12
Complaints
2
Crashes
0
Fires
0
Deaths
!

High Severity Issue

This component has been associated with crashes, fires, or deaths.

This Problem Across All Years

All Power Train Complaints

Showing 12 of 12
May 13, 2009 75,000 mi

TL*THE CONTACT OWNS A 1994 TOYOTA PICKUP. THE CONTACT TOOK HER VEHICLE TO PEP BOYS TO HAVE A NEW CLUTCH AND EXHAUST INSTALLED. THE MECHANIC DISCOVERED A DEFECT AND ATTEMPTED TO TOW THE VEHICLE TO A DEALER; HOWEVER, THE TOW DRIVER WOULD NOT TRANSPORT THE VEHICLE BECAUSE THE FRAME WAS FAULTY. THE DEALER CONFIRMED THAT THE FRAME WAS RUSTED AND UNSAFE. THE CURRENT AND FAILURE MILEAGES WERE 75,000. UPDATED 6/01/09 *CN THE CONSUMER STATED A NEW CLUTCH AND EXHAUST SYSTEM. UPDATED 06/02/09.*JB

May 13, 2009 75,000 mi

TL*THE CONTACT OWNS A 1994 TOYOTA PICKUP. THE CONTACT TOOK HER VEHICLE TO PEP BOYS TO HAVE A NEW CLUTCH AND EXHAUST INSTALLED. THE MECHANIC DISCOVERED A DEFECT AND ATTEMPTED TO TOW THE VEHICLE TO A DEALER; HOWEVER, THE TOW DRIVER WOULD NOT TRANSPORT THE VEHICLE BECAUSE THE FRAME WAS FAULTY. THE DEALER CONFIRMED THAT THE FRAME WAS RUSTED AND UNSAFE. THE CURRENT AND FAILURE MILEAGES WERE 75,000. UPDATED 6/01/09 *CN THE CONSUMER STATED A NEW CLUTCH AND EXHAUST SYSTEM. UPDATED 06/02/09.*JB

Jul 11, 2003 116,000 mi

THE DEALER INFORMED THE CONSUMER THE CYLINDER HEAD NEEDED TO BE REPLACED, BECAUSE OF A LEAKING HEAD GASKET. *JB THE CONSUMER WAS ALSO TOLD THE RADIATOR WAS LEAKING FROM THE TOP TANK, THE CLUTCH FLEX LINE AND POWER STEERING PUMP WAS ALSO LEAKING. THE GAS GAUGE WAS INOPERATIVE. THE DRIVE BELT AND TIMING BELTS WERE REPLACED. PH. *JB

Jul 11, 2003 116,000 mi

THE DEALER INFORMED THE CONSUMER THE CYLINDER HEAD NEEDED TO BE REPLACED, BECAUSE OF A LEAKING HEAD GASKET. *JB THE CONSUMER WAS ALSO TOLD THE RADIATOR WAS LEAKING FROM THE TOP TANK, THE CLUTCH FLEX LINE AND POWER STEERING PUMP WAS ALSO LEAKING. THE GAS GAUGE WAS INOPERATIVE. THE DRIVE BELT AND TIMING BELTS WERE REPLACED. PH. *JB

Dec 27, 2000

CONSUMER HAS TO PUT A HAIR DRYER ON THE NEUTRAL SAFETY SWITCH ON COLD DAYS, IT WILL NOT ENGAGE ON COLD DAYS, WHEN ENGAGING THE CLUTCH, THERE IS NO CONTACT WITH THE BATTERY. *SLC

Dec 27, 2000

CONSUMER HAS TO PUT A HAIR DRYER ON THE NEUTRAL SAFETY SWITCH ON COLD DAYS, IT WILL NOT ENGAGE ON COLD DAYS, WHEN ENGAGING THE CLUTCH, THERE IS NO CONTACT WITH THE BATTERY. *SLC

Feb 24, 2000

WHILE DRIVING COULD HEAR NOISE COMING FROM THE ENGINE WHEN SHIFTING GEARS. ALSO, ENGINE COOLANT LEAKED ALL THE TIME. *AK

Feb 24, 2000

WHILE DRIVING COULD HEAR NOISE COMING FROM THE ENGINE WHEN SHIFTING GEARS. ALSO, ENGINE COOLANT LEAKED ALL THE TIME. *AK

Dec 23, 1998

TRANMISSION LEAKED AND THE VEHICLE LOST POWER. ALSO, ENGINE HEAD GASKET HAD TO BE REPLACED. THE TRANMISSION HAD TO BE REPAIRED DUE TO THE OLD SEAL, AND THE DEALER FIXED THE SEAL TO STOP THE LEAKAGE. *AK

Dec 23, 1998

TRANMISSION LEAKED AND THE VEHICLE LOST POWER. ALSO, ENGINE HEAD GASKET HAD TO BE REPLACED. THE TRANMISSION HAD TO BE REPAIRED DUE TO THE OLD SEAL, AND THE DEALER FIXED THE SEAL TO STOP THE LEAKAGE. *AK

Jun 1, 1996 Crash

REAR SEAL LEAKED GREASE ALL OVER BRAKES, CAUSING THE REAR BRAKES TO LOCK UP/ACCIDENT/INJURY. *DH

Jun 1, 1996 Crash

REAR SEAL LEAKED GREASE ALL OVER BRAKES, CAUSING THE REAR BRAKES TO LOCK UP/ACCIDENT/INJURY. *DH