22
Complaints
0
Crashes
0
Fires
0
Deaths

This Problem Across All Years

All Visibility/wiper Complaints

Showing 20 of 22
Sep 15, 2014 15,280 mi

ALL BUSES DELIVERED W/ NO REGEN SWITCHES CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9). *TR

Sep 15, 2014 5,825 mi

CONSTANTLY REPLACING FOG LIGHT BULBS EMERGENCY WINDOW LATCHES ARE NOT OPERATIONAL, BREAK VERY EASILY AND DO NOT RELATCH ONCE OPENED CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9). *TR

Sep 15, 2014

?ALL BUSES DELIVERED W/ NO REGEN SWITCHES ?REAR HEATER INOPERABLE HEATER SWITCHES FOR REAR HEAT WERE NEVER INSTALLED UPON ARRIVAL CODE #1 ?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9) ?REAR A/C REPAIR BY THERMOKING ?DRIVER'S SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & WIRING, HEIGHT ADJUST MECHANISM IS INOPERABLE (HAD TO INSTALL A SCREW TO KEEP IT STEADY). *TR

Sep 15, 2014 15,280 mi

ALL BUSES DELIVERED W/ NO REGEN SWITCHES CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9). *TR

Sep 15, 2014 5,825 mi

CONSTANTLY REPLACING FOG LIGHT BULBS EMERGENCY WINDOW LATCHES ARE NOT OPERATIONAL, BREAK VERY EASILY AND DO NOT RELATCH ONCE OPENED CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9). *TR

Sep 15, 2014

?ALL BUSES DELIVERED W/ NO REGEN SWITCHES ?REAR HEATER INOPERABLE HEATER SWITCHES FOR REAR HEAT WERE NEVER INSTALLED UPON ARRIVAL CODE #1 ?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9) ?REAR A/C REPAIR BY THERMOKING ?DRIVER'S SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & WIRING, HEIGHT ADJUST MECHANISM IS INOPERABLE (HAD TO INSTALL A SCREW TO KEEP IT STEADY). *TR

Sep 11, 2014 2,581 mi

?DRIVER SEAT BELTS GET STUCK ONLY RETRACT SOMETIMES / BELT COVER CAUSES BELT TO BE INOPERABLE (REPLACED WITH AFTERMARKET BELTS) ?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9) ?PASSENGER SEATBELTS KEEP GETTING STUCK ( DO NOT UNLATCH TO OPEN AND SOMETIMES DO NOT RETRACT). *TR

Sep 11, 2014 8,750 mi

?CONSTANTLY REPLACE FOG LIGHT BULBS ?EMERGENCY WINDOW LATCHES ARE NOT OPERATIONAL, BREAK VERY EASILY AND DO NOT RELATCH ONCE OPENED ?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9). *TR

Sep 11, 2014 9,146 mi

?CONSTANTLY REPLACING FOG LIGHT BULBS ?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9) ?DRIVER?S SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & WIRING, HEIGHT ADJUST MECHANISM IS INOPERABLE (HAD TO INSTALL A SCREW TO KEEP IT STEADY). *TR

Sep 11, 2014 2,581 mi

?DRIVER SEAT BELTS GET STUCK ONLY RETRACT SOMETIMES / BELT COVER CAUSES BELT TO BE INOPERABLE (REPLACED WITH AFTERMARKET BELTS) ?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9) ?PASSENGER SEATBELTS KEEP GETTING STUCK ( DO NOT UNLATCH TO OPEN AND SOMETIMES DO NOT RETRACT). *TR

Sep 11, 2014 8,750 mi

?CONSTANTLY REPLACE FOG LIGHT BULBS ?EMERGENCY WINDOW LATCHES ARE NOT OPERATIONAL, BREAK VERY EASILY AND DO NOT RELATCH ONCE OPENED ?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9). *TR

Sep 11, 2014 9,146 mi

?CONSTANTLY REPLACING FOG LIGHT BULBS ?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9) ?DRIVER?S SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & WIRING, HEIGHT ADJUST MECHANISM IS INOPERABLE (HAD TO INSTALL A SCREW TO KEEP IT STEADY). *TR

Sep 5, 2014 4,334 mi

?DRIVER SEAT BELTS GET STUCK ONLY RETRACT SOMETIMES / BELT COVER CAUSES BELT TO BE INOPERABLE (REPLACED WITH AFTERMARKET BELTS) ?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9) ?DRIVER'S SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & WIRING, HEIGHT ADJUST MECHANISM IS INOPERABLE. *TR

Sep 5, 2014 3,691 mi

?DRIVER'S SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & WIRING, HEIGHT ADJUST MECHANISM IS INOPERABLE (HAD TO INSTALL A SCREW TO KEEP IT STEADY) ?DRIVER SEAT BELTS GET STUCK ONLY RETRACT SOMETIMES / BELT COVER CAUSES BELT TO BE INOPERABLE (REPLACED WITH AFTERMARKET BELTS) ?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9). *TR

Sep 5, 2014 2,300 mi

DRIVERS SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & WIRING, HEIGHT ADJUST MECHANISM IS INOPERABLE CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9) CONTINUOUSLY REPLACING FOG LIGHT BULBS

Sep 5, 2014 2,499 mi

DRIVER'S SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & WIRING, HEIGHT ADJUST MECHANISM IS INOPERABLE (HAD TO INSTALL A SCREW TO KEEP IT STEADY) CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9)

Sep 5, 2014 4,334 mi

?DRIVER SEAT BELTS GET STUCK ONLY RETRACT SOMETIMES / BELT COVER CAUSES BELT TO BE INOPERABLE (REPLACED WITH AFTERMARKET BELTS) ?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9) ?DRIVER'S SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & WIRING, HEIGHT ADJUST MECHANISM IS INOPERABLE. *TR

Sep 5, 2014 3,691 mi

?DRIVER'S SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & WIRING, HEIGHT ADJUST MECHANISM IS INOPERABLE (HAD TO INSTALL A SCREW TO KEEP IT STEADY) ?DRIVER SEAT BELTS GET STUCK ONLY RETRACT SOMETIMES / BELT COVER CAUSES BELT TO BE INOPERABLE (REPLACED WITH AFTERMARKET BELTS) ?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9). *TR

Sep 5, 2014 2,300 mi

DRIVERS SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & WIRING, HEIGHT ADJUST MECHANISM IS INOPERABLE CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9) CONTINUOUSLY REPLACING FOG LIGHT BULBS

Sep 5, 2014 2,499 mi

DRIVER'S SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & WIRING, HEIGHT ADJUST MECHANISM IS INOPERABLE (HAD TO INSTALL A SCREW TO KEEP IT STEADY) CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9)

Sep 4, 2014 5,729 mi

?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS BUSES HAD TO STAY STAIONARY AT RANDON LOCATIONS BECAUSE THE WIPERS DID NOT WORK IN RAIN (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9) ?DRIVER SEAT BELTS GET STUCK ONLY RETRACT SOMETIMES / BELT COVER CAUSES BELT TO BE INOPERABLE (WAS FORCED TO REPLACE WITH AFTERMARKET BELTS) ?DRIVER'S SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & ELECTRICAL WIRING, MAKING HEIGHT ADJUST MECHANISM IS INOPERABLE. *TR

Sep 4, 2014 5,729 mi

?CONSISTENT WIPE ISSUES, CONTINUOUSLY HAD TO RESET INVERTERS & REPLACE 24 VOLT RELAYS BUSES HAD TO STAY STAIONARY AT RANDON LOCATIONS BECAUSE THE WIPERS DID NOT WORK IN RAIN (MADE US REMOVE 2 PIECES FROM CIRCUIT BOARD D4+R9) ?DRIVER SEAT BELTS GET STUCK ONLY RETRACT SOMETIMES / BELT COVER CAUSES BELT TO BE INOPERABLE (WAS FORCED TO REPLACE WITH AFTERMARKET BELTS) ?DRIVER'S SEAT WAS ALLOWED TO GO TOO FAR BACK & IS LOCATED TOO LOW WHEN ADJUSTING SEAT IT WAS GOING BACK IT WAS CUTTING ALL AIR LINES & ELECTRICAL WIRING, MAKING HEIGHT ADJUST MECHANISM IS INOPERABLE. *TR