1995 PLYMOUTH ACCLAIM Problems & Recalls
Detailed safety information and owner complaints
Problem Breakdown
Compare to Other Years
Common Problems
TL* THE CONTACT OWNS A 1995 PLYMOUTH ACCLAIM. WHILE DRIVING 50 MPH, THE CONTACT STATED THAT THE RUBBER TIMING BELT SNAPPED. THE VEHICLE DECELERATED, COASTED, AND STOPPED IN TRAFFIC. THE VEHICLE WAS TOWED TO THE CONTACT'S HOME AND THEN TOWED TO APPLE DODGE HANOVER (200 EISENHOWER DR, HANOVER, PA 1733...
Mileage: 60,000
WHEN EXITING THE INTERSTATE DURING A HEAVY RAIN STORM I HIT A LARGE PUDDLE OF WATER AND THE SERPENTINE BELT CAME OFF MAKING IT DIFFICULT TO STEER THE CAR. THIS CAR WAS PURCHASED BRAND NEW AND SOLD TO ME 3 YEARS AGO. THIS HAD HAPPENED TO MY MOTHER NUMEROUS TIMES AND TWICE SINCE I'VE OWNED IT. IT ONLY...
Mileage: 88,000
DRIVER AND PASSENGER SEATS COLLAPSED INTO RECLINING POSITION WHEN HIT IN REAR AND THEN WHEN WE HIT THE CAR IN FRONT WE WERE THROWN FROM A LAYING POSITION UP TO THE DASH. *NLM
VEHICLE WAS IN MOTION WHEN SMOKE SUDDENLY STARTED COMING FROM STEERING COLUMN. CONSUMER QUICKLY PULLED OVER, AND GOT OUT WHEN IT BURSTED INTO FLAMES, TOTALLING VEHICLE. DEALER AND MANUFACTURER WERE NOT NOTIFIED. PLEASE PROVIDE MORE INFORMATION.*AK
TRANSMISSION HAD FAILURE IN LOW GEAR REQUIRING REPLACEMENT. NLM
TIRES CAME APART AT AREA OF BEAD. INFLATION WAS PROPER. *AK (DOT NUMBER: M6RV 27430 TIRESIZE: P185/70R14)
PREMATURE HEAD GASKET FAILURE CAUSING ENGINE OIL CONTAMINATION, NO HEAT AND EXCESSIVE COOLANT USAGE. *AK
WHILE DRIVING AT 55 MPH ENGINE CHECK LIGHT CAME ON. CONSUMER PULLED OVER TO THE SERVICE LANE. TEMPERATURE GAUGE WENT STRAIGHT UP. THEN, CONSUMER HEARD NOISE COMING FROM ENGINE, 4 MINUTES LATER, CONSUMER NOTICED SMOKE COMING FROM BACK OF CAR AND PULLED OVER. CONSUMER STATED CAR WAS T0TALED BECAUS...
WHILE DRIVING AT 55 MPH ENGINE CHECK LIGHT CAME ON. CONSUMER PULLED OVER TO THE SERVICE LANE. TEMPERATURE GAUGE WENT STRAIGHT UP. THEN, CONSUMER HEARD NOISE COMING FROM ENGINE, 4 MINUTES LATER, CONSUMER NOTICED SMOKE COMING FROM BACK OF CAR AND PULLED OVER. CONSUMER STATED CAR WAS T0TALED BECAUS...
WHILE DRIVING AT 55 MPH ENGINE CHECK LIGHT CAME ON. CONSUMER PULLED OVER TO THE SERVICE LANE. TEMPERATURE GAUGE WENT STRAIGHT UP. THEN, CONSUMER HEARD NOISE COMING FROM ENGINE, 4 MINUTES LATER, CONSUMER NOTICED SMOKE COMING FROM BACK OF CAR AND PULLED OVER. CONSUMER STATED CAR WAS T0TALED BECAUS...
WINDSHIELD WIPERS QUIT WORKING IN THE MIDDLE OF OPERATION. DRIVER HAS TO TIGHTEN THE PIVOT ARM NUTS BEFORE OPERATION CONTINUED. THE PROBLEM HAS NOT BEEN REPORTED TO THE DEALERSHIP. *AK *ML
WHEN MAKING A RIGHT OR LEFT TURN OR BACKING UP, DRIVER WOULD HEAR A STRANGE POPPING SOUND COMING FROM THE REAR. WHEN OWNER BROUGHT THE VEHICLE IN FOR AN OIL CHANGE, MECHANIC NOTICED THAT THE SWAY BAR WAS BROKEN ON THE RIGHT REAR AXLE. THE SWAY BAR HAS BEEN WELDED BACK TOGETHER. *AK
TIE ROD END WORN BADLY.
NOTHING
CRACKED REAR TRAILING ARM.
STABILIZER BAR FAILED, CAUSING THE REAR AXLE TO FALL OUT FROM UNDER CAR, RESULTING IN LOSS OF CONTROL.
BRAKE ROTORS PITTED.
WHILE DRIVING PASSENGER'S AUTOMATIC SHOULDER HARNESS MALFUNCTIONED. UPON TURNING OFF IGNITION, BELT TIGHTENED EXTREMELY THEN WON'T RELEASE, ALSO WHEN DOOR IS OPENED BELT WON'T RELEASE, MUST BE DONE MANUALLY, UNLATCH OR RESTART VEHICLE. *AK
THE REAR CROSSMEMBER BAR THAT CONNECTS THE TWO REAR TIRES TOGETHER BROKE. IT WAS REPLACED; HOWEVER, MANUFACTURER ONLY PAID HALF OF THE REPAIR COST INSTEAD OF THE TOTAL COST. CONSUME RFELT THA TIT WAS A MANUFACTURER'S DEFECT AND THAT THE MANUFACTURER SHOULD HAVE PICKED UP ALL THE REPAIR COSTS. *AK
AFTER PUTTING THE VEHICLE INTO DRIVE, THE VEHICLE WENT INTO REVERSE WHILE STILL IN THE DRIVE POSITION. *AK
PASSENGER'S SIDE SEAT BELT VERY LOOSE WILL NOT RETRACT. IF IN AN ACCIDENT THE SEAT BELT WOULD SERVE NO PURPOSE BECAUSE IT IS NOT SECURE. HAS NOT HAD VEHICLE REPAIRED BECAUSE OF WARRANTY. *AK
WITHOUT WARNING CIGARETTE LIGHTER EJECTED VIOLENTLY FROM ITS DASHBOARD LOCATION AND BOUNCED AND LANDED IN DRIVERS LAP BETWEEN HIS LEGS, ALMOST RESULTING IN CONTROL LOST.
AT 18,000 MILES ALL FOUR MICHELIN TIRES ARE LEAKING (SLOW LEAK MICHELIN P19570R14 XW4 ), TOOK TO TIRES MANUFACTURER, SAID THE TIRES HAVE A SLOW LEAK, CAR MANUFACTURER WANTS TO PUT A TUBE TO CORRECT THE PROBLEM. *AK DOT NUMBER IS HNHDP, MICHELIN STATED THAT THE ALUMINUM RIMS ARE WHAT IS CAUSING ...
FAILURE OF THE REAR SUPENSION, THE REAR SUSPENSION IS CAUSING THE VEHICLE TIRES TO WEAR OFTEN.*AK CRUISE WORKING IMPROPERLY, DEALER REPAIRED VACUUM LINE. REAR TRAILIN GARM FAILED, CAUSING NOISE IN FRONT END. *SLC
FAILURE OF THE REAR SUPENSION, THE REAR SUSPENSION IS CAUSING THE VEHICLE TIRES TO WEAR OFTEN.*AK CRUISE WORKING IMPROPERLY, DEALER REPAIRED VACUUM LINE. REAR TRAILIN GARM FAILED, CAUSING NOISE IN FRONT END. *SLC
WHEN TRUNK WAS FILLED WITH LUGGAGE AND UPON CLOSING THE GARMENT BAG JAMMED IN THE TRUNK LATCH, HOWEVER THE TRUNK APPEARED TO BE CLOSED, AFTER ABOUT 100 MILES OF TRAVEL THE LID VIBRATED UP ENOUGH TO ACTIVATE THE LIGHT, THE TRUNK WAS NOT NOTICEABLY OPEN. THE DESIGN FLAW LIES IN THE FACT THAT THE TRUN...
WHEN TRUNK WAS FILLED WITH LUGGAGE AND UPON CLOSING THE GARMENT BAG JAMMED IN THE TRUNK LATCH, HOWEVER THE TRUNK APPEARED TO BE CLOSED, AFTER ABOUT 100 MILES OF TRAVEL THE LID VIBRATED UP ENOUGH TO ACTIVATE THE LIGHT, THE TRUNK WAS NOT NOTICEABLY OPEN. THE DESIGN FLAW LIES IN THE FACT THAT THE TRUN...
ACCELERATOR PEDAL MUST BE DEPRESSED TO THE FLOOR FOR GAS TO GO TO CARBURETOR.
ODOR ENTERING VEHICLE, CAUSING ILLNESS.
VEHICLE JERKS WHILE DRIVING, DEALER CANNOT LOCATE PROBLEM. TT
THE SEAT BELT RETRACTOR ON THE PASSENGER SIDE TOOK OFF THE VEHICLE OWNERS FINGER TIP. TT
AUTOMATIC RESTRAINT TOOK OFF END OF WIFE'S FINGER ON RIGHT HAND WHILE TURNING TO REAR PASSENGER WHEN IGNITION TURNED ON AND SEAT BELT WENT TO END OF TRACK.*AK
SPEED SENSOR/OUTPUT SHAFT FAILED, CAUSING ENGINE HESITATION AND MIL ILLUMINATION. *SKD
WINDSHIELD WIPER FLUID FREEZES, DURING COLD CONDITIONS AND COMES OUT CLUMPY AND SMEARS THE WINDSHEILD. TT
EMERGENCY BRAKING SYSTEM IS COMPLETELY INOPERATIVE. TT