2002 FORD F-250 Power Train Problems

16 complaints about Power Train

16
Complaints
0
Crashes
0
Fires
0
Deaths

This Problem Across All Years

All Power Train Complaints (16)

May 30, 2014

TL* THE CONTACT OWNS A 2002 FORD F-250. THE CONTACT STATED THAT THE ACCELERATOR PEDAL FAILED TO RESPOND WITHOUT WARNING. THE VEHICLE WAS TAKEN TO A DEALER WHERE THE TECHNICIAN DIAGNOSED THAT A WIRE SHORTAGE AND THE TRANSMISSION SHIFT LEVER NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 215,000 AND THE CURRENT MILEAGE WAS 215,100. UPDATED 2/3/15*CN UPDATED 8/30/2017*CN

Mileage: 215,000

May 30, 2014

TL* THE CONTACT OWNS A 2002 FORD F-250. THE CONTACT STATED THAT THE ACCELERATOR PEDAL FAILED TO RESPOND WITHOUT WARNING. THE VEHICLE WAS TAKEN TO A DEALER WHERE THE TECHNICIAN DIAGNOSED THAT A WIRE SHORTAGE AND THE TRANSMISSION SHIFT LEVER NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 215,000 AND THE CURRENT MILEAGE WAS 215,100. UPDATED 2/3/15*CN UPDATED 8/30/2017*CN

Mileage: 215,000

Oct 10, 2012

AFTER COMING TO A STOP AT A RETAIL PARKING LOT, I COULD NOT SHIFT INTO PARK. IT FELT AS THOUGH THE SHIFT LEVER HAD BECOME UNATTACHED FROM THE TRANSMISSION. I SHUT THE VEHICLE OFF WHILE IN DRIVE AND APPLIED THE PARKING BRAKE. INVESTIGATION REVEALED THAT THE BRACKET THAT IS ATTACHED TO THE TRANSMISSION TO HOLD THE SHIFT CABLE TO ALLOW SHIFTING OF THE TRANSMISSION, BROKE AWAY FROM THE TRANSMISSION THREADED MOUNTING BOSSES. THE ALUMINUM THREADED MOUNTING BOSSES CRUMBLED WITH SEVERAL PIECES FALLING TO THE GROUND. THE INABILITY OF PLACING THE VEHICLE INTO NEUTRAL OR PARK ESPECIALLY AT A TIME OF URGENCY IS OF GREAT CONCERN TO ME. A REPAIR OPTION SHORT OF REPLACING THE TRANSMISSION HAS NOT YET BEEN DISCOVERED. SEVERAL FORD DEALERS SAID THAT THEY HAVE NEVER HEARD OF SUCH AN ISSUE. MY MECHANIC WHO IS TRYING TO DEVELOP A MAKE-SHIFT BRACKET STATED HE HAS SEEN MANY CASES ON WEB SITES THAT ARE AVAILABLE TO REPAIR STATIONS. ONE GOOGLE SEARCH ON FORD TRUCK FORUM SHOWED AN IDENTICAL PROBLEM SUCH AS MINE. THANK YOU *TR

Mileage: 61,253

Aug 23, 2011

HAVE HAD APPROXIMATELY $8000 IN CAR REPAIR BILLS IN LAST FEW MONTHS FOR OUR 2002 FORD F250 DIESEL TRUCK AND 2005 FORD EXPLORER XLT. TREMENDOUS FINANCIAL BURDEN 2002 FORD F250 DIESEL TRUCK - HUBS SEIZED, LOSS OF CONTROL OF VEHICLE PREMATURE RUSTING OF VEHICLE BODY, TAILGATE BUT MOST IMPORTANTLY THE OIL PAN IN WHICH REPLACING THE OLD PAN BECAME AN APPROXIMATELY $3,000 REPAIR BILL. 2005 FORD EXPLORER - TRANSMISSION WENT AT 80,000 MILES! HUBS SEIZE. *TR

Mileage: 70,000

Feb 22, 2007

FORD F250 WITH TRANSMISSION PROBLEMS. CONSUMER STATED THAT HE IS EXTREMELY FRUSTRATED AND DISPLEASED WITH THE BUSINESS PRACTICES OF DEALER**CC THE VEHICLE WAS PURCHASED USED. THE VEHICLE WAS TAKEN TO THE DEALER BECAUSE IT WOULD NOT OPERATE IN REVERSE. THE DEALER WAS UNABLE TO DETERMINE THE CAUSE OF THE PROBLEM THEREFORE THE VEHICLE WAS TAKEN TO ANOTHER DEALER. THAT DEALER DETERMINED THAT THE PROBLEM WAS WITH THE TRANSMISSION. SINCE THE VEHICLE WAS UNDER WARRANTY THE CONSUMER TOOK IT BACK TO THE SALES DEALER. THEY CLAIMED THAT THEY WOULD NOT BE ABLE TO REPAIR THE VEHICLE BECAUSE OF AFTER MARKET ALTERATIONS. ALL ALTERATIONS WERE MADE PRIOR TO THE CONSUMER ACQUIRING THE VEHICLE. *NM

May 31, 2005

ON TWO OCCASIONS, I HAVE HAD MY TRUCK IN PARK AND THE KEYS REMOVED AND THE TRUCK ROLLED. IT WAS NOT FULLY IN PARK. I WAS ON A SLIGHT INCLINE BOTH TIMES, ONCE FACING FORWARD AND ONCE BACKED IN. I TOOK IT TO THE DEALER AFTER THE FIRST TIME AND THEY ADJUSTED THE SHIFTER. I NOW HAVE TO TAKE IT BACK IN SINCE IT DID IT AGAIN.

Mileage: 28,000

Jan 20, 2004

CLUTCH ENGAGES WITHOUT WARNING. DEALER STATES THAT THIS IS A NORMAL PROCEDURE.*AK

Mileage: 39,500

Nov 18, 2002

CONSUMER STATES WHILE STUCK IN SNOW BANK WITH FOUR WHEEL DRIVE ON THE FOUR WHEEL DRIVE WOULD NOT ENGAGE. CONSUMER NOTICE GRINDING NOISE. DEALER HAS BEEN CONTACTED PLEASE PROVIDE FURTHER INFORMATION. TS

Aug 30, 2002

THE VEHICLE WILL LOSE POWER WITH THE ENGINE LIGHT COMING ON, CAUSE UNKNOWN. THE FORD DEALERSHIP HAS HAD THE VEHICLE FOR THREE DAYS, STATING THAT VEHICLE WAS GETTING SOME SORT OF RESISTANCE. THE VEHICLE WAS AGAIN FAILING WITH THE SAME PROBLEM. *AK THE CONSUMER STATES THAT HE HAD TAKEN THE VEHICLE TO ANOTHER FORD DEALER AND THEY SEEMED TO HAVE REMEDIED THE PROBLEM-LINKAGE ACCELERATOR. THE WINDSHIELD WAS LEAKING-RESEALED-STILL LEAKING. THE VEHICLE HAS BEEN OKAY SINCE THE LAST REPAIR. NOW THE WINDSHIELD IS LEAKING WATER, AND IS RUNNING BEHIND THE DASHBOARD. THE CONSUMER HAS ALSO EXPERIENCED THE FOLLOWING: WHEN STOPPING THE VEHICLE FEELS LIKE THE DRIVLINE SHIFTS FORWARD-LOUD BANG,WHEN STARTING OFF, THE VEHICLE SHIFTS BACKWARDS, THE CONNECTOR IS NOT FULLY SEATED(PCM MODULE), AND THE INJECTOR HARNESS INTERMITTENLY OPENS-REPAIR LOOSE LEFT VALVE COVER INJECTOR HARNESS CONNECTOR CAUSING HIGH RESISTANCE CLEARED. *SCC

Aug 30, 2002

THE VEHICLE WILL LOSE POWER WITH THE ENGINE LIGHT COMING ON, CAUSE UNKNOWN. THE FORD DEALERSHIP HAS HAD THE VEHICLE FOR THREE DAYS, STATING THAT VEHICLE WAS GETTING SOME SORT OF RESISTANCE. THE VEHICLE WAS AGAIN FAILING WITH THE SAME PROBLEM. *AK THE CONSUMER STATES THAT HE HAD TAKEN THE VEHICLE TO ANOTHER FORD DEALER AND THEY SEEMED TO HAVE REMEDIED THE PROBLEM-LINKAGE ACCELERATOR. THE WINDSHIELD WAS LEAKING-RESEALED-STILL LEAKING. THE VEHICLE HAS BEEN OKAY SINCE THE LAST REPAIR. NOW THE WINDSHIELD IS LEAKING WATER, AND IS RUNNING BEHIND THE DASHBOARD. THE CONSUMER HAS ALSO EXPERIENCED THE FOLLOWING: WHEN STOPPING THE VEHICLE FEELS LIKE THE DRIVLINE SHIFTS FORWARD-LOUD BANG,WHEN STARTING OFF, THE VEHICLE SHIFTS BACKWARDS, THE CONNECTOR IS NOT FULLY SEATED(PCM MODULE), AND THE INJECTOR HARNESS INTERMITTENLY OPENS-REPAIR LOOSE LEFT VALVE COVER INJECTOR HARNESS CONNECTOR CAUSING HIGH RESISTANCE CLEARED. *SCC

Aug 30, 2002

THE VEHICLE WILL LOSE POWER WITH THE ENGINE LIGHT COMING ON, CAUSE UNKNOWN. THE FORD DEALERSHIP HAS HAD THE VEHICLE FOR THREE DAYS, STATING THAT VEHICLE WAS GETTING SOME SORT OF RESISTANCE. THE VEHICLE WAS AGAIN FAILING WITH THE SAME PROBLEM. *AK THE CONSUMER STATES THAT HE HAD TAKEN THE VEHICLE TO ANOTHER FORD DEALER AND THEY SEEMED TO HAVE REMEDIED THE PROBLEM-LINKAGE ACCELERATOR. THE WINDSHIELD WAS LEAKING-RESEALED-STILL LEAKING. THE VEHICLE HAS BEEN OKAY SINCE THE LAST REPAIR. NOW THE WINDSHIELD IS LEAKING WATER, AND IS RUNNING BEHIND THE DASHBOARD. THE CONSUMER HAS ALSO EXPERIENCED THE FOLLOWING: WHEN STOPPING THE VEHICLE FEELS LIKE THE DRIVLINE SHIFTS FORWARD-LOUD BANG,WHEN STARTING OFF, THE VEHICLE SHIFTS BACKWARDS, THE CONNECTOR IS NOT FULLY SEATED(PCM MODULE), AND THE INJECTOR HARNESS INTERMITTENLY OPENS-REPAIR LOOSE LEFT VALVE COVER INJECTOR HARNESS CONNECTOR CAUSING HIGH RESISTANCE CLEARED. *SCC

Aug 26, 2002

AFTER MARKET TRACTION BARS DEFECTIVE. *AK

Jul 10, 2002

VEHICLE WAS PARKED AND OFF. 21/2 YEARS OLD CHILD WAS ABLE TO SHIFT GEAR OUT OF PARK. DEALER AND MANUFACTURER WERE NOT NOTIFIED AT THIS TIME. FEEL FREE TO PROVIDE ANY FURTHER INFROMATION.*AK

Jun 21, 2002

NO SUMMARY LISTED FOR ABOVE VEHICLE. *AK

Feb 22, 2002

THE MODULE ACTAVATING THE TORQUE CONVERTER IS ENGAGING AT IDLE, CAUSING TRANSMISSION TO ENGAGE, AND VEHICLE TO SURGED FORWARD WITHOUT MANUALLY APPLYING ACCELERATOR.*AK

Feb 22, 2002

THE MODULE ACTAVATING THE TORQUE CONVERTER IS ENGAGING AT IDLE, CAUSING TRANSMISSION TO ENGAGE, AND VEHICLE TO SURGED FORWARD WITHOUT MANUALLY APPLYING ACCELERATOR.*AK