2001 FORD F-250 SD Electrical System Problems

39 complaints about Electrical System

39
Complaints
1
Crashes
12
Fires
0
Deaths

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Electrical System Complaints (39)

Sep 17, 2013

TL* THE CONTACT OWNS A 2001 FORD F-250 SD. THE CONTACT STATED THAT AS HE STARTED THE ENGINE, EVERY LIGHT REMAINED ILLUMINATED OF THE INSTRUMENT PANEL. IN ADDITION, THE CONTACT STATED THAT THERE WAS A BROKEN SEAM IN THE WINDSHIELD THAT WOULD CAUSE WATER TO LEAK INTO THE VEHICLE AND ONTO THE ELECTRONIC CONTROL MODULE. THE VEHICLE WAS NOT TAKEN TO THE DEALER FOR INSPECTION. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 200,007.

Mileage: 200,007

Aug 31, 2012 Fire

TL* THE CONTACT OWNS 2001 FORD F-250. THE CONTACT STATED WHILE THE VEHICLE WAS PARKED IT CAUGHT FIRE AND THE FLAMES WERE COMING FROM UNDER THE HOOD. THE POLICE AND THE FIRE DEPARTMENT WERE NOTIFIED AND A REPORT WAS FILED. THE VEHICLE WAS TOWED TO THE DEALER FOR DIAGNOSTIC TESTING. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE AND CURRENT MILEAGE WAS 59,075.

Mileage: 59,075

Nov 2, 2011 Fire

TL* THE CONTACT OWNS A 2001 FORD F250 SD. THE CONTACT STATED THE VEHICLE WAS PARKED WHEN IT CAUGHT ON FIRE. THE FIRE DEPARTMENT WAS NOTIFIED AND EXTINGUISHED THE FIRE, ADVISING THAT THE FIRE WAS CAUSED BY AN ELECTRICAL MALFUNCTION. A FIRE REPORT WAS FILED. THE MANUFACTURER WAS NOTIFIED OF THE FIRE WHO ADVISED THAT THEY WOULD NOTIFY HIM WITHIN 15 DAYS. THE FAILURE MILEAGE WAS 54,000.

Mileage: 54,000

Apr 6, 2011

TL* THE CONTACT OWNS A 2001 FORD F-250 SD DIESEL. THE CONTACT STATED THAT THE VEHICLE WAS PARKED AND IDLE WHEN IT ATTEMPTED TO START INDEPENDENTLY. THE KEYS WERE NOT IN THE IGNITION AT THE TIME OF FAILURE. THE CONTACT DISCONNECTED AND RECHARGED THE BATTERY. ONCE THE BATTERY WAS REINSTALLED IN THE VEHICLE, THE VEHICLE FAILED TO START. HE THEN CONTACTED SEVERAL LOCAL MECHANICS ABOUT THE FAILURE BUT NO ONE COULD PROVIDE AN EXPLANATION OF THE FAILURE. SEVERAL AUTHORIZED DEALERS WERE ALSO CONTACTED BUT AGAIN THEY TOO, COULD NOT PROVIDE AN EXPLANATION FOR THE FAILURE. THE FAILURE DID NOT RECUR AND THE MANUFACTURER WAS NOT CONTACTED TO REPORT THE FAILURE. THE FAILURE AND CURRENT MILEAGE WAS 113,000.

Mileage: 113,000

Apr 20, 2010 Fire

2001 FORD F-250 SUPER DUTY PICKUP CAUGHT ON FIRE DUE TO FAULTY WIRING. *TR

Mileage: 110,000

Jan 28, 2010

BRAKE PRESSURE SWITCH.. HARNESS WAS REPLACED IN 2008 BUT THE SWITCH WAS NOT LEAKING AT THAT TIME. CRUISE CONTROL STOP WORKING IN 2009. FOUND SWITCH WAS LEAKING. WAS TOLD NO LONGER UNDER WARRANTY. TW*

Mileage: 54

Feb 7, 2009

I HAVE A 2001 FORD F250, THE WINDSHIELD LEAKED CAUSING THE GEM MODULE TO MAL-FUNCTION. THIS IS A PROBLEM IN ALOT OF FORD VEHICLES,NOT JUST MINE. THE SHORT CAUSES THE TRUCK TO MISS, STALL, A LOT OF ELECTRICAL PROBLEMS RESULT. *TR

Mileage: 80,000

Oct 13, 2008 Fire

TRUCK HAD BEEN PARKED IN MY DRIVEWAY APPROXIMATELY 30 MINUTES WHEN I HEARD A NOISE LOOKED OUT AND FRONT OF TRUCK WAS ENGULFED IN FLAMES. NO PRIOR WARNING WAS GIVEN OR NOTICED. CALLED 911, FIRE DEPARTMENT ARRIVED AND EXTINGUISH THE FLAMES. TRUCK WAS TOTALED. *TR

Mileage: 70,000

Sep 16, 2008 Fire

TL*THE CONTACT OWNS A 2001 FORD F-250 SD. WHEN THE GEAR SHIFTER IS USED, IT CAUSES THE ACCELERATOR PEDAL FUSE TO BLOW. SMOKE APPEARED OUT OF THE STEERING COLUMN. THE CONTACT BELIEVES THAT THE FAILURE WAS DUE TO BURNED WIRES AND ALL OF THE ISSUES WERE CONNECTED TO THE STEERING COLUMN ELECTRICAL SYSTEM. HE BELIEVES THAT THE WIRES WERE BURNED IN THE STEERING COLUMN. THE TOW PACKAGE BURNED AND THE RIGHT TURN SIGNAL AND BRAKE LIGHTS NO LONGER WORK. ALL OF THE DOORS APPEARED TO BE SHORT AND DO NOT CLOSE OR OPEN PROPERLY. IN ADDITION, THE OVERDRIVE FAILED ON THE STEERING COLUMN. WHEN THE CONTACT PRESSES THE BUTTON, NOTHING HAPPENS. THE DEALER STATED THAT THE VEHICLE WAS NOT UNDER WARRANTY AND DOES NOT HAVE ANY SAFETY RECALLS THAT APPLY TO THE VIN. THE CONTACT WOULD BE RESPONSIBLE FOR THE REPAIR COSTS. THE FAILURE MILEAGE WAS 142,000.

Mileage: 142,000

Jun 17, 2007

THE CAM POSITIONING SENSOR IN THE FORD POWER STROKE 7.3L DIESEL HAS GONE OUT AT 60,000 MILES. THIS CAUSED THE VEHICLE TO COMPLETELY SHUT DOWN. THIS WAS NOT THE ONLY TRUCK THIS HAS HAPPENED TO. MANY PEOPLE I KNOW HAD THIS HAPPEN WITHIN THE FIRST 100,000 MILES. FORD REPAIRED THE CPS FOR $400.00 AT MY EXPENSE. ALSO THE O RING IN THE HIGH PRESSURE OIL PUMP WENT OUT AT 71,000 MILES WITH NO WARNING, CAUSING ME TO DUMP ALL OF THE OIL OUT. I DISCOVERED IT BEFORE IT CAUSED MOTOR PROBLEMS. FORD FIXED THIS PROBLEM FOR $500.00. BOTH PROBLEMS A WERE VERY COMMON WITH THE 7.3L AND NEED TO BE ADDRESSED BY FORD. THEY WERE NOT ORDINARY PROBLEMS AND NEED SOME KIND OF ATTENTION FROM FORD. *AK

Mileage: 60,000

May 24, 2007

VEHICLE STALLED MULTIPLE (20) TIMES 30 MILES FROM HOME. RESTARTED SUCESSFULLY EACH TIME. DROVE 1/4 MILE TO 5 MILES IN BETWEEN EACH TIME IT STALLED. FINALLY GOT HOME. PURCHASE AND REPLACE THE SYNCHRONIZER (CAM POSITION SENSOR) #F7TZ-12K073-A. NO FAILURES SINCE. OLD PART IS AVAILABLE.

Mileage: 129,000

May 14, 2007

WHILE DRIVING ON A BUSY ROAD THE TRUCK CUT OFF. HARD TO DRIVE A DIESEL WHEN NOT RUNNING. MANAGED TO GET OFF ROAD. REPLACED FAILED CPS. F7TZ-12K073-A. *AK

Mileage: 112,570

Apr 23, 2007

I RECENTLY BOUGHT A USED 2001 FORD F-250 WITH THE 7.3 DIESEL FROM THE LOCAL FORD DEALER. IT HAD A RECENT COMPUTER REFLASH, SHOULD HAVE TOLD ME SOMETHING. ANYWAY THE CPS WAS BAD IN IT. IT WOULD SHUT DOWN, SOMETIMES STARTING RIGHT BACK, SOMETIMES AFTER A FEW MINUTES. I GOT TIRED OF THE RUN AROUND SO I PUT A NEW CPS IN IT MYSELF. I HAVE HAD NO MORE PROBLEMS, NO THANKS TO FORD. *JB

Mileage: 60,000

Apr 21, 2007

CAM SHAFT POSITION SENSOR HAS FAILED 2 DIFFERENT TIMES ON A 2001 POWERSTROKE FORD F250. FIRST TIME WHILE DRIVING THROUGH A PARKING LOT. SECOND TIME ON THE ROAD AT HIGHWAY SPEEDS. VEHICLE WAS DIFFICULT TO STOP AND STEER DUE TO LOSS OF POWER STEERING AND POWER BRAKES. *TR

Mileage: 62,000

Apr 12, 2007 Fire

2001 FORD F250 CREW CAB SPONTANIOUSLY CAUGHT ON FIRE WHILE PARKED IN THE DRIVEWAY. IT WAS A TOTAL LOSS ,AND SERVERLY DAMAGED THE HOUSE AND DRIVEWAY. FIRE CREWS STATED THE HOUSE WAS 2 MINUTES FROM IGNITING WHEN THEY FOAMED IT.*AK

Mileage: 138,000

Mar 21, 2007

I HAVE HAD MULTIPLE CPS FAILURES AND EACH TIME THE TRUCK DIED WHILE I WAS DRIVING LOSING POWER STEERING BRAKES ETC. IT IS VERY DANGEROUS AND A NEW PART SHOULD BE DEISGNED. THE PART NUMBER IS F7TZ-12K073-A. I HAVE REPLACED THIS SENSOR MUTLIPLE TIMES AND EVERY TIME IT IS REPLACED THE ENGINE STARTS RIGHT BACK UP.*AK

Mileage: 87,000

Mar 18, 2007

WHILE DRIVING WITH MY 17 MONTH OLD SON, MY TRUCK JUST QUIT WHILE ON THE HIGHWAY. NO WARNING, NO STEERING, NO BRAKES, ETC. WOULD NOT CRANK IMMEDIATELY, TOOK ABOUT 5-10 MINUTES BEFORE IT STARTED AGAIN, MEANWHILE I WAS BLOCKING TRAFFIC AND CREATING A LIFE HAZARD TO MY FAMILY AND OTHER MOTORISTS. THE TRUCK WOULD RUN FOR ABOUT 1 MILE AND DIE AGAIN, WITH NO WARNING AND IN TRAFFIC. THE PROBLEM WAS A CAM SENSOR PART CSS1603. THIS FAILURE COULD EASILY CAUSE AN ACCIDENT AND NEEDS TO BE RECALLED IMMEDIATELY!

Mileage: 78,912

Mar 2, 2007

(1)EVENT WAS INSTANT WITHOUT WARNING. ROADS WERE ICE AND SNOW COVERED. (2) POPPING SOUND FROM ENGINE AND SUDDEN LOSS IN POWER CAUSING MINOR LOSS IN CONTROL. SPEED WAS APPROX 35 MPH. ENGINE CONTINUED TO RUN WITH CONSTANT POPPING NOISE AFTER STOPPED. UPON PULLING OVER AND INSPECTING ENGINE I FOUND A BLOWN SPARK PLUG AND DAMAGE IGNITION COIL. (3) INITIAL CORRECTIVE ACTION WAS THE PURCHASE OF REPLACEMENT SPARK PLUG AND IGNITION COIL BASED ON SPARK PLUG MAINTENANCE. FURTHER INSPECTION REVEALED DAMAGE IN CYLINDER HEAD THREADS CAUSED BY POOR DESIGN STANDARDS. *JB

Mileage: 105,260

Feb 21, 2007

I HAVE A 2001 F250 7.3 DIESEL THAT HAS STALLED OR DIED USUALLY AT LOW SPEEDS WHILE TRYING TO STOP OR TURN A CORNER. RESULTING IN A LOSS OF POWER STEERING AND POWER BRAKES. THE CHECK ENGINE LIGHT HAS NEVER COME ON. I HAVE TAKEN IT TO A MECHANIC AND WAS TOLD IF THE CHECK ENGINE LIGHT WAS NOT ON HE COULD NOT CHECK FOR A TROUBLE CODE. HE ALSO SAID IT MOST LIKELY IS A CAMSHAFT POSITION SENSOR. I CHECKED WITH FORD,THEY WANT OVER $500.00 TO REPLACE IT. THE TRUCK IS NOW OUT OF WARRANTY AND I DON'T WANT TO SPEND $500.00 AND THAT NOT FIX THE PROBLEM. *NM

Mileage: 58,000

Nov 10, 2006

I SHUT OFF MY TRUCK AND SEVERAL COMPONENTS STAY ON, THEN I TURNED THE KEY ON AND OFF AGAIN AND THEY WENT OFF A FEW DAYS LATER THE SAME THING BUT THE WIPERS DID NOT WORK SINCE I AM AN AUTO TECHNICIAN I LOOKED INTO IT AT A FORD DEALER AND FOUND THAT FORD HAS HAD THIS MANY TIMES AND IT HAS BEEN INVESTIGATED BY THE SAFETY BOARD AND I AM NOT SURE WHERE IT WENT FROM THERE ALL I KNOW IS THAT IF I LOSS MY WIPERS ON THE HIGHWAY IN RAIN IT WOULD NOT BE SAFE. I KNOW IN CANADA THEY MADE THEM CALL THEM BACK AND FIX THE LEAKS THAT CAUSED THE WIPER FAILURE/GEM MODULE FAILURE TO FIX IT AT FORD WOULD BE 600.00 DOLLARS WHICH REQUIRES REPLACING THE GEM MODULE AND IT IS RECOMMENDED TO CHANGE THE FUSE PANEL ALSO AND TO FIX THE LEAK THERE WAS A BULLETIN TO SILICONE THE SEAMS WHICH IS A TEMPORARY REPAIR. *JB

Mileage: 89,000

Oct 3, 2006

I WAS DRIVING ON THE HIGHWAY WHEN SUDDENLY LOST POWER TO MY TRUCK. FORTUNATELY I WAS NOT ON A LONG TRIP WITH MY WIFE AND KIDS HAULING A LOAD. I TRIED TO CONTACT A DEALER AND WAS TOLD THEY WERE UNABLE TO SEE ME AFTER SEVERAL WEEKS AND SOME CALLS I WAS ABLE TO LOCATE ONE TO LOOK AT MY TRUCK. AFTER I GAVE MY APPROVAL TO REPAIR THE ENGINE THE RESULT WAS $13.23 IN PARTS AND $779.12 IN LABOR. APPARENTLY A WIRE HARNESS THAT RUNS UNDER THE VALVE COVERS SIMPLY CAME UN PLUGGED. THE DEALER TOLD ME THIS ONLY HAPPENS TO MY TYPE OF VEHICLE AND A STAND OFF BRACKET NEEDED TO BE PUT IN PLACE. I ASKED WHY THIS WASN'T A RECALL ITEM AND THE LADY AT THE COUNTER SAID I SHOULD CALL THE MANUFACTURER. *NM

Mileage: 77,950

Sep 10, 2006

FURTHEST BACK SPARK PLUG BLEW WHILE DRIVING MY 2001 FORD F250 PICK-UP. I ONLY HAVE 76100, MILES ON MY TRUCK THE WARRANTY JUST RAN OUT THE COST OF REPAIRING THIS IS $4300. I WAS TOLD THAT THIS IS A FACTORY DEFECT AND I WANT THIS PROBLEM PUT ON THE RECORD, SO THAT IT CAN BE INVESTIGATED. I STOPPED DRIVING AS SOON AS I HEARD A NOISE AND HAVE KEPT MY VEHICLE IN TOP SHAPE. *JB

Mileage: 76,267

Aug 30, 2006

DT*: THE CONTACT STATED WHILE DRIVING 25 MPH, THERE WAS A SLIGHT SNAPPING NOISE, AND ALL THE GAUGES ON THE INSTRUMENT PANEL FELL TO THE LOWEST READING. THE VEHICLE WAS TAKEN TO A SERVICE DEALER, WHERE THE DEALER WAS NOT ABLE TO DETERMINE THE PROBLEM. UPDATED 9/20/2006 - *NM

Mileage: 94,000

Aug 14, 2006 Fire

MY 2001 FORD F-250 WAS DESTROYED ON 8/11/06 AND APPROXIMATELY 75 ACRES OF RANGE LAND WAS BURNED WHEN THE TRUCK CAUGHT ON FIRE. CONTENTS VALUED AT $1800 WERE ALSO DESTROYED. NO ONE WAS INJURED. THE FIRE STARTED IN THE ENGINE COMPARTMENT WHEN THE ENGINE WAS OFF AND THE KEY WAS NOT IN THE IGNITION. *JB

Mileage: 97,000

Jul 24, 2006

VEHICLE WAS STALLING WITHOUT WARNING. THIS COULD EITHER BE AT A STOP OR MOVING. AFTER TROUBLESHOOTING, I LOCALIZED THE PROBLEM TO THE CAMSHAFT POSITION SENSOR. I TOOK IT TO RIVERTOWN FORD AND ASKED THEM TO PLEASE CHECK IT FOR CPS ERROR CODES, AND BASICALLY GOT BLOWN OFF AS IF I DID NOT KNOW WHAT I WAS TALKING ABOUT. I REPLACED THE CPS AND IT IS NO LONGER STALLING. THIS IS VERY DANGEROUS - I NEARLY WRECKED GOING AROUND A CORNER AT LESS THAN 35 MILES PER HOUR WHEN IT STALLED AND LOST POWER BRAKES AND POWER STEERING. *NM

Mileage: 89,000

Jun 28, 2006

TRAVELING AT NORMAL SPEED. THE ENGINE WOULD SHUT OFF, AS IF IT HAD RUN OUT OF FUEL.. AFTER DOING THIS THREE TIMES, I REPLACED THE CAM SHAFT SENSOR. I HAVE HAD NO PROBLEM SINCE. *JB

Mileage: 129,000

Jun 25, 2006

CAM SENSOR PROBLEMS 2001 F250 POWERSTOKE. *NM

Mileage: 85,000

May 18, 2006

2001 FORD SUPER DUTY PICKUP WITH 7.3 DIESEL, WHILE DRIVING DOWN HIGHWAY THE MOTOR WILL STOP RUNNING,WHICH WILL EFFECT THE POWER STEERING AS WELL AS THE BRAKES. I HAD THE FORD COMPANY CHECK FOR THE PROBLEM, IT WAS THE CAMSHAFT POSITION SENSOR, AFTER CHECKING WITH OTHER SOURCES, THIS IS A COMMON OCCURRENCE WHICH SHOULD BE CORRECTED. *JB

Mar 11, 2006

DRIVING ALONG BUSY ROAD WAY RUNNING FINE, THEN THE MOTOR JUST SHUT DOWN. LEFT STRANDED RIGHT IN THE MIDDLE OF THE ROAD. COULD NOT BE RESTARTED, TRUCK WAS TOWED TO GARAGE. CAM SHAFT SENOR REPLACED. *JB

Mileage: 48,600

Feb 13, 2006

OVERHEAD CONSOLE ON 2001 F250 CREW CAB DIESEL WENT BAD. SINCE THE VERY START THEY HAVE HAD TROUBLE. I HAVE BEEN ON THE NET TO AT LEAST FIVE THOUSAND PEOPLE AND ALL OF THEM HAVE THE MESSAGE CENTER FAILURE. THEY ARE MAKING A KILLING BECAUSE BEFORE YOU COULD BUY THE COMPUTER.THEY HAVE MADE IT NOW WHERE YOU HAVE TO BUY THE WHOLE CONSOLE. $ 300.00 IS THE CHEAPEST YOU WILL FIND. I HAVE MULTIPLE SCLEROSIS AND I NEED A COMPASS TO GET AROUND MY DIRECTION IS OFF. I WOULD CONSIDER THIS NEGLIGENCE BECAUSE THEY WILLINGLY AND KNOWINGLY HAVE KNOWN OF THIS PROBLEM AND HAVE NOT FIXED IT. *NM

Mileage: 12,220

Jul 25, 2005 Fire

DT: THE CONSUMER OWNS A 2001 FORD F250 SUPER DUTY. THE FIRE STARTED ON THE BRAKE PRESSURE SWITCH (WHICH IS THE CUT OFF SWITCH FOR THE CRUISE CONTROL, IT BURNED THE WIRING HARNESS IT BURNED ALL THE WAY UNTIL IT GOT INTO THE HARNESS, AND CAUGHT THE RUBBER BOOT ON FIRE WHICH COVERS THE STEERING CONTROL. THE FIRE WAS ELECTRICAL RELATED. *JB

Jul 18, 2005

WHILE OUT OF TOWN I HAD JUST EXITED THE INTERSTATE WHEN I HEARD A LOUD POP.MY TRUCK, A FORD F250 WITH A 5.4 LTR TRITON V8 STARTED RUNNING TERRIBLE AND MAKING A GOD AWFUL NOISE.I MANAGED TO MAKE IT TO A NEARBY PARKING LOT.I OPENED THE HOOD TO FIND AN IGNITION COIL PACK AND SPARKPLUG LAYING ON TOP OF THE ENGINE.I WAS ABLE TO REINSTALL THE SPARKPLUG AND REPLACED THE COIL PACK DUE (COIL PACK ATTACHMENT EAR HAD BROKEN OFF WHEN PLUG WAS EJECTED FROM ENGINE.).APPROXIMATELY 2 WEEKS LATER MY WIFE AND KIDS WERE ON THEIR WAY TO A LOCAL PARK.THEY HAD JUST TURNED OFF A MAJOR STREET WHEN THEY HEARD A LOUD POP,THEY DESCRIBED AS SOUNDING LIKE A GUNSHOT. THE SAME THING HAPPENED AND TO DATE I'M SUPRISED THAT A FIRE HAS NOT OCCURED OR NO SERIOUS INJURIES HAVE OCCURED. THIS IS VERY DANAGEROUS THE SPARK PLUG IS ACTUALLY EJECTED LIKE A MISSLE.

Mileage: 77,064

Jul 4, 2005 Crash

COMPLETE POWER FAILURE AT SPEEDS UNDER 55 HAS HAPPENED 4 TIMES. TWO TIMES ON A COVER CAUSING POWER STEERING FALURE - WAS UNABLE TO RECOVER AND WENT OFF THE ROAD. VEH WILL START RIGHT AFTER

Mileage: 54,000

Apr 21, 2005 Fire

2001 F250 REGULAR CAB PICKUP [XXX] THE PICKUP WAS PARKED AND CAUGHT ON FIRE. THE FIRE DEPARTMENT SURMISED THAT THE FIRE STARTED IN THE STEERING COLUMN UNDERNEATH THE DASH. THE PICKUP WAS TOTALED IN THE FIRE. *NM *JS INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6)

Dec 1, 2004 Fire

ON NOVEMBER 20TH I CAME HOOME HOME FROM SHOPPING AROUND 8:30PM ,PAPRKED IN DRIVEWAY ,TURNED TRUCK OFF WENT INSIDE TOOL CARE OF DOGS WENT OUT T TRUCK TO GET PACKAGES.CAME IN WENT TO BED AROUND 10:00PM. MY HUSBAND CAME HOME FROM WORK AT 1:30AM PARKED IN DRIVEWAY SDIDNT NOTICE ANYTHING . SUNDAY MORING NOVEMBER 21ST WENT TO START TRUCK(8:55 AM) TO WARM UP BEFORE GOING TOP GET THE PAPER , AND WHEN I OPENED MY DOOR TO THE TRUCK IT SMELT AND WAS BLACK , THE DASH MELTED I CALLED THE POLICE AND THEY CALLED THE FIRE COMPANY THE FIRE WAS OUT .I MADE A POLICE REPORT AND THE FIRE MARSHAL MADE A REPORT ,WHICH HE CONCLUDED THE FIRE STARTED IN THE FOUR WHEEL DRIVE SWICH . LATER THAT WEEK THE INSURANCE MAN CAME LOOKED AT TRUCK AND SAID IT WOULD PROBABLY BE A TOTAL LOSS,WHICH I JUST RECEIVED A LETTER FROM FORD, THEY CAN NOT HELP ME DEAL WITH THE INSURANCE CO.IT WOULD COST ABOUT 12,000. TO FIX AND THE BOOK VALUE IS 23,000.BUT THE FACT IS THAT THE WIRING FROM THE 4X4 SWICH IS WHAT STARTED THE FIRE .I PLAN ON GOING TO FORD WITH THIS BEING THEY DIDNT SEND ANYONE OUT TO LOOK AT MY TRUCK BUT ARE SAYING THEY CANT HELP ME .*AK

Nov 30, 2004

AFTER NOTICING DIFFERENT ELECTRICAL ITEMS REMAINING ENERGIZED AFTER THE IGNITION WAS TURNED OFF I BEGAN DOING SOME RESEARCH. WHAT I HAVE LEARNED THROUGH THE LOCAL FORD DEALER IS THAT THE WINDSHIELD SEALANT COMPOUND USED WAS OF POOR QUALITY FROM THE MANUFACTURER. OVERTIME THIS ALLOWS WATER TO SEEP IN AROUND THE FRONT WINDSHIELD AND DRAINS INTO THE DRIVERS SIDE DASH AREA. THIS LOCATION HOUSES THE FUSE PANEL AND GEM (GENERIC ELECTRONIC MODULE). THE WATER THAT ENTERS THE FUSE PANEL AND GEM CAUSES BOTH UNITS TO SHORT OUT, AND COULD POTENTIALLY CAUSE A FIRE. THE EARLY SIGNS OF A PROBLEM ARE THE AC FAN RUNNING WITH THE IGNITION OFF, THE CLOCK ON THE RADIO FLASHING WHEN IT SHOULD BE OFF (IGNITION OFF), AND THE ELECTRIC WINDOWS, DOOR LOCKS, AND POWER MIRRORS TO WORK INTERMITTENTLY. FORD DEALERS ARE VERY AWARE OF THIS PROBLEM AND STATE THAT THOUGH FORD MOTOR COMPANY ADMITS USING POOR QUALITY SEALANT, THEY REFUSE TO FIX ANY OF THE FUSE BOXES OR GEMS. WHILE INSPECTING THE UNDERSIDE OF MY DASH I HAVE ALSO NOTED THAT THE LINKAGE FOR THE BRAKES, PASSING THROUGH THE FIREWALL, IS EXTREMELY RUSTY. EVENTUALLY THIS RUST COULD CAUSE AN OWNER TO EXPERIENCE BRAKE FAILURE CAUSED BY A BROKEN LINKAGE. *AK

Oct 26, 2004 Fire

VEHICLE WAS PARKED FOR 75 MINUTES AND A PASSERBY NOTICED SMOKE AND ALERTED CONSUMER, WHO SAW FLAMES FROM LEFT FRONT WHEEL WELL. FIRE WAS EXTINGUISHED QUICKLY BY CONSUMER. DAMAGE LIMITED TO AREA WITHIN APPROXIMATELY 12 INCHES OF BRAKE MASTER CYLINDER. ELECTRICAL CONNECTOR BURNED OFF ON MASTER CYLINDER. CONSUMER STATED THAT CRUISE CONTROL STOPPED WORKING SEVERAL MONTHS PRIOR TO THE FIRE. #13 FUSE FOUND OPERATING. *AK

Mileage: 64,401

Nov 29, 2003

ENGINE MIS-FIRES AND LOSES POWER WHEN ACCELERATING FROM STOP/ GOING UP HILLS, ETC. THIS PROBLEM STARTED, ON AN INTERMITTENT BASIS, AT AN ODOMETER READING OF ONLY 9,000 MILES. VEHICLE WAS BROUGHT TO THE DEALER FOUR TIMES OVER 2 YEARS TO REMEDY - - COULD NOT DIAGNOSE OR REPAIR. SUDDENLY BECAME MUCH WORSE AT 48,000 MILES. TWO IGNITION COILS FOUND FAULTY AND REPLACED. NOW SEEING THE SAME PROBLEM AT 51,000 MILES. POTENTIAL SAFETY CONCERN, DUE TO HESITATION/ LACK OF POWER WHEN TURNING LEFT ACROSS TRAFFIC OR CROSSING TRAFFIC LANES. DEALER AND REGIONAL FORD REP. REFUSE TO COVER REPAIRS, EVEN THOUGH THE PROBLEM WAS IDENTIFIED UNDER WARRANTY, BUT NOT FOUND AND FIXED UNTIL OUT OF WARRANTY.*AK

Mileage: 9,423

Nov 28, 2001 Fire

CONSUMER WAS TRAVELING ON HIGHWAY, AND THERE WAS TRANSMISSION FLUID LEAKING FROM UNDER VEHICLE. ALSO THERE WAS A FIRE UNDER HOOD, IN WHICH CONSUMER BELIEVES STARTED WITH THE TRANSMISSION PROBLEMS PRIOR. *AK CONSUMER HAD PROBLEMS WITH TRANSMISSION, THE FIRST DEALER COULD NOT DUPLICATE THE PROBLEM, CONSUMER DECIDED TO TAKE THE VEHICLE TO ANOTHER DEALER FOR THE SECOND OPINION, WHILE ON HIS WAY TO THE DEALER, VEHICLE CAUGHT ON FIRE.*YD