High Severity Issue
This component has been associated with crashes, fires, or deaths.
This Problem Across All Years
MY STEERING WHEEL LOCKED UP IN MY YARD, HAVING TO GET IT TOWED TO THE PONTIAC SERVICE DEPARTMENT PAYING OVER $2,000 TO GET IT FIX. THEN AFTER A YEAR IT LOCKED UP AGAIN. BEEN SITTING IN MY GARAGE EVERY SINCE. I DON'T HAVE THAT TYPE OF MONEY TO CONTINUE TO GET THE PROBLEM FIX IF IT'S GONNA KEEP OCCURRING.
MY STEERING WHEEL LOCKED UP IN MY YARD, HAVING TO GET IT TOWED TO THE PONTIAC SERVICE DEPARTMENT PAYING OVER $2,000 TO GET IT FIX. THEN AFTER A YEAR IT LOCKED UP AGAIN. BEEN SITTING IN MY GARAGE EVERY SINCE. I DON'T HAVE THAT TYPE OF MONEY TO CONTINUE TO GET THE PROBLEM FIX IF IT'S GONNA KEEP OCCURRING.
TL* THE CONTACT OWNS A 2005 PONTIAC GTO. WHILE DRIVING 35 MPH, THE STEERING WHEEL SEIZED AND WAS VERY DIFFICULT TO MANEUVER. THE VEHICLE BEGAN TO LEAK OIL AND WAS TOWED TO A DEALER WHERE IT WAS DIAGNOSED THAT THE POWER FLUID LINE FRACTURED AND THE ROCKING PINION NUT NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 105,000.
TL* THE CONTACT OWNS A 2005 PONTIAC GTO. WHILE DRIVING 35 MPH, THE STEERING WHEEL SEIZED AND WAS VERY DIFFICULT TO MANEUVER. THE VEHICLE BEGAN TO LEAK OIL AND WAS TOWED TO A DEALER WHERE IT WAS DIAGNOSED THAT THE POWER FLUID LINE FRACTURED AND THE ROCKING PINION NUT NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 105,000.
WHEN I PUT MY KEY INTO THE IGNITION, IT FROZE. I COULDN'T TURN THE KEY. I COULDN'T MOVE THE CAR. THE IGNITION WAS LOCKED UP. I TRIED JUST REPLACING THE IGNITION CYLINDER, BUT THAT DID NOT WORK. I HAD TO HAVE THE ENTIRE STEERING COLUMN REPLACED. IT COST $1371.67 TO GET THIS CAR FIXED DUE TO NO FAULT OF MY OWN. I HAVE RESEARCHED THIS ISSUE AND IT SEEMS THAT ON THE WEEK MY VEHICLE WAS IN THE SHOP, 3 OTHER PONTIACS WERE IN THE SAME SHOP, FOR THE EXACT SAME ISSUE. UPON DOING MORE RESEARCH ONLINE, I HAVE FOUND THAT NUMEROUS PEOPLE ARE EXPERIENCING THIS EXACT ISSUE. DUE TO NO FAULT OF MY OWN AND DUE TO INSUFFICIENT FAULTY PARTS IN THE IGNITION, I HAD TO HAVE THIS REPAIRED. I HAD TO HAVE MY CAR TOWED BECAUSE YOU CAN NOT MOVE THIS CAR OR PUT IT IN NEUTRAL TO GET THE VEHICLE TO MOVE OTHERWISE. FUNNY HOW IT FAILED 2 MONTHS AFTER MY WARRANTY EXPIRED! HOW IS THIS FAIR THAT THEIR PART FAILED AND YET THEY ARE TAKING TO RESPONSIBILITY FOR THIS? THIS WAS A VERY EXPENSIVE FIX! PLEASE RECALL THE PONTIAC IGNITIONS! SO I AM OUT ALMOST $1500. BAD CALL GM! *TR
WHEN I PUT MY KEY INTO THE IGNITION, IT FROZE. I COULDN'T TURN THE KEY. I COULDN'T MOVE THE CAR. THE IGNITION WAS LOCKED UP. I TRIED JUST REPLACING THE IGNITION CYLINDER, BUT THAT DID NOT WORK. I HAD TO HAVE THE ENTIRE STEERING COLUMN REPLACED. IT COST $1371.67 TO GET THIS CAR FIXED DUE TO NO FAULT OF MY OWN. I HAVE RESEARCHED THIS ISSUE AND IT SEEMS THAT ON THE WEEK MY VEHICLE WAS IN THE SHOP, 3 OTHER PONTIACS WERE IN THE SAME SHOP, FOR THE EXACT SAME ISSUE. UPON DOING MORE RESEARCH ONLINE, I HAVE FOUND THAT NUMEROUS PEOPLE ARE EXPERIENCING THIS EXACT ISSUE. DUE TO NO FAULT OF MY OWN AND DUE TO INSUFFICIENT FAULTY PARTS IN THE IGNITION, I HAD TO HAVE THIS REPAIRED. I HAD TO HAVE MY CAR TOWED BECAUSE YOU CAN NOT MOVE THIS CAR OR PUT IT IN NEUTRAL TO GET THE VEHICLE TO MOVE OTHERWISE. FUNNY HOW IT FAILED 2 MONTHS AFTER MY WARRANTY EXPIRED! HOW IS THIS FAIR THAT THEIR PART FAILED AND YET THEY ARE TAKING TO RESPONSIBILITY FOR THIS? THIS WAS A VERY EXPENSIVE FIX! PLEASE RECALL THE PONTIAC IGNITIONS! SO I AM OUT ALMOST $1500. BAD CALL GM! *TR
TL*THE CONTACT OWNS A 2005 PONTIAC GTO. WHILE DRIVING APPROXIMATELY 62 MPH, THE VEHICLE UNEXPECTEDLY SWERVED TOWARDS THE RIGHT AND CRASHED INTO ANOTHER VEHICLE. THE CONTACT AND THE DRIVER OF THE OTHER VEHICLE SUFFERED PERSONAL INJURIES. A POLICE REPORT WAS FILED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED; HOWEVER, THE CONTACT STATED THE FAILURE WAS RELATED TO THE STEERING. THE FAILURE MILEAGE WAS 80,000. UPDATED 01/12/11*LJ UPDATED 01/14/11 *BF PICTURES RECEIVED 01/27/11 PRIOR TO THE ACCIDENT, THE REAR DIFFERENTIAL FAILED INTERNALLY, AND THE POWER STEERING HOSE WAS LEAKING. UPDATED 04/15/11
TL*THE CONTACT OWNS A 2005 PONTIAC GTO. WHILE DRIVING APPROXIMATELY 62 MPH, THE VEHICLE UNEXPECTEDLY SWERVED TOWARDS THE RIGHT AND CRASHED INTO ANOTHER VEHICLE. THE CONTACT AND THE DRIVER OF THE OTHER VEHICLE SUFFERED PERSONAL INJURIES. A POLICE REPORT WAS FILED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED; HOWEVER, THE CONTACT STATED THE FAILURE WAS RELATED TO THE STEERING. THE FAILURE MILEAGE WAS 80,000. UPDATED 01/12/11*LJ UPDATED 01/14/11 *BF PICTURES RECEIVED 01/27/11 PRIOR TO THE ACCIDENT, THE REAR DIFFERENTIAL FAILED INTERNALLY, AND THE POWER STEERING HOSE WAS LEAKING. UPDATED 04/15/11
THIS IS A DAILY PROBLEM WITH THE 2005 PONTIAC GTO HAVING ITS BOTH FRONT TIRES RUB AGAINST THE INSIDE SHOCKS DURING DRIVING. THE TIRE INSTALLED NI THE CAR ARE EXACTLY WHAT IS RECOMMENDED. I AM NOT THE ONLY ONE FACING THIS ISSUE. ALL THE OTHER OWNERS HAVE THE SAME ISSUE. THIS COULD RESULT IN AN ACCIDENT AS THE TIRE RUB INCREASES DURING A TURN OR BRAKING. CONSTANT RUB COULD LEAD TO TIRE DAMAGE AND BURAT DURING HIGHWAY DRIVING. I HAVE ALL THE TIRES ALIGNED ROTATED AND BALANCED ALSO. THE PROBLEM DOES NOT GET RESOLVE, PONTIAC SERVICEMAN SAY IT IS A FAULT IN THE CAR.. *TR
THIS IS A DAILY PROBLEM WITH THE 2005 PONTIAC GTO HAVING ITS BOTH FRONT TIRES RUB AGAINST THE INSIDE SHOCKS DURING DRIVING. THE TIRE INSTALLED NI THE CAR ARE EXACTLY WHAT IS RECOMMENDED. I AM NOT THE ONLY ONE FACING THIS ISSUE. ALL THE OTHER OWNERS HAVE THE SAME ISSUE. THIS COULD RESULT IN AN ACCIDENT AS THE TIRE RUB INCREASES DURING A TURN OR BRAKING. CONSTANT RUB COULD LEAD TO TIRE DAMAGE AND BURAT DURING HIGHWAY DRIVING. I HAVE ALL THE TIRES ALIGNED ROTATED AND BALANCED ALSO. THE PROBLEM DOES NOT GET RESOLVE, PONTIAC SERVICEMAN SAY IT IS A FAULT IN THE CAR.. *TR
DT: THE CONTACT STATES THERE ARE MULTIPLE PROBLEMS WITH THE VEHICLE. SHE HAS TAKEN THE VEHICLE TO THE DEALERSHIP. ON APRIL 26, 2005 THEY REPLACED THE COMPUTER, HARNESS, THROTTLE BODY, ENGINE RELAY SWITCH, CLAMPS AND HANGERS TO THE EXHAUST SYSTEM. THEN ON AUGUST 11, 2005 THEY REPLACED SOME MISSING STRUT TOWER NUTS. THERE WAS A WHISTLING SOUND COMING FROM THE VEHICLE WHEN STARTED. THE SAFETY AND CHECK OIL INDICATOR LIGHTS CAME ON. LATER, ON SEPTEMBER 27 , 2005 THE DEALERSHIP REPLACED THE ENGINE, EXHAUST HANGER AND CLAMPS AGAIN, PEDAL AND PEDAL SPRINGS AND ENGINE MANIFOLD GASKET. ON OCTOBER 19 THE LEFT TAIL LIGHT WAS LOOSE, AND THE CLUTCH PEDAL WENT DOWN TO THE FLOOR. THE TRACTION CONTROL BUTTON AND THE TRUNK RELEASE BUTTONS WOULD NOT WORK. ALSO, THE POWER STEERING BRACKET WAS LOOSE. THEY REPLACED THE LEFT TAIL LIGHT, CLUTCH PEDAL, AND THE MISSING RIGHT MUFFLER INSULATOR. *AK UPDATED11/29/05. *JB
DT: THE CONTACT STATES THERE ARE MULTIPLE PROBLEMS WITH THE VEHICLE. SHE HAS TAKEN THE VEHICLE TO THE DEALERSHIP. ON APRIL 26, 2005 THEY REPLACED THE COMPUTER, HARNESS, THROTTLE BODY, ENGINE RELAY SWITCH, CLAMPS AND HANGERS TO THE EXHAUST SYSTEM. THEN ON AUGUST 11, 2005 THEY REPLACED SOME MISSING STRUT TOWER NUTS. THERE WAS A WHISTLING SOUND COMING FROM THE VEHICLE WHEN STARTED. THE SAFETY AND CHECK OIL INDICATOR LIGHTS CAME ON. LATER, ON SEPTEMBER 27 , 2005 THE DEALERSHIP REPLACED THE ENGINE, EXHAUST HANGER AND CLAMPS AGAIN, PEDAL AND PEDAL SPRINGS AND ENGINE MANIFOLD GASKET. ON OCTOBER 19 THE LEFT TAIL LIGHT WAS LOOSE, AND THE CLUTCH PEDAL WENT DOWN TO THE FLOOR. THE TRACTION CONTROL BUTTON AND THE TRUNK RELEASE BUTTONS WOULD NOT WORK. ALSO, THE POWER STEERING BRACKET WAS LOOSE. THEY REPLACED THE LEFT TAIL LIGHT, CLUTCH PEDAL, AND THE MISSING RIGHT MUFFLER INSULATOR. *AK UPDATED11/29/05. *JB