1990 MERCURY GRAND MARQUIS Electrical System Problems

14 complaints about Electrical System

14
Complaints
0
Crashes
4
Fires
0
Deaths

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Electrical System Complaints (14)

Apr 2, 2002

THE CONSUMER WAS SEEKING RECALL ON THE TFI MODULE WHICH WAS DEFECTIVE. THE TFI MODULE FAILURE COULD RESULT IN ACCIDENT AND DEATH. CONSUMER STATED THAT THE CLASS ACTION SETTLEMENT DOES NOT FORCE A RECALL BUT ONLY COVERS REPLACEMENT COST AFTER FAILURE. *YH

Mar 5, 2002

CONSUMER STATES DURING HIGHWAY DRIVING VEHICLE COMPLETELY SHUT DOWN AND WOULD NOT RESTART. THICK FILM IGNITION MOUDLE HAD TO BE REPLACED. *TT

Aug 23, 2001

I WAS PROCEEDING HOME IN EVENING RUSH HOUR TRAFFIC WHEN THE CAR ENGINE QUIT INSTANTANEOUSLY. I WAS FORCED TO STOP IN THE RIGHT LANE OF TRAFFIC. ALTHOUGH IN THE RIGHT LANE I COULD NOT PULL OFF OF THE ROAD BECAUSE THERE WAS A BARRIER WITH NO SHOULDER FOR ME TO PULL ONTO. FORTUNATELY I WAS NOT HIT BY ANOTHER CAR ALTHOUGH I WAS SITTING WHERE TRAFFIC HAD TO STOP ABRUPTLY AND SWERVE TO AVOID HITTING ME. THE CAR WAS SITTING IN TRAFFIC UNTIL A TOW TRUCK ARRIVED APPROXIMATELY ONE HOUR LATER. THE VEHICLE TRAFFIC WHERE I WAS STALLED ROUTINELY MOVES AT OVER 50 MILES PER HOUR WHICH LUCKILY FOR ME DID NOT RESULT IN A MAJOR ACCIDENT. *AK

Jan 4, 2001 Fire

VEHICLE WAS DRIVEN APPROXIMATELY ONE MILE AND PARKED. UPON EXITING THE VEHICLE, THE OPERATOR NOTICED SMOKE COMING FROM UNDER THE HOOD. AFTER OPENING THE HOOD, THE OPERATOR IDENTIFIED THE SOURCE OF THE SMOKE AS THE ALTERNATOR. OPERATOR CONTINUED TO OBSERVE THE VEHICLE AND NOTED THAT THE VOLUME OF SMOKE WAS INCREASING. AFTER APPROXIMATELY TWO MINUTES, THE ALTERNATOR BURST INTO FLAMES. ARCING WAS SEEN AND HEARD WITHIN THE ALTERNATOR. THE ALTERNATOR HAD BEEN PREVIOUSLY REPLACED BY FETTE FORD IN WAYNE, NJ IN SEPT 1999 AND, UPON SUBSEQUENT FAILURE, AGAIN IN APPROXIMATELY JAN 2000. FETTE FORD STATED THAT REBUILT FORD ALTERNATORS WERE USED IN BOTH CASES. *AK

Mar 24, 1999

WIRING HARNESS SHORTED OUT, CAUSING ALL LIGHTS INSIDE VEHICLE, AS WELL AS TAIL LIGHTS AND PARK LIGHTS TO STAY ON. IN ADDITION, FUSE BURNED AND MELTED. REPAIRS MADE AT OWNER'S EXPENSE. *AK

Mar 24, 1999

WIRING HARNESS SHORTED OUT, CAUSING ALL LIGHTS INSIDE VEHICLE, AS WELL AS TAIL LIGHTS AND PARK LIGHTS TO STAY ON. IN ADDITION, FUSE BURNED AND MELTED. REPAIRS MADE AT OWNER'S EXPENSE. *AK

Feb 10, 1998 Fire

WHEN TRAVELING THE VEHICLE CAUGHT ON FIRE DUE TO AN ELECTRICAL SHORT IN THE ALTERNATOR. CONSUMER STATES THAT THE VEHICLE WAS A TOTAL LOSS. *AK

Oct 20, 1997 Fire

WIRING HARNESS FAILURE CAUSED FIRE.

Nov 19, 1996

OWNER UNABLE TO DETECT HORN BUTTONS ON STEERING WHEEL. *AK

Aug 7, 1996

THE VEHICLE IS EXPERIENCING ELECTRCAL PROBLEMS DUE TO THE IGNITION SWITCH. COULD START A FIRE. *AK

May 6, 1996

IGNITION SWITCH OVERHEATS. *SD

Jan 23, 1996

DIGITAL DASH DISPLAY; MAYBE TWICE A WEEK LIGHTS WILL DIM/GO OUT INCLUDING ABS LIGHT. PLEASE DESCRIBE DETAILS. TT

Dec 12, 1995 Fire

FIRE ERUPTED UNDER HOOD WHILE DRIVING; DETECTED EXTREME AMOUNT OF FUMES; STOPPED VEHICLE, SHUT OFF IGNITION; FLAMES BURST OUT WITH LOUD NOISE; TOTALED. TT

Jun 21, 1995

HORN BUTTON DIFFICULT TO LOCATE IF WHEEL IS TURNED AND DIFFICULT ACCESS. PLEASE DESCRIBE DETAILS. TT