1996 LEXUS ES300 Problems & Recalls
Detailed safety information and owner complaints
Problem Breakdown
Compare to Other Years
Common Problems
TL* THE CONTACT OWNS A 1996 LEXUS ES300. THE CONTACT STATED THAT WHILE PARKED, A STRONG ODOR OF FUEL WAS COMING FROM THE VEHICLE. THE VEHICLE WAS TAKEN TO A DEALER WHERE IT WAS DIAGNOSED THAT THE FUEL FILLER NECK NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED ...
WAS DRIVING HOME FROM SHOPPING AND WENT TO TURN LEFT AND ALL OF A SUDDEN THE CAR DID NOT RESPOND SMOOTHLY AND I ALMOST LOST CONTROL. TOOK IT TO THE MECHANIC AND HAD A LOWER CONTROL ARM PUT IN BECAUSE OF A BAD BUSHING BUT WAS TOLD THE RACK AND PINION IS ALSO BAD. THERE IS A LOT OF PLAY IN THE STEERIN...
Mileage: 126,558
WAS DRIVING HOME FROM SHOPPING AND WENT TO TURN LEFT AND ALL OF A SUDDEN THE CAR DID NOT RESPOND SMOOTHLY AND I ALMOST LOST CONTROL. TOOK IT TO THE MECHANIC AND HAD A LOWER CONTROL ARM PUT IN BECAUSE OF A BAD BUSHING BUT WAS TOLD THE RACK AND PINION IS ALSO BAD. THERE IS A LOT OF PLAY IN THE STEERIN...
Mileage: 126,558
CAR EXPLODED AND STARTED FIRE IN THE GARAGE AFTER THE CAR HAD BEEN PARKED FOR APPROXIMATELY 20 MINUTES. GOT HOME FROM WORK AND STOP AT GROCERY STORE. PARKED CAR IN GARAGE AND BROUGHT IN SOME GROCERIES. ABOUT 10 - 15 MINUTES LATER WENT OUT TO GET PAPER PRODUCTS (TP AND PAPER TOWELS) OUT OF TRUNK. ...
Mileage: 158,000
CAR EXPLODED AND STARTED FIRE IN THE GARAGE AFTER THE CAR HAD BEEN PARKED FOR APPROXIMATELY 20 MINUTES. GOT HOME FROM WORK AND STOP AT GROCERY STORE. PARKED CAR IN GARAGE AND BROUGHT IN SOME GROCERIES. ABOUT 10 - 15 MINUTES LATER WENT OUT TO GET PAPER PRODUCTS (TP AND PAPER TOWELS) OUT OF TRUNK. ...
Mileage: 158,000
TL*-THE CONTACT OWNS A 1996 LEXUS ES300. WHILE THE CONTACT WAS DRIVING APPROXIMATELY 15 MPH, A LOUD NOISE WAS COMING FROM THE ENGINE. THE VEHICLE INCREASED ACCELERATION UNEXPECTEDLY. THE IGNITION WAS TURNED OFF. THE VEHICLE CONTINUED AND CRASHED INTO THE SIDE OF A BUILDING. THERE WAS NO INJURY. THE ...
DT*: THE CONTACT STATED THE PANEL IN THE DASH FAILED AND NOTHING IN THE DASH COULD BE SEEN. THE VEHICLE WAS TAKEN TO A DEALERSHIP WERE A DIAGNOSTICS TEST WAS PERFORMED. IT WAS DETERMINED THAT THE INSTRUMENT CLUSTER PANEL NEEDED TO BE REPLACED. NO REPAIRS WERE MADE. THE MANUFACTURER HAS BEEN AL...
Mileage: 172,000
1996 LEXUS ES300; SLUDGE BUILD-UP; EXCESSIVE OIL CONSUMPTION; WHITE SMOKE ON START-UP; DEALER SAYS THE ENGINE NEEDS TO BE REBUILT AT A COST OF ABOUT $7000. THIS IS THE SAME PROBLEM THAT TOYOTA/LEXUS HAS ACKNOWLEDGED FOR 1997 TO 2001 MODELS WITH THE V-6 ENGINE. WHY WON'T THEY HONOR THE REPAIR TO T...
Mileage: 145,000
BATTERY EXPLODED.*AK
CHECK ENGINE LIGHT CAME ON. SERVICING DEALER REPLACED O2 SENSOR - BANK 2, SENSOR 1, PART NUMBER 89465-33080 - DEALER LISTED AS $183.30 FOR THE PART WHILE WARRANTY COMPANY LISTED AS $128.11 FOR THE SAME PART. WHEN CHECKING WARRANTY COVERAGE, WAS TOLD WARRANTY DID NOT EXIST - PAID $1,860.00 TO BREDE...
ENGINE SEIZED IN DECEMBER 2000. LEXUS SAID IT WAS OUT OF WARRANTY. SUGGESTED I FIND A THIRD PARTY TO PUT A NEW ENGINE IN THE CAR WHICH I DID.
Mileage: 121,000
ENGINE OIL SLUDGE WE SPENT A TOTAL OF 2716.00 FOR A USED ENGINE, THE MILEAGE 109,313, I BOUGHT THE ENGINE ON MARCH 10, 2003....AND THE BREAKDOWN OCCURED ABOUT A WEEK PRIOR..
Mileage: 109,000
"CHECK ENGINE" LIGHT ILLUMINATES INTERMITTENTLY, BLUE EXHAUST SMOKE ON STARTUP, EXCESSIVE OIL CONSUMPTION, GELLED OIL OR SLUDGE PRESENT BENEATH OIL FILLER CAP ON VALVE COVER AFTER GOING TO LEXUS THE BEST THEY WOULD OFFER WAS TO EAT THE PARTS COST, ABOUT $500 BUT I WOULD STILL HAVE TO PAY $...
Mileage: 98,143
MY OIL LIGHT CAME ON IN MARCH. I TOOK THE CAR TO THE LEXUS DEALER ON 141 IN NORCROSS BECAUSE I KNEW MY 3 YEAR WARRENTY RAN OUT IN MAY. THE LEXUS DEALER TOLD ME THAT THE OIL WAS NOT FLOWING PROPERLY. HE SUGGESTED THE PREVIOUS OWNER DID NOT CHANGE THE OIL AND THE OIL BECAME CAKED TO THE ENGINE. THE OI...
Mileage: 93,000
ENGINE FAILED (SEIZED UP) DUE TO OIL SLUDGE, DESPITE THE FACT THAT THE CAR'S OIL HAD BEEN REGULARLY CHANGED. IN FACT, THE CAR'S OIL WAS CHANGED EVERY 3-4,000 MILES, NOT EVERY 5,000 AS RECOMMENDED BY LEXUS. CAR WAS ALSO COMPLETELY SERVICED BY LEXUS AT 70,000 MILES AND THEY OBVIOUSLY DIDN'T LOOK AT ...
Mileage: 86,068
AIRBAG OVER-SENSITIVITY DEFECT.*MR THE CONSUMER FEELS THAT THE AIR BAG WAS TOO SENSITIVE. THE VEHICLE WAS INVOLVED IN AN ACCIDENT IN WHICH THE DRIVERS SIDE BUMPER AND QUARTER PANEL WAS DAMAGED. BOTH FRONT AIR BAGS DEPLOYED. AN INFANT CAR SEAT , WITH THE CONSUMER CHILD FASTENED INSIDE, WAS IN THE...
ENGINE CHECK LIGHT INTERMITTENTLY ON, BLUE EXHAUST IN ENGINE SMOKE, ABNORMAL OIL CONSUMPTION, GELLED OIL OR SLUDGE PRESENT INSIDE VALVE COVER BELOW OIL FILLER CAP. CALLED LEXUS AMERICA, BROUGHT CAR INTO DEALER, THEY TELL ME I MUST PAY $2,071.06 FOR REPAIRS AND PRETEND NOT TO KNOW OF THIS COMMON 3.0...
Mileage: 98,000
ENGINE CHECK LIGHT INTERMITTENTLY ON, BLUE EXHAUST IN ENGINE SMOKE, ABNORMAL OIL CONSUMPTION, GELLED OIL OR SLUDGE PRESENT INSIDE VALVE COVER BELOW OIL FILLER CAP. CALLED LEXUS AMERICA, BROUGHT CAR INTO DEALER, THEY TELL ME I MUST PAY $2,071.06 FOR REPAIRS AND PRETEND NOT TO KNOW OF THIS COMMON 3.0...
Mileage: 98,000
STEERING WHEEL LOCKED . LUCKILY WHILE PARKED. CAR TOWED TO LEXUS OF MARIN. BILL 3000. MILEAGE ON CAR BETWEEN 40-50000
Mileage: 45,000
EXCESSIVE BLUE SMOKE COMES OUT OF THE TAILPIPE. ENGINE OIL CONSUMPTION IS VERY HIGH. ENGINE DAMAGE DUE TO OIL GELLING/SLUDGE. *AK
TRIED TO VEER SLIGHTLY LEFT. CAR WENT OVER 3 LANES OF EXPRESSWAY.TRIED R THEN L 4 TIMES AND BRAKED, BUT EACH TIME WENT OVER ALL LANES AND IDN'T STOP. WOUND UP 180 DEGREES FACING THE WRONG WAY STALLED. MIRACULOUSLY ALL THE DRIVCERS BEHIND HAD JUST STOPPED. THOUGHT IT WAS MY DRIVING TECHNIQUE. 2 DAY...
LEXUS ES300 LEFT ROAD AND FLIPPED ONE TIME. DRIVER'S DOOR CAME OPEN AND BUCKLED SEATBELT DID NOT HOLD DRIVER IN CAR. DRIVER'S HEAD ENDED UP UNDER THE DRIVER'S SIDE ROOF DOOR JAMMED AND KILLED INSTANTLY.*AK
LEXUS ES300 LEFT ROAD AND FLIPPED ONE TIME. DRIVER'S DOOR CAME OPEN AND BUCKLED SEATBELT DID NOT HOLD DRIVER IN CAR. DRIVER'S HEAD ENDED UP UNDER THE DRIVER'S SIDE ROOF DOOR JAMMED AND KILLED INSTANTLY.*AK
I JUST RECENTLY PURCHARSED THIS CAR AND I AM ALREADY $1000.00 IN THE HOLE AND LOOKING AT $2000 JUST TO BE ABLE TO DRIVE IT.IT WAS A LEMON FROM THE START AND NOBODY IS WILLING TO COVER ARE ASSIT WITH THE REPAIR JUST TRYING TO SEE WHAT LEGAL OPTIONS I HAVE .I HAVE'NT MADE A PAYMENT ON IT YET ,BUT IT'S...
WHILE DRIVING ENGINE CHECK LIGHT WOULD COME ON. ENGINE BLEW DUE TO SLUDGE(HARD OIL IN ENGINE). VEHICLE WAS REPAIRED IN NOVEMBER. THE PROBLEM AROSE AGAIN IN DECEMBER. THERE WAS MAIN BEARING DAMAGE, TOO SEVERE TO REPAIR AND HAS HAD PROBLEMS WITH THE REAR MAIN OIL SEAL. *JG *AK
DANGEROUS. COULD NOT TURN OFF CAR EXCEPT TO DISCONNECT NEGATIVE TERMINAL ON BATTERY. VERY DANGEROUS. TOOK ALMOST 10 MINUTES TO TURN OFF CAR. REMOVING KEY DID NOTHING. THIS IS A HAZARD TO ALL. COULD HAVE BEEN DISASTROUS. LEXUS WAS NOTIFIED. *AK
WHILE DEFOGGING REAR WINDOW GLASS POPPED OUT INSIDE OF VEHICLE INTO LITTLE PIECES. DEALER HAS BEEN NOTIFIED. PLEASE PROVIDE FURTHER INFORMATION.*AK
STEERING SYSTEM FAILED WHILE DRIVING. STEERING BECAME VERY LOOSE. HEARD NOISES COMING FROM STEERING COLUMN. TOOK VEHICLE TO DEALERSHIP. WAS INFORMED THAT RACK AND PINION STEERING UNIT NEEDED TO BE REPLACED.*AK POWER STEERING PUMP ALSO NEEDED REPLACED. *SLC
STEERING SYSTEM FAILED WHILE DRIVING. STEERING BECAME VERY LOOSE. HEARD NOISES COMING FROM STEERING COLUMN. TOOK VEHICLE TO DEALERSHIP. WAS INFORMED THAT RACK AND PINION STEERING UNIT NEEDED TO BE REPLACED.*AK POWER STEERING PUMP ALSO NEEDED REPLACED. *SLC
STEERING SYSTEM FAILED AND WOULD MAKE NOISES. TOOK VEHICLE TO MECHANIC AND WAS INFORMED THAT RACK AND PINION STEERING WAS SHOT AND VEHICLE NOT SAFE TO DRIVE.*AK POWER STEERING PUMP WAS ALSO REPLACED AT COST TO CONSUMER. *SLC
STEERING SYSTEM FAILED AND WOULD MAKE NOISES. TOOK VEHICLE TO MECHANIC AND WAS INFORMED THAT RACK AND PINION STEERING WAS SHOT AND VEHICLE NOT SAFE TO DRIVE.*AK POWER STEERING PUMP WAS ALSO REPLACED AT COST TO CONSUMER. *SLC
CONSUMER WAS INVOLVED IN AN HEAD-ON COLLISION WHILE TRAVELING 40 MPH IN WHICH DRIVER'S SIDE AND PASSENGER'S SIDE AIR BAGS DID NOT DEPLOY, CAUSING INJURIES TO DRIVER'S SIDE OCCUPANT. PLEASE PROVIDE ANY FURTHER DETAILS. CONSUMER STATED VEHICLE WAS A TOTAL LOSS. *AK
CONSUMER WAS PULLING ON THE STRAP TO RESTRAIN THE BUCKLE BROKE OFF STRAP. DEALER DIDN'T SEEM TO BE CONCERNED ABOUT THE SAFETY. CONSUMER FELT THAT IF IN A CRASH IT WOULD BE VERY UNSAFE. *AK
CONSUMER WAS INVOLVED IN A MINOR COLLISION IN WHICH AIR BAGS DID NOT DEPLOY, KILLING INFANT IN THE PASSENGER'S SEAT. PLEASE GIVE ANY FURTHER DETAILS. *AK
CONSUMER WAS TRAVELING ON A SIDE STREET ENGAGED CRUISE CONTROL AND VEHICLE ACCELERATED. COULD NOT DISENGAGE CRUISE CONTROL. *AK
THE LAMINATION IN THE WINDSHIELD HAS DETRIORATED CAUSING THE WINDOW TO LOOK DISTORTED WHICH RESULTS IN POOR VISIBILITY. HOWEVER, THE VEHICLE WAS TAKEN TO DEALER & THE PROBLEM WAS CONFIRMED BY THE MECHANIC. *YC
WHILE DRIVING DOWN THE ROAD ANOTHER VEHICLE CROSSED OVER DOUBLE LINES AND SPUN AROUND AND HIT CONSUMER'S VEHICLE AND WENT INTO TREES AND THE HIT CONSUMER'S VEHICLE A THIRD TIME. AS A RESULT, DRIVER'S HEAD HIT WINDSHIELD. AIRBAGS DID NOT DEPLOY. CONSUMER CONTACTED DEALER AND MANUFACTURER. *AK
THERE WAS NO DEPLOYMENT OF THE AIRBAG AND THE TWO FRONT SEATS FULLY RECLINED DURING THE ACCIDENT.
THERE WAS NO DEPLOYMENT OF THE AIRBAG AND THE TWO FRONT SEATS FULLY RECLINED DURING THE ACCIDENT.
ENGINE FIRE.
NO DEPLOYMENT OF DRIVER'S AIR BAG IN ACCIDENT, RESULTING IN INJURIES.
BATTERY FAILED.
THE ENTIRE VEHICLE SHIMMIES, CAN FEEL THROUGH THE STEEERING COLUMN AND ALL OVER, CAUSE UNKNOWN: *AK
STEERING FAILURE, WHILE DRIVING AT SPEED OF 40MPH, SLIGHTLY TURNING THE WHEEL TO CHANGE LANES, VEHICLE WENT OUT OF CONTROL, IMPACT 12:00 POSITION. *AK CONSUMER WAS BRAKING MODERATELY WHILE TURNING STEERING WHEEL. *SLC