18
Complaints
0
Crashes
0
Fires
0
Deaths

This Problem Across All Years

All Engine And Engine Cooling Complaints

Showing 18 of 18
May 17, 2004 97,451 mi

CONSUMER TOOK VEHICLE FOR A REGULAR MAINTENANCE TO INDEPENDENT SHOP, AND MECHANIC DETERMINED THAT HEAD GASKET WAS LEAKING COOLANT, INTAKE MANIFOLD WAS REPLACED AT CONSUMER'S EXPENSE OF $410.00. *AK *NM

May 17, 2004 97,451 mi

CONSUMER TOOK VEHICLE FOR A REGULAR MAINTENANCE TO INDEPENDENT SHOP, AND MECHANIC DETERMINED THAT HEAD GASKET WAS LEAKING COOLANT, INTAKE MANIFOLD WAS REPLACED AT CONSUMER'S EXPENSE OF $410.00. *AK *NM

Apr 5, 2004 60,000 mi

THE CONSUMER HEARD A TICKING NOISE FROM THE ENGINE. UPON INSPECTION OF THE NOISE BY THE DEALERSHIP THEY NOTICED THAT THE INTAKE MANIFOLD GASKET WAS LEAKING COOLANT INTO THE OIL. THIS OCCURS BECAUSE THE MANIFOLD IS MAKE OF PLASTIC. *NM

Apr 5, 2004 60,000 mi

THE CONSUMER HEARD A TICKING NOISE FROM THE ENGINE. UPON INSPECTION OF THE NOISE BY THE DEALERSHIP THEY NOTICED THAT THE INTAKE MANIFOLD GASKET WAS LEAKING COOLANT INTO THE OIL. THIS OCCURS BECAUSE THE MANIFOLD IS MAKE OF PLASTIC. *NM

Mar 29, 2004

CAR PROBLEMS WITH 1996 CUTLASS KEEPS STALLING I HAVE ALREADY REPLACED INTAKE GASKET PUT NEW BATTERY IN AN HAD OTHER REPAIRS THIS CAR ONLY HAS 96000 MILES. *AK

Mar 29, 2004

CAR PROBLEMS WITH 1996 CUTLASS KEEPS STALLING I HAVE ALREADY REPLACED INTAKE GASKET PUT NEW BATTERY IN AN HAD OTHER REPAIRS THIS CAR ONLY HAS 96000 MILES. *AK

Mar 5, 2003 77,950 mi

WE GOT A LOW COOLANT LIGHT ON OUR DASHBOARD, AND FOUND THE COOLANT RESEVOIR TO BE COMPLETELY EMPTY. THIS WAS LESS THAN 3K MILES SINCE THE COOLANT SYSTEM WAS SERVICED - DRAINED, REFILLED, AND NEW RADIATOR HOSES INSTALLED. AFTER REFILLING, WE FOUND A SMALL COOLANT LEAK ON THE GROUND UNDER THE ENGINE (WHEN PARKED ON A DRY SURFACE INDOORS - NORMALLY THE CAR IS IN THE DRIVEWAY, WHERE SNOW, ICE, AND RAIN MAY HAVE MASKED A LONG-TIME SMALL LEAK). ON 3/3/03, OUR LOCAL MIDAS REPAIR SHOP FOUND THAT THE INTAKE MANIFOLD GASKET WAS FAILING, CAUSING THE LEAK. IT WAS REPLACED (ALONG WITH THERMOSTAT AND SOME OTHER GASKETS, WHICH WERE LITTLE ADDITIONAL EXPENSE), AT A COST OF OVER $900. NOTE THAT THIS IS THE VEHICLE PRIMARILY USED BY MY (PREGNANT) WIFE AND OUR 2 YEAR OLD SON, AND THAT I MYSELF WORK ABOUT 30 MILES FROM HOME, SO WE WERE HEADED FOR INCOVENIENCE AT BEST, DISASTER AT WORST. NOTE THAT THE VEHICLE USES DEXCOOL COOLANT, AS REQUIRED BY THE MANUFACTURER FOR PROPER TREATMENT OF ITS ALUMINUM RADIATOR.*JB

Mar 5, 2003 77,950 mi

WE GOT A LOW COOLANT LIGHT ON OUR DASHBOARD, AND FOUND THE COOLANT RESEVOIR TO BE COMPLETELY EMPTY. THIS WAS LESS THAN 3K MILES SINCE THE COOLANT SYSTEM WAS SERVICED - DRAINED, REFILLED, AND NEW RADIATOR HOSES INSTALLED. AFTER REFILLING, WE FOUND A SMALL COOLANT LEAK ON THE GROUND UNDER THE ENGINE (WHEN PARKED ON A DRY SURFACE INDOORS - NORMALLY THE CAR IS IN THE DRIVEWAY, WHERE SNOW, ICE, AND RAIN MAY HAVE MASKED A LONG-TIME SMALL LEAK). ON 3/3/03, OUR LOCAL MIDAS REPAIR SHOP FOUND THAT THE INTAKE MANIFOLD GASKET WAS FAILING, CAUSING THE LEAK. IT WAS REPLACED (ALONG WITH THERMOSTAT AND SOME OTHER GASKETS, WHICH WERE LITTLE ADDITIONAL EXPENSE), AT A COST OF OVER $900. NOTE THAT THIS IS THE VEHICLE PRIMARILY USED BY MY (PREGNANT) WIFE AND OUR 2 YEAR OLD SON, AND THAT I MYSELF WORK ABOUT 30 MILES FROM HOME, SO WE WERE HEADED FOR INCOVENIENCE AT BEST, DISASTER AT WORST. NOTE THAT THE VEHICLE USES DEXCOOL COOLANT, AS REQUIRED BY THE MANUFACTURER FOR PROPER TREATMENT OF ITS ALUMINUM RADIATOR.*JB

Aug 9, 2002

CONSUMER TOOK VEHICLE TO LOCAL DEALER WHERE A FAULTY MODULE WAS REPLACED POSSIBLY RELATING TO THE RADIATOR HOUSING. CONSUMER CONTINUES TO RECEIVE RECALL O-00058S NOTICES AFTER THE DEALER SAID THEY DID THE RECALL WORK. MANUFACTURER SAID THAT THERE IS NO RECORD OF THE WORK BEING DONE. MANUFACTURER TOLD CONSUMER THAT THEY NOW SHOW THAT RECALL WORK HAS BEEN DONE AND THE MATTER IS CLOSED, HOWEVER, WHEN CONSUMER ASKED FOR A WRITTEN STATEMENT OF THE RECALL WORK PERFORMED, THEY REFUSED TO SEND A LETTER AND REFERRED CONSUMER BACK TO THE DEALER WHO RECENTLY STILL SENT REMINDER CARDS TO BRING THE VEHICLE IN FOR THE RECALL WORK TO BE DONE. *TT

Aug 9, 2002

CONSUMER TOOK VEHICLE TO LOCAL DEALER WHERE A FAULTY MODULE WAS REPLACED POSSIBLY RELATING TO THE RADIATOR HOUSING. CONSUMER CONTINUES TO RECEIVE RECALL O-00058S NOTICES AFTER THE DEALER SAID THEY DID THE RECALL WORK. MANUFACTURER SAID THAT THERE IS NO RECORD OF THE WORK BEING DONE. MANUFACTURER TOLD CONSUMER THAT THEY NOW SHOW THAT RECALL WORK HAS BEEN DONE AND THE MATTER IS CLOSED, HOWEVER, WHEN CONSUMER ASKED FOR A WRITTEN STATEMENT OF THE RECALL WORK PERFORMED, THEY REFUSED TO SEND A LETTER AND REFERRED CONSUMER BACK TO THE DEALER WHO RECENTLY STILL SENT REMINDER CARDS TO BRING THE VEHICLE IN FOR THE RECALL WORK TO BE DONE. *TT

Mar 9, 2000

I PURCHASED THE VEHICLE AND ONE WEEK LATER THE TRANSMISSION HAD TO BE FIXED, DOOR MECHANISM HAD TO BE REPLACED, WINDSHIELD REPLACED 2 TIMES AND NOW THE COOLANT IS LEAKING ALONG WITH AN OIL VALVE AND THE CAR DOES NOT ACCELERATE. COST TO REPAIR THIS TIME IS ESTIMATED AT $1200

Mar 9, 2000

I PURCHASED THE VEHICLE AND ONE WEEK LATER THE TRANSMISSION HAD TO BE FIXED, DOOR MECHANISM HAD TO BE REPLACED, WINDSHIELD REPLACED 2 TIMES AND NOW THE COOLANT IS LEAKING ALONG WITH AN OIL VALVE AND THE CAR DOES NOT ACCELERATE. COST TO REPAIR THIS TIME IS ESTIMATED AT $1200

Mar 9, 2000

I PURCHASED THE VEHICLE AND ONE WEEK LATER THE TRANSMISSION HAD TO BE FIXED, DOOR MECHANISM HAD TO BE REPLACED, WINDSHIELD REPLACED 2 TIMES AND NOW THE COOLANT IS LEAKING ALONG WITH AN OIL VALVE AND THE CAR DOES NOT ACCELERATE. COST TO REPAIR THIS TIME IS ESTIMATED AT $1200

Mar 9, 2000

I PURCHASED THE VEHICLE AND ONE WEEK LATER THE TRANSMISSION HAD TO BE FIXED, DOOR MECHANISM HAD TO BE REPLACED, WINDSHIELD REPLACED 2 TIMES AND NOW THE COOLANT IS LEAKING ALONG WITH AN OIL VALVE AND THE CAR DOES NOT ACCELERATE. COST TO REPAIR THIS TIME IS ESTIMATED AT $1200

Mar 4, 1999

COOLANT LEAKING FROM INTAKE MANIFOLD. SERVICE TECH. REPLACED GASKET.

Mar 4, 1999

COOLANT LEAKING FROM INTAKE MANIFOLD. SERVICE TECH. REPLACED GASKET.

Jan 14, 1999

WE REPLACED THE FUEL FILTER BECAUSE IT WAS CLOGGED, HOWEVER, WE THEN HAD TO HAVE THE ENGINE CONTROL MODULE REPLACED AS WELL AS THE CATALITIC CONVERTER.

Jan 14, 1999

WE REPLACED THE FUEL FILTER BECAUSE IT WAS CLOGGED, HOWEVER, WE THEN HAD TO HAVE THE ENGINE CONTROL MODULE REPLACED AS WELL AS THE CATALITIC CONVERTER.