12
Complaints
0
Crashes
0
Fires
0
Deaths

This Problem Across All Years

All Power Train Complaints

Showing 12 of 12
Jan 16, 2014 140,000 mi

TL* THE CONTACT OWNS 2004 SUZUKI FORENZA. THE CONTACT STATED THAT WHILE DRIVING 70 MPH, THE SPEEDOMETER PROVIDED AN INACCURATE READING OF ZERO. THE CONTACT STATED THAT THE SPEEDOMETER RESET INDEPENDENTLY BUT THE VEHICLE WOULD NOT MAINTAIN SPEEDS OF OVER 70 MPH. THE VEHICLE WAS TAKEN TO THE DEALER FOR INSPECTION AND THEY STATED THAT THE TRANSMISSION NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 140,000.

Jan 16, 2014 140,000 mi

TL* THE CONTACT OWNS 2004 SUZUKI FORENZA. THE CONTACT STATED THAT WHILE DRIVING 70 MPH, THE SPEEDOMETER PROVIDED AN INACCURATE READING OF ZERO. THE CONTACT STATED THAT THE SPEEDOMETER RESET INDEPENDENTLY BUT THE VEHICLE WOULD NOT MAINTAIN SPEEDS OF OVER 70 MPH. THE VEHICLE WAS TAKEN TO THE DEALER FOR INSPECTION AND THEY STATED THAT THE TRANSMISSION NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 140,000.

Feb 12, 2008 50,000 mi

CAR HAS TROUBLE STARTING AND CHECK ENGINE LIGHT COMES ON INTERMITTENTLY. JULY 2007 TOOK CAR IN WITH 'HARD START" PROBLEM. THEY FOUND RESONATOR ASSEMBLY NEEDED REPLACING. THAT REPAIR WAS DONE ON AUGUST 3, 2007. CAR RAN FOR APPROX. 2 MONTHS AND WE TOOK IT BACK IN OCTOBER WITH THE CHECK ENGINE LIGHT ON AND THE SAME "HARD START" PROBLEM. THEY REPLACED THE STARTER OCTOBER 18, 2007 AND STATED IT WAS ARCING TO HIGH. TOOK CAR BACK OCTOBER 21, 2007 WITH THE SAME PROBLEM. OCTOBER 26, 2007 THE ECU COMPUTER WAS REPLACED. TOOK CAR BACK TO SHOP OCTOBER 29, 2007 WITH THE SAME "HARD START" PROBLEM. MOVED THE CAR TO ANOTHER DEALERSHIP NOVEMBER 7, 2007 AS NO ONE WAS WORKING ON THE CAR. THIS WAS SUGGESTED BY THE CORPORATION. A REPAIR WAS DONE ON THE CAR. DECEMBER 13, 2007 TOOK CAR BACK TO THIS DEALERSHIP WITH THE SAME "HARD START" PROBLEM. THEY CHECKED THE CODE AND RESET THE CHECK ENGINE LIGHT. DECEMBER 18, 2007 RETURNED TO THE DEALERSHIP WITH THE SAME PROBLEM. THEY REPLACED THE ENGINE WIRING HARNESS. JANUARY 25, 2008 THE CAR IS HAVING THE SAME "HARD START" PROBLEM AND IS SITTING IN THE YARD. *TR

Feb 12, 2008 50,000 mi

CAR HAS TROUBLE STARTING AND CHECK ENGINE LIGHT COMES ON INTERMITTENTLY. JULY 2007 TOOK CAR IN WITH 'HARD START" PROBLEM. THEY FOUND RESONATOR ASSEMBLY NEEDED REPLACING. THAT REPAIR WAS DONE ON AUGUST 3, 2007. CAR RAN FOR APPROX. 2 MONTHS AND WE TOOK IT BACK IN OCTOBER WITH THE CHECK ENGINE LIGHT ON AND THE SAME "HARD START" PROBLEM. THEY REPLACED THE STARTER OCTOBER 18, 2007 AND STATED IT WAS ARCING TO HIGH. TOOK CAR BACK OCTOBER 21, 2007 WITH THE SAME PROBLEM. OCTOBER 26, 2007 THE ECU COMPUTER WAS REPLACED. TOOK CAR BACK TO SHOP OCTOBER 29, 2007 WITH THE SAME "HARD START" PROBLEM. MOVED THE CAR TO ANOTHER DEALERSHIP NOVEMBER 7, 2007 AS NO ONE WAS WORKING ON THE CAR. THIS WAS SUGGESTED BY THE CORPORATION. A REPAIR WAS DONE ON THE CAR. DECEMBER 13, 2007 TOOK CAR BACK TO THIS DEALERSHIP WITH THE SAME "HARD START" PROBLEM. THEY CHECKED THE CODE AND RESET THE CHECK ENGINE LIGHT. DECEMBER 18, 2007 RETURNED TO THE DEALERSHIP WITH THE SAME PROBLEM. THEY REPLACED THE ENGINE WIRING HARNESS. JANUARY 25, 2008 THE CAR IS HAVING THE SAME "HARD START" PROBLEM AND IS SITTING IN THE YARD. *TR

Nov 7, 2005

DT: THE CONTACT STATED THE ENGINE REVVED, IT WAS RACING, AND THE RPM GAUGE RAN HIGHER THAN NORMAL. THE VEHICLE WILL HESITATE AT ANY SPEED. THERE WILL BE A LOSS OF POWER, AND THE VEHICLE JERKED WHEN POWER WENT BACK INTO THE VEHICLE. THERE WAS NO PRIOR WARNING. THIS HAPPENED EVERY TIME WHEN DRIVING THE VEHICLE. HE TOOK THE VEHICLE TO THE DEALER. THEY SAID THE ECM HAD TO BE REFLASHED. DEALER DID THE WORK. THE VEHICLE IS STILL HAVING THE SAME PROBLEM SINCE THEN. *AK ENGINE CHECK LIHT CAME ON, AND VEHICLE SEEMED TO RUN HIGHER WHEN COLD OUTSIDE. *AK

Nov 7, 2005

DT: THE CONTACT STATED THE ENGINE REVVED, IT WAS RACING, AND THE RPM GAUGE RAN HIGHER THAN NORMAL. THE VEHICLE WILL HESITATE AT ANY SPEED. THERE WILL BE A LOSS OF POWER, AND THE VEHICLE JERKED WHEN POWER WENT BACK INTO THE VEHICLE. THERE WAS NO PRIOR WARNING. THIS HAPPENED EVERY TIME WHEN DRIVING THE VEHICLE. HE TOOK THE VEHICLE TO THE DEALER. THEY SAID THE ECM HAD TO BE REFLASHED. DEALER DID THE WORK. THE VEHICLE IS STILL HAVING THE SAME PROBLEM SINCE THEN. *AK ENGINE CHECK LIHT CAME ON, AND VEHICLE SEEMED TO RUN HIGHER WHEN COLD OUTSIDE. *AK

Jun 9, 2005 85 mi

DT: CONSUMER'S VEHICLE REAREND. NOISE COMING FROM THE DRIVETRAIN. CONSUMER TOOK VEHICLE TO DEALER TO BE REPAIRED. DEALER COULD FIND NO PROBLEM , CONSUMER TOOK IT BACK TO THE DEALER AND THE DEALER KEPT THE VEHICLE FOR A WEEK. THEN, DEALER SAID PROBLEM WAS COMING FROM THE FIREWALL OR THE ASHTRAY, THE SECOND TIME, AFTER THE VEHICLE WAS PICKED UP BY THE CONSUMER, DID NOT RECEIVE PAPER WORK, WHEN CONSUMER RECEIVED PAPER WORK IT STATEDTHAT THE REAR BRAKES WERE RUSTED. *AK

Jun 9, 2005 85 mi

DT: CONSUMER'S VEHICLE REAREND. NOISE COMING FROM THE DRIVETRAIN. CONSUMER TOOK VEHICLE TO DEALER TO BE REPAIRED. DEALER COULD FIND NO PROBLEM , CONSUMER TOOK IT BACK TO THE DEALER AND THE DEALER KEPT THE VEHICLE FOR A WEEK. THEN, DEALER SAID PROBLEM WAS COMING FROM THE FIREWALL OR THE ASHTRAY, THE SECOND TIME, AFTER THE VEHICLE WAS PICKED UP BY THE CONSUMER, DID NOT RECEIVE PAPER WORK, WHEN CONSUMER RECEIVED PAPER WORK IT STATEDTHAT THE REAR BRAKES WERE RUSTED. *AK

Apr 1, 2005 5,000 mi

WHILE DRIVING 65 MPH CONSMER HEARD A KNOCKING NOISE COMING FROM THE ENGINE. ALSO, IT WAS HARD TO DOWN SHIFT THE GEARS. DEALERSHIP WAS NOTIFED, BUT DID NOT RESOLVE THE PROBLEM. *AK

Apr 1, 2005 5,000 mi

WHILE DRIVING 65 MPH CONSMER HEARD A KNOCKING NOISE COMING FROM THE ENGINE. ALSO, IT WAS HARD TO DOWN SHIFT THE GEARS. DEALERSHIP WAS NOTIFED, BUT DID NOT RESOLVE THE PROBLEM. *AK

Mar 25, 2005

DRIVER NOTICED THAT WHILE SHIFTING THE CLUTCH A LOUD WINDING SOUND CAME FROM THE FRONT. THE CLUTCH FAILED. DRIVER HAD THE VEHICLE TOWED TO DEALER FOR INSPECTION, AND MECHANIC DETERMINED THAT THE CLUTCH HOUSING ASSEMBLY BELL UNIT NEEDED TO BE REPLACED. *AK

Mar 25, 2005

DRIVER NOTICED THAT WHILE SHIFTING THE CLUTCH A LOUD WINDING SOUND CAME FROM THE FRONT. THE CLUTCH FAILED. DRIVER HAD THE VEHICLE TOWED TO DEALER FOR INSPECTION, AND MECHANIC DETERMINED THAT THE CLUTCH HOUSING ASSEMBLY BELL UNIT NEEDED TO BE REPLACED. *AK