10
Complaints
0
Crashes
2
Fires
0
Deaths
!

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Power Train Complaints

Showing 10 of 10
Sep 16, 2014 155,000 mi

THIS MORNING, MY WIFE WAS PARKING AT ONE OF OUR KID'S SCHOOLS WHEN THE TRANSMISSION SYSTEM FAILED TO RESPOND. SHE ATTEMPTED TO PUT THE VEHICLE IN PARK, BUT IT WOULD NOT INITIALLY. ONCE THE SHIFTER WOULD MOVE FORWARD, THE VEHICLE DIED, AND CONTINUED TO ROLL FORWARD EVEN THOUGH THE SHIFTER WAS POSITIONED AS IF IN PARK. SHE HAD THE PRESENCE OF MIND TO LET IT ROLL UNTIL STRIKING THE PARKING SPOT CEMENT BUMPER. SHE REMOVED THE KEY FROM THE IGNITION, THEN ATTEMPTED TO RESTART THE VEHICLE WITH NO SUCCESS AND THE SHIFTER BUTTON WOULD NOT DEPRESS. SHE PANICKED BECAUSE OF LOOSING CONTROL OF THE VEHICLE WITH SO MANY SMALL KIDS AROUND AND CALLED ME. I LEFT WORK, AND UPON ARRIVAL ATTEMPTED TO TROUBLESHOOT WHAT CAUSED THE INCIDENT. I STARTED AT THE SHIFTER, SO I LOOSENED ALL THE COVERS AROUND IT, IN CASE THERE WAS SOMETHING BINDING THE SHIFTER. I ACTUALLY DID FIND SEVERAL SMALL ITEMS THAT HAD FALLEN IN THE COMPARTMENT THROUGH THE FRONT EDGE OF THE CENTER CONSOLE COVER ASSEMBLY. REMOVING THESE ITEMS STILL DID NOT ALLOW RESTARTING OF THE VEHICLE. I THEN LOOKED UNDERNEATH THE VEHICLE, AND DISCOVERED THAT THE LINKAGE FROM THE SHIFTER TO THE TRANSMISSION HAD SEPARATED. I MANIPULATED THE INPUT LEVER AT THE TRANSMISSION WITH MY HAND AND NOTICED THAT IT HAD MOVEMENT IN BOTH DIRECTIONS, WHICH MEANT THE TRANSMISSION WAS ACTUALLY NOT IN PARK. AFTER POSITIONING THE INPUT LEVER AT THE TRANSMISSION TO PARK, THE VEHICLE DID START. I SHUT THE VEHICLE OFF AND RECONNECTED THE SEPARATED LINKAGE. I WAS SHOCKED TO SEE THAT THE PIECE THAT MAINTAINS SUCH AN IMPORTANT LINKAGE CONNECTED APPEARS TO BE MADE FROM A PLASTIC. TO ME THIS IS A MAJOR ISSUE THAT CAN CAUSE SOMEONE TO POTENTIALLY HAVE A VEHICLE STUCK IN A MOVEMENT CAUSING GEAR, AND DUE TO A LINKAGE SEPARATION HAVE NO WAY TO PROPERLY TURN THE VEHICLE OFF (UNTIL IT RUNS OUT OF GAS), TO MADE FROM PLASTIC. PLEASE LOOK INTO THIS. *TR

Sep 16, 2014 155,000 mi

THIS MORNING, MY WIFE WAS PARKING AT ONE OF OUR KID'S SCHOOLS WHEN THE TRANSMISSION SYSTEM FAILED TO RESPOND. SHE ATTEMPTED TO PUT THE VEHICLE IN PARK, BUT IT WOULD NOT INITIALLY. ONCE THE SHIFTER WOULD MOVE FORWARD, THE VEHICLE DIED, AND CONTINUED TO ROLL FORWARD EVEN THOUGH THE SHIFTER WAS POSITIONED AS IF IN PARK. SHE HAD THE PRESENCE OF MIND TO LET IT ROLL UNTIL STRIKING THE PARKING SPOT CEMENT BUMPER. SHE REMOVED THE KEY FROM THE IGNITION, THEN ATTEMPTED TO RESTART THE VEHICLE WITH NO SUCCESS AND THE SHIFTER BUTTON WOULD NOT DEPRESS. SHE PANICKED BECAUSE OF LOOSING CONTROL OF THE VEHICLE WITH SO MANY SMALL KIDS AROUND AND CALLED ME. I LEFT WORK, AND UPON ARRIVAL ATTEMPTED TO TROUBLESHOOT WHAT CAUSED THE INCIDENT. I STARTED AT THE SHIFTER, SO I LOOSENED ALL THE COVERS AROUND IT, IN CASE THERE WAS SOMETHING BINDING THE SHIFTER. I ACTUALLY DID FIND SEVERAL SMALL ITEMS THAT HAD FALLEN IN THE COMPARTMENT THROUGH THE FRONT EDGE OF THE CENTER CONSOLE COVER ASSEMBLY. REMOVING THESE ITEMS STILL DID NOT ALLOW RESTARTING OF THE VEHICLE. I THEN LOOKED UNDERNEATH THE VEHICLE, AND DISCOVERED THAT THE LINKAGE FROM THE SHIFTER TO THE TRANSMISSION HAD SEPARATED. I MANIPULATED THE INPUT LEVER AT THE TRANSMISSION WITH MY HAND AND NOTICED THAT IT HAD MOVEMENT IN BOTH DIRECTIONS, WHICH MEANT THE TRANSMISSION WAS ACTUALLY NOT IN PARK. AFTER POSITIONING THE INPUT LEVER AT THE TRANSMISSION TO PARK, THE VEHICLE DID START. I SHUT THE VEHICLE OFF AND RECONNECTED THE SEPARATED LINKAGE. I WAS SHOCKED TO SEE THAT THE PIECE THAT MAINTAINS SUCH AN IMPORTANT LINKAGE CONNECTED APPEARS TO BE MADE FROM A PLASTIC. TO ME THIS IS A MAJOR ISSUE THAT CAN CAUSE SOMEONE TO POTENTIALLY HAVE A VEHICLE STUCK IN A MOVEMENT CAUSING GEAR, AND DUE TO A LINKAGE SEPARATION HAVE NO WAY TO PROPERLY TURN THE VEHICLE OFF (UNTIL IT RUNS OUT OF GAS), TO MADE FROM PLASTIC. PLEASE LOOK INTO THIS. *TR

Feb 13, 2013 128,623 mi

TL* THE CONTACT OWNS A 2006 GMC ENVOY DENALI XL. THE CONTACT STATED THAT THE VEHICLE FAILED TO ACCELERATE OVER 40 MPH. THE CONTACT ALSO STATED THAT THE ENGINE AND THE LOW FUEL WARNING LIGHTS ILLUMINATED ALTHOUGH THE FUEL LEVEL WAS AT MAX. THE VEHICLE WAS TAKEN TO THE DEALER WHERE THE CONTACT WAS INFORMED THAT THE THROTTLE BODY AND FUEL PUMP NEEDED TO BE REPLACED. THE FAILURE MILEAGE WAS 128,623 AND THE CURRENT MILEAGE WAS 138,182...UPDATED 04-03-13 *BF UPDATED 04/22/2013 *JS

Feb 13, 2013 128,623 mi

TL* THE CONTACT OWNS A 2006 GMC ENVOY DENALI XL. THE CONTACT STATED THAT THE VEHICLE FAILED TO ACCELERATE OVER 40 MPH. THE CONTACT ALSO STATED THAT THE ENGINE AND THE LOW FUEL WARNING LIGHTS ILLUMINATED ALTHOUGH THE FUEL LEVEL WAS AT MAX. THE VEHICLE WAS TAKEN TO THE DEALER WHERE THE CONTACT WAS INFORMED THAT THE THROTTLE BODY AND FUEL PUMP NEEDED TO BE REPLACED. THE FAILURE MILEAGE WAS 128,623 AND THE CURRENT MILEAGE WAS 138,182...UPDATED 04-03-13 *BF UPDATED 04/22/2013 *JS

Jan 4, 2013 20,000 mi

VEHICLE GOES INTO REDUCED ENGINE POWER MODE UNEXPECTEDLY WHILE DRIVING WITH NO PRIOR WARNING. MIL LIGHT TURNS ON, REDUCED ENGINE POWER LIGHT TURNS ON, STABILITRAK OFF DIC MESSAGE DISPLAYS, RESULTS IN LOSS OF ACCELERATION AND REQUIRES THE DRIVER TO IMMEDIATELY TAKE EMERGENCY SAFETY ACTIONS. CODES INCLUDE P2135, P0121, AND P060E. ISSUE IS INTERMITTENT, APPEARS MORE FREQUENTLY IN COLD OR WET CONDITIONS. THE ISSUE HAS OCCURRED MORE THAN 10 TIMES SINCE THE INITIAL INCIDENT. DEALER UNABLE TO CORRECT THE ISSUE BY THROTTLE BODY CLEANING AND PCM REPLACEMENT. LATEST ATTEMPT IS TO REPLACE THE THROTTLE BODY. *TR

Jan 4, 2013 20,000 mi

VEHICLE GOES INTO REDUCED ENGINE POWER MODE UNEXPECTEDLY WHILE DRIVING WITH NO PRIOR WARNING. MIL LIGHT TURNS ON, REDUCED ENGINE POWER LIGHT TURNS ON, STABILITRAK OFF DIC MESSAGE DISPLAYS, RESULTS IN LOSS OF ACCELERATION AND REQUIRES THE DRIVER TO IMMEDIATELY TAKE EMERGENCY SAFETY ACTIONS. CODES INCLUDE P2135, P0121, AND P060E. ISSUE IS INTERMITTENT, APPEARS MORE FREQUENTLY IN COLD OR WET CONDITIONS. THE ISSUE HAS OCCURRED MORE THAN 10 TIMES SINCE THE INITIAL INCIDENT. DEALER UNABLE TO CORRECT THE ISSUE BY THROTTLE BODY CLEANING AND PCM REPLACEMENT. LATEST ATTEMPT IS TO REPLACE THE THROTTLE BODY. *TR

May 11, 2010 29,300 mi

ON MAY 3RD 2010, THE TRUCK JUST DIED IN THE MIDDLE OF THE ROAD WHILE DRIVING HOME WITH MY SON AT NIGHT. I HAD TO QUICKLY TRY TO GET TO THE SIDE OF THE ROAD WITHOUT ANY POWER ASSIST. THE ENVOY WOULD NOT START AGAIN, NOT EVEN TURN OVER. THE SHIFTER WAS LOCKED AND IT COULD NOT EVEN BE PUT INTO NEUTRAL TO PUSH IT OVER TO THE SIDE. VARIOUS MESSAGES SCROLLED BY ON THE VEHICLE DISPLAY AND MANY OF THE WARNING LIGHTS WERE DIMLY BLINKING. I HAD TO GET IT TOWED. I SCANNED THE FOLLOWING CODES P1516 & P1682, LOOKED UP THE SYMPTOMS ON THE INTERNET AND FOUND MANY HITS THAT SAID THE ISSUE WAS WITH A FAULTY IGNITION SWITCH. AFTER CHARGING UP THE BATTERY WHICH RAN DOWN ON THE HAZARDS WHILE WAITING AN HOUR FOR A TOW, I REPLACED THE IGNITION SWITCH AND THE ENVOY NOW WORKS AGAIN. IT HAS LESS THAN 30,000 MILES ON IT. THIS TYPE OF FAILURE CONCERNS ME VERY MUCH! I CONSIDER IT A HUGE SAFETY ISSUE THAT A VEHICLE CAN DIE WHILE DRIVING AND THEN BE SO COMPLETELY DISABLED BY A $30 PART. THIS COULD OF HAD MUCH MORE DIRE CONSEQUENCES HAD IT HAPPENED ON A FREEWAY AS OPPOSED TO A SUBURBAN SIDE STREET. *TR

May 11, 2010 29,300 mi

ON MAY 3RD 2010, THE TRUCK JUST DIED IN THE MIDDLE OF THE ROAD WHILE DRIVING HOME WITH MY SON AT NIGHT. I HAD TO QUICKLY TRY TO GET TO THE SIDE OF THE ROAD WITHOUT ANY POWER ASSIST. THE ENVOY WOULD NOT START AGAIN, NOT EVEN TURN OVER. THE SHIFTER WAS LOCKED AND IT COULD NOT EVEN BE PUT INTO NEUTRAL TO PUSH IT OVER TO THE SIDE. VARIOUS MESSAGES SCROLLED BY ON THE VEHICLE DISPLAY AND MANY OF THE WARNING LIGHTS WERE DIMLY BLINKING. I HAD TO GET IT TOWED. I SCANNED THE FOLLOWING CODES P1516 & P1682, LOOKED UP THE SYMPTOMS ON THE INTERNET AND FOUND MANY HITS THAT SAID THE ISSUE WAS WITH A FAULTY IGNITION SWITCH. AFTER CHARGING UP THE BATTERY WHICH RAN DOWN ON THE HAZARDS WHILE WAITING AN HOUR FOR A TOW, I REPLACED THE IGNITION SWITCH AND THE ENVOY NOW WORKS AGAIN. IT HAS LESS THAN 30,000 MILES ON IT. THIS TYPE OF FAILURE CONCERNS ME VERY MUCH! I CONSIDER IT A HUGE SAFETY ISSUE THAT A VEHICLE CAN DIE WHILE DRIVING AND THEN BE SO COMPLETELY DISABLED BY A $30 PART. THIS COULD OF HAD MUCH MORE DIRE CONSEQUENCES HAD IT HAPPENED ON A FREEWAY AS OPPOSED TO A SUBURBAN SIDE STREET. *TR

Mar 4, 2007 Fire 50,000 mi

I WAS DRIVING ALONG INTERSTATE 69 NEAR FORT WAYNE IN MY LEASED 2006 GMC ENVOY DENALI WITH MY BOSS ON COMPANY BUSINESS WHEN A CAR FROM BEHIND ME PULLED ALONG SIDE HONKING THEIR HORN AND YELLING FOR ME TO PULL OVER AND GET OUT OF MY CAR BECAUSE IT WAS ON FIRE. WE IMMEDIATELY STOPPED, GOT OUT, AND SAW FLAMES UNDERNEATH THE ENGINE COMPARTMENT OF MY VEHICLE. WE CALLED 911 WHO DISPATCHED FORT WAYNE FIRE AND INDIANA STATE POLICE PERSONNEL. THE CAR WAS TOWED TO THE LOCAL GMC DEALERSHIP. BOTH A THIRD PARTY INSURANCE INVESTIGATOR AND A GENERAL MOTORS INVESTIGATOR CONCUR THAT THE FRONT DIFFERENTIAL FAILED CAUSING LUBRICANT TO SPRAY ONTO THE CATALYTIC CONVERTER AND EXHAUST SYSTEM IGNITING A FIRE. GENERAL MOTORS HAS ADMITTED TO ME THAT THIS IS A DEFECT I COULD NOT POSSIBLY KNOWN ABOUT NOR WAS IT MY FAULT IN ANY WAY. GENERAL MOTORS WANTS TO "REPAIR" THE VEHICLE AND PUT ME BACK IN IT. I'VE TOLD THEM MY LIFE AND MY BOSS'S LIFE WERE AT STAKE BECAUSE OF THIS FIRE WHICH IF NO ONE HAD WARNED ME ABOUT AS I WAS DRIVING, THE CONSEQUENCE COULD HAVE BEEN TWO FATALITIES AS I DID NOT KNOW THE VEHICLE WAS ON FIRE AS I DROVE ALONG THE HIGHWAY. I'VE ASKED GENERAL MOTORS TO DO THE RIGHT THING, BREAK MY LEASE, AND THEY CAN HAVE THIS ENVOY TO DO WITH AS THEY PLEASE. TO DATE, THEY HAVE REFUSED TO ACCOMMODATE ME. I REFUSE TO PUT MYSELF OR MY TWO SMALL CHILDREN BACK INTO A VEHICLE THAT WAS ON FIRE AND COULD HAVE COST ME MY LIFE! *JB

Mar 4, 2007 Fire 50,000 mi

I WAS DRIVING ALONG INTERSTATE 69 NEAR FORT WAYNE IN MY LEASED 2006 GMC ENVOY DENALI WITH MY BOSS ON COMPANY BUSINESS WHEN A CAR FROM BEHIND ME PULLED ALONG SIDE HONKING THEIR HORN AND YELLING FOR ME TO PULL OVER AND GET OUT OF MY CAR BECAUSE IT WAS ON FIRE. WE IMMEDIATELY STOPPED, GOT OUT, AND SAW FLAMES UNDERNEATH THE ENGINE COMPARTMENT OF MY VEHICLE. WE CALLED 911 WHO DISPATCHED FORT WAYNE FIRE AND INDIANA STATE POLICE PERSONNEL. THE CAR WAS TOWED TO THE LOCAL GMC DEALERSHIP. BOTH A THIRD PARTY INSURANCE INVESTIGATOR AND A GENERAL MOTORS INVESTIGATOR CONCUR THAT THE FRONT DIFFERENTIAL FAILED CAUSING LUBRICANT TO SPRAY ONTO THE CATALYTIC CONVERTER AND EXHAUST SYSTEM IGNITING A FIRE. GENERAL MOTORS HAS ADMITTED TO ME THAT THIS IS A DEFECT I COULD NOT POSSIBLY KNOWN ABOUT NOR WAS IT MY FAULT IN ANY WAY. GENERAL MOTORS WANTS TO "REPAIR" THE VEHICLE AND PUT ME BACK IN IT. I'VE TOLD THEM MY LIFE AND MY BOSS'S LIFE WERE AT STAKE BECAUSE OF THIS FIRE WHICH IF NO ONE HAD WARNED ME ABOUT AS I WAS DRIVING, THE CONSEQUENCE COULD HAVE BEEN TWO FATALITIES AS I DID NOT KNOW THE VEHICLE WAS ON FIRE AS I DROVE ALONG THE HIGHWAY. I'VE ASKED GENERAL MOTORS TO DO THE RIGHT THING, BREAK MY LEASE, AND THEY CAN HAVE THIS ENVOY TO DO WITH AS THEY PLEASE. TO DATE, THEY HAVE REFUSED TO ACCOMMODATE ME. I REFUSE TO PUT MYSELF OR MY TWO SMALL CHILDREN BACK INTO A VEHICLE THAT WAS ON FIRE AND COULD HAVE COST ME MY LIFE! *JB