AND CURRENT MILEAGES WERE A LITTLE OVER 200,000.
Mileage: 200,000
I BOUGHT A CAR FROM A DEALER AND HAVE THE CAR FOR LESS THAN 30 DAYS AND THE TRANSMISSION IS GOING OUT. THE DEALER WOULD NOT GIVE ME A TEMPORARY TAG UNLESS I WENT TO HIS MECHANIC FOR A INSPECTION ALSO THE VEHICLE HAS BEEN CONSTANTLY LEAKING OIL SINCE THE 2ND DAY I PURCHASED. *JB
INTERMITTENTLY ENGINE STALLING. *JB
Mileage: 65
MULTIPLE FAILURES, CONTINUALLY BRAKE PROBLEMS. THE VEHICLE ALSO OVERHEATED, THERMOSTAT REPLACED SEVERAL TIMES. A/C COMPRESSOR MALFUNCTION, ETC. *BF A BLOWOUT RIPPED THE RUNNING BOARD ASSEMBLY, THE ABS LIGHT WAS INTERMITTENT AND THE MECHANIC COULD NOT FIGURE OUT WHY, THE BRAKES LOCKED UP ON THE VEHICLE AND VIOLENTLY SKIDDED TO A STOP, THE EXHAUST WAS REPLACED TWICE, THERE WAS A NOISE THAT LINGERED ON IN THE FRONT END AND A LOUD CREAKING SOUND. *SC
THE VEHICLES COOLING FAN CRACKED. THE CONSUMER WAS CONCERNED THAT THE FAN WOULD FAIL WHILE DRIVING. PLEASE PROVIDE ANY ADDITIONAL INFORMATION. *NLM
Mileage: 124,000
CYLINDER HEADS NEED REPLACING. *LA
VEHICLE FIRE. MR. WHILE DRIVING, THE CONSUMER NOTICED FLAMES COMING FROM UNDER THE HOOD, THE VEHICLE WAS TOTALED. *JB
CONSUMER WAS TRAVELLING APPROXIMATELY 60MPH ON THE HIGHWAY. WHEN CONSUMER REMOVED FOOT FROM ACCELERATOR PEDAL IN PREPARATION FOR EXIT, THE VEHICLE MADE A STRANGE "CLUNKING" NOISE AND BEGAN TO ACCELERATE SUDDENLY. ATTEMPTS TO SLOW DOWN UTILIZING THE BRAKES AND DOWNSHIFTING TRANSMISSION WERE UNSUCCESSFUL. CONSUMER HAD TO RUN VEHICLE OFF THE ROAD TO AVOID A COLLISION. VEHICLE FLIPPED OVER AND ENGINE WAS STILL "REVVING" HIGH. TS
VEHICLE SHAKES AT 60 MPH AND HIGHER. DEALER STATED A KIT TO REPLACE MOTOR MOUNTS WAS NEEDED. *AK
WHILE VEHICLE WAS PARKED, CONSUMERS NEIGHBOR NOTICED SMOKE COMING OUT OF THE WINDOWS, CONSUMER ATTEMPTED TO PUT OUT THE FIRE, HOWEVER BY THE TIME THE DOORS WERE OPENED FLAMES WERE SMOLDERING IN THE FRONT SEATS, FIRE DEPARTMENT COULD NOT DETERMINE THE CAUSE OF THE FIRE, VEHICLE WAS A TOTAL LOSS. *SLC
WHILE VEHICLE WAS PARKED, CONSUMERS NEIGHBOR NOTICED SMOKE COMING OUT OF THE WINDOWS, CONSUMER ATTEMPTED TO PUT OUT THE FIRE, HOWEVER BY THE TIME THE DOORS WERE OPENED FLAMES WERE SMOLDERING IN THE FRONT SEATS, FIRE DEPARTMENT COULD NOT DETERMINE THE CAUSE OF THE FIRE, VEHICLE WAS A TOTAL LOSS. *SLC
THE ENGINE, REGARDLESS OF SPEED OR DRIVING CONDITIONS SHUTS OFF AND CREATES A DANGEROUS SITUATION WHEN IT OCCURS IN THE MIDDLE OF TRAFFIC. THE LIGHTS, HORN, FLASHER FUNCTION ,BUT THE ENGINE JUST CRANKS WITHOUT STARTING SOMETIME 5 MINUTES, SOMETIMES ONE OR MORE HOURS BLOCKING TRAFFIC LANES. AAA HAS TOWED TO GARAGES A COUPLE OF TIMES AND WHEN THE MECHANICS TURN THE KEY, THE CAR STARTS RIGHT UP AND A DIAGNOSTIC CANNOT BE PERFORMED. I DO NOT WISH TO BE A VICTIM IN AN ACCIDENT WITH ANY VEHICLE BEFORE FORD DECIDES TO INVESTIGATE THIS FAILURE THAT IS BECOMING MORE FREQUENT. I CHECKED WITH FORD IN ORDER TO SEE IF THIS PROBLEM WAS RE CALLED, BUT IT WAS NOT AS OF 10/29/01. *AK
INSIDE LEFT DOOR HANDLE COMES COMPLETLY OFF IN HAND WHEN CLOSING DOOR. BOTTOM HINGE ON LEFT DOOR BROKE. CATALATIC CONVERTER RATTLES WHEN ACCELERATED TO 55 MPH. *AK
NO SUMMARY LISTED FOR ABOV EVEHICLE. *AK
VEHICLE STALLS MOSTLY AFTER DRIVING FOR AT LEAST 30 MINUTES, MOSTLY AT SPEEDS OF 40-70 MPH. HAS STALLED AT LEAST 12 TIMES. DEALER CANNOT REMEDY PROBLEM. *AK
WHILE DRIVING ABOUT 10 MPH CONSUMER NOTICED FLAMES FROM UNDERNEATH VEHICLE, PULLED OVER, AND SAW FLAMES UNDERNEATH FENDERS. VEHICLE BURNED, TOTALLED. FIRE CHIEF THOUGHT THAT CATALYTIC CONVERTER CAUSED FIRE. *AK
THIS IS ONE OF TWO EXPLORERS ON WHICH THE SAME COMPONENT FAILED. I HAD THE GUAGE REPLACED AT THE DATE AND MILEAGE NOTED, BUT IT FAILED LONG BEFORE THAT DATE. I FIND IT HARD TO BELIEVE I WAS UNLUCKY ENOUGH TO GET TWO BAD TEMPERATURE GUAGES. ESPECIALLY SINCE A FRIEND TOLD HIM HE HAD TO REPLACE THE GUAGE ON HIS 1997 EXPLORER. *AK
CONSUMER HEARD CLICKING SOUND WHILE AT STOP LIGHT, PULLED OVER,AND NOTICED THAT FLYWHEEL HAD FALLEN OFF AT 33000 MILES. *AK
INTAKE GASKETS FAILED / LOST COOLANT
NO SUMMARY
RUSTED CAUSING LOUD NOISE
INTAKE GASKETS FAILED / LOST COOLANT
NO SUMMARY
RUSTED CAUSING LOUD NOISE
PREMATURE HEAD GASKET FAILURE IS APPARENTLY A COMMON FORD PROBLEM. THIS HEAD GASKET BLEW AT ONLY 70,000 MILES ON A 6-YEAR OLD VEHICLE. THIS IS TOO EARLY FOR THIS TYPE OF PROBLEM TO HAPPEN. IT COULD BE A FLUKE, BUT THERE ARE INTERNET SITES ABOUT FORD VEHICLES WITH THIS SAME PROBLEM. REPAIRS ARE VERY COSTLY FOR PARTS THAT SHOULDN'T HAVE GONE BAD IN THE FIRST PLACE. THIS VEHICLE WAS NOT EVER DRIVEN ROUGHLY OR PUT UNDER UNUSUAL STRESS--JUST CITY DRIVING. I THINK THAT THERE IS A REAL PROBLEM WITH FORD HEAD GASKETS THAT SHOULD BE INVESTIGATED. THANK YOU.*AK
WHILE CONSUMER WAS TRAVELING ABOUT 55 MPH , THE SPRING FOR THE THROTTLE GAUGE BROKE, CAUSING THE VEHICLE TO GO INTO FULL THROTTLE. IN ORDER FOR CONSUMER TO STOP VEHICLE HE HAD TO APPLY THE BRAKES UNTIL THEY WERE WORN DOWN AND PUT VEHICLE IN PARK. *AK.ET.
MANUFACTURER FAILS TO MAKE LEFT ENGINE VALVE COVER FOR HIS PARTICULAR VEHICLE THAT NEEDS TO BE REPAIRED. FINALLY RECEIVED PART 5 WEEKS TO THE DAY AFTER IT WAS ORDERED. *AK
RESULTS IN OIL LEAK WHICH COULD LEAD TO FIRE AS WELL AS A SOURCE OF POLLUTION. FORD MOTOR COMPANY DOES NOT HAVE ANY REPLACEMENT VALVE COVERS ON HAND. HOW CAN A COMPANY OF THIS SIZE GET AWAY WITH SELLING AS MANY OF THESE VEHICLES AS THEY HAVE AND NOT HAVE REPLACEMENT PARTS AVAILABLE TO THERE CUSTOMERS? *AK
SPARK PLUGS WERE REPLACED BY H&L ON 4/19/99 PART # AWSF-4C, MILEAGE WAS 74,497. FAILURE OF PLUGS WAS DURING TRIP, AT ANOTHER DEALER RHINEBECK FORD, 914-876-4440, THEY REPLACED THEM WITH AWSF-42P- STATING WRONG PLUGS INSTALLED BY H&L. H&L RESPONDED INITIALLY THAT THESE WERE THE CORRECT PLUGS, BUT LATER AGREED THAT THE 42P WERE THE RIGHT ONES. SUBSEQUENT, THE VEHICLE RAN ROUGH AND HAD POOR PERFORMANCE. H&L CONTACTED REGARDING THIS, NOTED TO MONITOR FLUID LEVELS, TUNE UP WOULD NOT CURE PROBLEM. MANAGER STATED IT COULD BE A CRACKED HEAD. WITHIN 7 DAYS SINCE 10/11/99, ENGINE IS IN SHOP, WHITE SMOKE COMING OUT OF EXHAUST AND FLUIDS INDICATE A LEAK. MANAGER ALSO STATED THAT THIS IS A KNOWN PROBLEM WITH THE EXPLORER FOR THAT YEAR. CAR NO LONGER UNDER WARRANTY, EXPIRED AT 89,830. FEEL FORD IS RESPONSIBLE!
PLASTIC ENGINE COOLING FAN HAS SEVERAL CRACKS IN IT, CAUSING POTENTIAL SAFETY HAZARD. DEALER CANNOT DETERMINE CAUSE. *AK
WHILE DRIVING AN OIL LEAKAGE OCCURRED. IT SMOKED UP THE WHOLE VEHICLE .THEN WE STOPPED AND THE LEAK STOPPED ALSO AND DID NOT REOCCUR. *AK
WANTAGH FORD, THE SERVICING DEALER HAS ADVISED ME THAT THERE IS INTERNAL ENGINE WEAR/ LOW OIL PRESSURE, AND THAT I NEEDED A NEW ENGINE. *AK
WHILE TRAVELING VEHICLE CAUGHT ON FIRE IN ENGINE COMPARTMENT WITHOUT ANY INICATIONS, CAUSING DAMAGE TO THE VEHICLE. PLEASE PROVIDE FURTHER INFORMATION. *AK
THE MOVEMENT FREQUENCY OF THE ENGINE ALIGNS WITH THE TIRE ROTATION FREQUENCY CAUSING A VIRBRATION/SHAKE THAT CAUSES THE TRUCK TO BECOME DIFFICULT TO MANAGE. KNOWN PROBLEM WITH EXPLORER, HOWEVER THEY CLASSIFY IT AS A PROBLEM NOT A DEFECT. REQUIRES HORIZONTAL STABLIZERS TO BE ADDED TO THE TRUCK TO ELIMINATE THE VIBATION. FORD WILL NOT COVER AS A DEFECT.
ENGINE MOUNTS AND REAR AXLE-TO-FRAME LATERAL SHOCK ABSORBER KIT INSTALLED AS PER SERVICE BULLETIN DUE TO EXCESSIVE VIBRATION DUE TO COMPONENT FAILURES.
VEHICLE VIBRATES DUE TO TINY IMBALANCES IN DRIVETRAIN. THESE TINY FORCED VIBRATIONS IN DRIVETRAIN BEGIN TO EXCITE RESONANT VIBRATIONS IN EXHAUST SYSTEM. NEED STO REPLACE EXHAUST SYSTEM.
BATTERY/MANIFOLD ABSOLUTE PRESSURE (MAP) SENSOR/RADIUS ARM BUSHING/HYDRAULIC LIFT CYLINDERS (REAR DOOR) AND DRIVER'S SIDE MIRROR FAILED.
VEHICLE VIBRATES SEVERELY AT APPROX 65 MPH, RESULTING FROM ENGINE MOUNT PROBLEM THAT FORD IS AWARE OF.
ENGINE FIRE. (QC-AW)
OIL PAN GASKET FAILED, CRANKSHAFT SEAL ASSEMBLY FAILED,RESULTING IN LEAKAGE.
PISTON RING FAILURE RESULTING IN LEAKING.
COMPLETE ENGINE FAILURE, VALVE ROCKER GASKET FAILURE.
COMPLETE ENGINE FAILURE, VALVE ROCKER GASKET FAILURE.
THE TRUCK HAS A KNOWN DESIGN FLAW CAUSING THE TRUCK TO VIBRATE EXCESSIVELY BETWEEN 52 AND 67 MPH. THE DEALER GRAHAM FORD IN DICKSON LOOKED AT THE TRUCK AND WILL ONLY REPAIR THE TRUCK IF I BUY THE SERVICE KIT AND PAY LABOR. THE SERVICE MANAGER INFORMED ME THIS WAS A KNOWN DEFECT AND THAT THEY HAD TO BUY BACK A TRUCK THEY SOLD NEW ON ONE OCCASION. FORD IS AWARE OF THE PROBLEM AND EVEN SUPPLIED THIS DEALER A KIT WHILE UNDER DEVELOPMENT TO SEE IF FIXED THIS PROBLEM. THIS VIBRATION CAUSES THE TRUCK TO BECOM DIFFICULT TO CONTROL WHILE DRIVE IN THE ABOUT SPEED RANGES.
THE OIL SEALS ARE LEAKING INTO THE ENGINE. CONSUMER CANTACTED THE DEALER ABOUT THE PROBLEM. *AK
VEHICLE INTERMITTENTLY FAILS TO START OR STALLS DURING OPERATION.
WHILE DRIVING VEHICLE 20 MPH THE ABS DID NOT RESPOND WHEN STEPPING ON BRAKE PEDAL; THE VEHICLE HAD BEEN TAKEN TO THE SHOP MANY TIMES, THE MECHANIC DID REPLACED THE TOTAL BRAKING SYSTEM. *AK ALSO THE LEFT SPEAKER WAS INOPERABLE, AND DEALER REPLACED THE FRONT COVER GASKET DUE TO AN ANTIFREEZE LEAK. *JB
VEHICLE STALLS.
ENGINE STALLS ON OCCASION.
ANTI-FREEZE LEAKS.
REAR MAIN SEAL AND OIL PAN GASKET LEAK.
REAR MAIN SEAL AND OIL PAN GASKET LEAK.
THERMOSTAT STICKS.
SERPENTINE BELT CRACKED.
WATER WAS SUCKED INTO THE ENGINE WHEN DRIVING THROUGH A PUDDLE, CAUSING ENGINE DAMAGE/STALLING.
OIL LEAKS.
MOTOR MOUNTS WEAR OUT; FRONT END SEVERELY SHAKES AT 55 MPH; FRONT END CONSTANTLY REALIGNED. TT
VEHICLES PROTECTIVE SHIELD OF EXHAUST SYSTEM FELL OFF DUE TO DEFECTIVE WELDING/BRACKETS.DLR HAS SEEN SEVERAL OF THESE FAILURES. TT
THE MOTOR MOUNTS ARE BROKEN AND CAUSING A VIOLENT SHIMMY IN THE FRONT END. PLEASE DESCRIBE. TT
EXCESSIVE ENGINE OIL CONSUMPTION, VEHICLE BURNED A HALF QUART OF OIL EVERY 900 MILES. *AK
ENGINE MOUNT DESIGN PROBLEMS, CAUSE VEHICLE TO SHAKE VIOLENTLY AT SPEEDS OF 63 MPH. *SKD
THE ENGINE MOUNTS ARE DEFECTIVE. THE TRUCK SHAKES AND A THUMPING SOUND IS HEARD *AK
COOLANT LEAK. *AK
PROBLEM W/ENGINE MOUNTS CAUSES WHEELS TO VIBRATE/PREMATURE TIRE WEAR. *AW
ENGINE RUNS ROUGH, ALSO VEHICLE INTERMITTENTLY FAILS TO START.
EXCESSIVE ENGINE VIBRATION WHEN TRAVELING IN EXCESS OF 50 MPH. TT
OIL FILTER REPLACED 4 TIMES/ENGINE OVERHAULED DUE TO LARGE OIL CONSUMPTION, ALSO EXHAUST SYSTEM REPLACED DUE TO OIL ENTERING PIPE/NOISE.