18
Complaints
0
Crashes
4
Fires
0
Deaths
!

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Electrical System Complaints

Showing 18 of 18
Jul 2, 2016 94,000 mi

FUEL GAUGE SUDDENLY DROPS TO EMPTY. EVEN AFTER A COMPLETE TANK REFILL. IT WOULD SEEM TO BE AN ELECTRICAL MALFUNCTION IN EITHER THE SENSOR OR DASH GAUGE ITSELF. IT CAN BE "CLEARED" FROM BEING STUCK ON EMPTY BY SHUTTING OFF THE ENGINE AND THEN RESTARTING IT.

Jul 2, 2016 94,000 mi

FUEL GAUGE SUDDENLY DROPS TO EMPTY. EVEN AFTER A COMPLETE TANK REFILL. IT WOULD SEEM TO BE AN ELECTRICAL MALFUNCTION IN EITHER THE SENSOR OR DASH GAUGE ITSELF. IT CAN BE "CLEARED" FROM BEING STUCK ON EMPTY BY SHUTTING OFF THE ENGINE AND THEN RESTARTING IT.

Jan 19, 2016 173,000 mi

TL* THE CONTACT OWNS A 1999 PLYMOUTH NEON, WHILE DRIVING APPROXIMATELY 35 MPH, THE VEHICLE OVERHEATED AND THE TEMPERATURE GAUGE INDICATED HOT. THE CONTACT ATTEMPTED TO SHUT OFF THE VEHICLE, BUT THE IGNITION KEY WAS TOO HOT AND FAILED TO REMOVE FROM THE VEHICLE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC, BUT THE REPAIRS WERE UNKNOWN. THE FAILURE RECURRED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 173,000. THE VIN WAS UNAVAILABLE.

Jan 19, 2016 173,000 mi

TL* THE CONTACT OWNS A 1999 PLYMOUTH NEON, WHILE DRIVING APPROXIMATELY 35 MPH, THE VEHICLE OVERHEATED AND THE TEMPERATURE GAUGE INDICATED HOT. THE CONTACT ATTEMPTED TO SHUT OFF THE VEHICLE, BUT THE IGNITION KEY WAS TOO HOT AND FAILED TO REMOVE FROM THE VEHICLE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC, BUT THE REPAIRS WERE UNKNOWN. THE FAILURE RECURRED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 173,000. THE VIN WAS UNAVAILABLE.

Jun 22, 2005 100,400 mi

DT: THE VEHICLE WOULD NOT START,.OPENED THE HOOD, LOOKED LIKE AN ELECTRICAL SHORT, THE WIRING ON THE END GLOWED RED RIGHT ABOVE THE BATTERY. PREVIOUSLY, THERE WAS AN AIR CONDITIONING PROBLEM, AND THE CHECK ENGINE LIGHT CAME ON. THEY SAID IT WAS A SENSOR. ALSO A TRUNK LATCH.*AK

Jun 22, 2005 100,400 mi

DT: THE VEHICLE WOULD NOT START,.OPENED THE HOOD, LOOKED LIKE AN ELECTRICAL SHORT, THE WIRING ON THE END GLOWED RED RIGHT ABOVE THE BATTERY. PREVIOUSLY, THERE WAS AN AIR CONDITIONING PROBLEM, AND THE CHECK ENGINE LIGHT CAME ON. THEY SAID IT WAS A SENSOR. ALSO A TRUNK LATCH.*AK

Jun 6, 2002

TUMBLE OR TUMBLER IN IGNITION FELL APART. UNABLE TO START VEHICLE. DEALER REPLACED PART, PROBLEM REOCCURRED. *AKI

Jun 6, 2002

TUMBLE OR TUMBLER IN IGNITION FELL APART. UNABLE TO START VEHICLE. DEALER REPLACED PART, PROBLEM REOCCURRED. *AKI

Apr 10, 2002

HEAD GASKET REPLACED, THEN IT LOST ALL POWER, AND ENGINE SERVICE LIGHT CAME ON. I TOOK IT BACK, THEY SAID IT NEEDED SPARK PLUGS. I HAVE IT BACK, BUT IT IS STILL MISSING AND I AM NOT CONVINCED THAT MY PROBLEMS ARE OVER. *AK

Apr 10, 2002

HEAD GASKET REPLACED, THEN IT LOST ALL POWER, AND ENGINE SERVICE LIGHT CAME ON. I TOOK IT BACK, THEY SAID IT NEEDED SPARK PLUGS. I HAVE IT BACK, BUT IT IS STILL MISSING AND I AM NOT CONVINCED THAT MY PROBLEMS ARE OVER. *AK

Mar 14, 2002

DRIVER TOOK VEHICLE TO DEALER FOR A ROUTINE MAINTENANCE CHECK, AND SPARK PLUGS WERE REPLACED. MECHANIC TOLD CONSUMER THAT OIL WAS GETTING INTO ENGINE. DEALER STATED THIS COULD CAUSE ENGINE TO LOCK UP AND RESULT IN A FIRE. PLEASE PROVIDE ANY FURTHER INFORMATION.*AK

Mar 14, 2002

DRIVER TOOK VEHICLE TO DEALER FOR A ROUTINE MAINTENANCE CHECK, AND SPARK PLUGS WERE REPLACED. MECHANIC TOLD CONSUMER THAT OIL WAS GETTING INTO ENGINE. DEALER STATED THIS COULD CAUSE ENGINE TO LOCK UP AND RESULT IN A FIRE. PLEASE PROVIDE ANY FURTHER INFORMATION.*AK

Aug 20, 2001 Fire

NO SUMMARY LISTED FOR ABOVE VEHICLE. *AK

Aug 20, 2001 Fire

NO SUMMARY LISTED FOR ABOVE VEHICLE. *AK

Aug 20, 2001 Fire

NO SUMMARY LISTED FOR ABOVE VEHICLE. *AK

Aug 20, 2001 Fire

NO SUMMARY LISTED FOR ABOVE VEHICLE. *AK

Mar 5, 2001

OIL WAS LEAKING FROM UNDERNEATH VEHICLE. ENGINE CHECK LIGHT CAME ON DASHBOARD. DEALERSHIP REPLACED WIRE HARNESSS. LEAKING INSIDE OF BACK TRUCK AND A MOLD LIKE SUBSTANCE WAS INSIDE OF TRUCK. PASSENGER'S SIDE DOOR WAS LEAKING WHEN THERE WAS RAINY WEATHER. ALS, DEALERSHIP REPLACED A WEATHER STRIP ON SIDE OF PANEL.*AK

Mar 5, 2001

OIL WAS LEAKING FROM UNDERNEATH VEHICLE. ENGINE CHECK LIGHT CAME ON DASHBOARD. DEALERSHIP REPLACED WIRE HARNESSS. LEAKING INSIDE OF BACK TRUCK AND A MOLD LIKE SUBSTANCE WAS INSIDE OF TRUCK. PASSENGER'S SIDE DOOR WAS LEAKING WHEN THERE WAS RAINY WEATHER. ALS, DEALERSHIP REPLACED A WEATHER STRIP ON SIDE OF PANEL.*AK