Compare to Other Years

Complaints

Showing 20 of 110
May 23, 2015 Suspension 180,746 mi

WHILE DRIVEING AT 60 MPH THERE WAS A LOUD CRASH FROM THE LEFT REAR THEN A GRINDING POP FROM THE LEFT REAR ALL WHILE THE REAR END OF MY TRUCK FELT LIKE IT WAS FISH TAILING ON ICE OR LIKE SOME ONE HUGE WAS SHAKEING IT FROM SIDE TO SIDE I ALMOST LOST IT INTO A FIELD I WAS SO SUPRISED I GOT STOPPED TO L...

May 23, 2015 Suspension 180,746 mi

WHILE DRIVEING AT 60 MPH THERE WAS A LOUD CRASH FROM THE LEFT REAR THEN A GRINDING POP FROM THE LEFT REAR ALL WHILE THE REAR END OF MY TRUCK FELT LIKE IT WAS FISH TAILING ON ICE OR LIKE SOME ONE HUGE WAS SHAKEING IT FROM SIDE TO SIDE I ALMOST LOST IT INTO A FIELD I WAS SO SUPRISED I GOT STOPPED TO L...

Sep 17, 2014 Engine Fire 140,000 mi

THE TRUCK WAS PARKED IN A STRIP MALL PARKING LOT. A FEW MINUTES LATER SOMEONE SAID THAT THERE WERE FLAMES COMING FROM THE HOOD. THE CAR WAS A TOTAL IN 10 MINUTES. FOUR OFF DUTY FIREMEN WERE THERE AND COULD NOT PUT THE FLAMES OUT. NEAR BY FIRE STATION WAS CALLED. ITS RESPONSE WAS WITH IN A FEW ...

Sep 17, 2014 Engine Fire 140,000 mi

THE TRUCK WAS PARKED IN A STRIP MALL PARKING LOT. A FEW MINUTES LATER SOMEONE SAID THAT THERE WERE FLAMES COMING FROM THE HOOD. THE CAR WAS A TOTAL IN 10 MINUTES. FOUR OFF DUTY FIREMEN WERE THERE AND COULD NOT PUT THE FLAMES OUT. NEAR BY FIRE STATION WAS CALLED. ITS RESPONSE WAS WITH IN A FEW ...

Jul 16, 2014 Vehicle Speed Control 199,400 mi

WHILE DRIVING AT HIGHWAY SPEEDS, THE VEHICLE STARTED SURGING UP AND DOWN IN SPEED ERRATICALLY. I DID NOT REALIZE THAT IT HAD TO DO WITH THE SPEED CONTROL, BUT FINALLY TOOK IT OUT OF CRUISE FOR GOOD. THE SPEEDOMETER STILL WAS SURGING UP AND DOWN BETWEEN 4 AND 10 MPH DIFFERENCE FROM WHAT MY SPEED WA...

Jul 16, 2014 Vehicle Speed Control 199,400 mi

WHILE DRIVING AT HIGHWAY SPEEDS, THE VEHICLE STARTED SURGING UP AND DOWN IN SPEED ERRATICALLY. I DID NOT REALIZE THAT IT HAD TO DO WITH THE SPEED CONTROL, BUT FINALLY TOOK IT OUT OF CRUISE FOR GOOD. THE SPEEDOMETER STILL WAS SURGING UP AND DOWN BETWEEN 4 AND 10 MPH DIFFERENCE FROM WHAT MY SPEED WA...

Apr 24, 2012 Engine And Engine Cooling 82,000 mi

WHEN I FIRST BOUGHT THE TRUCK IN 2001, THE ENGINE HAD APPROXIMATELY 82K MILES. I WAS HAVING A HARD TIME STARTING AND SOMETIMES IT WOULD NOT START. AT FIRST THE DEALER THOUGHT IT WAS THE STARTER AND THEY REPLACED IT. THEY TOLD ME TO TAKE IT TO PEPBOYS TO GET THE STARTER REPLACED. WHEN THEY STARTE...

Apr 24, 2012 Engine And Engine Cooling 82,000 mi

WHEN I FIRST BOUGHT THE TRUCK IN 2001, THE ENGINE HAD APPROXIMATELY 82K MILES. I WAS HAVING A HARD TIME STARTING AND SOMETIMES IT WOULD NOT START. AT FIRST THE DEALER THOUGHT IT WAS THE STARTER AND THEY REPLACED IT. THEY TOLD ME TO TAKE IT TO PEPBOYS TO GET THE STARTER REPLACED. WHEN THEY STARTE...

Jan 16, 2012 Fuel System, Gasoline 165,091 mi

RECALL CORRECTION TURNS TO EXPLOSION DANGER! FORD ISSUED RECALL #11 S 21 ON THE REPLACEMENT OF THE FUEL TANK STRAPS. BEST FORD OF NASHUA PERFORMED THE SERVICE TO INSTALL NEW STRAPS ON OCTOBER 7, 2011. IN CONJUNCTION WITH THE RECALL WORK, A VEHICLE REPORT ON BEST FORD LETTERHEAD WAS PROVIDED SHOWI...

Jan 16, 2012 Fuel System, Gasoline 165,091 mi

RECALL CORRECTION TURNS TO EXPLOSION DANGER! FORD ISSUED RECALL #11 S 21 ON THE REPLACEMENT OF THE FUEL TANK STRAPS. BEST FORD OF NASHUA PERFORMED THE SERVICE TO INSTALL NEW STRAPS ON OCTOBER 7, 2011. IN CONJUNCTION WITH THE RECALL WORK, A VEHICLE REPORT ON BEST FORD LETTERHEAD WAS PROVIDED SHOWI...

May 15, 2011 Fuel System, Gasoline 150,000 mi

AFTER FILLING UP THE GAS TANK, PULLED OUT ON TO THE ROAD, SMALL BUMP IN THE INTERSECTION. RUSTED STRAPS BROKE AND GAS TANK FELL OFF. LUCKY IT WAS RAINING AND ROAD WAS WET OR COULD OF CAUSED FIRE. *TR

May 15, 2011 Fuel System, Gasoline 150,000 mi

AFTER FILLING UP THE GAS TANK, PULLED OUT ON TO THE ROAD, SMALL BUMP IN THE INTERSECTION. RUSTED STRAPS BROKE AND GAS TANK FELL OFF. LUCKY IT WAS RAINING AND ROAD WAS WET OR COULD OF CAUSED FIRE. *TR

Jan 4, 2011 Fuel System, Gasoline 126,393 mi

WAS FORTUNATE TO NOTICE GAS TANK HANGING DOWN FROM UNDER CARRIAGE... WAS PREPARING TO DRIVE 50 MILE IN ON INTERSTATE... WAS ABLE TO DRIVE TO LOCAL DEALER...NOT WHERE PURCHASED... AND THEY INSTALLED A NEW GAS TANK STRAP..WHICH WITH LABOR WAS 93 DOLLARS... WELL WORTH IT WHEN CONSIDERING WHAT COULD HAV...

Jan 4, 2011 Fuel System, Gasoline 126,393 mi

WAS FORTUNATE TO NOTICE GAS TANK HANGING DOWN FROM UNDER CARRIAGE... WAS PREPARING TO DRIVE 50 MILE IN ON INTERSTATE... WAS ABLE TO DRIVE TO LOCAL DEALER...NOT WHERE PURCHASED... AND THEY INSTALLED A NEW GAS TANK STRAP..WHICH WITH LABOR WAS 93 DOLLARS... WELL WORTH IT WHEN CONSIDERING WHAT COULD HAV...

Oct 4, 2010 Fuel System, Gasoline 173,051 mi

WALKING TO MY TRUCK I NOTICE THE REAR FUEL TANK STRAP BROKEN AND HANGING AND THE FUEL TANK HANGING FROM THE FRONT STRAP ONLY. THE REAR STRAP WAS TOTALLY RUSTED THROUGH. THE RUST ALSO RUSTED THE TANK I AND I HAD TO REPLACE THE TANK AS WELL ON 10/3/2010. *TR

Oct 4, 2010 Fuel System, Gasoline 173,051 mi

WALKING TO MY TRUCK I NOTICE THE REAR FUEL TANK STRAP BROKEN AND HANGING AND THE FUEL TANK HANGING FROM THE FRONT STRAP ONLY. THE REAR STRAP WAS TOTALLY RUSTED THROUGH. THE RUST ALSO RUSTED THE TANK I AND I HAD TO REPLACE THE TANK AS WELL ON 10/3/2010. *TR

Sep 14, 2010 Fuel System, Other 184,000 mi

I OWN A 1997 FORD F-150 PIK UP TRUCK. BOTH STRAPS THAT HOLD THE GAS TANK IN PLACE HAVE BROKEN IN TWO SEPARATE INCIDENTS. *TR

Sep 14, 2010 Fuel System, Other 184,000 mi

I OWN A 1997 FORD F-150 PIK UP TRUCK. BOTH STRAPS THAT HOLD THE GAS TANK IN PLACE HAVE BROKEN IN TWO SEPARATE INCIDENTS. *TR

Aug 18, 2010 Electrical System Fire 200,000 mi

ON AUGUST 1, 2010, OUR FORD F150 (VIN [XXX]) STARTED ON FIRE AND BURNED FROM THE ENGINE ON OUT. THE HOOD IS TOTALLY BURNED THROUGH AND THE WINDSHIELD ALSO BURNED. THE ENTIRE ENGINE COMPARTMENT IS RUINED. THE TRUCK WAS IN OUR DRIVEWAY AT THE TIME AND WE WERE ALERTED MY NEIGHBORS WHO SAW FLAMES SHOOTI...

Aug 18, 2010 Fuel System, Other Fire 200,000 mi

ON AUGUST 1, 2010, OUR FORD F150 (VIN [XXX]) STARTED ON FIRE AND BURNED FROM THE ENGINE ON OUT. THE HOOD IS TOTALLY BURNED THROUGH AND THE WINDSHIELD ALSO BURNED. THE ENTIRE ENGINE COMPARTMENT IS RUINED. THE TRUCK WAS IN OUR DRIVEWAY AT THE TIME AND WE WERE ALERTED MY NEIGHBORS WHO SAW FLAMES SHOOTI...

Aug 18, 2010 Electrical System Fire 200,000 mi

ON AUGUST 1, 2010, OUR FORD F150 (VIN [XXX]) STARTED ON FIRE AND BURNED FROM THE ENGINE ON OUT. THE HOOD IS TOTALLY BURNED THROUGH AND THE WINDSHIELD ALSO BURNED. THE ENTIRE ENGINE COMPARTMENT IS RUINED. THE TRUCK WAS IN OUR DRIVEWAY AT THE TIME AND WE WERE ALERTED MY NEIGHBORS WHO SAW FLAMES SHOOTI...

Aug 18, 2010 Fuel System, Other Fire 200,000 mi

ON AUGUST 1, 2010, OUR FORD F150 (VIN [XXX]) STARTED ON FIRE AND BURNED FROM THE ENGINE ON OUT. THE HOOD IS TOTALLY BURNED THROUGH AND THE WINDSHIELD ALSO BURNED. THE ENTIRE ENGINE COMPARTMENT IS RUINED. THE TRUCK WAS IN OUR DRIVEWAY AT THE TIME AND WE WERE ALERTED MY NEIGHBORS WHO SAW FLAMES SHOOTI...

Apr 18, 2010 Engine And Engine Cooling 161,030 mi

ENGINE COOLANT LEVEL KEEPS RUNNING LOW .TRUCK STARTING TO SKIP OR MISFIRE ON CYLINDER. NO VISIBLE LEAKAGE ON THE OUT SIDE OF MOTOR. *TR

Apr 18, 2010 Engine And Engine Cooling 161,030 mi

ENGINE COOLANT LEVEL KEEPS RUNNING LOW .TRUCK STARTING TO SKIP OR MISFIRE ON CYLINDER. NO VISIBLE LEAKAGE ON THE OUT SIDE OF MOTOR. *TR

Jul 8, 2008 Engine And Engine Cooling 110 mi

WENT TO START TRUCK. HYDRO LOCKED. WOULD NOT START. *TR

Jul 8, 2008 Engine And Engine Cooling 110 mi

WENT TO START TRUCK. HYDRO LOCKED. WOULD NOT START. *TR

Dec 18, 2007 Engine And Engine Cooling 131,000 mi

1997 F150 ENGINE FAILURE 4.2L 6 CYL MOTOR BENT OR BLEW A ROD AFTER SOUND CAME FROM ENGINE AFTER STARTING IT. *TR

Dec 18, 2007 Engine And Engine Cooling 131,000 mi

1997 F150 ENGINE FAILURE 4.2L 6 CYL MOTOR BENT OR BLEW A ROD AFTER SOUND CAME FROM ENGINE AFTER STARTING IT. *TR

Dec 16, 2007 Engine And Engine Cooling 120,000 mi

FAULTY HEAD GASKET CAUSING OIL AND COOLANT TO MIX. EVENTUALLY HAVING TO REPLACE THE ENGINE DUE TO BENT RODS. *TR

Dec 16, 2007 Engine And Engine Cooling 120,000 mi

FAULTY HEAD GASKET CAUSING OIL AND COOLANT TO MIX. EVENTUALLY HAVING TO REPLACE THE ENGINE DUE TO BENT RODS. *TR

Apr 7, 2007 Engine And Engine Cooling 90,000 mi

4.2 ENGINE PROBLEM, THE 1997 FORD F150 HAS 90,000 MILES ON IT, AS OF THIS DATE THE ENGINE MAIN BEARING WORE OUT. THIS VEHICLE HAS ALL WAYS BEEN SERVICED, AND WITH OIL CHANGES EVERY THREE MONTHS OR 3000 MILES SINCE I PURCHASED IT WITH 6 MILES ON IT. AND THIS WAS A ONE OWNER VEHICLE. I THINK THE BEAR...

Apr 7, 2007 Engine And Engine Cooling 90,000 mi

4.2 ENGINE PROBLEM, THE 1997 FORD F150 HAS 90,000 MILES ON IT, AS OF THIS DATE THE ENGINE MAIN BEARING WORE OUT. THIS VEHICLE HAS ALL WAYS BEEN SERVICED, AND WITH OIL CHANGES EVERY THREE MONTHS OR 3000 MILES SINCE I PURCHASED IT WITH 6 MILES ON IT. AND THIS WAS A ONE OWNER VEHICLE. I THINK THE BEAR...

Feb 13, 2007 Vehicle Speed Control 87,600 mi

THROTTLE HUNG THREE TIMES: ONE UNDER CRUISE, TWICE WITHOUT. ALL INSTANCES STARTED AT HIGHWAY SPEEDS WHEN TEMPS WHERE EXTREMELY COLD. PUMPING PEDDLE TO BREAK ACCELERATION ONLY ALLOWED FOR PARTIAL DECELERATION. REPEATED ATTEMPTS REQUIRED TO REDUCE SPEED. COULD HAVE CAUSED FATALITY IN SECOND OCCURRE...

Feb 13, 2007 Vehicle Speed Control 87,600 mi

THROTTLE HUNG THREE TIMES: ONE UNDER CRUISE, TWICE WITHOUT. ALL INSTANCES STARTED AT HIGHWAY SPEEDS WHEN TEMPS WHERE EXTREMELY COLD. PUMPING PEDDLE TO BREAK ACCELERATION ONLY ALLOWED FOR PARTIAL DECELERATION. REPEATED ATTEMPTS REQUIRED TO REDUCE SPEED. COULD HAVE CAUSED FATALITY IN SECOND OCCURRE...

Dec 22, 2006 Tires

FIRESTONE STORES AT 11865 W 95 OVERLAND PARK KS 66214 AND ONE AT 7575 WORNALL RD KANSAS CITY MO 64114 ARE FALSIFYING DOT REGISTRATION ON OVER 90% OF TIRES SOLD. PROCESS USED IS THAT A FICTITIOUS NUMBER THAT HAS THE RIGHT SERIES OF CHARACTERS IS USED ON ALL TIRE INVOICES REGARDLESS OF SIZE OR TYPE. ...

Dec 22, 2006 Tires

FIRESTONE STORES AT 11865 W 95 OVERLAND PARK KS 66214 AND ONE AT 7575 WORNALL RD KANSAS CITY MO 64114 ARE FALSIFYING DOT REGISTRATION ON OVER 90% OF TIRES SOLD. PROCESS USED IS THAT A FICTITIOUS NUMBER THAT HAS THE RIGHT SERIES OF CHARACTERS IS USED ON ALL TIRE INVOICES REGARDLESS OF SIZE OR TYPE. ...

Oct 25, 2006 Engine And Engine Cooling 116,000 mi

'97 FORD F-150 4.2L V-6, LOWER INTAKE GASKETS FAILED, LEADING TO HYDROLOCKED ENGINE. I HAVE READ HUNDREDS OF INSTANCES OF THIS HAPPENING. TRUCK IS NOW INOPERABLE. *NM

Oct 25, 2006 Engine And Engine Cooling 116,000 mi

'97 FORD F-150 4.2L V-6, LOWER INTAKE GASKETS FAILED, LEADING TO HYDROLOCKED ENGINE. I HAVE READ HUNDREDS OF INSTANCES OF THIS HAPPENING. TRUCK IS NOW INOPERABLE. *NM

Jun 24, 2006 Engine And Engine Cooling

FORD LOWER INTAKE GASKET ON 1997 F150 4.2L ENGINE CAUSING COOLANT LOSS. *NM

Jun 24, 2006 Engine And Engine Cooling

FORD LOWER INTAKE GASKET ON 1997 F150 4.2L ENGINE CAUSING COOLANT LOSS. *NM

May 15, 2006 Engine And Engine Cooling 86,000 mi

PERIODIC LOW COOLANT LEVELS WITH NO VISIBLE LEAKS, PROGRESSIVELY WORSE LOW OIL PRESSURE, TROUBLE STARTING, STEAM IN EXHAUST COOLANT LEAKING INTO CYLINDER CAUSED BENT ROD AND NECESSITATED ENGINE REBUILD. *NM

May 15, 2006 Engine And Engine Cooling 86,000 mi

PERIODIC LOW COOLANT LEVELS WITH NO VISIBLE LEAKS, PROGRESSIVELY WORSE LOW OIL PRESSURE, TROUBLE STARTING, STEAM IN EXHAUST COOLANT LEAKING INTO CYLINDER CAUSED BENT ROD AND NECESSITATED ENGINE REBUILD. *NM

Feb 6, 2006 Engine And Engine Cooling 84,000 mi

1. LOSS OF COOLANT 2. PRESSURE TEST SHOWED FRONT GASKET LEAKING 3.FRONT GASKET REPLACED AT COST OF $1000.00 , MAY HAVE LOWER INTAKE GASKET LEAK NOW, ALL COMMON SERVICE ISSUE , NEEDS TO BE RECALLED. *JB

Feb 6, 2006 Engine And Engine Cooling 84,000 mi

1. LOSS OF COOLANT 2. PRESSURE TEST SHOWED FRONT GASKET LEAKING 3.FRONT GASKET REPLACED AT COST OF $1000.00 , MAY HAVE LOWER INTAKE GASKET LEAK NOW, ALL COMMON SERVICE ISSUE , NEEDS TO BE RECALLED. *JB

Jan 9, 2006 Engine And Engine Cooling 168,000 mi

ENGINE DEAD DUE TO FAULTY GASKETS, COOLANT LEAKING INTO ENGINE. *NM

Jan 9, 2006 Engine And Engine Cooling 168,000 mi

ENGINE DEAD DUE TO FAULTY GASKETS, COOLANT LEAKING INTO ENGINE. *NM

Dec 5, 2005 Steering Crash 80,000 mi

MY SON APPLIED HIS BRAKES ON A 1997 FORD F-150 AND TRIED TO AVOID HITTING THE CAR IN FRONT OF HIM, HOWEVER; HE CLAIMS THE STEERING WHEEL "LOCKED" PROHIBITING HIM FROM AVOIDING THE WRECK. HE SAID IT WAS LIKE WHEN THE STEERING WHEEL LOCKS WHEN YOU DON'T HAVE THE KEY FOR THE CAR. I WOULD LIKE TO KNOW...

Dec 5, 2005 Steering Crash 80,000 mi

MY SON APPLIED HIS BRAKES ON A 1997 FORD F-150 AND TRIED TO AVOID HITTING THE CAR IN FRONT OF HIM, HOWEVER; HE CLAIMS THE STEERING WHEEL "LOCKED" PROHIBITING HIM FROM AVOIDING THE WRECK. HE SAID IT WAS LIKE WHEN THE STEERING WHEEL LOCKS WHEN YOU DON'T HAVE THE KEY FOR THE CAR. I WOULD LIKE TO KNOW...

Aug 28, 2005 Engine And Engine Cooling 135,000 mi

I DIDN'T REALLY NOTICE ANYTHING JUST ONE DAY MY ENGINE STARTED MAKING LOUD KNOCKING SOUND TOOK IT IN FOR SERVICING AND FOUND OUT I SPUN A ROD I REPLACED THE ENGINE. *JB

Aug 28, 2005 Engine And Engine Cooling 135,000 mi

I DIDN'T REALLY NOTICE ANYTHING JUST ONE DAY MY ENGINE STARTED MAKING LOUD KNOCKING SOUND TOOK IT IN FOR SERVICING AND FOUND OUT I SPUN A ROD I REPLACED THE ENGINE. *JB

Aug 17, 2005 Engine And Engine Cooling 140,000 mi

UPON STARTING MY TRUCK, A LOUD BANGING OR RATTLING NOISE COULD BE HEARD. THE NOISE WAS NOT PRESENT PRIOR TO THAT DAY. I SHUT IT DOWN AND UPON DOING RESEARCH ON THE INTERNET, FOUND NUMEROUS PEOPLE WHO CLAIM THAT A FAULTY GASKET DESIGN CAUSED WATER TO LEAK INTO ONE OF THE CYLINDERS INSPECTION OF THE...

Aug 17, 2005 Engine And Engine Cooling 140,000 mi

UPON STARTING MY TRUCK, A LOUD BANGING OR RATTLING NOISE COULD BE HEARD. THE NOISE WAS NOT PRESENT PRIOR TO THAT DAY. I SHUT IT DOWN AND UPON DOING RESEARCH ON THE INTERNET, FOUND NUMEROUS PEOPLE WHO CLAIM THAT A FAULTY GASKET DESIGN CAUSED WATER TO LEAK INTO ONE OF THE CYLINDERS INSPECTION OF THE...

Jul 19, 2005 Electrical System Fire 100,000 mi

1997 FORD TRUCK F250

Jul 19, 2005 Vehicle Speed Control Fire 100,000 mi

1997 FORD TRUCK F250

Jul 19, 2005 Electrical System Fire 100,000 mi

1997 FORD TRUCK F250

Jul 19, 2005 Vehicle Speed Control Fire 100,000 mi

1997 FORD TRUCK F250

Jul 1, 2005 Electrical System Fire 145,000 mi

JUNE 5, 2005- ABOUT 1:30AM, MY WIFE AND I WERE AWAKEN BY THE NEIGHBORS AND THE FIRE DEPT. THEY INFORMED US THAT OUR TRUCK WAS ON FIRE IN THE DRIVEWAY. THE HOOD WAS MELTED AWAY AND THE FRONT HALF OF THE TRUCK WAS ENGULFED IN FLAMES. THE FIRE DEPT. DEEMED THE SOURCE IN THE AREA OF THE MASTER CYLINDER ...

Jul 1, 2005 Electrical System Fire 145,000 mi

JUNE 5, 2005- ABOUT 1:30AM, MY WIFE AND I WERE AWAKEN BY THE NEIGHBORS AND THE FIRE DEPT. THEY INFORMED US THAT OUR TRUCK WAS ON FIRE IN THE DRIVEWAY. THE HOOD WAS MELTED AWAY AND THE FRONT HALF OF THE TRUCK WAS ENGULFED IN FLAMES. THE FIRE DEPT. DEEMED THE SOURCE IN THE AREA OF THE MASTER CYLINDER ...

May 2, 2005 Electrical System Fire

AFTER BEING PARKED FOR 4HRS.AND UNATTENDED MY 1997 FORD F-150 4X4 TRUCK VIN.# [XXX] CAUGHT FIRE IN ENGINE COMPARTMENT. FIRE APPEARS TO HAVE STARTED IN THE AREA OF THE MASTER CYLINDER. THIS WAS OBSERVED FROM THE HOLE THAT WAS BURNT IN THE HOOD ON THE LEFT FRONT OF VEHICLE'S HOOD. FIRE REPORT STATES E...

May 2, 2005 Electrical System Fire

AFTER BEING PARKED FOR 4HRS.AND UNATTENDED MY 1997 FORD F-150 4X4 TRUCK VIN.# [XXX] CAUGHT FIRE IN ENGINE COMPARTMENT. FIRE APPEARS TO HAVE STARTED IN THE AREA OF THE MASTER CYLINDER. THIS WAS OBSERVED FROM THE HOLE THAT WAS BURNT IN THE HOOD ON THE LEFT FRONT OF VEHICLE'S HOOD. FIRE REPORT STATES E...

Apr 28, 2005 Engine And Engine Cooling 106,976 mi

FRONT ENGIN COVER GASKET FAILED IN LINE WITH RECALL 99B29 COST OF RECOVERY BY DEALER 4,700, IT WOULD APPEAR RECALL WAS INADEQUATE AND RESULTED IN ENGIN FAILER.

Apr 28, 2005 Engine And Engine Cooling 106,976 mi

FRONT ENGIN COVER GASKET FAILED IN LINE WITH RECALL 99B29 COST OF RECOVERY BY DEALER 4,700, IT WOULD APPEAR RECALL WAS INADEQUATE AND RESULTED IN ENGIN FAILER.

Mar 31, 2005 Electrical System Fire 151,000 mi

1997 FORD F 150 STARTED ON FIRE AND BURNED. THE VEHICLE WAS NOT RUNNING. IT WAS A TOTAL LOSS.

Mar 31, 2005 Electrical System Fire 151,000 mi

1997 FORD F 150 STARTED ON FIRE AND BURNED. THE VEHICLE WAS NOT RUNNING. IT WAS A TOTAL LOSS.

Mar 23, 2005 Vehicle Speed Control 165,000 mi

I HAVE A 1997 FORD F150 4X4 4.6 LITRE PICKUP. THE CRUISE CONTROL SYSTEM HAS BEEN MALFUNCTIONING FOR THE PAST 6 MONTHS. WHILE DRIVING FOR AN EXTENDED PERIOD, THE CRUISE CONTROL WILL DEACTIVATE ON ITS OWN. WHEN I PRESS RESUME, IT WILL PICK BACK UP AND WORK FINE FOR AN UNDETERMINED PERIOD. IT IS A RAND...

Mar 23, 2005 Vehicle Speed Control Fire 160,000 mi

TRUCK STARTED; HOWEVER, WOULD NOT GO INTO DRIVE. CONNECTOR FOR CRUISE CONTROL SHUT OFF ON BRAKE MASTER CYLINDAR WAS BURNT. OCCURED WHILE IN PARKING LOT WITH ENGINE SHUT OFF. APPEARS THAT THE BRAKE RELAY LEAKED BRAKE FLUID INTO CONNECTOR CAUSING SHORT. FORD DID NOT REPLACE CONNECTOR. CRUISE CONT...

Mar 23, 2005 Electrical System Fire 160,000 mi

TRUCK STARTED; HOWEVER, WOULD NOT GO INTO DRIVE. CONNECTOR FOR CRUISE CONTROL SHUT OFF ON BRAKE MASTER CYLINDAR WAS BURNT. OCCURED WHILE IN PARKING LOT WITH ENGINE SHUT OFF. APPEARS THAT THE BRAKE RELAY LEAKED BRAKE FLUID INTO CONNECTOR CAUSING SHORT. FORD DID NOT REPLACE CONNECTOR. CRUISE CONT...

Mar 23, 2005 Service Brakes, Hydraulic Fire 160,000 mi

TRUCK STARTED; HOWEVER, WOULD NOT GO INTO DRIVE. CONNECTOR FOR CRUISE CONTROL SHUT OFF ON BRAKE MASTER CYLINDAR WAS BURNT. OCCURED WHILE IN PARKING LOT WITH ENGINE SHUT OFF. APPEARS THAT THE BRAKE RELAY LEAKED BRAKE FLUID INTO CONNECTOR CAUSING SHORT. FORD DID NOT REPLACE CONNECTOR. CRUISE CONT...

Mar 23, 2005 Vehicle Speed Control 165,000 mi

I HAVE A 1997 FORD F150 4X4 4.6 LITRE PICKUP. THE CRUISE CONTROL SYSTEM HAS BEEN MALFUNCTIONING FOR THE PAST 6 MONTHS. WHILE DRIVING FOR AN EXTENDED PERIOD, THE CRUISE CONTROL WILL DEACTIVATE ON ITS OWN. WHEN I PRESS RESUME, IT WILL PICK BACK UP AND WORK FINE FOR AN UNDETERMINED PERIOD. IT IS A RAND...

Mar 23, 2005 Vehicle Speed Control Fire 160,000 mi

TRUCK STARTED; HOWEVER, WOULD NOT GO INTO DRIVE. CONNECTOR FOR CRUISE CONTROL SHUT OFF ON BRAKE MASTER CYLINDAR WAS BURNT. OCCURED WHILE IN PARKING LOT WITH ENGINE SHUT OFF. APPEARS THAT THE BRAKE RELAY LEAKED BRAKE FLUID INTO CONNECTOR CAUSING SHORT. FORD DID NOT REPLACE CONNECTOR. CRUISE CONT...

Mar 23, 2005 Electrical System Fire 160,000 mi

TRUCK STARTED; HOWEVER, WOULD NOT GO INTO DRIVE. CONNECTOR FOR CRUISE CONTROL SHUT OFF ON BRAKE MASTER CYLINDAR WAS BURNT. OCCURED WHILE IN PARKING LOT WITH ENGINE SHUT OFF. APPEARS THAT THE BRAKE RELAY LEAKED BRAKE FLUID INTO CONNECTOR CAUSING SHORT. FORD DID NOT REPLACE CONNECTOR. CRUISE CONT...

Mar 23, 2005 Service Brakes, Hydraulic Fire 160,000 mi

TRUCK STARTED; HOWEVER, WOULD NOT GO INTO DRIVE. CONNECTOR FOR CRUISE CONTROL SHUT OFF ON BRAKE MASTER CYLINDAR WAS BURNT. OCCURED WHILE IN PARKING LOT WITH ENGINE SHUT OFF. APPEARS THAT THE BRAKE RELAY LEAKED BRAKE FLUID INTO CONNECTOR CAUSING SHORT. FORD DID NOT REPLACE CONNECTOR. CRUISE CONT...

Jan 3, 2005 Service Brakes, Hydraulic 113,000 mi

BRAKE LINES RUSTED THROUGH, LOSS OF BRAKES. *AK

Jan 3, 2005 Service Brakes, Hydraulic 113,000 mi

BRAKE LINES RUSTED THROUGH, LOSS OF BRAKES. *AK

Oct 26, 2004 Structure

CRACKS ON DOOR FORD 1997 TRUCK. JUST TO GIVE YOU AN IDEA THERE ARE 18 TRUCKS IN THE PARKING LOT 12 OUT OF THE 18 HAVE CRACKS.. THIS NEEDS TO BE LOOKED AT BY FORD!!!!!!!!*AK

Oct 26, 2004 Structure

CRACKS ON DOOR FORD 1997 TRUCK. JUST TO GIVE YOU AN IDEA THERE ARE 18 TRUCKS IN THE PARKING LOT 12 OUT OF THE 18 HAVE CRACKS.. THIS NEEDS TO BE LOOKED AT BY FORD!!!!!!!!*AK

Sep 17, 2004 Engine And Engine Cooling 96,000 mi

CONSUMER REQUEST A RESPONSE TO A QUESTION HE SUBMITTED TO NHTSA RE THE 4.6 LITER ENGINE EXPLODING IN HIS 1997 FORD F-SERIES PICKUP TRUCK. *MR THE VEHICLE'S ENGINE EXPLODED AS THE CONSUMER TURNED THE KEY IN THE IGNITION. *NM

Sep 17, 2004 Engine And Engine Cooling 96,000 mi

CONSUMER REQUEST A RESPONSE TO A QUESTION HE SUBMITTED TO NHTSA RE THE 4.6 LITER ENGINE EXPLODING IN HIS 1997 FORD F-SERIES PICKUP TRUCK. *MR THE VEHICLE'S ENGINE EXPLODED AS THE CONSUMER TURNED THE KEY IN THE IGNITION. *NM

Jan 15, 2004 Engine And Engine Cooling 75,000 mi

COOLANT IS LEAKING INTO THE ENGINE- LIKELY DUE TO GASKET FAILURE - HEAT NON- FUNCTIONING AS A RESULT

Jan 15, 2004 Power Train

OVER DRIVE WENT OUT SOME WERE AROUND 56000-58000 MILES NOW AT 94,000 MILES THERE IS NO REVERSE

Jan 15, 2004 Unknown Or Other 70,000 mi

LIGHTS STAY ON CONTINUOUSLY - HAVE TO REMOVE FUSES - BACK UP LIGHTS AND DOME LIGHT WON'T GO OUT. DAYTIME RUNNING LIGHTS STAY ON WHEN VEHICLE IS OFF. BOTH TIE ROD ENDS HAVE FALLEN OFF (AT DIFFERENT TIMES) ENGINE IS GONE. INFERIOR GASKETS LEAKED COOLANT INTO THE ENGINE AND DESTROYED MAIN BEARINGS. ...

Jan 15, 2004 Engine And Engine Cooling 70,000 mi

LIGHTS STAY ON CONTINUOUSLY - HAVE TO REMOVE FUSES - BACK UP LIGHTS AND DOME LIGHT WON'T GO OUT. DAYTIME RUNNING LIGHTS STAY ON WHEN VEHICLE IS OFF. BOTH TIE ROD ENDS HAVE FALLEN OFF (AT DIFFERENT TIMES) ENGINE IS GONE. INFERIOR GASKETS LEAKED COOLANT INTO THE ENGINE AND DESTROYED MAIN BEARINGS. ...

Jan 15, 2004 Suspension 70,000 mi

LIGHTS STAY ON CONTINUOUSLY - HAVE TO REMOVE FUSES - BACK UP LIGHTS AND DOME LIGHT WON'T GO OUT. DAYTIME RUNNING LIGHTS STAY ON WHEN VEHICLE IS OFF. BOTH TIE ROD ENDS HAVE FALLEN OFF (AT DIFFERENT TIMES) ENGINE IS GONE. INFERIOR GASKETS LEAKED COOLANT INTO THE ENGINE AND DESTROYED MAIN BEARINGS. ...

Jan 15, 2004 Structure 63,000 mi

I HAVE THE SAME DOOR CRACK AROUND THE WINDOW AS MANY OTHERS. I TALKED TO THE DEALER THAT I BOUGHT THE TRUCK FROM, B UT MY EXTENDED WARRANTY DOES NOT COVER THIS TYPE OF DEFECT. I THEN WENT TO THE FORD DEALER IN TOWN TO SEE IF FORD WAS DOING ANUTHING TO CORRECT THIS ISSUE AND SAVE THE STRUCTURAL INTEG...

Jan 15, 2004 Engine And Engine Cooling 75,000 mi

COOLANT IS LEAKING INTO THE ENGINE- LIKELY DUE TO GASKET FAILURE - HEAT NON- FUNCTIONING AS A RESULT

Jan 15, 2004 Power Train

OVER DRIVE WENT OUT SOME WERE AROUND 56000-58000 MILES NOW AT 94,000 MILES THERE IS NO REVERSE

Jan 15, 2004 Unknown Or Other 70,000 mi

LIGHTS STAY ON CONTINUOUSLY - HAVE TO REMOVE FUSES - BACK UP LIGHTS AND DOME LIGHT WON'T GO OUT. DAYTIME RUNNING LIGHTS STAY ON WHEN VEHICLE IS OFF. BOTH TIE ROD ENDS HAVE FALLEN OFF (AT DIFFERENT TIMES) ENGINE IS GONE. INFERIOR GASKETS LEAKED COOLANT INTO THE ENGINE AND DESTROYED MAIN BEARINGS. ...

Jan 15, 2004 Engine And Engine Cooling 70,000 mi

LIGHTS STAY ON CONTINUOUSLY - HAVE TO REMOVE FUSES - BACK UP LIGHTS AND DOME LIGHT WON'T GO OUT. DAYTIME RUNNING LIGHTS STAY ON WHEN VEHICLE IS OFF. BOTH TIE ROD ENDS HAVE FALLEN OFF (AT DIFFERENT TIMES) ENGINE IS GONE. INFERIOR GASKETS LEAKED COOLANT INTO THE ENGINE AND DESTROYED MAIN BEARINGS. ...

Jan 15, 2004 Suspension 70,000 mi

LIGHTS STAY ON CONTINUOUSLY - HAVE TO REMOVE FUSES - BACK UP LIGHTS AND DOME LIGHT WON'T GO OUT. DAYTIME RUNNING LIGHTS STAY ON WHEN VEHICLE IS OFF. BOTH TIE ROD ENDS HAVE FALLEN OFF (AT DIFFERENT TIMES) ENGINE IS GONE. INFERIOR GASKETS LEAKED COOLANT INTO THE ENGINE AND DESTROYED MAIN BEARINGS. ...

Jan 15, 2004 Structure 63,000 mi

I HAVE THE SAME DOOR CRACK AROUND THE WINDOW AS MANY OTHERS. I TALKED TO THE DEALER THAT I BOUGHT THE TRUCK FROM, B UT MY EXTENDED WARRANTY DOES NOT COVER THIS TYPE OF DEFECT. I THEN WENT TO THE FORD DEALER IN TOWN TO SEE IF FORD WAS DOING ANUTHING TO CORRECT THIS ISSUE AND SAVE THE STRUCTURAL INTEG...

Jun 11, 2003 Steering 71,455 mi

COMPLETE LOSS OF STEERING, WENT THROUGH 3 LANES OF TRAFFIC LUCKILY THERE WAS NO ACCIDENT OR INJURY. FORD MOTOR WARRANTY SAID CONTACT GARAGE IT WOULD BE UP TO THEM TO REIMBURSE ANY REPAIR COST BECAUSE VEHICLE WAS OFF WARRANTY, GARAGE ALSO SAID THEY WOULD NOT CONTACT FORD WARRANTY TO DISCUSS PROBLEM I...

Jun 11, 2003 Steering 71,455 mi

COMPLETE LOSS OF STEERING, WENT THROUGH 3 LANES OF TRAFFIC LUCKILY THERE WAS NO ACCIDENT OR INJURY. FORD MOTOR WARRANTY SAID CONTACT GARAGE IT WOULD BE UP TO THEM TO REIMBURSE ANY REPAIR COST BECAUSE VEHICLE WAS OFF WARRANTY, GARAGE ALSO SAID THEY WOULD NOT CONTACT FORD WARRANTY TO DISCUSS PROBLEM I...

May 9, 2003 Engine And Engine Cooling 95,500 mi

97 F150 BEGAN TO HAVE AN UNPREDICTABLE COOLANT LEAK, NEVER GOING BELOW MINIMUM COOLANT LEVEL. WITHIN THE WEEK NOTICED WATER IN THE OIL AND WENT TO TAKE THE VEHICLE TO A SERVICE STATION. WHEN I STARTED THE TRUCK THERE WAS A LOUD KNOCKING, PROVING TO BE A DAMAGED ROD. LATER RESEARCH SHOWED THAT THI...

May 9, 2003 Engine And Engine Cooling 95,500 mi

97 F150 BEGAN TO HAVE AN UNPREDICTABLE COOLANT LEAK, NEVER GOING BELOW MINIMUM COOLANT LEVEL. WITHIN THE WEEK NOTICED WATER IN THE OIL AND WENT TO TAKE THE VEHICLE TO A SERVICE STATION. WHEN I STARTED THE TRUCK THERE WAS A LOUD KNOCKING, PROVING TO BE A DAMAGED ROD. LATER RESEARCH SHOWED THAT THI...

Apr 18, 2003 Engine And Engine Cooling Fire

FIRE STARTED IN ENGINE AREA AFTER BEING PARKED FOR APPROXIMATELY 2 HOURS. VEHICLE AT A COMPLETE LOSS. FIREFIGHTERS COULD NOT DETERMINE CAUSE OF FIRE OTHER THAN IT ORIGINATING IN MIDDLE OF ENGINE COMPARTMENT. *NLM

Apr 18, 2003 Engine And Engine Cooling Fire

FIRE STARTED IN ENGINE AREA AFTER BEING PARKED FOR APPROXIMATELY 2 HOURS. VEHICLE AT A COMPLETE LOSS. FIREFIGHTERS COULD NOT DETERMINE CAUSE OF FIRE OTHER THAN IT ORIGINATING IN MIDDLE OF ENGINE COMPARTMENT. *NLM

Apr 11, 2003 Engine And Engine Cooling 73,000 mi

ENGINE FAILURE AT 73000 MILES, FOLLOWED ALL FORDS RECOMMENDED MAINTENANCE. *JB

Apr 11, 2003 Engine And Engine Cooling 73,000 mi

ENGINE FAILURE AT 73000 MILES, FOLLOWED ALL FORDS RECOMMENDED MAINTENANCE. *JB

Feb 11, 2003 Suspension 81,000 mi

BROKEN FRONT TORSION BAR (RS) ON A 1997 FORD F150 4WD. NO CRASH, NO PROPERTY DAMAGE . SAW PREVIOUS INVESTIGATION WHILE SEARCHING FOR RECALLS. ALSO SPOKE TO FORD DEALER WHO STATED THIS WAS NOT UNCOMMON.I AM CURIOUS AS TO WHY THIS INVESTIGATION WAS CLOSED SO QUICKLY.

Feb 11, 2003 Suspension 81,000 mi

BROKEN FRONT TORSION BAR (RS) ON A 1997 FORD F150 4WD. NO CRASH, NO PROPERTY DAMAGE . SAW PREVIOUS INVESTIGATION WHILE SEARCHING FOR RECALLS. ALSO SPOKE TO FORD DEALER WHO STATED THIS WAS NOT UNCOMMON.I AM CURIOUS AS TO WHY THIS INVESTIGATION WAS CLOSED SO QUICKLY.

Mar 14, 2001 Visibility

DEALERSHIP INFORMED CONSUMER THAT SEALER HOLDING WINDSHIELD IN PLACE WAS LEAKING. THIS CAUSED A SHORT IN FUSE AND RADIO. PLEASE PROVIDE FURTHER INFORMATION.

Mar 14, 2001 Electrical System

DEALERSHIP INFORMED CONSUMER THAT SEALER HOLDING WINDSHIELD IN PLACE WAS LEAKING. THIS CAUSED A SHORT IN FUSE AND RADIO. PLEASE PROVIDE FURTHER INFORMATION.

Mar 14, 2001 Equipment

DEALERSHIP INFORMED CONSUMER THAT SEALER HOLDING WINDSHIELD IN PLACE WAS LEAKING. THIS CAUSED A SHORT IN FUSE AND RADIO. PLEASE PROVIDE FURTHER INFORMATION.

Mar 14, 2001 Visibility

DEALERSHIP INFORMED CONSUMER THAT SEALER HOLDING WINDSHIELD IN PLACE WAS LEAKING. THIS CAUSED A SHORT IN FUSE AND RADIO. PLEASE PROVIDE FURTHER INFORMATION.

Mar 14, 2001 Electrical System

DEALERSHIP INFORMED CONSUMER THAT SEALER HOLDING WINDSHIELD IN PLACE WAS LEAKING. THIS CAUSED A SHORT IN FUSE AND RADIO. PLEASE PROVIDE FURTHER INFORMATION.

Mar 14, 2001 Equipment

DEALERSHIP INFORMED CONSUMER THAT SEALER HOLDING WINDSHIELD IN PLACE WAS LEAKING. THIS CAUSED A SHORT IN FUSE AND RADIO. PLEASE PROVIDE FURTHER INFORMATION.

Aug 14, 2000 Tires

PE00-020, FIRESTONE WILDERNESS HT, ORIGINAL EQUIPPED TIRE, SIZE P23570R16 AND DOT W281PT. CONSUMER WAS DRIVING AT APPROXIMATELY 75 MPH WHEN RIGHT FRONT TIRE TREAD CAME COMPLETELY OFF ALL THE WAY TO STEEL BELT, CAUSING DAMAGE TO FENDER. TIRE DID NOT DEFLATE AND HAD ONLY 22,000 MILES. MINUTES PRIOR ...

Aug 14, 2000 Tires

PE00-020, FIRESTONE WILDERNESS HT, ORIGINAL EQUIPPED TIRE, SIZE P23570R16 AND DOT W281PT. CONSUMER WAS DRIVING AT APPROXIMATELY 75 MPH WHEN RIGHT FRONT TIRE TREAD CAME COMPLETELY OFF ALL THE WAY TO STEEL BELT, CAUSING DAMAGE TO FENDER. TIRE DID NOT DEFLATE AND HAD ONLY 22,000 MILES. MINUTES PRIOR ...

Oct 12, 1998 Engine And Engine Cooling Fire

VEHICLE ENGINE FIRE.

Oct 12, 1998 Engine And Engine Cooling Fire

VEHICLE ENGINE FIRE.