Compare to Other Years

Complaints

Showing 6 of 6
Aug 20, 2017 Electrical System 3,000 mi

ECM FAILURE AT 3000 MILES. THE MOTORCYCLE BEGAN STALLING AND RUNNING ROUGH. WHILE MOVING THE BIKE STALLED. AFTER RESTARTING THE MOTOR RAN VERY ROUGH, STARTING AND STALLING, AND THE CHECK ENGINE CAME ON. THIS HAPPENED ON A CITY STREET. BECAUSE OF THE LURCHING OF THE ENGINE I NEARLY DROPPED THE BIK...

Aug 20, 2017 Electrical System 3,000 mi

ECM FAILURE AT 3000 MILES. THE MOTORCYCLE BEGAN STALLING AND RUNNING ROUGH. WHILE MOVING THE BIKE STALLED. AFTER RESTARTING THE MOTOR RAN VERY ROUGH, STARTING AND STALLING, AND THE CHECK ENGINE CAME ON. THIS HAPPENED ON A CITY STREET. BECAUSE OF THE LURCHING OF THE ENGINE I NEARLY DROPPED THE BIK...

Aug 1, 2017 Electrical System 3,000 mi

MOTORCYCLE WITH 3000 MILES STALLS WHILE IN MOTION AND IS DIFFICULT TO RESTART WHEN THIS HAPPENS. ONCE RESTARTED IT RUNS ROUGH AND STALLS AND CHECK ENGINE LIGHT COMES ON. TOOK TO DEALER AND THEY REPLACED THE CRANK POSITION SENSOR. PROBLEM HAPPENED AGAIN AND NEARLY RESULTED IN ME DROPPING THE BIKE BEC...

Aug 1, 2017 Electrical System 3,000 mi

MOTORCYCLE WITH 3000 MILES STALLS WHILE IN MOTION AND IS DIFFICULT TO RESTART WHEN THIS HAPPENS. ONCE RESTARTED IT RUNS ROUGH AND STALLS AND CHECK ENGINE LIGHT COMES ON. TOOK TO DEALER AND THEY REPLACED THE CRANK POSITION SENSOR. PROBLEM HAPPENED AGAIN AND NEARLY RESULTED IN ME DROPPING THE BIKE BEC...

Jun 21, 2017 Electrical System 9,560 mi

WHILE IN A GROUP RIDE IN STAGGERED FORMAT ON THE 15S FREEWAY ON SATURDAY, JUNE 10TH AT APPROX. 8:20 AM, IN THE RAIN, I WAS CORNERING ON THE TRANSITION RAMP TO THE 163S AND LET HAND OFF THROTTLE, BUT ENGINE ACCELERATED WITHOUT THROTTLE INPUT TO 4000 RPMS. I WAVED BACK OTHER RIDERS, PULLED THE CLUTCH...

Jun 21, 2017 Electrical System 9,560 mi

WHILE IN A GROUP RIDE IN STAGGERED FORMAT ON THE 15S FREEWAY ON SATURDAY, JUNE 10TH AT APPROX. 8:20 AM, IN THE RAIN, I WAS CORNERING ON THE TRANSITION RAMP TO THE 163S AND LET HAND OFF THROTTLE, BUT ENGINE ACCELERATED WITHOUT THROTTLE INPUT TO 4000 RPMS. I WAVED BACK OTHER RIDERS, PULLED THE CLUTCH...