1995 MITSUBISHI MONTERO Engine And Engine Cooling Problems
35 complaints about Engine And Engine Cooling
This Problem Across All Years
All Engine And Engine Cooling Complaints (35)
WHILE DRIVING ABOUT 20 MPH CRANKSHAFT PULLEY BOLT BROKE. *TR
Mileage: 219,000
TL*THE CONTACT OWNS A 1995 MITSUBISHI MONTERO. WHILE DRIVING LESS THAN 55 MPH, THE POWER STEERING FAILED AND THE CONTACT ALMOST STRUCK A PEDESTRIAN. UPON FURTHER INVESTIGATION, HE FOUND THAT A PULLEY FAILED IN THE CRANKSHAFT. THE MANUFACTURER STATED THAT HIS VIN WAS INCLUDED IN A RECALL. DUE TO THE AGE OF THE VEHICLE, THE CONTACT WAS INFORMED THAT HE WOULD HAVE HAD TO HAVE THE TIMING BELT REPLACED AT SOME POINT, WHICH WOULD HAVE ALSO TAKEN CARE OF THE RECALL. MITSUBISHI REFUSED TO PERFORM THE RECALL REPAIR. THE CONTACT WAS WELL WITHIN THE STATUTE OF LIMITATIONS TO HAVE HIS VEHICLE REPAIRED ACCORDING TO THE RECALL. NHTSA CAMPAIGN ID NUMBER 00V311001. THE CURRENT AND FAILURE MILEAGES WERE LESS THAN 215,000. UPDATED 7/9/09 *CN THE BOLT HOLDING THE HARMONIC BALANCER PULLEY ON, FELL OUT WHICH ALLOWED THE PULLEY TO ALSO FALL OFF. UPDATED 07/17/09.*JB
Mileage: 215,000
TL*THE CONTACT OWNS A 1995 MITSUBISHI MONTERO. WHILE AT A STOP SIGN, THE INSTRUMENT PANEL LIGHTS ILLUMINATED AND THE VEHICLE BECAME DIFFICULT TO STEER. THE MECHANIC STATED THAT THE PULLEY WAS NOT WORKING PROPERLY. THE VIN WAS NOT INCLUDED IN NHTSA CAMPAIGN ID NUMBER 00V311001 (ENGINE AND ENGINE COOLING:ENGINE). THE CURRENT AND FAILURE MILEAGES WERE 152,000. UPDATED 09/16/08. *LJ UPDATED 09/18/08. *JB
Mileage: 152,000
CRANKSHAFT PULLY FAILED AND IS NOW BEING REPAIRED FOR 3RD TIME IN ONE YEAR. *TR
THE CRANKSHAFT PULLEY BOLT BECAME LOOSE, CAUSING THE VEHICLE TO LOSE POWER STEERING,CHARGING SYSTEM, AND THE VEHICLE BECAME HOT. MY WIFE WAS PUT IN DANGER BECAUSE OF THE STEERING LOSS DURING HER COMMUTE FROM WORK IN RUSH HOUR TRAFFIC. THERE IS AN ACTIVE RECALL FOR THIS PROBLEM, NHTSA I.D. 00V311001 BUT THE BOLT WAS NEVER REPLACED JUST INSPECTED. I TALKED TO THE DEALER AND MANUFACTURER SERVICE REP'S AND WAS INFORMED BY BOTH THAT ,MY VEHICLE WAS OUT OF THE "RECALL WARRANTY" EVEN THOUGH THE ORIGINAL DEFECTIVE BOLT CAUSED THE PROBLEM. *JB
Mileage: 142,103
DT*: THE CONTACT STATED WHILE TRAVELING 40 MPH ON DRY ROAD CONDITIONS, A CLUNKING NOISE WAS HEARD FROM THE ENGINE BAY, AND POWER STEERING WAS LOST. ALSO, THE ACCELERATOR PEDAL WAS INOPERABLE. THE CONTACT MANAGED TO PULL THE VEHICLE OVER, AND WAS TOWED TO THE DEALERSHIP. UPON INSPECTION, THE DEALER DETERMINED THAT THE CRANKSHAFT PULLEY BOLT HAD FRACTURED, AND THE BOLT NEEDED TO BE REPLACED. THE BOLT WAS REPLACED. THE MANUFACTURER WAS CONTACTED, WHO DENIED RESPONSIBILITY FOR THE FRACTURED BOLT BECAUSE A SAFETY RECALL WAS PERFORMED 5 YEARS EARLIER FOR THE RETORQING OF THE BOLT. THE VEHICLE HAD AIR CONDITIONING WORK AND THE TIMING CHAIN REPLACEMENT PERFORMED ONE MONTH PRIOR TO THE INCIDENT, AND THE CONTACT WAS NOT SURE IF THAT WORK COULD HAVE AFFECTED THE CRANKSHAFT PULLEY BOLT.
Mileage: 110,000
THE MECHANIC THE OWNER OF AN INDEPENDENT SHOP, COMPLETED A TUNE UP OF THE 3.0 LITER ENGINE, THAT WAS RUNNING FINE WHEN BROUGHT TO HIM. THE ENGINE WAS RUNNING AND THEN THE ENGINE HAD A LOUD GRINDING AND SOUNDED LIKE IT WAS BLOWING UP. THE MECHANIC TOOK THE SPARK PLUGS OUT AND USED A LIGHT TO DETERMINE THE CYLINDER HEAD WAS CRACKED AND RUINED FROM A LOOSE PIECE OF METAL THE SIZE OF A MANS TOE NAIL. THE ENGINE IS COMPLETELY RUINED AND MUST BE REPLACED. THE MECHANIC DISPUTES THE FACT HE DID ANYTHING TO CAUSE THE DAMAGE BUT WAS WILLING TO INSTALL ANOTHER ENGINE IF I PURCHASED IT. THIS IS THE THIRD ENGINE THAT THIS HAS OCCURRED ON AND THE LAST TIME WAS WHILE I OWNED THE VEHICLE TOO. I HAD THE VEHICLE INTO A REPUTABLE MECHANIC FOR A TUNE UP. THEY DID A TUNE UP FOR $625, WHICH THEY FIRST CALLED AND QUOTED $350 THEN CALLED BACK AND CHANGED IT TO THE $625. THEY COMPLETED THE TUNE UP MOVED THE CAR OUT TO SEE HOW IT RAN. THE VEHICLE RAN FINE BUT ABOUT FIVE MINUTES AFTER IDLING THAT LENGTH OF TIME A PIECE OF METAL THE SIZE OF A SPARK PLUG ELECTRODE WAS LOOSE IN A CYLINDER AND RUINED THE ENGINE. THE SHOP DID NOT WANT TO REPLACE THE ENGINE BECAUSE THEY INSIST THE FAILURE IS NOT THEIR FAULT, BUT SINCE IT HAPPENED UNDER THEIR CARE THEY ACTUALLY FOUND A WRECKED MONTERO WITH A60,000 MILE ENGINE AND INSTALLED IT FOR THE PRICE OF THE TUNE UP. THE CAR WAS OUT OF COMMISSION FOR THREE WEEKS AND WE WERE NOT REIMBURSED FOR TIME AND EXPENSE BUT THE SHOP DID A PRETTY GOOD JOB OF REPLACING. THE ENGINE BLOCK OF THE OLD ENGINE WAS SITTING ON THE FLOOR OF THE SHOP WHEN I PICKED UP THE CAR. THE CYLINDER THAT WAS RUINED WAS SCRATCHED AND SCOURED COMPLETELY OVER THE WHOLE THING. SHOULD I FIND AND INSTALL AN ENGINE IT WILL BE NUMBER FOUR, THE ORIGINAL OWNER HAD TO REPLACE AN ENGINE WHEN HE OWNED IT. *JB
Mileage: 175,000
DT: THE CALLER SAID SMOKE CAME OUT OF TAIL PIPE WHEN VEHICLE FIRST ACCELERATED. HE HAD TO PUT OIL IN THE VEHICLE MORE OFTEN THAN NORMAL. DEALER TOLD HIM VEHICLE IDLED TOO SLOWLY, AND THAT OIL WAS GETTING ON THE VALVES, CAUSING THE SMOKE. HE WAS TOLD THE GUIDES WERE DROPPING TOO LOW, AND THAT WAS LETTING THE OIL LEAK ONTO THE VALVES. DEALER AND MANUFACTURER OFFERED NO HELP FOR FREE. *AK
Mileage: 88,000
DT: THE CALLER SAID SMOKE CAME OUT OF TAIL PIPE WHEN VEHICLE FIRST ACCELERATED. HE HAD TO PUT OIL IN THE VEHICLE MORE OFTEN THAN NORMAL. DEALER TOLD HIM VEHICLE IDLED TOO SLOWLY, AND THAT OIL WAS GETTING ON THE VALVES, CAUSING THE SMOKE. HE WAS TOLD THE GUIDES WERE DROPPING TOO LOW, AND THAT WAS LETTING THE OIL LEAK ONTO THE VALVES. DEALER AND MANUFACTURER OFFERED NO HELP FOR FREE. *AK
Mileage: 88,000
CRANKSHAFT PULLEY BOLT BROKE OFF INSIDE THE CRANK SHAFT. PULLEY BEGAN WOBBLING AND SHREDDING THE BELTS CAUSING LOSS OF POWER STEERING AT HIGHWAY SPEEDS. VEHICLE TOWED 130 MILES BACK TO DEALER LOCATION. TOLD BY DEALER THE DEFECTIVE BOLT WAS DUE TO RECENT HEAD GASKET WORK AND HAD NOTHING TO DO WITH THE MULTIPLE REPORTS OF THIS BOLT FAILING OR THE SAFETY RECALL THAT HAD BEEN ISSUED. *LA
Mileage: 199,367
WHILE DRIVING AT 40 MPH VEHICLE LOST POWER STEERING. VEHICLE VEERED OFF OF THE ROAD ONTO A GRASSY AREA. THE VEHICLE NEARLY COLLIDED WITH OTHER VEHICLES COMING TOWARDS IT. A MECHANIC EXAMINED THE VEHICLE, AND FOUND THAT THE CRANK SHAFT PULLEY WAS DEFECTIVE.*AK
WHILE DRIVING 50 MPH VEHICLE LOST POWER STEERING . CONSUMER HAD NO CONTROL OVER VEHICLE. AFTER COMING TO A STOP CONSUMER NOTICED THAT PULLEY FELL OFF. DEALER DETERMINED THAT CRANKSHAFT PULLEY BOLT DETACHED, CAUSING $900.00 DAMAGE TO VEHICLE. MANUFACTURER STATED THIS VEHICLE WAS NOT AFFECTED BY THE CRANK SHAFT PULLEY BOLT RECALL DUE TO VIN. *AK
VEHICLE EXPERIENCED A PROBLEM WITH THE CRANKSHAFT PULLEY. THIS PROBLEM IS THE SAME AS THE MONTERO SPORT WHICH IS UNDER RE-CALL. THIS VEHICLE DOES NOT APPLY UNDER THE RE-CALL BECAUSE OF THE VIN# AND VEHICLE IDENTIFICATION. PROVIDE FURTHER DETAILS. *JB
Mileage: 149,000
CRANKSHAFT PULLEY BOLT BROKE WHILE DRIVING AT 45 MPH. PULLEY CAME OFF, CAUSING THE VEHICLE TO SHUT DOWN, AND LOSE POWER. *AK
THE CRANKSHAFT PULLEY BOLT HAS BROKEN 3 TIMES IN 2003 WHILE DRIVING. POWERSTEERING IS LOST AND THE LAST TIME CAR DIED WHILE DRIVING.THE PREVIOS OWNER FIXED IT ON FEB.7, 2003. IT BROKE WHILE MY HUSBAND WAS ON THE FREEWAY MAY 15TH, 2003 AND THEN IT BROKE AGAIN SEPT.4,2003. THERE IS A RECALL ON THIS BOLT FOR THE MONTERO 3.0 L ENGINE AND THE GALANT SAME YEAR. WHY NO RECALL ON THE MONTERO 3.5 L? NO FATALITIES THIS TIME.
Mileage: 70,000
WHILE DRIVING ON THE HIGHWAY AND WITHOUT WARNING VEHICLE SHUT DOWN DUE TO THE CRANKSHAFT PULLEY BELT FALLING OFF. *AK
WHILE TRAVELING ABOUT 40MPH ON THE HIGHWAY AND WITHOUT PRIOR WARNING.THE PULLEY CAME OFF, CAUSING THE VEHICLE TO SHUT DOWN AND LOSE ALL POWER. *AK
THE VEHICLE EXPERIENCED THE SAME DEFECT WITH THE CRANKSHAFT PULLEY BOLT AS STATED IN RECALL 00 V 311 001, HOWEVER THE VEHICLE IDENTIFICATION NUMBER WAS NOT INCLUDED IN THE RECALL. *JB
Mileage: 120,000
CRANKSHAFT PULLEY BOLT AND COLLATERAL DAMAGES HAVE NEEDED TO BE REPAIRED 3 TIMES WITHIN EIGHTEEN MONTHS, LOSS OF POWER STEERING WHILE DRIVING AND NO NOTIFICATION OF RECALL 00V311001.*JB
Mileage: 143,000
VEHICLE WAS AT A COMPLETE STOP, CONSUMER NOTICED SMOKE COMING FROM THE ENGINE. CONSUMER CHECKED UNDER THE HOOD AND NOTICE A OIL LEAK. CONSUMER HAD VEHICLE SERVICED BY THE DEALERSHIP, WHO INDICATED THAT THE POROUS HEAD CAUSED THE ENGINE LEAK. PLEASE PROVIDE MORE DETAILS. TS
Mileage: 100,000
CRANKSHAFT AND SPROCKET HAD TO BE CHANGED BECAUSE THEY FAILED. MR
WHILE DRIVING ALL LIGHST ON DASHBOARD CAME ON, AND POWER STEERING STOPPED WORKING. THIS WAS AS A RESULT OF CRANKSHAFT PULLEY DISCONNECTING FROM MOTOR. THIS HAPPENED 3 TIMES. DEALERSHIP COULD NOT FIX PROBLEM.*AK
CRANKSHAFT/ PULLEY BOLT SEPARATED, CAUSING DAMAGE TO VEHICLE. RECALL 00V311001 HAS BEEN ISSUED ON SIMILAR MAKES AND MODELS; HOWEVER, THIS VEHICLE WAS NOT INCLUDED DUE TO VIN. 3.5 LITER ENGINE. PLEASE PROVIDE FURTHER INFORMATION.*AK
BOLT THAT HOLDS PULLEY INTO THE CRANKSHAFT BROKE WHILE CONSUMER WAS DRIVING AT 30 MPH. CONTACTED DEALER, AND THE DEALER WAS NOT WILLING TO DO ANYTHING.*AK
VEHICLE WAS RUNNING ROUGH AT 50-60 MPH, THEN LOST ALL POWER. ALL LIGHTS ON DASH CAME ON, VEHICLE TOWED TO REPAIRSHOP. MECHANIC DETERMINED CRANKSHAFT PULLEY BOLT HAD BROKEN. *AK
ENGINE PULLEY CAME APART, DAMAGING ENGINE. PLEASE PROVIDE ADDITIONAL INFORMATION. *AK
THE BOLT SECURING THE CRANKSHAFT BROKE PRIOR TO RECALL 00V-311 WHILE DRIVING UP INTO THE MOUNTAINS AND ROUNDING A CORNER THE DRIVER LOST CONTROL OF THE VEHICLE BUT WAS ABLE TO MANEUVER IT TO THE SIDE OF THE ROAD. NLM
WHILE DRIVING, CONSUMER HEARD A STRANGE KNOCKING NOISE FROM ENGINE, THE NOISE CONTINUED FOR A FEW MORE MINUTES AND THEN ALL OF A SUDDEN A VERY LOUD EXPLOSIVE NOISE ERUPTED FROM THE ENGINE AND A SUDDEN LOSS OF POWER ENSUED, THIS WAS THEN FOLLOWED BY A VIOLENT SHAKING AND STEAM COMING FROM THE VEHICLE, CONSUMER WAS ABLE TO PULL OVER ON THE FREEWAY, VEHICLE WAS TOWED IN TO BE INSPECTED AND IT WAS DETERMINED THAT THE ENTIRE ENGINE NEEDED TO BE REPLACED BECAUSE THE CONNECTING ROD BROKE AND IT PUNCTURED A HOLE THROUGH THE BLOCK, NO ONE COULD REALLY EXPLAIN TO THE CONSUMER WHAT CAUSED THIS BUT WAS TOLD MAYBE IT WAS DUE TO LACK OF OIL IN WHICH CONSUMER TOTALLY DISAGREED, CONSUMER STATES NONE OF THE PANELS LIGHTS CAME ON TO ALERT HER OF ANY POSSIBILE PROBLEMS, HOWEVER CONSUMER DID PAY FOR THE NECESSARY REPAIRS BUT WONDERS IF THIS IS A DESIGN FLAW IN A VEHICLE THAT IS BARELY FIVE YEARS OLD. *JB
PULLEY FELL OFF CRANKSHAFT AND VEHICLE LOST POWER STEERING AND ALMOST HAD AN ACCIDENT. DEALERSHIP IS AWARE OF PROBLEM.*AK
WHILE DRIVING ABOUT 20 MPH CRANKSHAFT PULLEY BOLT BROKE, THERE IS A RECALL FOR THIS COMPONENT, BUT THIS VEHICLE WAS NOT AFFECTED DUE TO VIN. *AK THE CONSUMER POINTS OUT THAT THE RECALL SHOULD HAVE INCLUDED THIS VEHICLCE BECAUSE BOTH 3.0 AND 3.5 ENGINE BLOCK WERE THE SAME. THE CONSUMER WANTS THE SITUATION TO BE INVESTIGATED. *YH
RECALL 00V311001 NOTICE RECEIVED. IT WAS A FOREIGN PURCHASED VEHICLE, AND DEALERSHIP WAS INFORMING HIM THEY HAD NO WAY TO BILL CARRBEAN MITSUBISHI. PLEASE PROVIDE ANY ADDITIONAL INFORMATIONL.*AK
BOLT OF CRANKSHAFT HAS FALLEN OUT, CAUSING DAMAGE TO CRANKSHAFT A TOTAL OF 3 TIMES. CONSUMER CONTACTED MANUFACTURER, AND WAS TOLD VEHICLE NOT INCLUDED IN RECALL 00V311001 DUE TO VIN ALTHOUGH IT HAD SAME EXACT DEFECT.*AK
PUT IN 4.5 QUARTS OF OIL INTO TANK THAT SHOULD LAST 3000 MILES. BUT WHEN CHECKING DIP STICK AT 3000, THERE WAS NO OIL LEFT. DEALER SAID OIL MIGHT BE LEAKING IN ENGINE VALVES, AND IT WAS NORMAL FOR AT LEAST A QUART OF OIL TO BE BURNED UP. *AK
THE VEHICLE CONSUMES EXCESSIVE AMOUNTS OF OIL AND THE CONSUMER HAS TO KEEP PUTTING A QUART OF ENGINE OIL EVERY MONTH. DEALERSHIP IS NOT ABLE TO DETERMINE CAUSE, WHICH IS HOW THE ENGINE WAS MAUNFACTURED. *ET
WHEN THE WINDOWS DOWN AND STOP AT A LIGHT THERE IS A BAD SMELL IN THE CAR CHILD GOT SICK FROM THE FUMES . TT