1992 FORD THUNDERBIRD Electrical System Problems

28 complaints about Electrical System

28
Complaints
0
Crashes
9
Fires
0
Deaths

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Electrical System Complaints (28)

Sep 15, 2010

1992 FORD THUNDERBIRD RECALLED FOR REPLACEMENT OF IGNITION SWITCH A FEW YEARS BACK (NHTSA ACTION NUMBER: EA95002). DEFECTIVE SWITCH WAS REPLACED WITH EXACT SAME PART THAT WAS RECALLED AND FAILED AGAIN WITHIN ONE YEAR WITH TWO HALVES OF UNIT AGAIN COMING APART. I HAVE JUST REPLACED FOR THE FIFTH TIME WITH EXACT SAME DEFECTIVE UNIT, THIS BEING THE ONLY THING AVAILABLE FROM FORD AND FROM AFTERMARKET SUPPLIERS. HOW DOES REPLACING DEFECTIVE PART WITH EXACTLY SAME PART ELIMINATE FIRE HAZARD ASSOCIATED WITH THIS PART WHICH PROMPTED RECALL IN THE FIRST PLACE??? *TR

Sep 15, 2010

1992 FORD THUNDERBIRD RECALLED FOR REPLACEMENT OF IGNITION SWITCH A FEW YEARS BACK (NHTSA ACTION NUMBER: EA95002). DEFECTIVE SWITCH WAS REPLACED WITH EXACT SAME PART THAT WAS RECALLED AND FAILED AGAIN WITHIN ONE YEAR WITH TWO HALVES OF UNIT AGAIN COMING APART. I HAVE JUST REPLACED FOR THE FIFTH TIME WITH EXACT SAME DEFECTIVE UNIT, THIS BEING THE ONLY THING AVAILABLE FROM FORD AND FROM AFTERMARKET SUPPLIERS. HOW DOES REPLACING DEFECTIVE PART WITH EXACTLY SAME PART ELIMINATE FIRE HAZARD ASSOCIATED WITH THIS PART WHICH PROMPTED RECALL IN THE FIRST PLACE??? *TR

Jan 24, 2005

CONSUMER' S VEHICLE EXPERIENCED THE SAME PROBLEMS AS STATED IN NHTSA RECALLS 96V071000 AND 99V27500 CONCERNING IGNITION SYSTEM AND HEADLIGHTS. THE DEALERSHIP INDICATED CONSUMER'S VEHICLE NOT INCLUDED IN THE RECALL DUE TO VIN. *AK *NM

Mileage: 98,000

Aug 24, 2004 Fire

WHILE DRIVING CONSUMER SMELLED SMOKE COMING IN FROM THE VENTS. CONSUMER PULLED OVER, LIFTED THE HOOD UP, AND VEHICLE CAUGHT ON FIRE. CONSUMER WAS ABLE TO EXTINGUISH THE FIRE. CONSUMER HAD THE VEHICLE TOWED TO THE DEALER FOR INSPECTION. *AK

Aug 13, 2004

WHILE PLACING THE KEY INSIDE OF THE IGNITION SWITCH THE KEY FAILED TO COME OUT FROM THE IGNITION. CONSUMER HAD THE VEHICLE TOWED TO THE DEALER FOR INSPECTION, AND MECHANIC DETERMINED THAT THE IGNITION SWITCH NEEDED TO BE REPLACED. *AK

May 12, 2004

WHILE PLACING THE KEY IN THE IGNITION SWITCH VEHICLE FAILED TO START. CONSUMER TURNED OFF THE VEHICLE, AND THEN RESTARTED IT. DROVE IT TO THE DEALER FOR INSPECTION, AND MECHANIC REPLACED SOLENOID SWITCH INSIDE THE IGNITION DUE TO A BURNT OUT WIRE. *AK

Apr 15, 2003

WHILE DRIVING THE EEC FUSE BLEW OUT AND CAUSED THE VEHICLE TO STALL. THE DEALER WAS NOTIFIED. *NLM

Aug 26, 2002

SOMETIMES TURN SIGNAL WORKS AND SOMETIMES THEY DO NOT WORK. CONSUMER HAS TO WIGGLE KEY, AND SIGNALS MAY OR MAY NOT ILLUMINATE. CAUSE UNKNOWN. RECALL 96 V 071 000 DESCRIBED THE SAME PROBLEM. PLEASE PROVIDE ANY FURTHER INFORMATION. *AK

Aug 21, 2002 Fire

THE HARNESS AT THE ALTERNATOR HAS CAUGHT FIRE TWICE AND I HAVE REPLACED THE ALTERNATOR THREE TIMES IN TWO YEARS. THIS IS A VERY DANGEROUS SITUATION. IT STARTS SMOKING AND SUET COMES OUT AND YOU THINK THE CAR IS GOING TO BLOW UP. IT IS A VERY FRIGHTENING EXPERIENCE. THE MECHANIC FOUND SERVICE BULLENTIN ARTICLE #96-21-4 WHICH DESCRIBES THIS. IT HAS HAPPENED TO ME TWICE IN LESS THAN TWO YEARS. I AM VERY DISTRUBED. PLEASE HELP ME.*AK

Jul 9, 2002

VEHICLE EXHIBITS SYMPTOMS SIMILAR TO EARLIER MODELS WITH TFI; SUDDEN STALL AT ANY SPEED OR CONFIGURATION. ALWAYS ASSOCIATED WITH HIGH AMBIENT/ENGINE TEMPERATURE. PROBLEM HAS OCCURED ON HIGHWAY, CREATING EXTRAORDINARILY DANGEROUS SITUATION. DEALER TECHNICIAN DISMISSED POSSIBLE IGNITION FAILURE WHEN ASKED.

Jun 13, 2001

HEADLIGHTS GOE OUT FOR VARIOUS INTERVALS WHICH MAY BE PRECEDED BY FLICKERING OR BLINKING AS A RESULT OF CIRCUIT BREAKER OPENING. DEALER HAS BEEN NOTIFIED. PLEASE PROVIDE FURTHER INFORMATION.*AK

Feb 6, 2001

IGNITION MODULE MALFUNCTIONED. FORD CANNOT PROVIDE PART, STOPPED PRODUCING THE PART. *AK

Jan 22, 2001

WHILE VEHICLE WAS BEING DRIVEN A MALFUNCTION OCCURRED WITHIN IGNITION MODULE, CAUSING VEHICLE TO COMPLETELY SHUTDOWN. PLEASE GIVE ANY FURTHER DETAILS.*AK

Sep 19, 2000

RECALL 96V-071 (FORD 95S28) WAS ORIGINALLY REPAIRED ON 12/2/97. VEHICLE IS NOW EXPERIENCING A SIMILAR PROBLEM. DEALER WILL NOT HONOR RECALL REPAIR, AND CONSUMER IS BENG CHARGED FOR EXPENSE OF INSTALLING ANOTHER NEW IGNITION SWITCH.*AK

Aug 30, 2000

WHILE DRIVING DOWN THE ROAD AT NIGHT HEADLIGHTS WILL JUST GO OUT. CONSUMER HAD A RECALL ON THE HEADLIGHTS. TOOK VEHICLE TO DEALER , AND THEY REPLACED HEADLIGHT SWITCH AND SOME OTHER WIRES. ABOUT TWO WEEKS LATER, THE SAME PROBLEM RETURNED. *AK

Jun 9, 2000

NHTSA RECALL 96V071000 AND MANUFACTURER'S RECALL 95S28/ IGNITION SYSTEM FAILURE. HAD RECALL DONE ON MAY 26,1999, AND REMEDY FAILED. OWNER REPLACED THE PART HIMSELF, IGNITION SWITCH WAS FOUND SEPARATED FROM THE MOUNTING HARWARE. CONTACTED FORD ABOUT THE PROBLEM, BUT THEY SHOWED NO CONCERN. *AK *ML

Feb 17, 2000 Fire

VEHICLE EXPERIENCED FAILURE OF THE RECALL COMPONENT (96V-071) PRIOR TO RECALL NOTICE, RESULTING IN FIRE. *MJS

Jan 30, 2000

IN THE U.S. MILITARY STATIONED IN EUROPE. FUEL PUMP AND RELAY MALFUNCTIONED. WHILE INSTALLING NEW FUEL PUMP AND RELAY, THE FORD TECHNICIAN FOUND THE WIRING HARNESS PROVIDING CURRENT TO THE PUMP WAS IMPROPERLY INSTALLED OR WAS A FAULTY DESIGN. IT HAD CHAFFED THROUGH THE HARNESS CASING EXPOSING THE CHARRED AND MELTED WIRES INSIDE. SUBSEQUENT CHAFFING OF INNER WIRES CAUSED A SHORT IN THE CIRCUIT AND MELTING OF THE WIRES THEMSELVES. DUE TO THE PROXIMITY OF THE SHORT, AN EXPLOSION COULD OCCUR IF FUEL VAPORS ARE PRESENT. THE TECHNICIAN WAS SURPRISED IT HAD NOT EXPLODED. THIS VEHICLE HAS A CURRENT RECALL FOR OTHER FUEL SYSTEM DEFECTS. A COMBINATION OF THE 2 COULD BE DEADLY IF THE OWNER IN UNAWARE OF EITHER PROBLEM AREA. I HAVE AND WILL RETAIN THE HARNESS FOR FURTHER INVESTIGATION IF NEEDED. *AK

Jan 27, 1999

WHILE DRIVING VEHICLE AT 40MPH AT NIGHT, HEADLIGHTS WOULD GO OUT. WOULD NOT HAVE ANY WARNING. THE HEADLIGHTS WERE REPAIRED AT LEAST 3 DIFFERENT TIMES FOR THE ELECTRICAL PROBLEM. (RQ 98015). *AK

Aug 20, 1998

VEHICLE EXPERIENCED SUDDEN ACCELERATION WHICH DAMAGED ENGINE DUE TO FAILURE OF THE COMPUTER UNIT.

Jun 23, 1998 Fire

96V071000; RECALL WORK WAS DONE BY KOONS FORD, FALLS CHURCH, VA. THE CONSUMER WAS DRIVING AND THE STEERING COLUMN WIRES MELTED AND SMOLDERED, THE CONSUMER IS NOT SATISFIED WITH THE WORK DONE PRIOR TO THE INCIDENT. CURRENTLY THE DEALER CANNOT DUPLICATE THE PROBLEM. *AK

May 29, 1998

ELECTRICAL SYSTEM SHORTED OUT CAUSING LIGHTS TO GO ON AND OFF CONTINUOUSLY.

Mar 23, 1998 Fire

VEHICLE WAS PARKED FOR 20-25 MINUTES WHEN A DEFECTIVE ALTERNATOR, CAUSED A FIRE IN THE ENGINE COMPARTMENT AREA. DEALER HAS BEEN NOTIFIED. *AK

Mar 3, 1997 Fire

BRAKES: BRAKES HAS BEEN REPLACED THREE TIMES WITHIN THREE YEARS. BRAKES VIBRATE AND WEAR OUT WITHIN A YEAR. HAD NEW BRAKE PADS INSTALLED AND ROTORS TURNED. ALSO VEHICLE CAUGHT FIRE ON THE LEFT SIDE 3-2-97. PROBABLE CAUSE ELECTRICAL. RECALL 96V071. *AK

Dec 2, 1996

CONSUMER WAS DRIVING AND SMOKE CAME FROM THE IGNITION ( STEERING COLUMN ) . PLEASE DESCRIBE . *AK

Jul 22, 1996 Fire

ELECTRICAL SHORT IN THE IGNITION SWITCH, CAUSING THE VEHICLE TO CATCH ON FIRE IN THE STEERING COLUMN. *AK

Apr 22, 1996 Fire

VEHICLE WAS PARKED, UNDER THE INTERIOR COMPARTMENT, UNDER THE DASH, ELECTRICAL SHORT. *AK

Mar 26, 1996 Fire

ELECTRICIAL FIRE IN THE STEERING COLUMN OF THE DASH BOARD, RESULTING IN A BAD FIRE. *AK