18
Complaints
0
Crashes
0
Fires
0
Deaths

This Problem Across All Years

All Engine And Engine Cooling Complaints

Showing 18 of 18
Dec 2, 2004

VEHICLE WAS TAKEN FOR EMISSIONS TEST AND FAILED. MECHANIC DETERMINED THAT A NEW CATALYTIC CONVERTER WAS NEEDED. CONSUMER NOTIFIED MANUFACTURER TO SEE IF ANY RECALLS WERE ISSUED. NO RECALLS WERE AVAILABLE PERTAINING TO THIS.*AK

Dec 2, 2004

VEHICLE WAS TAKEN FOR EMISSIONS TEST AND FAILED. MECHANIC DETERMINED THAT A NEW CATALYTIC CONVERTER WAS NEEDED. CONSUMER NOTIFIED MANUFACTURER TO SEE IF ANY RECALLS WERE ISSUED. NO RECALLS WERE AVAILABLE PERTAINING TO THIS.*AK

Jul 3, 2004 46,578 mi

WE WERE NORMALLY DRIVING THE VEHICLE WHEN A STRANGE NOISE STARTED UNDER THE HOOD. UPON INVESTIGATION YOU COULD OBSERVE THE MAIN PULLEY WOBBLING. THE VEHICLE WAS IMMEDIANTELY BROUGHT TO A REPAIR FACILITY. UPON INSPECTION IT WAS FOUND THAT THE BOLT FROM THE MAIN PULLEY INTO THE CRANKSHAFT WAS DAMAGED. WHEN A WRENCH WAS PLACED ON THE BOLT IT BROKE OFF. IT WAS APPARENT THAT THIS BOLT WAS INSTALLED STRIPPED WHICH RESULTED IN THIS FAILURE. PICTURES OF THE BOLT ARE AVAILABLE. THE VEHICLE WAS TOWED TO A HONDA DEALERSHIP. AFTER NUMEROUS PHONE CALLS, HONDA USA DID AGREE TO SPLIT THE COST TO REPLACE THE CRANKSHFT. MY SHARE WAS $1270.09. I REALIZE THAT THE WARRANTY WAS 36 MONTHS / 36000 MILES AND THE VEHICLE DID ACHIEVE THIS. BUT AT 46579 MILES AND 72 MONTHS A MAIN COMPONENT ON A PROPERLY MAINTAINED VEHICLE SHOULD NOT FAIL. PARTICULARLY WHEN IT IS APPARENT THE BOLT RESPONSIBLE FOR THIS WAS INCORRECTLY INSTALLED OR FAILED. *AK

Jul 3, 2004 46,578 mi

WE WERE NORMALLY DRIVING THE VEHICLE WHEN A STRANGE NOISE STARTED UNDER THE HOOD. UPON INVESTIGATION YOU COULD OBSERVE THE MAIN PULLEY WOBBLING. THE VEHICLE WAS IMMEDIANTELY BROUGHT TO A REPAIR FACILITY. UPON INSPECTION IT WAS FOUND THAT THE BOLT FROM THE MAIN PULLEY INTO THE CRANKSHAFT WAS DAMAGED. WHEN A WRENCH WAS PLACED ON THE BOLT IT BROKE OFF. IT WAS APPARENT THAT THIS BOLT WAS INSTALLED STRIPPED WHICH RESULTED IN THIS FAILURE. PICTURES OF THE BOLT ARE AVAILABLE. THE VEHICLE WAS TOWED TO A HONDA DEALERSHIP. AFTER NUMEROUS PHONE CALLS, HONDA USA DID AGREE TO SPLIT THE COST TO REPLACE THE CRANKSHFT. MY SHARE WAS $1270.09. I REALIZE THAT THE WARRANTY WAS 36 MONTHS / 36000 MILES AND THE VEHICLE DID ACHIEVE THIS. BUT AT 46579 MILES AND 72 MONTHS A MAIN COMPONENT ON A PROPERLY MAINTAINED VEHICLE SHOULD NOT FAIL. PARTICULARLY WHEN IT IS APPARENT THE BOLT RESPONSIBLE FOR THIS WAS INCORRECTLY INSTALLED OR FAILED. *AK

Dec 4, 2003 123,552 mi

THE VEHICLE LOST POWER WHILE DRIVING ON THE HIGHWAY AND DROVE ROUGHLY. DEALER DISCOVERED A BURNT #3 VALVE IN THE ENGINE TO BE THE CAUSE OF THE PROBLEM. *AK THE CHECK ENGINE WARNING LIGHT HAD COME ON BEFORE THE LOST OF POWER AND ROUGH RUNNING OCCURRED. *SCC *JB

Dec 4, 2003 123,552 mi

THE VEHICLE LOST POWER WHILE DRIVING ON THE HIGHWAY AND DROVE ROUGHLY. DEALER DISCOVERED A BURNT #3 VALVE IN THE ENGINE TO BE THE CAUSE OF THE PROBLEM. *AK THE CHECK ENGINE WARNING LIGHT HAD COME ON BEFORE THE LOST OF POWER AND ROUGH RUNNING OCCURRED. *SCC *JB

Sep 4, 2003

THERE IS VIBRATION IN THE ENTIRE VEHICLE DUE TO ENGINE VALVE FAILURE. DEALERSHIP HAS CONTINUOUSLY REPLACED ENGINE VALVE, BUT THE CAUSE OF THE FAILURE WAS UNDETERMINED. *AK

Sep 4, 2003

THERE IS VIBRATION IN THE ENTIRE VEHICLE DUE TO ENGINE VALVE FAILURE. DEALERSHIP HAS CONTINUOUSLY REPLACED ENGINE VALVE, BUT THE CAUSE OF THE FAILURE WAS UNDETERMINED. *AK

Aug 29, 2003 101,510 mi

1998 HOND CR-V NGINE TROUBLE. FLASHING WARNING LIGHT AT 101K MILES. BURNT #3 EXHAUST VALVE AND TIGHT VALVE CLEARANCES ON ALL EXHAUST VALVES. NOTICED THAT THERE ARE A FEW CR-V'S IN THE 1999 AND 2000 WITH THIS PROBLEM, ALL DUE TO POOR WORDING IN THE MAINTENANCE SECTION OF THE OWNER'S MANUAL. ALL THEY RECCOMMEND IS TO CHECK VALVES AT 105K MILES AND ADJUST THEM IF THE ENGINE IS NOISY. *AK

Aug 29, 2003 101,510 mi

1998 HOND CR-V NGINE TROUBLE. FLASHING WARNING LIGHT AT 101K MILES. BURNT #3 EXHAUST VALVE AND TIGHT VALVE CLEARANCES ON ALL EXHAUST VALVES. NOTICED THAT THERE ARE A FEW CR-V'S IN THE 1999 AND 2000 WITH THIS PROBLEM, ALL DUE TO POOR WORDING IN THE MAINTENANCE SECTION OF THE OWNER'S MANUAL. ALL THEY RECCOMMEND IS TO CHECK VALVES AT 105K MILES AND ADJUST THEM IF THE ENGINE IS NOISY. *AK

Aug 11, 2003 180,000 mi

CONSUMER STATES ENGINE LIGHT ILLUMINATES, AND VEHICLE IS MAKING A CLICKING NOISE AND JERKING WHILE DRIVING. TOOK VEHICLE TO DEALER, DEALER REPLACED CATALYTIC CONVERTER. *AK

Aug 11, 2003 180,000 mi

CONSUMER STATES ENGINE LIGHT ILLUMINATES, AND VEHICLE IS MAKING A CLICKING NOISE AND JERKING WHILE DRIVING. TOOK VEHICLE TO DEALER, DEALER REPLACED CATALYTIC CONVERTER. *AK

Dec 10, 2001

WHILE TRAVELING AT HIGHWAY SPEED OF 60-65 MPH THE VEHICLE SHUT DOWN WITHOUT ANY INDICATION, EVERY THING WENT DEAD; DEALER NOTIFIED AND INFORMED THAT THE PROBLEM WAS DUE TO THE IGNITION SWITCH, WHICH WAS REPLACE. FEEL FREE TO PROVIDE ANY FURTHER INFORMATION CONCERNING THIS MATTER.

Dec 10, 2001

WHILE TRAVELING AT HIGHWAY SPEED OF 60-65 MPH THE VEHICLE SHUT DOWN WITHOUT ANY INDICATION, EVERY THING WENT DEAD; DEALER NOTIFIED AND INFORMED THAT THE PROBLEM WAS DUE TO THE IGNITION SWITCH, WHICH WAS REPLACE. FEEL FREE TO PROVIDE ANY FURTHER INFORMATION CONCERNING THIS MATTER.

Dec 30, 1999

ENGINE REPAIRED ON FOUR OCCASIONS DUE TO HESITATION AND PROBLEMS, UNABLE TO BE RECTIFIED. MJS

Dec 30, 1999

ENGINE REPAIRED ON FOUR OCCASIONS DUE TO HESITATION AND PROBLEMS, UNABLE TO BE RECTIFIED. MJS

Mar 18, 1999

WHILE TRYING TO MAKE A STOP VEHICLE STALLED WIITHOUT ANY INDICATION. PLEASE PROVIDE FURTHER INFORMATON. *AK

Mar 18, 1999

WHILE TRYING TO MAKE A STOP VEHICLE STALLED WIITHOUT ANY INDICATION. PLEASE PROVIDE FURTHER INFORMATON. *AK