1988 FORD F150 Power Train Problems

10 complaints about Power Train

10
Complaints
0
Crashes
0
Fires
0
Deaths

This Problem Across All Years

All Power Train Complaints (10)

Aug 11, 1998

THE YOKE THAT HOLDS THE DRIVE SHAFT RUSTED AND BROKE OFF AND DAMAGED THE SIDE OF THE FUEL TANK.

Jun 12, 1998

CLUTCH REPLACED BY LOCAL MECHANIC LASTED 8942 MILES. CLUTCH REPLACED BY DEALER LASTED 4861 MILES.

Jul 15, 1997

CLUTCH ASSEMBLY LINKAGE UNDERNEATH THE DASHBOARD GIVES OUT. ALSO, THEY'VE HAD THE TRANSMISSION REPLACED 3 TIMES. CONSUMER STATED THAT WHILE DRIVING DOWN THE FREEWAY AT ABOUT 65 MPH THE VEHICLE MAKES A NOISE AND THE GEARS JUST FALL APART, THEY JUST STOP WORKING.

Nov 30, 1995

CLUTCH MASTER CYLINDER DETACHED FROM THE FIREWALL. TT

Sep 24, 1995

TRANSMISSION FAILED 3 TIMES. *SD

Jun 14, 1995

DIFFERENTIAL REPLACED DUE TO OIL LEAK.

Jun 14, 1995

U JOINTS REPLACED. *SKD

Jun 14, 1995

AXLES FAILED, CAUSING GRINDING NOISE.

May 11, 1995

MAN-TRAN: RUBBER PLUGS AT TOP OF TRANSMISSION FAILED, CAUSING TRANSMISSION FLUID LEAK AND FAILURE; NO WARNING. TT

Apr 26, 1995

CLUTCH PEDAL BROKE AWAY FROM MOUNTING ON FIREWALL, MAKING IT IMPOSSIBLE TO SHIFT GEARS. *TW