This Problem Across All Years
FAULTY CAM AND CRANKSHAFT POSITION SENSOR CAUSED ENGINE TO DIE (STALL) IN THE MID TRAFFIC ON THREE SEPARATE OCCASIONS WITHIN A PERIOD OF TWO WEEKS. DEALER REPLACED CAM POSITION SENSOR 003-153-28-28 AND SENDER UNIT 004-153-69-28, INDICATING THE CAUSE AS AN INTERNAL FAULT. DEALER'S SERVICE REP INDICATED THAT THIS WAS A COMMON PROBLEM. *TR
FAULTY CAM AND CRANKSHAFT POSITION SENSOR CAUSED ENGINE TO DIE (STALL) IN THE MID TRAFFIC ON THREE SEPARATE OCCASIONS WITHIN A PERIOD OF TWO WEEKS. DEALER REPLACED CAM POSITION SENSOR 003-153-28-28 AND SENDER UNIT 004-153-69-28, INDICATING THE CAUSE AS AN INTERNAL FAULT. DEALER'S SERVICE REP INDICATED THAT THIS WAS A COMMON PROBLEM. *TR
TL*THE CONTACT OWNS A 2000 MERCEDES BENZ E CLASS 320 WAGON WHICH WAS PURCHASED USED IN MARCH 2003. HE STATED THAT WHILE DRIVING AT SPEEDS OF LESS THAN 40 MPH, THE CONTACT THOUGHT HE HAD RUN OVER SOMETHING AND THERE WAS A VIOLENT VIBRATION IN THE STEERING WHEEL. THEN, WHILE MAKING A LEFT TURN HE COULD HEARD A GRINDING AND THUMPING SOUND COMING FROM UNDER THE VEHICLE. HE THEN NOTICED THE FRONT PASSENGER'S SIDE WHEEL WAS ACTUALLY INSIDE THE WHEEL WELL. THE VEHICLE WAS TOWED TO THE NEAREST DEALER WHERE THEY FOUND THE FRONT PASSENGER'S SIDE COIL SPRING PERCH FAILED CAUSING THE FRONT END PASSENGER'S SIDE OF THE VEHICLE TO COLLAPSE. THE CURRENT AND FAILURE MILEAGES WERE UNDER 130,000. UPDATED 01/19/10 *BF THE AIR MASS FLOW SENSOR AND OUTER TIE ROD WERE REPLACED. THE LOWER BALL JOINTS WERE WORN AND WERE REPLACED. THE CRANK SENSOR WAS REPLACED. THE ENGINE WAS CONSUMING LARGE AMOUNTS OF OIL. THE DEALER STATED THE VEHICLE NEEDED NEW RINGS AND A VALVE SEAL. THE TRANSMISSION WOULD SLIP DURING COLD WEATHER CONDITIONS. THERE WAS AN INTERNAL FAULT WITH THE CLUTCHES. THE GEAR SHIFTER HAD EXCESSIVE PLAY. THE LEFT WINDOW REGULATOR HAD TO BE REPLACED, BECAUSE IT WOULD NOT CLOSE. THE LEFT REAR DOOR LATCH WAS INOPERATIVE. UPDATED 01/20/10.*JB
TL*THE CONTACT OWNS A 2000 MERCEDES BENZ E CLASS 320 WAGON WHICH WAS PURCHASED USED IN MARCH 2003. HE STATED THAT WHILE DRIVING AT SPEEDS OF LESS THAN 40 MPH, THE CONTACT THOUGHT HE HAD RUN OVER SOMETHING AND THERE WAS A VIOLENT VIBRATION IN THE STEERING WHEEL. THEN, WHILE MAKING A LEFT TURN HE COULD HEARD A GRINDING AND THUMPING SOUND COMING FROM UNDER THE VEHICLE. HE THEN NOTICED THE FRONT PASSENGER'S SIDE WHEEL WAS ACTUALLY INSIDE THE WHEEL WELL. THE VEHICLE WAS TOWED TO THE NEAREST DEALER WHERE THEY FOUND THE FRONT PASSENGER'S SIDE COIL SPRING PERCH FAILED CAUSING THE FRONT END PASSENGER'S SIDE OF THE VEHICLE TO COLLAPSE. THE CURRENT AND FAILURE MILEAGES WERE UNDER 130,000. UPDATED 01/19/10 *BF THE AIR MASS FLOW SENSOR AND OUTER TIE ROD WERE REPLACED. THE LOWER BALL JOINTS WERE WORN AND WERE REPLACED. THE CRANK SENSOR WAS REPLACED. THE ENGINE WAS CONSUMING LARGE AMOUNTS OF OIL. THE DEALER STATED THE VEHICLE NEEDED NEW RINGS AND A VALVE SEAL. THE TRANSMISSION WOULD SLIP DURING COLD WEATHER CONDITIONS. THERE WAS AN INTERNAL FAULT WITH THE CLUTCHES. THE GEAR SHIFTER HAD EXCESSIVE PLAY. THE LEFT WINDOW REGULATOR HAD TO BE REPLACED, BECAUSE IT WOULD NOT CLOSE. THE LEFT REAR DOOR LATCH WAS INOPERATIVE. UPDATED 01/20/10.*JB
TL*THE CONTACT OWNS A 2000 MERCEDES BENZ E CLASS 320 WAGON WHICH WAS PURCHASED USED IN MARCH 2003. HE STATED THAT WHILE DRIVING AT SPEEDS OF LESS THAN 40 MPH, THE CONTACT THOUGHT HE HAD RUN OVER SOMETHING AND THERE WAS A VIOLENT VIBRATION IN THE STEERING WHEEL. THEN, WHILE MAKING A LEFT TURN HE COULD HEARD A GRINDING AND THUMPING SOUND COMING FROM UNDER THE VEHICLE. HE THEN NOTICED THE FRONT PASSENGER'S SIDE WHEEL WAS ACTUALLY INSIDE THE WHEEL WELL. THE VEHICLE WAS TOWED TO THE NEAREST DEALER WHERE THEY FOUND THE FRONT PASSENGER'S SIDE COIL SPRING PERCH FAILED CAUSING THE FRONT END PASSENGER'S SIDE OF THE VEHICLE TO COLLAPSE. THE CURRENT AND FAILURE MILEAGES WERE UNDER 130,000. UPDATED 01/19/10 *BF THE AIR MASS FLOW SENSOR AND OUTER TIE ROD WERE REPLACED. THE LOWER BALL JOINTS WERE WORN AND WERE REPLACED. THE CRANK SENSOR WAS REPLACED. THE ENGINE WAS CONSUMING LARGE AMOUNTS OF OIL. THE DEALER STATED THE VEHICLE NEEDED NEW RINGS AND A VALVE SEAL. THE TRANSMISSION WOULD SLIP DURING COLD WEATHER CONDITIONS. THERE WAS AN INTERNAL FAULT WITH THE CLUTCHES. THE GEAR SHIFTER HAD EXCESSIVE PLAY. THE LEFT WINDOW REGULATOR HAD TO BE REPLACED, BECAUSE IT WOULD NOT CLOSE. THE LEFT REAR DOOR LATCH WAS INOPERATIVE. UPDATED 01/20/10.*JB
TL*THE CONTACT OWNS A 2000 MERCEDES BENZ E CLASS 320 WAGON WHICH WAS PURCHASED USED IN MARCH 2003. HE STATED THAT WHILE DRIVING AT SPEEDS OF LESS THAN 40 MPH, THE CONTACT THOUGHT HE HAD RUN OVER SOMETHING AND THERE WAS A VIOLENT VIBRATION IN THE STEERING WHEEL. THEN, WHILE MAKING A LEFT TURN HE COULD HEARD A GRINDING AND THUMPING SOUND COMING FROM UNDER THE VEHICLE. HE THEN NOTICED THE FRONT PASSENGER'S SIDE WHEEL WAS ACTUALLY INSIDE THE WHEEL WELL. THE VEHICLE WAS TOWED TO THE NEAREST DEALER WHERE THEY FOUND THE FRONT PASSENGER'S SIDE COIL SPRING PERCH FAILED CAUSING THE FRONT END PASSENGER'S SIDE OF THE VEHICLE TO COLLAPSE. THE CURRENT AND FAILURE MILEAGES WERE UNDER 130,000. UPDATED 01/19/10 *BF THE AIR MASS FLOW SENSOR AND OUTER TIE ROD WERE REPLACED. THE LOWER BALL JOINTS WERE WORN AND WERE REPLACED. THE CRANK SENSOR WAS REPLACED. THE ENGINE WAS CONSUMING LARGE AMOUNTS OF OIL. THE DEALER STATED THE VEHICLE NEEDED NEW RINGS AND A VALVE SEAL. THE TRANSMISSION WOULD SLIP DURING COLD WEATHER CONDITIONS. THERE WAS AN INTERNAL FAULT WITH THE CLUTCHES. THE GEAR SHIFTER HAD EXCESSIVE PLAY. THE LEFT WINDOW REGULATOR HAD TO BE REPLACED, BECAUSE IT WOULD NOT CLOSE. THE LEFT REAR DOOR LATCH WAS INOPERATIVE. UPDATED 01/20/10.*JB
DRIVER SIDE ENGINE MOUNT BROKE WHILE DRIVING AND AS A RESULT, THE HEAT SHIELD AROUND THE STEERING COLUMN BENT FROM THE ENGINE ROTATING. THIS RESULTED IN THE ALUMINUM SHIELD JAMMING THE STEERING COLUMN FROM TURNING. THIS OCCURRED DURING A SHARP CORNER AND STEERING INPUTS TO STRAIGHTEN THE VEHICLE DID NOT PRODUCE ANY RESULTS. VEHICLE NEARLY CRASHED INTO ONCOMING TRAFFIC. NEW HEAT SHIELD AND MOTOR MOUNTS ARE BEING REPLACED. OLD MOUNT WAS KEPT. THIS IS A WELL DOCUMENTED FAILURE ON MERCEDES BENZ E55 MOTORS. *TR
DRIVER SIDE ENGINE MOUNT BROKE WHILE DRIVING AND AS A RESULT, THE HEAT SHIELD AROUND THE STEERING COLUMN BENT FROM THE ENGINE ROTATING. THIS RESULTED IN THE ALUMINUM SHIELD JAMMING THE STEERING COLUMN FROM TURNING. THIS OCCURRED DURING A SHARP CORNER AND STEERING INPUTS TO STRAIGHTEN THE VEHICLE DID NOT PRODUCE ANY RESULTS. VEHICLE NEARLY CRASHED INTO ONCOMING TRAFFIC. NEW HEAT SHIELD AND MOTOR MOUNTS ARE BEING REPLACED. OLD MOUNT WAS KEPT. THIS IS A WELL DOCUMENTED FAILURE ON MERCEDES BENZ E55 MOTORS. *TR
DT*: THE CONTACT STATED WHILE DRIVING 65 MPH ON THE HIGHWAY, THERE WAS A LOSS OF ALL VEHICLE POWER, AND THE ENGINE STALLED WITHOUT WARNING. THE CONTACT MANEUVERED THE VEHICLE TO THE SIDE OF THE ROAD. THE ENGINE WOULD NOT RESTART. THE VEHICLE WAS TOWED TO THE DEALER, WHO DETERMINED THE ME CONTROL MODULE OF THE ENGINE FAILED AND NEEDED TO BE REPLACED. THE MANUFACTURER WAS ALERTED.
DT*: THE CONTACT STATED WHILE DRIVING 65 MPH ON THE HIGHWAY, THERE WAS A LOSS OF ALL VEHICLE POWER, AND THE ENGINE STALLED WITHOUT WARNING. THE CONTACT MANEUVERED THE VEHICLE TO THE SIDE OF THE ROAD. THE ENGINE WOULD NOT RESTART. THE VEHICLE WAS TOWED TO THE DEALER, WHO DETERMINED THE ME CONTROL MODULE OF THE ENGINE FAILED AND NEEDED TO BE REPLACED. THE MANUFACTURER WAS ALERTED.
SEVER LOSS OF POWER DURING OPERATION AS A RESULT OF FAULTY CATALYTIC CONVERTERS IN MERCEDES E300 (2000 MODEL). *NM
SEVER LOSS OF POWER DURING OPERATION AS A RESULT OF FAULTY CATALYTIC CONVERTERS IN MERCEDES E300 (2000 MODEL). *NM
DT: ON THE HIGHWAY THE ENGINE STOPPED SUDDENLY. THEY PUSHED THE VEHICLE TO THE SIDE OF THE ROAD AND THEN CALLED A TOW TRUCK. CONSUMER WAITED 30-45 MINUTES AND THE ENGINE STARTED. THE VEHICLE WAS THEN MOVED APPROXIMATELY 2-3 MILES AND THE IT STALLED AGAIN. THE VEHICLE WAS TOWED TO THE DEALERSHIP; THEY WERE CURRENTLY LOOKING AT THE VEHICLE. THE CHECK ENGINE LIGHT DID COME ON. THERE HAD BEEN NO PROBLEMS WITH THE ENGINE PRIOR TO THIS. THE VEHICLE HAD BEEN INSPECTED A MONTH PRIOR, THE CONSUMER HAD SPILLED COFFEE IN THE GEAR SHIFTER.*AK
DT: ON THE HIGHWAY THE ENGINE STOPPED SUDDENLY. THEY PUSHED THE VEHICLE TO THE SIDE OF THE ROAD AND THEN CALLED A TOW TRUCK. CONSUMER WAITED 30-45 MINUTES AND THE ENGINE STARTED. THE VEHICLE WAS THEN MOVED APPROXIMATELY 2-3 MILES AND THE IT STALLED AGAIN. THE VEHICLE WAS TOWED TO THE DEALERSHIP; THEY WERE CURRENTLY LOOKING AT THE VEHICLE. THE CHECK ENGINE LIGHT DID COME ON. THERE HAD BEEN NO PROBLEMS WITH THE ENGINE PRIOR TO THIS. THE VEHICLE HAD BEEN INSPECTED A MONTH PRIOR, THE CONSUMER HAD SPILLED COFFEE IN THE GEAR SHIFTER.*AK
VEHICLE LOST BELT ON THE HIGHWAY AT 55 MPH. CONSUMER COULD STILL DRIVE CAR BUT POWER STEERING WAS LOST. CONSUMER WAS ABLE TO MAKE IT TO THE SERVICE ROAD. THEN, VEHICLE WAS TOWED. THE SERPENTINE BELT MELTED AND FELL OFF. *AK CONSUMER STATED THE BATTERY/ALTERNATOR LIGHT CAME ON AND THE POWER STEERING DID NOT WORKING. THE A/C COMPRESSOR ALSO SIEZED. *BF *NM
VEHICLE LOST BELT ON THE HIGHWAY AT 55 MPH. CONSUMER COULD STILL DRIVE CAR BUT POWER STEERING WAS LOST. CONSUMER WAS ABLE TO MAKE IT TO THE SERVICE ROAD. THEN, VEHICLE WAS TOWED. THE SERPENTINE BELT MELTED AND FELL OFF. *AK CONSUMER STATED THE BATTERY/ALTERNATOR LIGHT CAME ON AND THE POWER STEERING DID NOT WORKING. THE A/C COMPRESSOR ALSO SIEZED. *BF *NM