18
Complaints
0
Crashes
2
Fires
0
Deaths
!

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Engine Complaints

Showing 18 of 18
Sep 7, 2016 125,000 mi

TL* THE CONTACT OWNS A 2008 FORD F-250 SD. WHILE DRIVING, THE ENGINE FAILED TO RESPOND. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE ENGINE NEEDED TO BE REPLACED DUE TO A CRACK IN THE NUMBER EIGHT CYLINDER WALL. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTUER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 125,000.

Sep 7, 2016 125,000 mi

TL* THE CONTACT OWNS A 2008 FORD F-250 SD. WHILE DRIVING, THE ENGINE FAILED TO RESPOND. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE ENGINE NEEDED TO BE REPLACED DUE TO A CRACK IN THE NUMBER EIGHT CYLINDER WALL. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTUER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 125,000.

Jan 27, 2016 37,060 mi

I WAS BACKING UP IN THE PARKING AREA OF MY HOUSE IN MY 2008 F250 (DIESEL), AND APPLIED THE BRAKES TO STOP AND CHANGE DIRECTION. AS I STARTED BRAKING, THE ENGINE STARTED ACCELERATING, EVEN THOUGH I WAS APPLYING THE BRAKES. THE VEHICLE KEPT MOVING BACKWARD, AND I HAD TO STAND ON THE BRAKES AND SHIFT INTO NEUTRAL TO GET IT TO STOP MOVING BACKWARD. AFTER A FEW SECONDS THE PROBLEM STOPPED. I THEN CONTINUED ON MY WAY. THE VEHICLE HAD 37,060 MILES.

Jan 27, 2016 37,060 mi

I WAS BACKING UP IN THE PARKING AREA OF MY HOUSE IN MY 2008 F250 (DIESEL), AND APPLIED THE BRAKES TO STOP AND CHANGE DIRECTION. AS I STARTED BRAKING, THE ENGINE STARTED ACCELERATING, EVEN THOUGH I WAS APPLYING THE BRAKES. THE VEHICLE KEPT MOVING BACKWARD, AND I HAD TO STAND ON THE BRAKES AND SHIFT INTO NEUTRAL TO GET IT TO STOP MOVING BACKWARD. AFTER A FEW SECONDS THE PROBLEM STOPPED. I THEN CONTINUED ON MY WAY. THE VEHICLE HAD 37,060 MILES.

Apr 8, 2015 80,121 mi

WE PURCHASED THIS 2008 FORD F-250 SUPER DUTY NEW AT THE FORD STORE IN SAN LEANDRO, CA ON JULY 21, 2007 AND CONTINUE TO BE THE ORIGINAL OWNERS. THIS VEHICLE IS EQUIPPED WITH A 6.4 TURBO-DIESEL ENGINE. THIS VEHICLE IS SUBJECT TO TSB 07-26-2 (WIRING HARNESS DEFECT ON HPFP) ISSUED AUGUST 2007. ON THE MORNING OF MARCH 27, 2015, WHILE ACCELERATING ONTO A FREEWAY AND AT AN APPROXIMATE SPEED OF 50 MPH, THE ENGINE SHUT DOWN WITHOUT ANY WARNING. I LOST ALL ACCELERATION AND THE ENGINE DIED. BRAKING AND STEERING WERE ALSO DIMINISHED. I GOT LUCKY AND WAS ABLE TO AVOID A COLLISION AND COAST TO THE SIDE OF THE ROAD WHERE THE VEHICLE WOULD NOT RESTART. THE VEHICLE WAS TOWED TO A LOCAL REPAIR SHOP (BUD ADAMS - CASTRO VALLEY, CA; BAR#:228593 CAL#:66801). DIAGNOSIS REVEALED A SHORT IN THE WIRING OF THE HIGH PRESSURE FUEL PUMP GASKET WIRING HARNESS (THE SUBJECT OF TSB 07-26-2 WHEREIN FORD RECOGNIZED ON OR ABOUT AUGUST OF 2007 A PROBLEM WITH UNPROTECTED WIRING WITHIN THE HPFP WIRING HARNESS). REPAIRS WERE EXTREMELY COSTLY ($3,791.89 REDUCED TO $2,591.89) BUT MORE IMPORTANTLY THIS INSTANTANEOUS FAILURE WITHOUT WARNING IS GOING TO CAUSE AN ACCIDENT, INJURY OR DEATH; IT IS ONLY A MATTER OF TIME. I GOT LUCKY. I SEE OTHER COMPLAINANTS WHO HAD HOURS STUCK IN THE DESERT, SOMEONE WITH A LOAD OF CATTLE STUCK WITHOUT WARNING, THE LIST GOES ON. IN EACH REPORTED INSTANCE THE OPERATOR DESCRIBED AN IMMEDIATE LOSS OF POWER PLANT WITH NO WARNING. I URGE THE NTSB TO INVESTIGATE THESE UNPLANNED SHUT DOWNS OF THIS VEHICLE'S POWER PLANT. UNDER CERTAIN CIRCUMSTANCES THIS MAY LEAD TO LOSS OF CONTROL OF THE VEHICLE, COLLISION, INJURY AND POSSIBLY DEATH. FORD HAS KNOWN ABOUT THIS ISSUE SINCE AUGUST OF 2007 YET HAS NOT ISSUED A RECALL. SOME MAY SAY THIS IS DUE TO THE LARGE COSTS INVOLVED TO REMOVE AND REPLACE THE HPFP GASKET AND WIRING HARNESS (IN PART INVOLVING THE REMOVAL OF THE VEHICLE'S CAB). *TR

Apr 8, 2015 80,121 mi

WE PURCHASED THIS 2008 FORD F-250 SUPER DUTY NEW AT THE FORD STORE IN SAN LEANDRO, CA ON JULY 21, 2007 AND CONTINUE TO BE THE ORIGINAL OWNERS. THIS VEHICLE IS EQUIPPED WITH A 6.4 TURBO-DIESEL ENGINE. THIS VEHICLE IS SUBJECT TO TSB 07-26-2 (WIRING HARNESS DEFECT ON HPFP) ISSUED AUGUST 2007. ON THE MORNING OF MARCH 27, 2015, WHILE ACCELERATING ONTO A FREEWAY AND AT AN APPROXIMATE SPEED OF 50 MPH, THE ENGINE SHUT DOWN WITHOUT ANY WARNING. I LOST ALL ACCELERATION AND THE ENGINE DIED. BRAKING AND STEERING WERE ALSO DIMINISHED. I GOT LUCKY AND WAS ABLE TO AVOID A COLLISION AND COAST TO THE SIDE OF THE ROAD WHERE THE VEHICLE WOULD NOT RESTART. THE VEHICLE WAS TOWED TO A LOCAL REPAIR SHOP (BUD ADAMS - CASTRO VALLEY, CA; BAR#:228593 CAL#:66801). DIAGNOSIS REVEALED A SHORT IN THE WIRING OF THE HIGH PRESSURE FUEL PUMP GASKET WIRING HARNESS (THE SUBJECT OF TSB 07-26-2 WHEREIN FORD RECOGNIZED ON OR ABOUT AUGUST OF 2007 A PROBLEM WITH UNPROTECTED WIRING WITHIN THE HPFP WIRING HARNESS). REPAIRS WERE EXTREMELY COSTLY ($3,791.89 REDUCED TO $2,591.89) BUT MORE IMPORTANTLY THIS INSTANTANEOUS FAILURE WITHOUT WARNING IS GOING TO CAUSE AN ACCIDENT, INJURY OR DEATH; IT IS ONLY A MATTER OF TIME. I GOT LUCKY. I SEE OTHER COMPLAINANTS WHO HAD HOURS STUCK IN THE DESERT, SOMEONE WITH A LOAD OF CATTLE STUCK WITHOUT WARNING, THE LIST GOES ON. IN EACH REPORTED INSTANCE THE OPERATOR DESCRIBED AN IMMEDIATE LOSS OF POWER PLANT WITH NO WARNING. I URGE THE NTSB TO INVESTIGATE THESE UNPLANNED SHUT DOWNS OF THIS VEHICLE'S POWER PLANT. UNDER CERTAIN CIRCUMSTANCES THIS MAY LEAD TO LOSS OF CONTROL OF THE VEHICLE, COLLISION, INJURY AND POSSIBLY DEATH. FORD HAS KNOWN ABOUT THIS ISSUE SINCE AUGUST OF 2007 YET HAS NOT ISSUED A RECALL. SOME MAY SAY THIS IS DUE TO THE LARGE COSTS INVOLVED TO REMOVE AND REPLACE THE HPFP GASKET AND WIRING HARNESS (IN PART INVOLVING THE REMOVAL OF THE VEHICLE'S CAB). *TR

Oct 28, 2014 130,000 mi

TL* THE CONTACT OWNS A 2008 FORD F-250 SUPER DUTY. WHILE DRIVING 65 MPH, THE STEERING FAILED AS A LOUD ABNORMAL POP SOUND EMITTED FROM THE ENGINE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE ISSUE. THE APPROXIMATE FAILURE MILEAGE WAS 130,000. THE VIN WAS UNAVAILABLE. UPDATED 12/2/14*CN THE CONSUMER STATED THE BOLTS HOLDING THE STEERING BOX ON THE FRAME SHEARED OFF. UPDATED 01/08/15

Oct 28, 2014 130,000 mi

TL* THE CONTACT OWNS A 2008 FORD F-250 SUPER DUTY. WHILE DRIVING 65 MPH, THE STEERING FAILED AS A LOUD ABNORMAL POP SOUND EMITTED FROM THE ENGINE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE ISSUE. THE APPROXIMATE FAILURE MILEAGE WAS 130,000. THE VIN WAS UNAVAILABLE. UPDATED 12/2/14*CN THE CONSUMER STATED THE BOLTS HOLDING THE STEERING BOX ON THE FRAME SHEARED OFF. UPDATED 01/08/15

Aug 20, 2014 30,000 mi

2008 FORD F 250 SUPER DUTY DIESEL 6.4 ENGINE - ENGINE QUIT RUNNING WITH NO WARNING, WOULD NOT RESTART. WAS IN THE MIDDLE OF A LONG BRIDGE OVER THE MISSISSIPPI RIVER. THIS WAS A MAJOR INCONVENIENCE. HAD TO BE TOWED TO DEALER. TSB 07-26-2 WAS PERFORMED TO FIX THE KNOWN PROBLEM OF AN UNPROTECTED WIRE IN THE HIGH PRESSURE FUEL PUMP GASKET CHAFFING THROUGH. THIS WAS AN EXPENSIVE REPAIR SINCE THE CAB HAD TO BE REMOVED. A REVISED GASKET WITH PROTECTED WIRE WAS INSTALLED. LUCKILY I WAS NOT TOWING OUR 5TH WHEEL AT THE TIME. THIS IS A SERIOUS SAFETY RISK. FORD SHOULD RECALL AND COVER THE EXPENSE TO REPAIR AS THIS WAS A KNOWN DESIGN FLAW. *TR

Aug 20, 2014 30,000 mi

2008 FORD F 250 SUPER DUTY DIESEL 6.4 ENGINE - ENGINE QUIT RUNNING WITH NO WARNING, WOULD NOT RESTART. WAS IN THE MIDDLE OF A LONG BRIDGE OVER THE MISSISSIPPI RIVER. THIS WAS A MAJOR INCONVENIENCE. HAD TO BE TOWED TO DEALER. TSB 07-26-2 WAS PERFORMED TO FIX THE KNOWN PROBLEM OF AN UNPROTECTED WIRE IN THE HIGH PRESSURE FUEL PUMP GASKET CHAFFING THROUGH. THIS WAS AN EXPENSIVE REPAIR SINCE THE CAB HAD TO BE REMOVED. A REVISED GASKET WITH PROTECTED WIRE WAS INSTALLED. LUCKILY I WAS NOT TOWING OUR 5TH WHEEL AT THE TIME. THIS IS A SERIOUS SAFETY RISK. FORD SHOULD RECALL AND COVER THE EXPENSE TO REPAIR AS THIS WAS A KNOWN DESIGN FLAW. *TR

Jun 20, 2013 160,000 mi

2008 FORD F-250 SD DIESEL NO WARNING DRIVING 55 ON THE FREEWAY TOWING A TRAILER THE TRUCK SHUTS DOWN NO POWER. THIS IS THE 3RD TIME THIS TRUCK HAS SHUT DOWN ON THE FREEWAY WITH NO WARNING. HOW CAN FORD SELL THEIR CUSTOMERS A TRUCK AS WHAT ONE OTHER PERSON STATES: A $55,000.00 TRUCK THAT IS ADVERTISED TO BE SUPER DUTY AND SHOULD LAST 400000 TO 500000 MILES WITH ONLY MINER ENGINE REPAIRS, THIS SHOULD NOT BE HAPPENING. FORD KNOWS FOR A FACT THAT THEY HAVE A FAULTY MOTOR AND FAULTY INTERNAL PARTS ON ALL THE 2008 THRU 2010 6.4 L DIESEL MOTORS. THAT'S WHY THEY DESIGNED A NEW MOTOR AND ARE SUING NAVISTAR THE ENGINE DESIGNER. NOW YOU CAN GO ALL OVER THE INTERNET AND FIND THOUSANDS OF CUSTOMERS WITH THE SAME PROBLEMS AND MORE. THIS IS OUR SECOND TIME TO ENTER A COMPLAINT IN THE NHTSA (#10435125) DOES ANYTHING HAPPEN WITH THIS INFORMATION? *TR

Jun 20, 2013 160,000 mi

2008 FORD F-250 SD DIESEL NO WARNING DRIVING 55 ON THE FREEWAY TOWING A TRAILER THE TRUCK SHUTS DOWN NO POWER. THIS IS THE 3RD TIME THIS TRUCK HAS SHUT DOWN ON THE FREEWAY WITH NO WARNING. HOW CAN FORD SELL THEIR CUSTOMERS A TRUCK AS WHAT ONE OTHER PERSON STATES: A $55,000.00 TRUCK THAT IS ADVERTISED TO BE SUPER DUTY AND SHOULD LAST 400000 TO 500000 MILES WITH ONLY MINER ENGINE REPAIRS, THIS SHOULD NOT BE HAPPENING. FORD KNOWS FOR A FACT THAT THEY HAVE A FAULTY MOTOR AND FAULTY INTERNAL PARTS ON ALL THE 2008 THRU 2010 6.4 L DIESEL MOTORS. THAT'S WHY THEY DESIGNED A NEW MOTOR AND ARE SUING NAVISTAR THE ENGINE DESIGNER. NOW YOU CAN GO ALL OVER THE INTERNET AND FIND THOUSANDS OF CUSTOMERS WITH THE SAME PROBLEMS AND MORE. THIS IS OUR SECOND TIME TO ENTER A COMPLAINT IN THE NHTSA (#10435125) DOES ANYTHING HAPPEN WITH THIS INFORMATION? *TR

Apr 1, 2013 Fire 179,000 mi

TL* THE CONTACT OWNS A 2008 FORD F-250 SD. THE CONTACT STATED THAT WHILE DRIVING AT VARIOUS SPEEDS HE NOTICED THAT WHITE SMOKE WOULD EMIT FROM THE EXHAUST SYSTEM. THE CONTACT STATED THAT THE EXHAUST SYSTEM WAS EQUIPPED WITH A SELF-CLEANING FUNCTION HOWEVER, THE WHITE SMOKE STILL EMITTED AFTER THE FUNCTION WAS COMPLETED. THE VEHICLE WAS NOT TAKEN TO THE DEALER OR AN INDEPENDENT MECHANIC. THE MANUFACTURER WAS CONTACTED AND THEY OFFERED NO ASSISTANCE. THE FAILURE MILEAGE WAS APPROXIMATELY 179,000. THE CURRENT MILEAGE WAS APPROXIMATELY 180,000. THE VIN WAS UNAVAILABLE. *TR

Apr 1, 2013 Fire 179,000 mi

TL* THE CONTACT OWNS A 2008 FORD F-250 SD. THE CONTACT STATED THAT WHILE DRIVING AT VARIOUS SPEEDS HE NOTICED THAT WHITE SMOKE WOULD EMIT FROM THE EXHAUST SYSTEM. THE CONTACT STATED THAT THE EXHAUST SYSTEM WAS EQUIPPED WITH A SELF-CLEANING FUNCTION HOWEVER, THE WHITE SMOKE STILL EMITTED AFTER THE FUNCTION WAS COMPLETED. THE VEHICLE WAS NOT TAKEN TO THE DEALER OR AN INDEPENDENT MECHANIC. THE MANUFACTURER WAS CONTACTED AND THEY OFFERED NO ASSISTANCE. THE FAILURE MILEAGE WAS APPROXIMATELY 179,000. THE CURRENT MILEAGE WAS APPROXIMATELY 180,000. THE VIN WAS UNAVAILABLE. *TR

Dec 28, 2012 107,000 mi

EXHAUST LEAK FROM BEHIND THE TURBO. EXHAUST ENTERS THE INSIDE OF THE CAB. SEEMS TO BE A COMMON PROBLEM. EXPENSIVE TO FIX. MUST REMOVE CAB FROM FRAME TO REPAIR. HAZARDOUS FUMES ENTER VEHICLE CAUSING HEADACHES. DEALER IS ACTING LIKE THIS IS RARE BUT IN SEARCHING THE WEB I HAVE SEEN NUMEROUS COMPLAINTS OF THE SAME PROBLEM I AM HAVING. *TR ## VIN FAILED ##

Dec 28, 2012 107,000 mi

EXHAUST LEAK FROM BEHIND THE TURBO. EXHAUST ENTERS THE INSIDE OF THE CAB. SEEMS TO BE A COMMON PROBLEM. EXPENSIVE TO FIX. MUST REMOVE CAB FROM FRAME TO REPAIR. HAZARDOUS FUMES ENTER VEHICLE CAUSING HEADACHES. DEALER IS ACTING LIKE THIS IS RARE BUT IN SEARCHING THE WEB I HAVE SEEN NUMEROUS COMPLAINTS OF THE SAME PROBLEM I AM HAVING. *TR ## VIN FAILED ##

Jul 8, 2012 39,000 mi

I NOTICED THAT SOMETHING WAS DRIPPING FROM THE FRONT END OF MY TRUCK AND SUSPECTED THAT THE RADIATOR WAS LEAKING. I TOOK IT TO THE DEALERSHIP TO DIAGNOSE THE PROBLEM. I ALSO GAVE THEM SEVERAL TSBSS CONCERNING THE RADIATOR LEAK TO MAKE THEM AWARE THAT THIS IS A KNOWN PROBLEM TO FORD. OBVIOUSLY THEY CALLED ME BACK AND SAID THAT THE ENTIRE COOLING SYSTEM (RADIATOR, HOSES AND DEGAS BOTTLE) NEEDED REPLACEMENT, IT WASN'T UNDER WARRANTY AND I WOULD NEED TO PAY $1,776. I ONLY HAVE 39K MILES ON IT AND I NEVER THOUGHT THAT I WOULD BE REPLACING A RADIATOR THIS SOON. I HAVE ALWAYS BABIED THIS TRUCK AND MAINTAINED IT REGULARLY. I FEEL THAT FORD KNEW ABOUT THIS DESIGN FLAW AND SHOULD BE HELD ACCOUNTABLE FOR THE COSTS INCURRED BY ME TO REPAIR THE PROBLEM. WHO IS TO SAY THAT THIS MAY NOT OCCUR AGAIN DOWN THE ROAD? I HAVE READ THAT IT IS NOT UNCOMMON FOR TRUCKS NEEDING SEVERAL REPLACEMENT RADIATORS. IT'S CONCERNING TO ME THAT FORD CAN GET AWAY WITH THIS KIND OF DESIGN FLAW (OR SCAM) WITHOUT ANY REPERCUSSION FROM OUR GOVERNMENT. *TR

Jul 8, 2012 39,000 mi

I NOTICED THAT SOMETHING WAS DRIPPING FROM THE FRONT END OF MY TRUCK AND SUSPECTED THAT THE RADIATOR WAS LEAKING. I TOOK IT TO THE DEALERSHIP TO DIAGNOSE THE PROBLEM. I ALSO GAVE THEM SEVERAL TSBSS CONCERNING THE RADIATOR LEAK TO MAKE THEM AWARE THAT THIS IS A KNOWN PROBLEM TO FORD. OBVIOUSLY THEY CALLED ME BACK AND SAID THAT THE ENTIRE COOLING SYSTEM (RADIATOR, HOSES AND DEGAS BOTTLE) NEEDED REPLACEMENT, IT WASN'T UNDER WARRANTY AND I WOULD NEED TO PAY $1,776. I ONLY HAVE 39K MILES ON IT AND I NEVER THOUGHT THAT I WOULD BE REPLACING A RADIATOR THIS SOON. I HAVE ALWAYS BABIED THIS TRUCK AND MAINTAINED IT REGULARLY. I FEEL THAT FORD KNEW ABOUT THIS DESIGN FLAW AND SHOULD BE HELD ACCOUNTABLE FOR THE COSTS INCURRED BY ME TO REPAIR THE PROBLEM. WHO IS TO SAY THAT THIS MAY NOT OCCUR AGAIN DOWN THE ROAD? I HAVE READ THAT IT IS NOT UNCOMMON FOR TRUCKS NEEDING SEVERAL REPLACEMENT RADIATORS. IT'S CONCERNING TO ME THAT FORD CAN GET AWAY WITH THIS KIND OF DESIGN FLAW (OR SCAM) WITHOUT ANY REPERCUSSION FROM OUR GOVERNMENT. *TR