1993 MITSUBISHI MONTERO Problems & Recalls
Detailed safety information and owner complaints
Problem Breakdown
Compare to Other Years
Common Problems
DT*: THE CONTACT STATED WHILE PARKED WITH THE ENGINE IDLING, IT WAS NOTICED THAT THE PULLEY FOR THE POWER STEERING WAS LOOSE. AS THE CONTACT ALREADY HAD THE RECALL # 00V311001, REGARDING ENGINE AND ENGINE COOLING:ENGINE REPAIRS PERFORMED ONCE, THE VEHICLE WAS TAKEN TO THE DEALERSHIP WHO DETERMINED ...
Mileage: 275,000
DT*: THE CONTACT STATED WHILE PARKED WITH THE ENGINE IDLING, IT WAS NOTICED THAT THE PULLEY FOR THE POWER STEERING WAS LOOSE. AS THE CONTACT ALREADY HAD THE RECALL # 00V311001, REGARDING ENGINE AND ENGINE COOLING:ENGINE REPAIRS PERFORMED ONCE, THE VEHICLE WAS TAKEN TO THE DEALERSHIP WHO DETERMINED ...
Mileage: 275,000
PULLED OUT OF DRIVEWAY AND PROCEEDED FORWARD WHEN THE RIGHT WHEEL DID NOT STEER. DROVE VEHICLE BACK INTO DRIVEWAY. PASSENGER SIDE INNER TIE-ROD PULLED OUT OF THE TREADED TUBE. ORDERED PARTS TO REPLACE BOTH INNER AND OUTER TIE-RODS WITH CONNECTING THREADED TUBE. IT'S A GOOD THING IT DIDN'T HAPPE...
Mileage: 150,000
ADDITION TO COMPLAINT 10088338. FTER HAVING THE VEHICLE CHECKED BY MY MECHANIC, THE PROBLEM IS THAT THE BOLT (THE ONE LISTED IN THE ORIGINAL RECALL) BACKED OUT OF THE CRANK SHAFT CAUSING THE PULLY TO WOBBLE (DISTROYING THE PULLEY IN THE PROCESS). ONCE THE BOLT WAS 3/4 OF THE WAY OUT, IT SNAPPED IN ...
Mileage: 169,000
ON 03/16/01 RECALL WORK WAS DONE AT SERVICE DEALER. ON DATE OF INCIDENT, CRANK BOLT SHEERED OFF OR CAME OUT WHILE DRIVING AT 45M MPH. *JB
Mileage: 45
ENGINE STALLED IN THE MIDDLE OF AN INTERSECTION WHILE DRIVING AT 55 MPH. VEHICLE WAS TOWED TO INDEPENDENT SHOP. TECHNICIAN STATED THAT BOLT SECURING THE CRANKSHAFT PULLEY BROKE. AS A RESULT, ENGINE WAS OVERHAULED AT OWNER'S EXPENSE.*AK
Mileage: 79,000
WHILE DRIVING AT 65MPH CRANKSHAFT BOLT SNAPPED, CAUSING MOTOR TO SHUTOFF WITH NO WARNING. DEALER NOTIFIED.*AK
CRANKSHAFT PULLEY BOLT CAME LOOSE, CAUSING THE CRANKSHAFT TO STRIP OUT THE GEARING. THE VEHICLE SEEMED TO LOOSE POWER & WAS LESS RESPONSIVE ... & THE HIDEOUS SCREECHING SOUND SCARED THE HECK OUT OF ALL THE DRIVERS & PEDESTRIANS WHO WERE NEARBY AT THE INTERSECTION. REPAIRS ARE ESTIMATED TO BE AROUN...
THE CRANKSHAFT BOLTS FAILED WHILE DRIVING CAUSING A SUDDEN LOSS OF POWER STEERING PRIOR TO RECALL NOTICE 00V-311, THE CONSUMER REQUEST REIMBURSEMENT. NLM
WHILE DRIVING OUT OF PARKING LOT AND WAS MAKING A LEFT TURN, STEERING COLUMN DROPPED DOWN. IT WAS AN ADJUSTED STEERING COLUMN. TRIED TO READJUST IT, WHICH WAS NOT A PROBLEM. DROVE VEHICLE HOME AND PARKED IT. CHECKED UNDER DASH NEAR COLUMN AND NOTICED A BOLT HAD FALLEN OUT, AND NEEDED TO BE REPLACED....
ON MITSUBISHI, MONTERO 1993, WITH B.F.GOODRICH TA 30 X 9.5 TIRES, CONSUMER NOTICED A CRACK IN THE RIGHT FRONT TIRE. CONSUMER FELT TREAD MAY HAVE BEEN SEPARATING.*AK
STEERING WHEEL DEVELOPED A 2 TO 3 INCH FRONT TO BACK MOTION. TRUCK WILL NOT PASS PA INSPECTION. A MITSU MASTER MECHANIC SAYS WHOLE STEERING COLUMN MUST BE REPLACED AS BAD BEARING IN COLUMN CAN NOT BE. AS FOR BROKEN MANIFOLD BOLT ON LEFT SIDE OF ENGINE IT ALLOWS A HIGH PRESSURE EXHAUST LEAK ...
STEERING WHEEL DEVELOPED A 2 TO 3 INCH FRONT TO BACK MOTION. TRUCK WILL NOT PASS PA INSPECTION. A MITSU MASTER MECHANIC SAYS WHOLE STEERING COLUMN MUST BE REPLACED AS BAD BEARING IN COLUMN CAN NOT BE. AS FOR BROKEN MANIFOLD BOLT ON LEFT SIDE OF ENGINE IT ALLOWS A HIGH PRESSURE EXHAUST LEAK ...
THE CORROSION WERE RECENTLY DISCOVERED. JUST BELOW THE RIGHTSIDE OF THE MAIN FRAME BY THE FRONT RIGHT DOOR. THE PAINT BLOATED OUT BULGING, BUT INTACT. AS THE RESULT OF THE RUST CRIPPLING UNDERNEATH. WHEREIN THERE IS NO USUAL DINGS NOR SCRATCHES TO THE SURFACE. SUGGESTING A FAILURE OF THE MANUFACTURE...
ELECTRICAL SHORT, CAUISNG THE WIRING TO TO MELT CAUSING THE VEHICLE TO CUT OFF.*AK
ELECTRICAL SHORT, CAUISNG THE WIRING TO TO MELT CAUSING THE VEHICLE TO CUT OFF.*AK
WIRES SHORTED OUT MELTING POST DOWN IN GAS TANK. TT